ML17304A299

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Insp Rept 50-528/88-24 on 880705-08.Violations Noted.Major Areas Inspected:Inoperablity of Essential Chilled Water Trains
ML17304A299
Person / Time
Site: Palo Verde 
Issue date: 07/14/1988
From: Polich T, Richards S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17304A298 List:
References
50-528-88-24, NUDOCS 8808030087
Download: ML17304A299 (11)


See also: IR 05000528/1988024

Text

EA-88-182

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report No:

Docket No:

License

No:

Licensee:

Facility Name:

50-528/88-24

50-528

NPF-41

Arizona Nuclear

Power Project

P. 0.

Box 52034

Phoenix,

AZ. 85072-2034

Palo Verde Nuclear Generating Station Unit 1

Inspection

Conducted:

July 5-8,

1988

Inspector:

o ~c

,

en>or

es)

ent

nspector

ate

>gne

Approved By:

7-i I-SS

~Summa r:

S ecial

Ins ection

on Jul

5 throu

h Jul

8

1988

Re ort Number 50-528 88-24

.

Areas Ins ected:

This special

inspection

reviewed the inoperability of both

trains

o

ssential

Chilled Water at Unit 1 during the period of May 20-29,

1988.

During this inspection, the following inspection

modules

were covered:

30703

and 93702.

v+

Results:

One;:.violation of: Technical Specifications

was identified in that two

trains of Essential

Chilled Water were inoperable for a period of approximately

nine days.-

8808030087

880715

PDR

ADQCK 05000528,

G

~

PNU;i~

DETAILS

Persons

Contacted:

The below listed technical

and supervisory

personnel

were

among those

contacted:

Arizona Nuclear

Power Pro ect

(ANPP

  • J. Al 1 en
  • W. Doyle, Jr.
  • J. Driscoll
  • R. Gouge
  • J. Haynes
  • W. Ide
  • D. Karner
  • J. Kirby
  • R. Logan
  • K. Oberdorf
  • T. Schriver
  • J. Sills

Plant Manager, Unit

1

Manager, Unit 2 Radiation Protection

Assistant

Vice Pres. ident,

ANPP Admin.

Operations

Manager, Unit 3

Vice President,

Nuclear Production

Plant Manager,

Unit 2

Exec.

Vice President,

ANPP Administration

Director, Site Services

Supervisor,

Central Radiation Protection

Manager, Unit

1 Radiation Protection

Manager,

Compliance

Supervisor,

Radiation Protection

Standards

The inspector also talked with other licensee

and contractor

personnel

during the course of the inspection.

"Attended the Exit Meeting on July 8, 1988.

Ins ection

Back round

The Essential

Chilled Water

(EC) system consists of two 100 percent

capacity chilled water trains.

Each train consists

of a single

100

percent capacity essential

chiller unit.

The

EC system supplies chilled

water to the Essential Air Cooling Units

(ACUs) for the Control Building,

Auxiliary Building, and Main Steam Support Structure.

At approximately

0955

MST on May 29, 1988,

a manual start attempt

was

made

on the Train "A" Essential Chiller to support surveillance testing

of the steam driven Auxiliary Feedwater

pump.

When the chiller did not

start,

an Auxiliary Operator

(AO) was sent to investigate

the chiller

breaker

and found "n'o indication of an electrical fault.

The

AO was directed

to the local annunciator

panel for further investigation

and found

a low

flow alarm indicated.

A second

attempt

was

made to start the chiller and

was again unsuccessful.

The Assistant Shift Supervisor

(A/SS) then went

to the Control Building to investigate

the valve lineup, in accordance

with

the alarm response

procedure.

The A/SS found that the root isolation valves

for the flow instrumentation

loop were closed.

The flow instrumentation

loop consists of a non-safety related flow indicator

gauge with isolation

valves;

and

a safety related flow transmitter,

which supplies

a signal to

satisfy

a compressor

"run" interlock.

The "as found" valve lineup was

contrary to the proper system lineup,

because

the safety related flow

transmitter

was isolated,

preventing the transmitter

from sensing

system

water flow and thereby satisfying the compressor

run interlock.

The

licensee 'immediately entered

Technical Specification Limiting Condition

for Operation

(LCO) 3.7.6

and concurrently

opened

the root isolation valves.

The chiller was successfully started

and the Train "A" EC system

was

declared

operable at 1020 MST.

The operability of Train "B" was then investigated

and Train "B" was

declared

inoperable at 1022

MST.

The root isolations for the Train "B"

instrumentation

loop were also found isolated

and subsequently

opened.

