ML17291A132
| ML17291A132 | |
| Person / Time | |
|---|---|
| Site: | Columbia |
| Issue date: | 06/06/1994 |
| From: | Kirsch D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML17291A131 | List: |
| References | |
| 50-397-94-15, NUDOCS 9406150024 | |
| Download: ML17291A132 (25) | |
See also: IR 05000397/1994015
Text
APPENDIX
U.S.
NUCLEAR REGULATORY COMMISSION
REGION IV
Inspection Report:
50-397/94-15
Operating
License:
Licensee:
Washington Public Power Supply System
P. 0.
Box 968
Richland,
WA 99352
Facility Name:
Washington Nuclear Project
2
(WNP-2)
Inspection At:
WNP-2 site near Richland,
Inspection
Conducted:
Harch
28 through
Hay 7,
1994
Inspectors:
R.
C. Barr, Senior Resident
Inspector
D. L. Proulx, Resident
Inspector
Approved:
irsc,
re,
eactor
roJect
rane
c,suua&4
6
Ins ection
Summar
~AI
4:
Ep ii,
d,
- id
i
p ti
ftt
discovery that degraded
Buna-N components,
in scram solenoid pilot
valves
(SSPVs)
caused
Control Rod 06-39 not to insert
and four other control
rods to exhibit slow movement,
but within Technical Specification
(TS) limits,
on start of motion
(SOH) during surveillance testing.
During the inspection,
Inspection
Procedures
92901,
92903,
92904,
and
93702 were used.
Results:
General
Conclusions
and
S ecific Findin s:
On December
4,
1993,
the supply system failed to take prompt corrective action
upon finding significantly increased
time for SOH for Control Rod 14-55.
This
failure resulted in the time for SOH of this control rod to be in excess of TS
limits on January
7,
1994, at which time the licensee
inserted the rod in
compliance with the TS.
On February
7 and 17,
1994, the supply system failed
to take prompt corrective action
upon finding significantly degraded
in the
and 14-55, respectively.
These
failures resulted in reactor
operation for 7 weeks with a significantly
degraded
control rod system
and the failure of Control Rod 06-39 to insert
during surveillance testing conducted
on March 26,
1994.
9406150024
940606
ADOCK 05000397
8
'
4
~
~
The supply system failed to adhere to procedures
requiring the performance of
prompt operability assessments
(POAs)
when finding physical
evidence of
degraded
equipment.
On December
4,
1993, the licensee
found the time for SON
of Control Rod 14-55 to have degraded
by approximately
a factor of three
and
did not perform
a
POA.
On February
7 and
17,
1994, the supply system
found
significantly degraded
in the
and
14-55, respectively,
and failed to perform POAs.
The supply system failed to adequately
trend rod control system performance
and failed to implement
an effective preventive maintenance
program in
response
to industry information associated
with Buna-N components
in the
Weaknesses:
This inspection identified additional
examples of the following problems that
the
NRC has previously identified at the supply system:
failure to take
prompt corrective actions
when finding degraded
safety-reTated
components,
inadequate
evaluation
and corrective action for problems identified by
industry communications,
inadequate
management
oversight,
poor communications
between organizations,
and the failure to adhere to procedures.
Summar
of Ins ection Findin s:
~
Apparent Violation 397/9415-01
was opened
(Section 6).
~
Apparent Violation 397/9415-02
was
opened
(Section 6).
Attachment:
~
Persons
Contacted
and Exit Meeting
~
T
DETAILS
1
PLANT STATUS
At the start of this inspection period, the plant was operating at
approximately
68 percent
power with five control rods fully inserted.
54-15,
30-31,
and 10-15 were fully inserted
because
operators
had
declared
these
rods inoperable
when the control rods exhibited slow
SOM during
surveillance testing performed
on March 26,
1994.
Control Rod 30-03 was fully
inserted
on March 26,
1994, since it could not,be
scram time tested
due to a
failed transponder
card that was located in the"testing circuitry.
Licensee
craftsmen
were replacing the Buna-N components
(diaphragms), of the
SSPVs for
the four control rods that had exhibited slow SOM.
Because
had failed to insert
on March 26,
1994, licensee
engineers
were testing the
diaphragms that
had
been
removed
from Control Rod 06-39.
At the conclusion of
the period,
the reactor
was shut
down in Mode
5 (Refueling)
and the Buna-N
diaphragms of all the
had
been replaced.
2
CONTROL ROD SYSTEM DESCRIPTION AND DESIGN BASES
The control rod system is one of the reactivity control
systems for the
WNP-2
boiling water reactor
(BWR).
The reactor control rods are positioned
by
hydraulics.
The control rods
can
be positioned in small increments
or rapidly
inserted into the core
(scrammed).
Rapid control rod insertion is achieved
by
the following means:
(1) automatically,
the reactor protection
system
deenergizes
the
SSPVs of each of the
185 control rods which redirects
the
pneumatics of each individual control rod;
(2) automatically,
the reactor
protection
system energizes
the backup
SSPVs which redirects
the pneumatics of
all control rods;
and (3) automatically,
when reactor level reaches
-50 inches
or reactor pressure
reaches
1076 psig, the anticipated transient without
scram automatic
rod insertion
scram system which redirects the pneumatics of
all control rods.
Each of the individual control rod SSPVs,
which the
licensee
procured
as guality Class
1 components,
has four normally energized
Automatic Switch Company
(ASCO) solenoid operated
valves that have internal
components
made of Buna-N rubber.
The system also contains
two normally
deenergized
backup
SSPVs consisting of two ASCO solenoid valves,
which were
procured
as guality Class
2 components.
