ML17291A967

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Insp Rept 50-397/95-20 on 950604-0715.Violations Noted. Major Areas Inspected:Cr Operations,Licensee Action on Previous Insp Findings,Operational Safety Verification & Surveillance Program
ML17291A967
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 08/09/1995
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17291A965 List:
References
50-397-95-20, NUDOCS 9508220165
Download: ML17291A967 (25)


See also: IR 05000397/1995020

Text

ENCLOSURE

2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I V

NRC Inspection

Report:

50-397/95-20

License:

NPF-21

Licensee:

Washington Public

Power Supply System

3000 George

Washington

Way

P.O.

Box 968,

MD 1023

Richland,

Washington

Faci)ity Name:

Washington Nuclear Project-2

(WNP-2)

Inspection At:

WNP-2 site near Richland,

Washington

Inspection

Conducted:

June

4 through July 15,

1995

Inspectors:

R.

C. Barr, Senior Resident

Inspector

D. L. Proulx,

Resident

Inspector

Approved

H. J.

Wong,

C

'

rope

rane

Ins ection

Summar

Areas

Ins ected:

Routine,

announced

inspection

by resident

inspectors of

control

room operations,

licensee

action

on previous

inspection findings,

operational

safety verification, surveillance

program,

maintenance

program

and

licensee

event reports.

Results

and Assessments:

~0erations

Operators

demonstrated

weaknesses

in properly performing

and overseeing

control

rod manipulations.

An operator incorrectly positioned

a control

rod during surveillance testing.

The control

rod second verifier accepted

a phone call during rod manipulation contrary to management's

expectations.

Operators

made three errors

in documenting control rod

manipulations.

There

have

been similar problems

in the past in this area

(Section 3).

The plant startup

coming out of the refueling outage

was generally

performed conservatively,

in

a deliberate

manner,

and in accordance

with

licensee

procedures

(Section 3).

9508220i65

950816

PDR

ADOCK 05000397

8

PDR

~

Operators failed to restore

two nonsafety-related

circuit breakers

to

their proper position after removing clearance

orders.

Problems

in the

processing of clearance

orders

have

been

a problem in the past

(Section 3).

~

Operators

made

two administrative errors in the Limiting Condition for

Operation

(LCO) log (Section 3).

Maintenance

A safety significant

human performance error occurred

when maintenance

craftsmen

removed

an incorrect lead during surveillance testing

and caused

a reduction in reactor water level

(Section 2.2).

~

Due to inadequate

procedures,

the control

rod drive

(CRD) housing support

was not installed per design

requirements

even

though the support

had

been

accepted

as installed properly (Section

2. 1).

~

Surveillances

were otherwise

performed properly and in accordance

with

procedures

(Section 6).

~

Maintenance

tasks

were performed

and documented

properly (Section 7).

~E

~

A design

change

associated

with containment

pressure

indication was

generally well designed

and

implemented

(Section

4. 1).

~

The requirements

of 10 CFR 50.59

and licensee

procedures

to perform

a

safety evaluation

were not fully implemented for two temporary

modifications (Section 4.2).

Plant

Su

ort

~

Plant housekeeping

and cleanliness

were very good, with the exception of a

fan which was inadequately

restrained

near the safety-related

automatic

depressurization

system

gas bottles

(Sections

3 and 5.3).

Summar

of Ins ection Findin s:

~

Violation 397/9520-01

(Section

2. 1.5)

was opened.

~

Violation 397/9520-02

(Section 2.2.3)

was opened.

~

Violation 397/9520-03

(Section 4.2.3)

was opened.

~

Licensee

Event Report 397/95-01,

Revision

0 (Section

9. 1) was closed.

~

Licensee

Event Report 397/95-02,

Revision

0 (Section

9. 1)

was closed.

~

Licensee

Event Report 397/95-04,

Revision

0 (Section

9. 1)

was closed.

Licensee

Event Report 397/95-05,

Revision

0 (Section

9. 1) was closed.

~

Licensee

Event Report 397/95-06,

Revisions

0 and

1 (Section

9. 1) were

closed.

~

Licensee

Event Report 397/95-07,

Revision

0 (Section

9. 1)

was closed.

~

Unresolved

Item 397/93-18-02

(Section 8.1)

was reviewed

and closed.

Attachments:

Attachment

1 - Persons

Contacted

and Exit Meeting

~

Attachment

2 - Acronyms

DETAILS

1

PLANT STATUS

At the beginning of the inspection period,

the plant was in Mode

4 (cold

shutdown) during Refueling Outage

R10.

At the conclusion of the outage,

the

plant entered

Mode

2 (startup)

on June

9,

1995.

On June

13,

1995,

the plant

entered

Mode

1.

The main generator

was temporarily synchronized

to the grid.

The reactor

was shut

down to Mode

3 (hot shutdown)

on June

15,

1995, directed

by the Bonneville Power Administration due to

an excess

generation

of

electricity.

The licensee

used this period to conduct maintenance

that could

only be performed during cold shutdown.

The reactor entered

Mode

2 on

June

30,

1995.

The plant entered

Hode

1

on July 3,

1995.

One hundred percent

power was achieved

on July 14,

1995.