The Train "B" EC system

was declared

operable at 1040

MST after

successfully starting the "B" chiller.

A yellow plastic caution sign

was mounted

near both sets of root

isolation valves.

The sign read

"CAUTION valves to remain closed

except

when reading gauge."

The licensee initiated

a four hour notification to the

NRC Operation

Center

and initiated an internal report, Potentially Reportable

Occurrence

(PRO)

No. 1-88-065.

Subsequently

the licensee initiated

a Special

Plant Event Evaluation

and submitted Licensee

Event Report

(LER) 1-88-017 to the

NRC, which describes

the above event in detail.

Ins ection Findin s

The inspector

performed

a review to determine

the circumstances

which

led to this event.

Valve alignment procedures

410P-1EC01

and 410P-IEC02

were revised

on

May ll, 1988, to include

a note indicating the importance of assuring

that non-class

flow indicators are isolated

from the class flow transmitter

loop.

The valve alignments

were properly performed in all three units

when the revision was

implemented.

A Unit 3 Shift Supervisor,

in response

to the procedure revision,

had

a

set of yellow laminated plastic signs

made for all three units.

The

signs read,

"CAUTION valves to remain closed except

when reading gauge."

'he Shift Supervisor did not inform his management

or the management

of

the other units of his decision to make or install the signs.

When the

signs were made, Unit 3 installed the signs

near the flow

indicators'solation

valves

and delivered the remaining signs to Units

1 and 2.

On May 19,

1988,

both Essential

Chillers were operated satisfactorily.

On May 20,

1988, Unit I received

two signs

and

a note with the flow

indicator numbers

and

no additional instructions

as to their intended

use.

The Assistant Shift Supervisor

(A/SS) did not inform the Shift Supervisor

of the signs,

but directed

a Reactor Operator

(RO) to research

the

appropriate

Operating

Procedures

for more information.

The

RO found the

appropriate

procedure

pages

in 410P-1ECOl

and 410P-lEC02

and copied those

pages.

The

RO also looked

up the valves that were located nearest

the

flow instrument valves

on the system drawing and wrote those valve numbers

on the note containing the flow indicator numbers that accompanied

the signs.

The numbered valves were the flow instrumentation

loop root isolation valves,

which are the last valves

shown

and numbered

on system drawings.

The

licensee

does not label local instrumentation isolation valves.

The

RO

then called

a relief shift Auxiliary Operator

(AO) to hang the signs.

When the

AO arrived in the Control

Room he was given the signs,

the note

containing flow indicator and valve numbers,

and the appropriate

pages

from the valve alignment procedures.

The

RO told the

AO to hang the

signs

on the flow indicators.

A phone call then interrupted the

RO, and

when

he finished the phone conversation,

the

AO was

gone

and

had not

taken the copies of the valve alignment procedure

pages.

Since the

AO

was reading the information when the phone rang,

the

RO assumed

the

AO

understood

the instructions

and didn't need

the valve alignment procedure

pages.

The

AO proceeded

to the Control Building and located the

instruments

and valves

on the note

and installed the signs next to the

valves which he observed

to be root isolation valves.

When the

AO

installed the signs,

he also noted that the valves

were

open

and closed

them to correspond

to the directions

on the signs.

The

AO traced

the

valves to the flow indicators to ensure

that the valves did, in fact,

isolate the flow indicator.

He also observed that the valves isolated

a

flow transmitter.

The

AO returned to the Control

Room and informed the

A/SS that

he

had hung the 'signs,

shut the valves,

and asked if there

was

any paper work to fill out;

The A/SS assumed

that the

AO had installed

the signs correctly,

and that the valves the

AO closed were the local

instrumentation isolation valves

and not the instrumentation

root valves.

In an interview with the AO, he stated that at the time,

he

had

made

a

statement,

not specifically directed to the A/SS,

as to how stupid

he

thought it was to isolate all flow indication.

The A/SS was not aware

of the AO's comment

and did not respond.

The

AO stated to the inspector

that since

he did not get

a response

and it was not his normal crew,

he

did not feel free to pursue

the matter any further.

Thus, the valves

remained

closed

and the signs installed at the incor rect location until

the discovery

by the licensee

on May 29,

1988.

Licensee

Followu

The licensee

has described

the event in Licensee

Event Report

(LER)

88-017-00,

dated

June

28,

1988.

The

LER classified the event

as

a condition prohibited by Technical Specifications,

a condition which

could have resulted in the plant being in an unanalyzed

condition that

significantly compromised plant safety,

and

an event that could have

prevented

the fulfillment of the safety function of a system

needed

to

mitigate the consequences

of an accident.