The internal
components
of the backup
scram valves are
made of Buna-N rubber.
The anticipated transient without
scram-automatic
rod insertion
system
uses
valves that do not contain
Buna-N
components.
The design basis of the reactivity control
system is to provide sufficient
nuclear reactivity control devices
(control rods) to control excess reactivity
in the core
and to provide For adjustments
of the control rods to permit power
generation.
The safety functions of the reactivity control
system are to
provide sufficient excess
negative reactivity to keep the reactor shut
down
and to provide sufficient rapid insertion of control rods (reactivity) so that
no fuel
damage results
from any operating transient.
3
CONTROL ROD DRIVE (CRD)
SYSTEM TS AND BASES
The following TS are applicable to the control rods while in operational
conditions
one
and two:
TS 3. 1.3. 1
All control rods shall
be operable.
TS 3. 1.3.2
The maximum scram insertion time of each control rod from the
fully withdrawn position to notch Position 6,
based
on deenergization
of the
'SPVs
as time zero, shall not exceed
7 seconds.
TS 3. 1.3.4
The average
scram insertion time of all operable control rods
from the fully withdrawn position, for control rods arranged
in a two-by-two
array,
based
on the deenergization
of the
as time zero shall not exceed
any of the following:
I
Position Inserted
From Fully Withdrawn
Average
Scram Insertion
Time (Seconds)
45
39
25
5
0.430
0.868
1.936
3.497
The following sentences
describe
the bases for these
TS.
The requirements for
the various
scram time measurements
ensure that any indication of systematic
problems with rod drives will be investigated
on
a timely basis.
The
occurrence of scram times longer than those specified
should
be viewed
as
an
indication of a systemic
problem with the rod drives and, therefore,
the
surveillance interval is reduced
in order to prevent operation of the reactor
for long periods with a potential
serious
problem.
The number of control rods
permitted to be inoperable
could be more than eight allowed by the TS, =but the
occurrence of eight inoperable
rods could be indicative of a generic
problem
and the reactor must
be shutdown for resolution of the problem.
4
INDUSTRY EXPERIENCE
(92904)
4. 1
NRC Information Bulletin
IB
78-14
"Deterioration of Buna-N
Com onents
in ASCO Solenoids"
On December
19,
1978, the
NRC issued
IB 78-14 to notify licensee's
operating
BWRs about the thermal
aging of SSPV
Buna-N components.
This IB required that
licensees
with an operating license:
(1) review Buna-N material applications
in control rod scram systems,
determine the time since installation,.and
describe
a schedule for replacement,
both in response
to this IB and for
periodic maintenance;
(2) report the results of that review;
and (3) describe
the basis for the replacement
schedule
and describe
any proposed
replacement
time in excess of 3 years.
For all
BWR licensees
with construction permits,
which applied to WNP-2 in 1978, this IB was provided for information only.
The licensee initiated
a plant tracking log (PTL) item to track the
development
and implementation of a preventive maintenance
task to perform
periodic replacement
of Buna-N components
in SSPVs.
In an interoffice memorandum,
licensee
management
determined to replace
Buna-N
and 0-rings of SSPVs at
a rate of 25 percent
per year, starting in
April 1986.
In an inspection
conducted during March 1-5 and March 15-19,
1982,
the
NRC closed this IB based
on the licensee's
interoffice memorandum
plan to initiate
a 25 percent
replacement
program.
During this inspection,
the inspectors
found that the licensee
did not implement this plan.
This
deviation from a commitment is not being cited due to the
age of the issue,
the complete refurbishment of the
SSPVs in 1994,
and the supply system's
intent to replace
the
Buna-N components
with Viton components
in 1995.
The inspectors
found that the licensee
replaced
the Buna-N components
of
10 percent of the control rod
SSPVs in 1986.
Following this replacement,
the
licensee
changed
the preventive maintenance
scheduling
method.
As a result of
this change,
the planned
replacements
in 1987,
1988,
and
1989 did not occur.
In Hay of 1989,
when the
SSPVs of two control rods failed due to hardened
Buna-N components,
the licensee identified that they had not implemented the
specified replacement
program.
Therefore,
the licensee
decided to replace the
Buna-N components
of all the
SSPVs in Hay of 1990.
The licensee
did not
notify the
NRC that they had failed to implement the
25 percent
replacement
commitment.
The licensee
also failed to notify the
NRC that they did not plan
to implement
a 25 percent
replacement
following the
1990 refurbishment,
since
they had qualified the
Buna-N components
to a service life of 5.5 years
based
on their operating experience.
4.2
"Scram Solenoid Pilot Valve Rebuild Kit
Problems
On September
2,
1986, the
NRC issued this notice to alert licensees
to
potential
problems with kits used to refurbish
This notice described
quality control
problems
associated
with the
SSPV rebuild kits.
The licensee
took no action in response
to this notice.
The licensee
noted that,
in
May 1986,
38 SSPVs
had
been rebuilt and were properly functioning.
The system
engineer
noted that close attention would be given to the control rods with
the rebuilt SSPVs.
4.3
NRC Generic Letter
"0 eratin
Ex erience
Feedback
Re ort
Solenoid-0 crated
Valve Problems At U.S. Reactors"
This
GL dated
September
23,
1991, required
no specific action or written
response
by the licensee.
However, the
NRC expected that the licensee
would
review the information presented
in the
GL and consider actions
as appropriate
to avoid similar problems.
The
GL specifically mentioned control rod failures
in
BWRs due to hardening of Buna-N components.
On October
22,
1991,
the licensee
performed
an initial screening
and
determined that the
GL was applicable to WNP-2.