2

ONSITE FOLLOWUP TO EVENTS

(93702)

2. 1

De raded

CRD Housin

Su

ort

Background

On June

6,

1995,

the inspector

performed

an

end of refueling

outage closeout

walkdown of the drywell.

To serve

as the licensee's

final

drywell walkdown, the operations

manager

and the drywell coordinator

accompanied

the inspector.

The inspector

noted that the drywell was very

clean except for a few small pieces of polyethylene

bags

and wiring

insulation.

While looking under the reactor vessel,

the drywell coordinator

identified that

a jam nut was missing from the

CRD housing support.

2. 1. 1

CRD Housing Support Function

The

FSAR and the

Bases for-the Technical Specifications

(TS) provide

a

description of and the safety analysis for the

CRD housing support.

FSAR Section 4.6.2.

1 states,

"The

CRD housing supports

prevent

any significant

nuclear transient

in the event

a drive housing breaks

or separates

from the

bottom of the reactor vessel."

Section 4.6. 1.2.2 states,

"The

CRD housing supports

meet the following safety

design

bases:

a) following a postulated

CRD housing failure, control rod

downward motion shall

be limited so that

any resulting nuclear transient

could

not

be sufficient to cause

fuel damage;

b) the clearance

between

the

CRD

housings

and the supports

shall

be sufficient to prevent vertical contact

stresses

caused

by thermal

expansion

during plant operation."

TS 3.1.3.8 requires

the

CRD housing

support to be in place in operational

Modes

1,

2,

and 3.

TS 4.1.3.8 states

"the

CRD housing support shall

be

verified to be in place

by

a visual

inspection prior to startup

any time it

has

been disassembled

or when maintenance

has

been

performed

in the

CRD

housing support area."

I

At normal operating

temperature,

a gap of approximately I/4 inch exists

between

the

CRD housing

and the supports.

At lower temperatures

the gap is

greater.

2. 1.2

Sequence

of Events

On June

1,

1995,

the shift manager

contacted

the duty maintenance

manager

and

requested

that

a maintenance

supervisor

sign off Step

29 of Plant Procedures

Manual

(PPM) 3. 1. 1, "Master Startup Checklist."

Step

29 oF

PPH 3. 1. 1 verified

that the

CRD housing support

was in place per

TS 4. 1.3.8.

The duty

maintenance

manager

contacted

an instrument

and controls

( I&C) supervisor

(who

was knowledgeable

of the housing support structure)

and requested

he initial

Step

29.

The

I&C supervisor

had previously observed

work undervessel

and

noted that the

CRD housing support

was in place.

He initialed off Step

29.

The

I&C supervisor

and the shift manager

had noted that Step

29 of PPM 3. 1. I

required

a mechanical

maintenance

supervisor's initials; however,

they

considered

the

ILC supervisor to be technically qualified for this

verification.

During the drywell inspection with the inspector

on June

6,

1995,

the drywell

coordinator noted that

a jam nut on the

CRD housing support

was missing.

Subsequent

licensee

reinspection

of the housing support structure identified

the gaps

between

the

CRD housings

and the supports

were not within design

tolerances.

On June 8,

1994,

at the

NRC's request,

the licensee participated

in a

teleconference

to discuss

the

sequence

of events

and the safety significance

oF this event.

The licensee

described

the information contained

in

Problem Evaluation

Request

(PER)

295-0718 concerning

the as-found condition of

the

CRD housing support.

The licensee

also presented

GE's conclusions

concerning

the operability of the system.

During this teleconference,

the

NRC questioned

the identification of the

deficiency during

a drywell tour rather

than during the performance of TS

surveillance.

The licensee

stated that they had not yet performed this

surveillance.

They indicated the discrepancies

would have

been

found during

the surveillance.

The

NRC representatives

requested

that the licensee verify

this information.

Later on June

8,

1995,

the licensee

discovered

that the surveillance

(PPH

3 . 1. 1, "Master Startup Checklist, " Step

29) that veriFied the correct

installation of the

CRD support

housing

had

been

signed off.

Furthermore,

the

licensee

found that

an

I&C supervisor initialed the step rather than

a

mechanical

maintenance

supervisor,

as required

by

PPM 3. 1. 1, "Master Startup

Checklist," Step

29.

The licensee

found that the signoff for the surveillance

had already occurred.

The licensee notified the

NRC of these findings.

On June

9,

1995,

the licensee

conducted

an Incident Review Board

(IRB) to

determine

the circumstances

of the event

and corrected

the material

discrepancies.

2. 1.3

Licensee

Evaluation

and Corrective Action

t

PER 295-0718 discussed

the operability of the housing support.

The

PER

explained that the licensee

contacted

General

Electric concerning

the proper

configuration of the

CRD housing supports.

GE stated that the

1 a

. 12 inch

specification

was the standard for most housing supports.

However,

the

smaller dimension

(7/8 inch)

was found to be more critical than the

maximum of

1 1/8 inch.

GE provided

an analysis that would allow a maximum gap of

1 1/2 inch.

Because all the gap discrepancies

were in the 7/8 -

1 1/2 inch

band,

the licensee

considered

the

CRD housing support operable.

The licensee

corrected

the material deficiencies

and verified the installation of the

CRD

housing support.

