ML17305B705

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Special Rept 2-SR-91-001:on 910811 Unusual Event Declared Due to Identified Leakage of RCS Exceeding TS 3.4.5.2 Limiting Condition for Operation.Caused by Leakage from HX Seal Injection Drain Valves.Seal Injection Isolated
ML17305B705
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 08/16/1991
From: James M. Levine
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
192-00735-JML-T, 192-735-JML-T, 2-SR-91-001, 2-SR-91-1, NUDOCS 9109030007
Download: ML17305B705 (8)


Text

ACCELERATED DIGBUTION DEMONST1TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) 05000529

/

A ACCESSION NBR:9109030007 DOC.DATE: 91/08/16 NOTARIZED:

NO DOCKET FACIL:STN-50-529 Palo Verde Nuclear'Station, Unit 2, Arizona Publi 05000529 AUTH.NAME AUTHOR AFFILIATION LEVINE,J.M.

Arizona Public Service Co.

(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Special Rept 2-SR-91-001:on 910811 unusual event declared due to identified leakage of RCS exceeding TS 3.4.5.2 limitinq condition for operation. Caused by leakage from HX seal ingection drain valves. Seal injection isolated.

DISTRIBUTION CODE:

IE22D COPIES RECEIVED:LTR I

ENCL 3 SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:Standardized plant.

RECIPIENT ID CODE/NAME PD5 LA TRAMMELL,C INTERNAL: ACNW

.AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB8H3 NRR/DST/SRXB 8E RES/DSIR/EIB EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POOREPW NOTES COPIES LTTR ENCL 1

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1 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M ACRS AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB 8D N~/~S/S PLB8 D1

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~RGN5 FILE 01 L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1

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D NOTE TO ALL"RIDS" RECIPIENTS:

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PLEASE HELP US TO REDI 'l. E 'iVASTI'ONTACTTHE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO LLIMINAI L YOUR NAAIEFROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 35 ENCL 35

Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O. BOX 52034

~

PHOENIX. ARIZONA85072-2034 JAMES M, LEVINE VICE PRESIDENT NUCLEAR PRODUCTION 192-00735-JML/TRB/KR August 16, 1991 U.

ST Nuclear Regulatory Commission Attention: Document Control Desk Mail Station Pl-37 Washington, D.C.

20555

Dear Sirs:

Sub) ect:

Palo Verde Nuclear Generating Station (PVNGS)

Unit 2 Docket No.

STN 50-529 (License No. NPF-51)

Special Report 2-SR-91-001 File 91-020-404 Attached please find Special Report 2-SR-91-001 prepared and submitted pursuant to Emergency Plan Implementing Procedure (EPIP-03).

This report discusses a condition requiring the NOTIFICATION OF UNUSUAL EVENT wherein -the Technical Specification 3.4.5.2 Limiting Condition for Operation for reactor coolant system'leakage limit of one (1) gallon per minute UNIDENTIFIED LEAKAGE was exceeded.

If you have any questions, please contact T. R. Bradish, Compliance Manager at (602) 393-2521.

Very truly yours, JML/TRB/KR/nk Attachment cc:

W. F.

J.

B.

D. H.

A. C.

A. H.

Conway Martin Coe Gehr Gutterman (all with attachment) p h q r, rI q 910YVBVLILI7 Y1 VQ>)~'DR ADOCK 05000529 8

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Palo Verde Nuclear Generating Station Unit 2 Notification of Unusual Event Docket No. 50-529 License No. NPF-51 Special Report No. 2-SR-91-001 This Special Report is being provided pursuant to Emergency Plan Implementing Procedure (EPIP)-03, "Notification of Unusual Event Implementing Aetio'ns" to report a condition requiring the declaration of a Notification of Unusual Event for Palo Verde Unit 2 from August 11, 1991 at 2330 MST to August 12, 1991 at 0230 MST.

On August 11, 1991, at approximately 2330 MST, Palo Verde Unit 2 was in Mode 3

(HOT STANDBY) when the Unit 2 Shift Supervisor declared a Notification of Unusual Event due to UNIDENTIFIED LEAKAGE exceeding the Technical Specification (TS) 3.4.5.2 Limiting Condition for Operation (LCO) for reactor coolant system leakage limit of one (1) gallon per minute (gpm).

Emergency Plan Implementing Procedures require the declaration of a Notification of Unusual Event for exceeding TS leakage limits.

TS 3.4.5.2 ACTION (b) requires a reduction in the leakage rate to within limits within four (4) hours or be in at least HOT STANDBY within the next six (6) hours and in COLD SHUTDOWN within the following thirty (30) hours.

At approximately 2342 MST, Unit 2 personnel notified the appropriate state and local agencies.

At approximately 0005 MST on August 12,

1991, the Nuclear Regulatory Commission (NRC)'perations Center was notified of the condition requiring the declaration of a Notification of Unusual Event (i.e.,

UNIDENTIFIED LEAKAGE exceeding TS leakage limit) ~

Prior to the declaration of a Notification of Unusual Event for the UNIDENTIFIED LEAKAGE, at approximately 1633 MST the reactor coolant system (RCS) water inventory balance procedure was initiated following completion of corrective maintenance on a leaking reactor coolant pump seal injection heat exchanger thermal relief valve.

Prior to completion of the RCS water inventory balance procedure, Control Room personnel determined that the reactor coolant pump seal injection heat exchanger drain valves were not fully seated.

The drain valves had been opened during the corrective maintenance on the thermal relief valve The Control Room Shift Supervisor terminated the RCS water inventory balance procedure.

However, subsequent to the termination of the RCS water inventory balance procedure, at approximately 1833
MST, a

reactor operator reported that the RCS water inventory balance computer-generated computation calculated the UNIDENTIFIED LEAKAGE to be approximately 2.780 gpm.

Engineering and Unit 2 personnel investigated and verified that the reactor coolant system leakage was attributed to leakage from the reactor coolant pump seal injection heat exchanger drain valves.

The leakage was directed to the non-Engineered Safety'eature sump located in the Auxiliary Building.

At approximately 2134 MST, following a review of the RCS water inventory balance calculation, the Shift Supervisor determined that the leakage should be classified as UNIDENTIFIED LEAKAGE and entered TS 3.4.5.2 ACTION (b).

'i I

Il

NRC Document Control Desk Page 2

Special Report 2-SR-91-001 At approximately 2330

MST, a

PVNGS management review determined that a Notification of Unusual Event should be declared

because, although the source of the UNIDENTIFIED LEAKAGE was known to be from the drain valves, the amount of the leakage was not quantified.

At approximately 2350 MST, on August ll, 1991, Unit 2 personnel isolated the seal injection to the reactor coolant pumps prior to re-performing the RCS water inventory balance procedure.

At approximately 0008 MST, on August 12,

1991, the second RCS water inventory balance procedure was initiated.

At approximately 0230 MST, on August 12, 1991, following the performance of the RCS water inventory balance procedure, Control Room personnel verified that reactor coolant system UNIDENTIFIED LEAKAGE had been reduced to within limits (approximately 0.303 gpm) with t'e seal injection isolated and TS 3.4.-5.2 ACTION (b) was exited.

In addition, the condition requiring the declaration of a Notification of Unusual Event was terminated.

Unit 2 had remained in the TS ACTION statement for approximately five (5) hours.

At approximately 0252 MST, on August 12,

1991, seal injection to the reactor coolant pumps was restored.

Further investigation into the circumstances surrounding this event is being performed in accordance with the PVNGS Incident Investigation Program.

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