The licensee
completed
the screening
on September
2,
1993,
by assigning
actions to evaluate
the
\\I
-6-
recommendations
of NUREG 1275,
Volume 6, "Operating Experience
Feedback
Report,
Solenoid-Operated
Valve Problems."
The actions
were being tracked
by PTL 44726.
This
PTL item was
open at the time of the failure of Control Rod 06-39 to insert.
The
NRC inspectors
found that the lack of timeliness
of this review had
been previously discussed
in NRC Inspection
Report 50-397/94-08.
The failure to consistently
perform detailed timely
assessment
of industry experience
is
a continuing problem.
4.4
Service Information Letters
4.4.1
128
GE issued
SIL Number 128, Revision 0, "Preventive Maintenance for Control
Rod
Drive (CRD) Scram Pilot Valves,"
on March 31,
1975.
The SIL discussed
failures,
due to diaphragm cracking, of SSPV
Buna-N components.
The purpose
of the SIL was to recommend
a maintenance
program for scheduled
replacement
of
all
GE recommended
that licensees
establish
a program
so
that all
were replaced after 3-4 years of initial service.
The SIL noted that the initial operating service life was due to the longer
storage
time of the rubber parts prior to initial plant operation.
GE also
stated that the replacement
of these
components
could be performed while the
reactor
was operating at high powers.
Because
WNP-2 was in construction,
the
licensee
took no immediate action.
GE issued
Revision
1 to this SIL on January
30,
1976.
This revision notified
customers of the unacceptability of performing diaphragm replacements
at power
since the replacement
conflicted with GE fuel preconditioning
recommendations
for minimizing CRD movements
at high power levels.
Because
WNP-2 was in
construction,
the licensee
took no immediate action.
GE issued
Revision
1, Supplement
1, to this SIL in August 1978.
This
supplement .notified customers
of the delayed
CRD insertion of two control rods
at
an operating
BWR.
The purpose of the SIL was to discuss
the cause of the
occurrence
and to recommend
a preventive
program to help in preventing future
occurrences.
GE recommended
the following:
(1) establish
a preventive
maintenance
program to replace all core assemblies,
and associated
parts in all SSPVs,
backup
scram valves,
and scram discharge
volume vent and
drain pilot valves at periodic intervals,
and (2) rebuild the
periodically to assure
that the Buna-N parts
do not exceed
a combined shelf
life-service life of 7 years.
Because
WNP-2 was in construction,
the licensee
took no immediate action.
The licensee initiated operation evaluation report
(OER)
75003 to track the development
and implementation of a preventive
maintenance
program for the
GE issued
Revision
1, Supplement
2, to this SIL on March 2,
1984.
This
supplement notified customers
to discontinue
using "Loctite" on the acorn nut
on the solenoid housing.
In this supplement,
GE reemphasized
their
recommendation
that the Buna-N components for the
be replaced
periodically to assure
that the
age of these
components
would not exceed
7 years.
The licensee
incorporated this recommendation
in OER 75003.
On July 2,
1984, the licensee
closed out all actions associated
with this SIL
by revising their scheduled
maintenance
system to include
a preventive
maintenance
task that would begin replacement of Buna-N components,
in
25 percent of the
in April 1986.
4.4.2
575
'E issued
"CRD Slow Start of Motion (SOH)," on October 27,
1993.
This SIL described
the failures
and offered recommendations
for preventing
recurrence of CRD slow SOH.
The purpose of the SIL was to recommend
actions
which would reduce
the probability that slow scram
SOM times would occur.
stated that there
was
no safety concern
because
scram time surveillances
would
identify any slow
SOH drives.
GE provided the following recommendations:
(1) routinely check the scram air header
pressure
to be wi.thin 70 to
75 pounds;
(2) pay close attention to degradation
of the
SOH times and, if
unusual
SOM times are detected,
replace
the Buna-N components;
and (3) Buna-N
components
should
be limited to approximately
4 years of plant service
and,
before extending the service life of Buna-N components
beyond the recommended
3-4 years,
evaluate
the components
based
on plant specific operating service
conditions to determine whether they will perform acceptably.
On November
14,
1993,
the licensee initiated t)ER 75003G to consider the
recommendations
of this SIL.
On January
21,
1994, the licensee
closed the
after having implemented actions to address
GE's recommendations.
In their
response
to this
OER, the licensee
noted that their program was working
because
surveillance testing
had identified that Control Rod 14-55 had slow
SOH on December
4,
1993.
However, the licensee failed to note that the delay
in replacing the
SSPVs of Control Rod 14-55 did not conform to GE's
recommendation
to replace the Buna-N components if unusual
SOH times were
detected
and that this delay resulted
in operating in violation of TS 3. 1.3.4.
The licensee
implemented
the other recommendations
of this SIL.
4.5
Conclusions
During the period of 1986 through
1989, the licensee failed to implement the
commitment to perform an annual
replacement of the Buna-N components
in
25 percent of the control rod SSPVs.
Further,
the inspector concluded that
the Supply System
was not timely in evaluating
and did not
effectively implement all the recommendations
5
FAILURE TO INSERT
(92901)
5. 1
Licensee
Immediate
Res
onse to Control Rod 06-39 Failure to Insert
At 1:43 p.m.
(PST),
Saturday,
March 26,
1994, with the reactor at 75 percent
power, Control Rod 06-39 failed to insert when
WNP-2 operators initiated
a
scram signal during surveillance testing.
Licensed operators
concluded that
the control rod had malfunctioned
because
the positions of Control Rod 06-39
switches
and valves
had
been verified as correct.