The

IRB and

PER 295-0730 discussed

the improper signature

made

by the

IKC

supervisor

in

PPM 3. 1. 1.

The

IRB recommended

that

a checklist

be developed

to

verify the design

requirements

of the

CRD housing support.

PPH 3. 1. 1 was

revised to allow for flexibility in designating

a qualified individual to sign

Step

29.

The licensee

conducted

a lessons-learned

session

with maintenance

personnel.

2. 1.4

Previous History

On June

21,

1994,

craftsmen

completed installing and verifying correct

configuration of the

CRD housing support during Refueling Outage

R9.

Following the reinstallation of the housing support,

the craftsmen

documented

that two jam nuts

had

been missing since Refueling Outage

R7.

Therefore,

the

CRD housing support

may have

been in a degraded

condition for two operating

cycles.

Following the craft verification of the

CRD housing support,

the

system engineer

performed

a walkdown of the

CRD housing support.

The system

engineer

not only noted that two jam nuts

had

been missing,

but that the

housing support

was improperly spaced.

The licensee initiated

PER 294-0698 to

document this occurrence.

The licensee initiated

a work order to correct

these deficiencies.

The corrective actions for PER 294-0698 included:

(1) performing

an

evaluation to determine if additional training was required

on

CRD housing

support installation (the evaluation

concluded additional training should

performed to be completed

by Refueling Outage

R11);

(2) providing training for

maintenance

supervision

on work order paokage

closeouts;

and

(3) counseling

the applicable craft supervision

on maintaining

a "questioning attitude."

These corrective actions

were completed

in December

1994.

2. 1.5

Inspector

Findings

The inspector

found that it had

been

the licensee's

practice

in previous

verifications of the installation of the

CRD housing support,

a checklist or

a

procedure

was not used to identify the specific criteria to be verified.

The

inspector

considered

that without

a detailed checklist or procedure,

the

critical parameters

of the

CRD housing support could not

be assured.

TS 6.S'il.d requires

a procedure for each surveillance listed in the

TS and the

procedure

be implemented.

In addition,

FSAR Section 4.6.3.2.

1 states,

"When

the support structure

is reinstalled, it is inspected for correct

assembly

with particular attention to maintaining the correct

gap between

the

CRD

flange lower contact surface

and the grid."

The licensee failed to have

a

procedure with appropriate criteria for inspection of the

CRD housing support

which reflected the commitments

in the

FSAR.

The failure to have

a procedure

appropriate

to the circumstances

with appropriate quantitative or qualitative

acceptance criteria for inspection of the

CRD housing support is

a violation

of 10 CFR Part 50, Appendix B, Criterion

V (Violation 397/9520-01).

2. 1.6

Safety Significance

Because

the as-found

gap in the

CRD housing support would not result in

excessive

stresses,

a failure of the housing support would not result in rod

ejection of greater

than

3 inches

and

one jam nut missing would not affect the

operability of the housing support, this event

had low safety significance.

2. 1.7

Conclusions

The licensee

had not established

appropriate

controls to assure

correct

configuration of the

CRD housing support resulting in

a violation of

Appendix B, Criterion V, of 10 CFR Part 50.

The licensee's

previous

corrective actions for improper installation of the

CRD housing support were

not adequate

to prevent the problems

encountered

during Refueling Outage

R10.

The licensee's

investigation

was not thorough

because it did not address

the

missed opportunities

to correct this problem

and did not identify that

personnel

who performed the verification of the

CRD housing installation did

not use procedures

appropriate

to the circumstance.

2.2

Reactor

Vessel

Level Transient

Due to Wron

Lead Lifted

2.2. 1

Unplanned

Level Transient

On July 12,

1995, during performance of surveillance

PPM 7.4.3.7.5. 18,

Revision 6, "Accident Monitoring Instrumentation

Reactor

Core Isolation

Cooling

(RCIC) Flow Indication Channel

Check," reactor

pressure

vessel

(RPV)

level decreased

from +36 inches to +23 inches

due to

IKC technicians lifting

of an incorrect lead.

The licensee initiated

PER 295-0845

and conducted

an

IRB.

2.2.2

Licensee

Investigation

and Corrective Actions

The licensee's

investigation

found that

PPM 7.4.3.7.5. 18,

Steps

7.3.2

and

7.3.3 required the technicians

to identify and lift leads for Terminal

Block E51A-SRU-1 in the rear of Cabinet

H13-P612.

(Cabinet

H13-P612 is

divided into two sections,

one for the

RCIC system

and

one for the feedwater

level control system.)

The two technicians

assigned

to perform the

surveillance

worked in the feedwater level control

system section of

Cabinet

H13-P612

instead of the

RCIC system section.

The technicians

located

Terminal Block C34A-SRU-1 instead of E51A-SRU-1

and lifted the wrong leads.

The two technicians

indicated that they believed the

"SRU-1" portion of the

label

was the

key indicator

and

removed the leads;

however,

the procedure

was

particularly clear in requiring the field wires associated

with E51A-SRU-1

be

lifted.

The leads that the technicians lifted provided

one of the four inputs into the

total

steam flow portion of the feedwater control system.

With one of the

inputs

removed,

the circuit sensed

a decrease

in steam flow.

This created

a

feed

and

steam flow mismatch.