The licensee

determined

the root cause to be

a cognitive personnel

error

on the part of the Auxiliary Operator

(AO) and Reactor Operator

(RO), in

that they did not take adequate

measures

to ensure that the signs were placed

properly.

First, inadequate

communication occurred

between

the two

operators

in that the direction given was not sufficient to ensure that

the tags were properly placed.

Second,

the

AO repositioned

the flow

transmitter

val,ves without proper valve position documentation

and

verification as required

by Operating

Department Guidelines.

Finally,

the

AO and Assistant Shift Supervisor did not ensure that appropriate

actions

were taken

upon closing of the valves

due to inadequate

communications.

The licensee

is conducting

an evaluation to determine

the effects of the

loss of essential

chillers.

Based

on this evaluation

the licensee will

provide

a supplement to LER 88-017 describing

the safety

consequences

and

implications of the event.

The licensee's

immediate corrective actions consisted of returning the

chillers to service

and placing the caution signs in the correct location.

The corresponding

valves at Units

2 and

3 were checked

and found to be

properly positioned.

As an interim corrective action, warning labels

will not be installed without the Plant Manager's

approval.

Management

directives

were issued requiring all Unit

1 operations

personnel

to

review administrative

requirements

governing valve manipulation,

and for

all Unit 1 personnel

to be more formal in communications

when discussing

plant status

and to adopt

a more conservative

approach

when plant conditions

or indications are off normal.

As long term corrective action

a policy regarding

the installation

and

control of warning tags will be developed

and implemented.

The

administrative controls for conduct of Shift Operations will be revised

to delineate

communications

standards.

Additionally, a

Human Performance

Evaluation

System

(HPES) review is being performed.

The specific

corrective actions which result from HPES will also

be included in the

supplement

to the

LER.

The licensee

conducted

a Special

Plant Event Evaluation to determine

why

the Essential

Chilled (EC) water flow instrumentation

loop root valves

were closed, contrary to the valve alignment procedures.

The results of

the evaluation

are documented

in Special

Plant Event Evaluation Report

(SPEER)

number 88-01-007.

This report was approved

by licensee

management

on June 30,

1988.

The

SPEER noted the following three concerns

as

a result of the

investigation.

1.

The

EC system

was rendered

inoperable

when the flow instrumentation

loop root valves were closed instead of the flow indicator isolation

valves.

The valves were closed during the installation of a laminated

information tag.

No guidance is provided for control of these

tags

within the plant.

2.

The communications

between

the individuals performing the installations

of the tags

was not adequate.

3.

The flow transmitter root valves were repositioned without proper

valve position verification notification per Operating

Department

Guidelines.

The resolution

and analysis of each

concern

were discussed

in the

SPEER,

as well as

the* recommended

corrective actions.

The corrective actions

for concern

1 are scheduled

to be complete within 90 days

from the

approval of the

SPEER.

And the corrective actions associated

with

concerns

2 and

3 are to be completed within 60 days.

Conclusions

Unit 1 was operating in Mode

1 for the entire period that the Essential

Chilled Water Trains "A" and "8" were rendered

inoperable.

This is

a

violation of Technical Specification 3.7.6, which requires

both trains

of Essential

Chilled Water to be operabld in Modes 1, 2, 3,

and

4

(50-528/88-24-01).

The

AO showed

a disregard for Administrative Controls

and Operations

Department Guidelines

concerning manipulation of safety

system valves

and

the tracking of those manipulations.

Ineffective communication

was noted

between

the Unit 3 Shift Supervisor

and Unit I, with regard to the purpose

for placement of the warning signs;

between

the Unit I

RO and

AO as to

the instructions to install the signs

and not manipulate valves;

and

between

the Unit

1

AO and the A/SS as to the safety

system valve

manipulations

that took place

and the documentation

required for their

manipulation.

Additionally, the inspector

was concerned with the relief

shift AO's apparent

reluctance

to clearly stress

to the A/SS his concern

that isolation of all flow indication was improper.

As mentioned in paragraph

4, the licensee's

investigation

appears

to have

encompassed

the inspector's

concerns

and conclusions,

with the exception

of the information which will be obtained

by further licensee

evaluations

and included in a supplement

to LER 88-017.

The inspector

met with licensee

management

representatives

periodically

during the inspection

and held an exit on July 8, 1988.

During the exit

meeting,

the inspector

discussed

recent operating

experiences

involving

personnel

error, emphasizing

the

need for greater attention to detail

and

.

management

attention.

A

I'