At 1:52 p.m., the operators
manually inserted
Control Rod 06-39, deenergized
its electrical
components
and declared it inoperable
in accordance
with WNP-2
TS 3. 1.3. l.a. l.a.
The shift manager
(SH) notified supply system
management
of
the malfunction;
however,
he did not notify the
NRC resident
inspector of this
failure.
The
SH initiated problem evaluation request
(PER)
294-0235 to document the
failure of Control Rod 06-39 to insert.
He initiated emergency
Work
Order
HS 28 to remove,
disassemble,
and rebuild CRD-V-117 and CRD-V-118, the
SSPVs for Control Rod 06-39.
At 3 p.m., the
SH decided to perform scram time
testing
on 20 of the
185 control rods to eliminate the concern over
a generic
failure mode.
Subsequently,
the plant manager
testing of all
185 control rods
was necessary
to ensure
acceptable
operation.
At 8: 16 p.m.,
on March 27,
1994, the 'operators
completed
the scram time
testing of the
185 control rods.
The testing identified that four control
rods
(54-47,
54-15, 30-31,
and 10-15) were slow on
SOH, but within the time
limits of TS 3. 1.3.4.
Additionally,'perators
had also fully inserted
Control Rod 30-03 because it could not be scram time tested,
due to a failure of a
transponder
card in the control rod testing circuitry.
At approximately
6 p.m.,
March 26,
1994, the system engineer
determined that
had failed to insert because
the Buna-N exhaust
diaphr agm,
an environmentally qualified (Eg) component of SSPV CRD-V-118,
had failed due
to hardening.
The system engineer characterized
the failure as brittle
cracking of the exhaust
diaphragm of CRD-V-118, with the crack going
approximately
180 degrees
around the interior circumference of the exhaust
and hardening without cracking of the pressure
At
8 p.m., the licensee
concluded that the failure of the exhaust
diaphragm could
have
caused
the failure of the rod to scram
due to the air leakage rate into
the exhaust
being greater
than the rate being exhausted
through the
vent.
On March 27,
1994, at 3:58 p.m., the repair of the
was completed
and operators
declared that control rod operable.
At 8: 16 p.m.,
operators
completed
the scram time testing of all
185 control rods
and
increased
reactor
power to 88 percent.
Based
on the guidance
provided in licensee
Plant Procedure
Manual
(PPH) 1.3. 12B, "Operability Evaluation," Revision 0, the
SM considered that,
with the exception of the four rods which were slow on
SOH and the one rod
that could not be tested,
all the control rods were operable
because
the rods
had met surveillance
requirements.
Paragraph
3.7 of PPH 1.3. 12B states that,
when qualification is called into question,
performance of surveillance
requirements
alone
may not
be sufficient to determine operability, unless
the
surveillance testing adequately verifies the capability of the equipment
by
accounting for the degraded
condition.
5.2
Licensee
Followu
Res
onse to Control Rod 06-39 Failure to Insert
At
1 p.m.,
on March 28,
1994, the
PH met with resident
inspectors
and
discussed
the failure of Control Rod 06-39 to insert.
The
PM confirmed that
he considered that the control rods were operable
because
the control rods
had
repeatedly
met surveillance
requirements
during the testing performed over the
weekend.
The
PM discussed
the safety significance of the event
and the supply
system's
planned actions to prevent event recurrence.
The planned actions
included replacing the Buna-N components of the
SSPVs for the five control
rods that had
been declared
The
PH considered
that the failure
of Control Rod 06-39 to insert
and the slow SO) of the other four control
rods
had limited safety significance
because
the safety analysis
assumes
one
rod does not insert
and that
up to eight control rods
can
be slow without
adverse
impact to fuel.
He also noted that the backup
scram valves would
probably have functioned, resulting in the insertion of all control rods
(including 06-39).
At 4:45 p.m., the
PH agreed to
a
10 a.m.,
March 29,
1994,
conference call with the
NRC to discuss
the failure of Control Rod 06-39 to
insert
and licensee corrective actions.
On the evening of March 28,
1994, after having examined the diaphragms of the
SSPVs that
had
been refurbished,
the licensee
decided to rebuild the
SSPVs of
all
185 control rods (six at
a time) with the reactor operating at reduced
power.
At 10 a.m.,
March 29,,1994,
the licensee,
NRC Region V, and the Office of
Nuclear
Reactor Regulation
(NRR) had
a conference
telephone call to discuss
the events of March 26,
1994, licensee
actions to prevent recurrence
of these
events,
and supply system
and industry experience with Buna-N components
in
The participants
discussed
continued
power operation with
degraded
the operability of the control rods,
and the
replacement
of the
while at power.
The licensee related that
they had reviewed the scram times of the control rods
and believed that they
could predict the condition and failure of the
based
on scram
times.
The licensee
stated that they planned to have
an operability
determination
and
a basis for continued operation
(BCO) completed
by March 30,
1994.
The
PM also committed to scram testing the control rods each
week and
to immediately shut
down the reactor if another control rod failed to insert
during the
and replacement.
From Harch 29-31,
1994, the licensee
continued to rebuild SSPVs,
to collect
and organize data to incorporate
in the
BCO,
and to hold Plant Operating
Committee meetings to discuss drafts of the
BCO.
The licensee
found that the
diaphragms installed in the
had
come from procurements
in 3 separate
years
1983,
1987,
and
1990.
Furthermore,
th'e licensee
found that they
h'ad
not maintained records to be able identify which lot diaphragms
were in which
valves.
A technical
expert from GE arrived
on site to assist
the licensee
in
assessing
the degradation of the control rod SSPVs.