The feedwater control

system sent

a signal for the feed

pumps to decrease

flow.

This decrease

in feed flow caused

RPV water level to decrease.

When

operators

received

the

RPV low level annunciator

at +30.5 inches,

they

directed the technicians

to restore

any leads that

had

been lifted.

When the

technicians

restored

the leads,

the level transient

stopped..

The surveillance

was stopped until after the event investigation

was completed.

The licensee's

corrective actions for this event included:

counseling

the

personnel

involved, providing self-checking training for the individuals,

and

using operations

personnel

for second verification of selected

surveillances.

In addition,

although the operators

responded

well to the event,

the licensee

provided additional training on feedwater control

system failures (e.g.,

taking the system to manual

or single element control).

2.2.3

Conclusions

The failure of the technicians

to implement

PPH 7.4.3.7.5.18,

Steps

7.3.2

and

7.3.3 that required the identification and lifting of leads for Terminal

Block E51A-SRU-1

was

a violation of TS 6.8. l.d (Violation 397/9520-02).

This

violation had safety significance

in that the event resulted

in

a level

transient that

had the potential to result in a reactor

scram

on low reactor

water level.

The licensee's

corrective actions

were adequate.

This event

represented

an additional

human performance error that resulted

from the

failure of individuals to self-check

and inadequate field supervision.

3

PLANT OPERATIONS

(71707,

92901)

3. 1

Plant Tours

The inspectors

toured the following plant areas:

Reactor Building

Primary Containment

Control

Room

Diesel

Generator

Building

Radwaste

Building

Service Water Buildings

Technical

Support Center

~

Turbine Generator

Building

~

Yard Area and Perimeter

3.2

Ins ector Observations

3.2.

1

Control

Rod Manipulations

The inspectors

observed

portions of the plant startup

coming out of Refueling

Outage

R10.

The inspectors

noted that operators

generally performed in

a

conservative

and deliberate

manner.

The following instances

indicate that operator manipulation of control rods

requires

improvement.

3.2. 1. 1

Background

Licensee

PPM 1.3. 1,

"Department Policies

and Practices,"

Section 4.6.2.f,

states

"the second

person at H13-P603 must.

.

.

have

no other concurrent

duties while control rod manipulations

are in progress."

" Licensee

management

stated that the intent of this step

was to ensure that personnel

would not

be

distracted

during rod movement.

3.2. 1.2

Operator Distractions

On July 4,

1995, operators

were moving control rods to increase

reactor

power.

A control

room operator

(CRO) m'anipulated

the control

rods while the shift

technical

advisor

(STA) verified the correct

movements.

The inspector

observed

that while

a control rod was being

moved the lead

CRO received

a

phone call

and

passed

the telephone

to the

STA.

When rod movement

was ceased

for that control rod, the

CRO stopped control rod movement until the

STA

completed his phone call.

The inspector contacted

the shift manager

and explained his observation.

The

shift manager

discussed

this event with the

STA and informed the inspector

that this instance

was not safety significant because

no rod movement errors

were

made

and the

CRO only had two notches left until the rod was full out

when the

STA accepted

the phone call.

The operations

manager

indicated to the

inspector that the

STA did not meet his expectations.

3.2. 1.3

Administrative Errors Associated with Control

Rod Manipulations

The inspector

reviewed the rod manipulation

sheets

to determine if the

sequence

of control rod movements

was correct

and the movements

were properly

documented.

The inspector

found three

instances

in which operators correctly

manipulated

control rods,

but failed to sign the rod pull sheets.

The

inspector notified the shift manager,

who directed

the

CROs involved to sign

for the rod movements.

-10-

3.2. 1.4

Rod Control Error During Surveillance

On July 13,

1995,

the licensee initiated

PER 295-0846 to document

an error

during control

rod manipulation.

During performance of PPH 7.4. 1.3. 1.2,

"Control

Rod Exercising," the

CRO inserted

a control

rod an extra notch.

PPH 7.4.1.3. 1.2 requires

operators

to insert control

rods

one notch from

position

48 to 46 and then return to 48 (control rod exercising).

On July 13,

1995, while moving Control Rod 06-23 from position

48 to'46,

the operators

received

an annunciator

on the stator water cooling system.

The second

verifier left the rod console to address

the alarm, while CROI waited at the

panel.

After completing the annunciator

alarm response

actions,

the second

verifier returned to complete the control rod exercises.

Operators

mistakenly

inserted

Control Rod 06-23 again,

such that the control rod was then located

at position 44.

The operators

informed the control

room supervisor

and

initiated

a

PER.

The licensee

determined that the root cause of this error was the failure to

self-check.

A contributing cause of the error was that operators

were

distracted

by the alarm.

As corrective action,

the operations

manager

counselled

the involved personnel.

3.2. 1.5

Safety Significance

The inspectors

determined that this event

was not technically safety-

significant.

The control rod was mispositioned

one notch,

which did not

impact reactor

power,

thermal limits, or the preconditioning envelope.

3.2. 1.6

Inspector Conclusions

NRC Inspection

Reports

50-397/93-24,

94-27,

94-32,

and 94-33 all discuss

concerns with control rod operations'hile

these

discrepancies

had minor

safety significance,

they represent

a continuing lack of sensitivity for the

importance of deliberate

and thoughtful manipulation of control rods.