On March 31,
1994,
the licensee,
NRC Region V, and
NRR had
a conference
telephone call to discuss
the licensee's
progress
in developing
and
-10-
documenting
and
BCO.
The licensee
discussed
their assessment
of the data that had
been recently collected.
The licensee
noted that,
instead of refurbishing the four SSPVs of each control rod, only
the exhaust
diaphragms of each
CRD-V-118 valve would be replaced.
When
performing this replacement, if the exhaust
was found to be brittle,
the pressure
diaphragm of the CRD-V-118 valve would also
be replaced.
The
licensee related that the
BCO had not been completed,
but would be available
in draft for discussion
on April 1,
1994.
On April 1,
1994, the licensee,
NRC Region
V, and
NRR had
a conference
telephone call to discuss
the draft
BCO.
In the draft
BCO the licensee
concluded
the following:
(1) data taken
and reviewed
showed that when severe
degradation
is present,
there is increased
scram time;
(2) catastrophic
failures have not resulted in failure to scram,
but rather increased
time;
(3) shelf-life and storage
are minimal contributors to the degradation,
and installed service in the plant under elevated
temperature
and stress
are
major contributors to degradation;
(4) the failure of Control Rod 06-39 was
an
unusual failure of two or more diaphragms
in the
(5) based
on scram
time testing,
there were
no SSPVs
and control rods which would not perform
their safety function.
With respect
to operability, the
BCO stated that successful
testing
demonstrates
that the currently installed elastomers
are meeting their design
basis function.
However, all remaining diaphragms
were being replaced
on
an
expedited basis.
The
NRC participants
had the following comments with respect
to the
BCO:
(1) it did not appear that time to scram
was
a reliable
means of determining
the extent of degradation
and, without understanding
the extent of
degradation, it would be difficult to predict the remaining useful life of the
(2) the
BCO stated that it took the failure of two diaphragms
to
cause
the failure of a control rod to insert but that the licensee
could not
reproduce this in testing
and the pressure
diaphragm of CRD-V-118 for Control Rod 06-39
had not failed, it was only stiff and brittle; and (3) the licensee
believed that the degradation
was temperature
related
although the data did
not support the assumption.
The licensee
stated that these
comments
would be factored into the final
BCO.
The
PH reiterated that
he believed all the control rods would function if
required.
On April 8,
1994,
the licensee,
NRC Region IV, the Walnut Creek Field Office,
and
NRR had
a conference
telephone call to discuss
the final
BCO.
The
BCO
discussed
the previous
NRC comments.
The licensee
stated
they believed that
the failures of the diaphragms
was
a generic industry issue
and that they
would continue with their root cause
evaluation.
They statused
the diaphragm
replacement,
stating the effort would be completed
by April 12,
1994.
At the close of the inspection period,
the licensee
was continuing with their
root cause evaluation.
To date,
they had identified that all the severely
degraded
appeared
to have
been procured in 1989, that there
appeared
to be manufacturing
and chemical differences
between
the diaphragms
procured
in 1989
and those
procured earlier,
and that the configuration of the
failure of the exhaust
was critical in determining the control rod
insertion time.
5.3
Conclusions
The licensee
was not timely in developing
a
BCO.
The licensee's initial
appeared
to rely heavily on control rods meeting
surveillance
requirements
and not on data collected
from the disassembly
and
examination of the
14-55,
and 06-39.
The
licensee
refurbishment of the
was generally well controlled.
6
FOLLOWUP OF CONTROL ROD SURVEILLANCE TESTING AND REPAIR
(92701)
6. 1
NRC Followu
Ins ection of the Failure of Control Rod 06-39 to Scram
and
the Slow
SOH of Four Other Control
Rods
On March 28,
1994, during the resident
inspector's daily plant walkdown, the
inspector learned that Control Rod 06-39 failed to automatically insert, that
54-15, 30-31,
10-15 were slow on
SOH,
and that Control Rod 30-03 could not be scram time tested
due to a failed transponder
card.
In
reviewing the event against
the
WNP-2 TSs,
the resident
inspectors identified
that the licensed
operators
had incorrectly logged that the facility entered
limiting condition for operation 3. 1.3. l.a. l.a instead of 3. 1.3. l.b. l.b.
This
error had
no safety significance;
however,
the error indicates
a weakness
in
operator understanding
of the TSs
and incomplete
management
oversight.
The
operators
corrected
the log entry on March 29,
1994.
At
1 p.m., the resident
inspector
met with the licensee to further discuss
actions that the licensee
planned with respect to the failure of Control Rod 06-39 to insert
and the slow
SOH of the other four rods.
The
PH stated
that the
SSPVs for the four slow rods would be rebuilt prior to declaring the
rods operable.
Additionally, he stated that
he considered
that the other
180 rods were operable
because
these
rods
had consistently
passed
surveillance
tests
and
showed
no history of being slow.
The inspector identified that,
even though the licensee
considered
that the control rods were operable,
the
licensee
did not perform
a
POA.
PPH 1.3. 12B, "Operability Evaluation,"
Revision 0, required
a
POA be performed that included documenting the problem,
the basis for considering
the equipment operable,
and the
BCO.
The failure to
perform
a
POA is
an apparent violation of 10 CFR Part 50, Appendix B,
Criterion
V (Violation 397/9415-01).
6.2
Followu
of Previous
Control
Rod Deficiencies
6.2. 1
Control Rod 14-55 Slow
SOM
On March 28,
1994, at
5 p.m.,
when, performing followup inspection of failure
of Control Rod 06-39 to scram,
the
NRC resident
inspector learned
from a
-12-
licensee materials
engineer that, during surveillance testing performed
on
December
4,
1994, Control Rod 14-55
had exhibited increased
SOM time.
On
August 8,
1993, during previous surveillance testing,
inserted in 0.28 seconds
and
had
a 2X2 array
SOH of 0.31 seconds.
On
December
4,
1993,
SOH time was 0.72 seconds
and the
2X2 array
SOH time was 0.41 seconds.
Even though Control Rod 14-55 exhibited
an approximately three times slower insertion
speed,
the
2X2 array
SOH was
only 0.030 of a second
from exceeding
the
TS limit, and the control rod had
never previously exhibited increased
insertion time, the licensee
did not
initiate a
PER.
The inspector
found that the licensee
did not initiate a
PER
because
the
2X2 array average
SOM time did not exceed
TS limits.
Also, the
licensee did not establish
an increased
surveillance
frequency to minimize the
chance of exceeding
the
TS limit.
Early in January
1994,
the licensee
wrote Maintenance
Work Request
DL93 to
replace the
On January
7,
1994, prior to
replacing the
the licensee
again performed surveillance testing
on
That testing identified that Control Rod 14-55 inserted in
1.20 seconds
and that the
2X2 array
SOM time was 0.58 seconds,
which exceeded
the
TS limit of 0.43 seconds.
The licensee,
therefore,
declared
entered
the appropriate
TS limiting condition for
operation, initiated
PER 294-0014,
and replaced
the SSPVs.
In PER 294-0014 the licensee
stated,
"following removal of the SSPVs,
they
will be retained for disassembly
and inspection to determine possible failure
modes
and
any generic implications for valves remaining in service."
On
March 9,
1994,
the licensee initiated the following PTL actions associated
with this
PER:
(1) by April 1,
1994,
perform
a material
analysis of the
elastomers
from Hydraulic Control Units 02-19
and 14-55;
(2) by April 1,
1994,
perform
a review of scram time history to determine
SSPV rebuild impact to
Refueling Outage
9;
and (3) by April 15,
1994, evaluate
the need to rebuild
the
SSPVs in Refueling Outage
9 vice Refueling Outage
10.
The inspector
learned that the licensee
planned to have
GE perform
a failure analysis of the
6.2.2
Control Rod 02-19 Air Leakage
The inspector also learned
from the materials
engineer that
on January
31,
1994,
a licensee
system engineer
had identified air leakage
coming from the
vent of the
SSPVs for Control Rod 02-19.
The engineer
documented this
deficiency in
PER 294-0067.
In this
PER, the engineer,
based
on discussions
with GE, concluded,
"the cause of the problem
was likely due to air leakage
past the exhaust
diaphragm of SSPV CRD-V-117, but could have resulted
from
leakage
by the pressure
diaphragm of solenoid valve CRD-V-118."
The licensee
also concluded that the air leakage
did not prevent the control rod from
performing its intended
scram safety function.
It was understood,
however,
that the control rod may not meet its
SOH limits.
The system engineer
recommended
rebuilding the
SSPVs at the next available opportunity.
-13-
On February
1,
1994,
the licensee
performed
a prompt operability assessment.
In this assessment
the licensee
concluded that Control Rod 02-19 was operable
and
recommended
that the
be replaced
in the near
term.
The licensee
stated
in the assessment
that
GE believed the most likely
source of air leakage
was past the seat of the CRD-V-117 exhaust
and
not past the CRD-V-118 pressure
The licensee further stated that
GE felt, based
on the recent
scram time for Control Rod 02-19, that the
were reaching
normal end-of-life for the diaphragm material
(Buna-N) in the
SSPVs for this control rod.
Even though Control Rod 14-55 had
exhibited slow rod motion in January
1994
and the cause
was determined to be
the Buna-N components
reaching end-of-life, the licensee
concluded that the
diaphragm seat
leakage
would not interfere with normal
scram time or
contribute to increased
rod insertion time.
The licensee did not scram time
test Control Rod 14-55 to verify their assumption.
The licensee initiated the following PTL action associated
with this
PER:
by
March 18,
1994,
perform
a material
analysis of the elastomers
from Hydraulic
Control Units 02-19
and 14-55 to support rebuild in Refueling Outages
9 or 10.
6.2.3
Disassembly
and Inspection of the
and
14-55
On February 6,
1994, the licensee
received
GE's cost estimate for the
disassembly
and failure analysis of Control Rod 14-55 SSPVs.
Because
the
estimate
was high, the licensee
performed the failure analysis
themselves.
On
February 7,
1994, after having replaced
the CRD-V-117 and CRD-V-118 valves for
Control Rod 02-19, licensee
engineers
disassembled
and inspected
those
The engineers
found that the exhaust
diaphragm of CRD-V-118 had cracked
180 degrees
around its outer circumference,
and the pressure
while
intact,
was stiff and very brittle.
Even though the findings of this
disassembly significantly differed from the conclusions
the licensee
reached
in
PER 294-0067
and the licensee
committed to perform
a generic
impact
assessment,
the licensee
did not revise the previous operability assessment
or
perform
a new prompt operability determination.
PPM 1.3.12B, "Operability
Evaluation," Revision 0, requires
a prompt operability determination
when
finding physical
evidence of degraded
or nonconforming
components
that have
undergone
physical
change
from a previous acceptable
condition or has failed
testing requirements.
The failure to perform
a prompt operability
determination is
an apparent violation of 10 CFR Part 50, Appendix B,
Criterion
V (Violation 397/9415-01).
On February
17,
1994, the licensee
disassembled
and inspected
the
SSPVs of
Control Rod 14-55, which had
been replaced
on January
7,
1994.