3.2.2

Operating

Logs

and Records

The inspectors

reviewed operating

logs

and records

against

TS and

administrative control procedure

requirements.

3.2.2.

1

LCO and Inoperable

Log

On June

13,

1995,

the inspector

reviewed the

LCO log and identified two

administrative errors.

The entry for the inoperability of Sample

Point

8 (SP-8),

an inline conductivity monitor, discussed

actions to be taken

if chemistry

was out of specification,

rather than actions to be taken if both

sample points were inoperable.

The entry for the inoperability of Temperature

Element

SW-TE-2B discussed

actions to be taken for Hodes

4 and 5, yet the

-11-

plant was in Mode 1.

These errors

had the potential

to mislead other

operators.

The inspector notified the shift manager

and the entries

were

corrected.

3,2.3

Monitoring Instrumentation

The inspectors

observed

process

instruments for correlation

between

channels

and for conformance with TS requirements,

and

no discrepancies

were

identified.

3.2.4

Shift Manning

The inspectors

observed

control

room and shift manning for conformance with

10 CFR 50.54(k),

TS,

and administrative

procedures.

The inspectors

also

observed

the attentiveness

of the operators

in the execution of their duties.

The inspectors

concluded that shift manning

was in conformance with the

applicable

requirements

and operators

were generally attentive to duties.

The

control

room was observed

to be free of distractions

such

as nonwork-related

radios

and reading materials.

3.2.5

Equipment

Lineups

The inspectors verified that valves

and electrical

breakers

were in the

position or condition required

by TS and administrative

procedures

for the

applicable plant mode.

This verification included routine control

board

indication reviews

and conduct of partial

system lineups.

Appropriate entry

into TS

LCO was verified by direct observation.

The inspectors

performed verification that selected

breakers

were in the

proper position following the licensee's

completion of the breaker lineups per

PPM 2.7. 1B,

"480 Volt and Below AC Electrical

Power Distribution System,"

prior to plant startup.

3.2.5.1

Inspectors

Observations

On June

5,

1995, the inspectors

found Breaker

PP7BC-13

in the

"ON" position

rather than

"OFF" as required

by

PPM 2.7. 1B.

Breaker

PP-7BC-13

was

a spare

breaker.

The licensee initiated

PER 295-0708 to document this issue.

The

inspector

noted that Breaker

PP7BC-13

had

been repositioned

to support

a

clearance

order following completion of PPM 2.7. 1B, but had not been restored

to its proper position following removal of the clearance

order.

The licensee

repositioned

the breaker

and verified its position'.

On June

7,

1995,

the inspector

found Breaker

PP-7AE-38 in the

"ON" position

rather than the

"OFF" position,

as required

by

PPM 2.7. 1.B.

This breaker

interrupted

power to

a system

no longer in use.

The licensee initiated

PER 295-0722 to document this issue.

The inspector

noted that Breaker

PP-7AE-

38 had

been repositioned

to support

a clearance

order, following completion of

-12-

PPH 2.7. IB, but had not been restored

to its proper position following removal

of the clearance

order.

The licensee

repositioned

the breaker

and verified

its position.

The inspector considered

the licensee's

corrective actions for these

two

findings adequate

and noted that these

problems

were not safety

significant'he

failures to properly position these

breakers

constitute

a violation of

minor significance

and are being treated

as

a noncited violation, consistent

with Section

IV of the

NRC Enforcement Policy.

These

problems

represent

additional

human performance

errors associated

with

the clearance

order process.

3.2.6

Equipment

Tagging

The inspectors

observed

selected

equipment,

for which tagging requests

had

been initiated, to verify that tags

were in place

and the equipment

was in the

condition specified.

The inspectors

noted the following issues

with respect

to clearance

tagging.

3.2.7

General

Plant

Equipment Conditions

The inspectors

observed

plant equipment for indications of system leakage,

improper lubrication, or other conditions that would 'prevent the system

from

fulfillingits functional requirements.

Annunciators

were observed

to

ascertain their status

and operability.

3.2.7.

1

Improperly Restrained

Equipment

During

a tour of the

441 foot elevation in the reactor building, the inspector

noted that

a piece of equipment did not appear to be properly secured.

A

reactor building ventilation fan (approximately

4 foot diameter)

was tied down

onto

a maintenance

cart that

was only 2 feet wide.

While the configuration

met licensee

procedure

requirements, it appeared

to be seismically unstable

and

was very close to the automatic depressurization

system

gas bottles.

The

inspector notified the shift manager,

who had the fan

and cart moved.

3.3

En ineered

Safet

Features

Walkdown

The inspectors

walked

down selected

engineered

safety features

(and systems

important to safety) to confirm that the systems

were aligned in accordance

with plant procedures.

During the walkdown of the systems,

items

such

as

hangers,

supports,

electrical

power supplies,

cabinets,

and cables

were

inspected

to determine that they were operable

and in

a condition to perform

their required functions.

Proper lubrication and cooling of major components

were also observed for adequacy.