The licensee
found that the CRD-V-118 exhaust
was hardened
and cracked
(having
a
360 degree
crack around its inner circumference),
and the pressure
was brittle and stiff.
The licensee
did not initiate a prompt operability
determination to assess
the impact of finding severely
degraded
components.
PPM 1.3. 12B, "Operability Evaluation," Revision 0, requires
a prompt
when finding physical
evidence of degraded
or
nonconforming
components that have
undergone
physical
change
from a previous
acceptable
condition or has failed testing requirements.
The failure to
perform
a prompt operability determination
is
an apparent violation of 10 CFR Part 50, Appendix B, Criterion
V (Violation 397/9415-01).
The inspector learned that the licensee
engineers
considered
that
a new or
revised operability assessment
was not necessary.
The engineers
considered
that the hardened
were confirmation of their*assumptions
in
PERs
294-0014
and 294-0067.
The inspector
considered this logic incorrect,
since the earlier assumptions
did not consider
complete failure of the exhaust
and believed the air leakage to be originating from the exhaust
diaphragms of CRD-V-117.
The inspector
also learned that equipment
qualification personnel
had not been
informed of the failed diaphragms,
even
though the engineers
were fully aware that these
components
were qualified
components.
On one occasion,
one of the engineers
involved with the diaphragm
failures asked
an equipment qualification engineer questions
about
Buna-N
qualification but did not mention that the
had failed.
The
inspector visually examined the failed diaphragms of the
SSPVs for Control Rod 14-55.
The diaphragms
were
so severely
hardened that any torsional or
twisting force resulted
in the diaphragm cracking.
The inspector also noted
the circumferential
cracking of the exhaust
The inspector
considered that the degraded
and failed Buna-N components
(the diaphragms)
were
a significant condition adverse
to quality.
The inspector also learned that the licensee's
senior nuclear
managers
were
aware of the failures of the
and 02-19.
The
senior managers,
however,
had not seen
the diaphragms.
Because
they had not
seen
the diaphragms,
the managers
were not personally
aware of the extent of
degradation.
On March 4,
1994, the Senior Management
Review Group met to
discuss
budget
and planning.
In this meeting the Senior Management
Review
Group reallocated
resources
to perform the
SSPV refurbishment
in Refueling
Outage
9 vice Refueling Outage
10.
The
PM decided to begin the refurbishment
on about April 4,
1994.
The refurbishment
was to be performed
one control rod
at
a time, with the intent of minimizing the impact
on power production.
10 CFR Part 50, Appendix B, Criterion XVI, requires that measures
be
established
to assure
that conditions
adverse
to quality,
such
as failures,
nonconformances,
and defective material
and equipment
are promptly identified
and corrected.
In the case of significant conditions
adverse to quality, the
measures
shall
assure
that the cause of the condition is determined
and
corrective action taken to preclude repetition.
The identification of the
significant condition adverse
to quality, the cause of the condition,
and the
corrective action shall
be documented
and reported to the appropriate
levels
of management.
The licensee
did not promptly identify and correct the
condition of failed and degraded
Buna-N components
in the
SSPVs to prevent the
repetitive failures.
This is
an apparent violation of 10 CFR Part 50,
Appendix B, Criterion XVI (Violation 397/9415-02).
6.2.4
and 58-35 Air Leakage
On May 3,
1989, with the reactor shut
down
and
a half-scram inserted,
the
licensee
found air issuing from the vents of the
-15-
and 58-35.
The system engineer wrote Plant Problem Material Deficiency
Report 289-0309 to immediately rebuild the
and
58-35
and rebuild all the control rod
SSPVs in 1990.
When the licensee
disassembled
the
they found that the valves'una-N
0-Rings were
extremely brittle, resembling bakelite.
The licensee
concluded that
fragments of the hardened
0-Rings prevented
internal
components
from moving,
causing air leakage
and valve malfunction.
The licensee
noted that the Buna-N
diaphragms of these
SSPVs were flexible.
The craftsmen
noted that the
diaphragms of the
SSPVs for Control Rod 54-35 were covered with a powdery
substance
that resembled
copper or brass dust.
The licensee
concluded that
the powdery substance
most likely originated
from the air supply tubing;
however,
a confirmatory analysis
was not perfonhed;
The licensee
concluded that the root cause of the
SSPV failures
was that
previous corrective actions
had not been
implemented.
Specifically, the
25 percent
replacement
schedule of SSPV Buna-N components
had not been
implemented.
The corrective action to prevent recurrence
was to replace
the
Buna-N components
in all
SSPVs in 1990.
The inspector considered this action
imprudent
and untimely.
The licensee
did not evaluate
a larger sample of
SSPVs to determine
the extent of the problem.
The action was untimely because
deferring the replacement
until 1990 resulted
in exceeding
the qualified life
of the Buna-N components.
The licensee
did not implement
a corrective action
to periodically replace
the
SSPV Buna-N components,
which was the root cause
of the event.
In 1990,
when the
Buna-N components of the
SSPVs were replaced,
the work
request did not include instructions that required the craftsmen to document
the condition of the
Buna-N components
upon replacement.
The system enginee}
kept approximately
15 of the diaphragms.
These
were flexible.
The
engineer,'owever,
did not record from which valves the diaphragms
were
removed.
Without traceability, the licensee
could not determine length of
service life.
6.2.5
Conclusions
The licensee failed to adhere to procedures
and perform prompt operability
assessments
on several
occasions
when finding safety-related
components
significantly degraded.
On three occasions
the licensee failed to take prompt
corrective action to prevent recurring failures of safety-related
components.