The inspectors

also verified that certain

system valves were in the required position

by both local

and remote position

indication,

as applicable'

-13-

The inspectors

walked

down selected

portions of the following systems:

Diesel

Generator,

Divisions

1,

2,

and

3

Low Pressure

Coolant Injection, Trains A, B,

and

C

Low Pressure

Core Spray

(LPCS)

High Pressure

Core Spray

Residual

Heat

Removal Trains

A and

B

Standby

Gas Treatment

(SGT)

Standby Liquid Control

125-Vdc Electrical Distribution, Divisions

1 and

2

250-Vdc Electrical Distribution

The inspectors

noted that the engineered

safety features

systems

were

generally in good material condition

and were aligned in accordance

with

applicable licensee

procedures

for the portions walked down.

4

ONSITE ENGINEERING

(37551,

92903)

The inspectors

performed

inspections

of the following onsite engineering

related activities during this inspection period:

4. 1

Desi

n Chan

e Packa

e Review

The inspector

reviewed Plant Modification Record

(PMR) 91-0338-OA which

installed tubing

and gauges

to indicate drywell and wetwell pressures

locally.

This

PMR installed

Gauges

CMS-PI-9 and CMS-PI-10.

The inspector

reviewed the

PHR package,

the applicable

procedures,

the safety evaluation,

the top tier

drawings,

and the implementing work orders to determine if the modifications

were performed in accordance

with licensee

procedures.

The inspector

performed

a walkdown of the

new equipment to ensure that the applicable

requirements

were met.

The inspector

determined that the design

and

implementation of PHR 91-0338 were performed in a thorough

and conservative

manner.

4.2

Review of Tem orar

Modification Re uest

THR

Lo

The inspector

reviewed selected

entries

in the licensee's

THR log to determine

if temporary modifications

and lifted leads

and jumpers

were installed in

accordance

with NRC and license requirements,

The inspector

noted the

following concern with the

TMR log.

4.2.1

Removal of Valve Position Indication

The inspector

reviewed

TMR 95-030,

which removed position indication from the

disc of Valve RCIC-V-66,

a testable

check valve

and

a containment isolation

valve.

The licensee

implemented

the

THR because

the position indication

lights for RCIC-V-66 provided the operators

with false indication that the

valve was closed

when it was actually open.

No

10 CFR 50.59 evaluation

had

been

performed to support

the removal of the position indication.

The

-14-

inspector

reviewed the

TMR sheets,

the licensee's

evaluation,

the applicable

procedures

and drawings,

and

PER 295-0641.

4.2.2

Requirements

10 CFR 50.59(b)(1) states,

"The licensee

shall maintain records of changes

in

the facility.

.

.

made pursuant

to this section,

to the extent that these

changes

constitute

a change to the facility and described

in the safety

analysis report.

These

changes

must include

a written safety evaluation

which

provides

a basis for determination that the change,

test,

or experiment

does

not involve an unreviewed safety question."

PPH 1.3.43,

Revision 6, Section

5. 1. I.b states

a

10 CFR 50.59 review and, if

required,

a safety evaluation will be required only for temporary

modifications not covered

by

a previously evaluated

and approved

document

such

as

a plant procedure

or

a

PHR.

Additionally, Attachment

7.3 states

a change

to the design of the plant

as described

in the licensing basis

document will

require safety evaluation.

4.2.3

Licensee

Assessment

of the Requirement for a Safety Evaluation

The licensee's

screening

evaluation of the issue

concluded that

a

10 CFR 50.59

evaluation for this

TMR was not required for the following two reasons:

(1) there were

no licensing basis

documents

that required the position

indication to be in place,

and

(2)

10 CFR 50.59 evaluations

are not required

for the interim disposition of problems if the timeliness for corrective

action completion is such that it can

be demonstrated

for a particular case

that the degraded

or nonconforming condition has not or will not become

a

defacto

change.

4.2.4

NRC Inspection

The inspector

reviewed the

FSAR and found that Section 5.4.6.2.4 described

Valve RCIC-V-66 stating,

"valve test provisions

are provided including limit

switches to indicate disc movement."

Based

on the inspector's

finding, the

licensee initiated

PER 295-0826 to document this problem.

The licensee

determined that

an inadequate

search of the licensing basis

documents

had

been

performed.

The system engineer

had performed

a key word search

on

an

electronic version of the

FSAR and

had not used the appropriate

key word.

As

corrective actions,

the licensee

performed

a

10 CFR 50.59 safety evaluation

and concluded

no unreviewed safety questions

were identified.

On July 13,

1995,

the licensee initiated

PER 295-0864 which indicated that

TMR 95-050

had

also

been

implemented without the required

10 CFR 50.59 safety evaluation.

The inspector

reviewed

PPH 1.3. 12A.

Attachment 8.2 of this procedure

states

a

10 CFR 50.59 evaluation is not required for an interim disposition of a

problem if the timeliness for corrective action completion is such that it can

be demonstrated- for a particular case that the degraded

or nonconforming

condition has not or will not become

a defacto

change.

While it appears

that

the change

was not intended to be permanent,

based

on the location of

-15-

Valve RCIC-V-66 (inside containment),

the

TMR would likely be in place for

approximately

I year

and, therefore,

this change

was essentially

a long-term

change.

4.2.5

Conclusions

The failure to perform

a written safety evaluation for the implementation of

THR 95-030 is

a violation of 10 CFR 50.59 {Violation 397/9520-03).

While the

violation itself had little safety significance,

the

NRC is concerned

that the

inadequate

electronic

search

performed for the safety evaluation creates

the

potential for a more significant error to occurr.

In addition,

the licensee

identified another

case

in which

a safety evaluation

had not been

performed.

5

PLANT SUPPORT ACTIVITIES

(71750)

The inspectors

evaluated

plant support activities based

on observation of work

activities,

review of records,

and facility tours.

The inspectors

noted the

following during this evaluation.

5. 1

Fire Protection

The inspectors

observed fire fighting equipment

and controls for conformance

with administrative

procedures.

The inspectors

noted that

a high number of

fire impairments existed for which fire tours were being conducted

because

of

concerns with Thermo-Lag

and fire seals,

and the number of propped

open fire

doors to support work.

5.2

Radiation Protection Controls

The inspectors

periodically observed

radiological protection practices

to

determine whether the licensee's

program

was being

implemented

in conformance

with facility policies

and procedures

and in compliance with regulatory

requirements.

The inspectors

also observed

compliance with radiation work

permits,

proper wearing of protective

equipment

and personnel

monitoring

devices,

and personnel

frisking practices.

Radiation monitoring equipment

was

frequently monitored to verify operability and adherence

to calibration

frequency.

5.3

Plant

Housekee

in

The inspectors

observed

plant conditions

and material

and equipment

storage

to

determine

the general

state of cleanliness

and housekeeping.

Housekeeping

in

the radiologically controlled area

was evaluated

with respect

to controlling

the spread of surface

and airborne contamination.

Housekeeping

was observed

to be generally

good during the inspection period.

S.4

~Securit

The inspectors periodically observed

security practices

to ascertain

that the

licensee's

implementation of the security plan was in accordance

with site

procedures,

that the search

equipment at the access

control points

was

operational,

that the vital area portals

were kept locked

and alarmed,

that

personnel

allowed access

to the protected

area

were

badged

and monitored,

and

that the monitoring equipment

was functional.

No problems

were noted during

these observations.

5.5

Emer enc

Plannin

The inspectors

toured the

Emergency Operations Facility, the Operations

Support Center,

and the Technical

Support Center

and ensured

that these

emergency facilities were in

a state of readiness.

Housekeeping

was noted to

be very good

and all necessary

equipment

appeared

to be functional.

5.6

Plant Chemistr

The inspectors

reviewed chemical

analyses

and trend results for conformance

with TS and administrative control procedures.

Plant chemistry

was

satisfactory during this inspection period.

5.7

Conclusions

Plant support

performance

was generally

good during this inspection period.

6

SURVEILLANCE TESTING

{61726)

The inspectors

reviewed

TS surveillance tests

on

a sampling basis to verify

that:

~

a technically adequate

procedure

existed for performance of the

surveillance tests;

~

the surveillance tests

had

been

performed at the frequency specified in

the

TS and in accordance

with the

TS surveillance

requirements;

and

~

test results satisfied

acceptance

criteria or were properly dispositioned.

The inspectors

witnessed

portions of the following surveillance tests:

Procedure

Descri tion

7.4.4.3.2.6

7.4.1.4.1.3

HPCS/Reactor

Coolant

System

Interface

Valve and Keepfill

System

Checks

Rod Worth Minimizer Control

Rod Sequence

Verification

-17-

7. 4. 1. 3. 2

7.0.0

Control

Rod Scram

Time Testing

Shift and Daily Instrument

Checks

Overall, surveillance testing

was performed

and documented

properly.

7

MAINTENANCE OBSERVATIONS

(62703)

During this period,

the inspectors

observed

and reviewed documentation

associated

with maintenance

and problem investigation activities to verify

compliance with regulatory requirements

and with administrative

and

maintenance

procedures,

required quality assurance/quality

control

involvement,

proper

use of clearance

tags,

proper equipment

alignment

and

use

of jumpers,

personnel

qualifications,

and proper retesting.

7. 1

Control

Rod Multi lexer Card

Re lacement

On July 4,

1995,

the inspector

observed

Work Order Task VN59-01,

"Replace

Multiplexer Card for Control Rod 18-11."

This work required deenergization

of

the entire rod position indication system.

The deactivation of the rod

position indication system required

the plant to enter

a 1-hour

LCO action

statement.

The inspector

observed

that the licensee

performed

thorough

planning

and

a good preevolution briefing.

The inspector

noted that during the work the craftsmen

did not use

a grounding

strap.

The inspector

had observed

replacement

of these

cards previously

and

on those

occasions

craftsmen

used

a grounding strap.

When the inspector

notified the craftsmen of this concern,

the craftsmen

stated that the

grounding strap

was not required

by procedure.

The craftsmen

completed

the

work and restored

the system satisfactorily.

The operators

successfully

completed

.the surveillance for Control Rod 18-11,

and the control

rod was

declared

operable.

The inspector

considered

the failure to use

a grounding strap while working on

sensitive electronic

components

a poor work practice.

7.2

Other Maintenance

Observations

The inspectors

also observed

JIS-95-3596

"Replacement

of Relay RFW-CIS-CNB,"

"Troubleshoot

and Repair MSLC-FT-3D," and "Replace

Scram Solenoid Pilot Valve

for Control Rod 46-15."