7
Eg
OF SSPV
BUNA-N COMPONENTS
(92903)
7. 1
E
Histor
of Control
Rod
SSPV Buna-N
Com onents
The inspector reviewed the
SSPV environmental qualification documentation
(WNP-2 gID number
16700,
Revision 6)
and discussed
this material with the
licensee
equipment qualification personnel.
The licensee
described
the
following qualification history of the
Buna-N components:
(1)
From January
1976 to August 1978, the licensee,
based
on
-16-
Revision
1, considered
Buna-N component service life to be
3 to 4 years
and
total life (service life plus shelf life) 9 years.
(2)
From August
1978 to December
1978,
the licensee,
based
on
Revision
1, Supplement
1, considered
Buna-N component life to be
7 years.
(3) In December
1985,
the licensee,
based
on the supply system's
engineering
standard,
determined that,
when
Buna-N components
were properly stored,
shelf
life had little effect on natural
aging.
(4) In June
1987,
based
on a
the licensee
again
concluded that shelf life had little affect
on natural
aging
and that service
life was 5.6 years.
(5) In July 1990,
the licensee,
based
on WNP-2 operating experience
(the
Buna-N component failure described
in paragraph
6.2.4),
revised service life
to 5.5 years in their qualification documents.
The inspector
noted that in 1990 the licensee
had used operating experience
as
the method for determining qualified life of the diaphragms for the
and
NRC Branch Technical
Positions permit qualifying equipment
using operating experience;
however, qualification by operating experience
is
a lesser preferred
method.
The inspector
noted that the licensee
determined
that the qualified life of the Buna-N diaphragms
used in the
was
5.5 years.
The licensee
selected
5.5 years
because
the diaphragms installed
in 1983 successfully
operated until Hay of 1989 with no failures.
As
described
in paragraph
6.2.4,
Buna-N components of the
and 58-35 failed on Hay 3,
1989.
7.2
Conclusions
It appeared
to the inspector that the selection of 5.5 years only marginally
met the intent of qualifying equipment
using operating experience.
The Buna-N
components
in 1990 had failed catastrophically.
These
components
had
obviously been
degraded
and were not reliable for some time before the
failure.
The licensee
used
a very limited sample,
two failed valves,
in
determining operating experience.
The licensee
assumed that the Buna-N
components
of the other valves were acceptable
because
the valves
had not
failed.
The licensee
did not expand their sample size to determine
the extent
of the problem.
Additionally, the licensee
considered
the degradation
of the
Buna-N components to result from thermal degradation;
however,
they did not
perform
a temperature
survey of the other
SSPVs to identify other potentially
affected valves.
8
APPARENT VIOLATIONS
10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," states,
"Heasures
shall
be established
to assure
that conditions
adverse
to quality,
such
as failures, malfunctions, deviations,
defective material
and equipment,
and nonconformances
are promptly identified and corrected.
In the case of
"
~
1
0
-17-
significant conditions
adverse
to quality, the measures
shall
assure that the
cause of the condition is determined
and corrective action taken to preclude
repetition."
Because
the hardening
and failure of the
SSPV diaphragms of the
CRD-V-118 valves for Control Rods 02-19
and
14-55 were significant conditions
adverse
to quality and the licensee
did not take corrective action to preclude
failure of diaphragms for the remaining control rod SSPVs, this is
an apparent
violation of 10 CFR Part 50, Appendix B, Criterion XVI.
10 CFR 50, Appendix B, Criterion
V states,
in part, "Activities affecting
quality shall
be prescribed
by documented
instructions,
procedures, or,
drawings of a type appropriate
to the circumstances
and shall
be accomplished
in accordance
with these instructions,
procedures,
or drawings."
WNP-2
PPM 1.3. 12B, Revision 0, paragraph
4.2.3.a,
states,
"For degraded
conditions impacting equipment operability identified by physical
evidence at
the Plant,
the Prompt Operability Assessment
should
be completed
and
documented within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of when the physical
evidence
was identified."
Because
on February
5 and
16 and March 26,
1994,
a
POA was not performed
upon
finding significantly degraded
Buna-N components
in SSPVs for Control Rods 14-58,
21-55
and 06-39, this is an apparent violation of 10 CFR Part 50,
Appendix B, Criterion V.
~
s
~ <
~
.,i
ATTACHMENT
1
PERSONS
CONTACTED
V. Parrish,
Assistant
Managing Director for Operations
- H. Flasch,
Engineering Director
"J. Swailes,
Plant Manager
- G. Smith, Operations Division Manager
- H. Reddemann,
Technical
Services
Division Manager
- M. Honopoli, Maintenance Division Manager
- J. Sampson,
Maintenance
Production
Manager
- P. Bemis, Regulatory
Programs
Manager
- H. Kook, Licensing Manager
D. Larkin, Engineering Services
Manager
D. Whitcomb, Nuclear Engineering
Manager
- J. Benjamin,
equality Assessments
Manager
- J. HcDonald,
equality Support
Manager
R. Barbee,
System Engineering
Manager
S. Washington,
Nuclear Safety Assurance
Division Manager
- C. Noyes,
Engineering
Programs
Manager
- J. Muth, Plant Assessments
Manager
- B. Hugo, Licensing Engineer
The inspectors
also inter viewed various control
room operators,
shift
supervisors
and shift managers,
maintenance,
engineering,
quality assurance,
and management
personnel.
- Attended the exit meeting
on Hay 13,
1994.
2
EXIT MEETING
An exit meeting
was conducted
on Hay 13,
1994.
During this meeting,
the
inspectors
reviewed the scope
and findings of the report.
The licensee
acknowledged
the inspectors'indings.
The licensee
did not identify as
proprietary
any of the information provided to, or reviewed by, the
inspectors.