The inspectors

determined that these

maintenance

tasks

were performed

and

documented

properly.

8

FOLLOWUP

(92901,

92902,

92903,

92904)

The inspectors

reviewed records,

interviewed personnel,

and inspected

plant

conditions relative to licensee

actions

in response

to previous

open

items.

-18-

8. 1

Closed

Unresolved

Item 397 93-18-02:

"Reactor Vessel

Drainin

without

Secondar

Containment or Standb

Gas Treatment

S stem

SGTS

"

To lower reactor

vessel

water level to the normal

range at the

end of a

refueling outage,

operators

drain the reactor vessel.

This drain path

was

through the residual

heat

removal

system which tapped off the

RPV below the

top of the active fuel.

The licensee

did not establish

secondary

containment

and the

SGTS

was inoperable

at the time.

The

WNP-2

TS require that the

licensee

secure

"operations with a potential for draining the reactor

vessel

(OPDRV)" when secondary

containment

and

SGTS are inoperable.

The

inspector

was concerned

that the licensee

was not meeting

the TS.

The

licensee

stated that lowering of RPV level through the normal drain paths

was

not

an

OPDRV as long

as the system isolations

and emergency

core cooling

system actuation trips were operable.

The inspector

performed followup of the licensee's

definition of an

OPDRV and

found it to be consistent

with the industry definition and satisfactory for

safe operation.

9

LICENSEE EVENT REPORT

REVIEWS

(90712,

92700)

9. 1

In-Office Review

The inspectors

reviewed the following Licensee

Event Reports

(LERs)

based

on

in-office review.

The inspectors

considered

that the licensee

identified the

root causes

and corrective action to prevent recurrence.

LER Number

Title

95-01,

Revision

0

95-02,

Revision

0

95-04,

Revision

0

Inability to Satisfy Single failure

Criteria for Containment Isolation

Function

Due to Missing Electrical

Separation

Plate in Control

Panel

Reactor

Scram

Due to Personnel

Error

Reactor

Scram

Due to Hain Turbine Control

System Malfunction

95-05,

Revision

0

95-06,

Revisions

0 and

1

95-07,

Revision

0

TS Action Statement for Intermediate

Range

Monitoring Instrumentation

Not Met

Reactor

Scram During Surveillance Testing

Due to Protective

System

Relay Failure

Emergency

Diesel Start

Due to Voltage

Transient

on

BPA Grid

ATTACHMENT 1

1

PERSONS

CONTACTED

Washin ton Public Power

Su

1

S stem

V. Parrish,

Vice President

Nuclear Operations

  • J. Burn, Engineering Director
  • G. Smith, equality Assurance

Director

  • P. Bemis, Regulatory

and Industry Affairs Director

  • R. Webring, Support Services Director
  • J. Swailes,

Plant General

Hanager

  • G. Gelhaus,

WNP-2 Projects

Manager

  • C. Schwarz,

Operations

Manager

  • T. Love, Chemistry Manager
  • J. McDonald, Technical

Services

Manager

  • J. Albers, Radiation Protection

Manager

  • R. Barbee,

System Engineering

Manager

  • H. Manopoli, Maintenance

Manager

  • G. Gelhaus,

Projects

Manager

  • D. Atkinson, Reactor

and Fuels

Engineering

Manager

  • D. Swank,

Licensing Manager

  • W. Sawyer,

Operations

Services

Manager

  • J. Huth, Plant Assessments

Manager

  • D. Coleman,

Regulatory Services

Manager

  • P. Inserra,

equality Assurance

Manager

G. Sanford,

Planning,

Scheduling,

Outage

Manager

  • B. Hugo,

Compliance

Engineer

  • H. Brant, Operations

Contractor

U.S. Nuclear

Re ulator

Commission

  • H. Wong, Chief, Project

Branch

E

  • R. Barr, Senior Resident

Inspector

  • D. Proulx, Resident

Inspector

The inspectors

also interviewed various

CROs, shift supervisors,

shift

managers,

and maintenance,

engineering,

quality assurance,

and management

personnel.

  • Attended the exit meeting

on August 4,

1995.

2

EXIT MEETING

An exit meeting

was conducted

on August 4,

1995.

During this meeting,

the

inspectors

reviewed the scope

and findings of the report.

The licensee

acknowledged

the inspectors'indings.

The licensee

did not identify that

any

proprietary information was provided to or reviewed

by the inspectors.

ATTACHMENT 2

ACRONYMS

CRD

CRO

FSAR

IKC

IRB

LCO

LER

NRC

OPORV

PER

PMR

POC

ppM

RCIC

RPV

STA

SGTS

TMR

TS

WNP-2

control

rod drive

control

room operator

Final Safety Analysis Report

instrument

and controls

Incident Review Board

limiting condition for operation

licensee

event report

U.S. Nuclear Regulatory

Commission

operations with a potential for draining the reactor

vessel

problem evaluation request

plant modification record

Plant Operating

Committee

plant procedures

manual

reactor core isolation cooling

reactor pressure

vessel

shift technical

advisor

standby

gas treatment

system

temporary modification request

Technical Specifications

Washington

Nuclear Project

2