ML17290B122

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Insp Rept 50-397/94-12 on 940222-0402.Violation Noted.Major Areas Inspected:Cr Operations,Licensee Action on Previous Insp Findings,Operational Safety Verification,Surveillance Program,Maint Program,Ler & Special Insp Topics
ML17290B122
Person / Time
Site: Columbia 
Issue date: 04/22/1994
From: Kirsch D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17290B120 List:
References
50-397-94-12, NUDOCS 9405020176
Download: ML17290B122 (27)


See also: IR 05000397/1994012

Text

APPENDIX B

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection

Report:

50-397/94-12

Operating

License:

NPF-21

Licensee:

Washington Public Power Supply System

P.O.

Box 968

Richland,

WA

99352

Facility Name:

Washington Nuclear Project

2

(WNP-2)

Inspection At:

WNP-2 site near Richland,

Washington

Inspection

Conducted:

February

22 through April 2,

1994

Inspectors:

R.

C. Barr, Senior Resident

Inspector

D. L. Proulx, Resident

Inspector

S.

P. Sjnchez,

Resident

NRR Intern

Approved by

D. F. ir

, Ch'

Project

Branch

a e Si

ne

Ins ection

Summar

~Al<<d:

R tf,

dt

d tt

by

td tt*d t

f

control

room operations,

licensee

action

on previous inspection findings,

operational

safety verification, surveillance

program,

maintenance

program,

licensee

event reports,

special

inspection, topics,

and procedural

adherence.

During this inspection,

Inspection

Procedures

61726,

62702,

62703,

71707,

71710,

92700,

92701,

92702,

and 93702 were used.

Results:

Strenqths:

The licensee

has developed

a thorough,

comprehensive

Refueling Outage

9 plan.

Weaknesses:

~

Interorganizational

communications

were weak in making decisions with

respect to extending

Cycle

9 operations

(paragraph

2.2).

~

Work quality was poor during the overhaul of fuel pool Cooling

Pump

FPC-

P-lA (paragraph

5).

940S020l76

940422

PDR

ADOCK 05000397

Q

PDR

~

Long-standing deficiencies

were not promptly corrected

on the control

room emergency chillers that rendered

the chillers inoperable for over

1 year (paragraph 6.2).

~

The licensee's

review of NRC Information Notice (IN) 89-44 was incomplete

because

the review did not consider that potential control

room

habitability problems could occur due to the location of nitrogen storage

tanks

(paragraph

6.3).

~

Plant Procedures

Hanual

(PPH) 2. 10.3,

Revision 21, "Control Cable

and

Critical Switchgear

Rooms

HVAC," was inadequate

in that the wrong gage

was referenced for system adjustments

and the electrical

breaker

lineup

prescribed

the wrong position for several

breakers

(paragraph

6.4).

~

Operators failed to follow the procedure for the control

room ventilation

systems

in that several

controllers

were set improperly (paragraph

6.5).

~

A number of material deficiencies

and drawing errors existed.

These

items indicated that the system

management

program

and the system

engineer

walkdowns were not of sufficient detail

(paragraphs

6.6 and

6.7).

~

Implementation of the outage planning process

was weak (paragraph

8).

Summar

of Ins ection Findin s:

~

Violations 397/9412-01,

and 397/9412-02

were opened

(paragraphs

6.2, 6.4,

and 6.5).

~

Violations 397/9318-01,

397/9318-10,

397/9318-12,

and 397/9324-02

were

closed

(paragraph

7).

Attachment:

~

Persons

Contacted

and Exit Heeting

DETAILS

1

PLANT STATUS

At the start of the inspection period, the plant was operating at

100 percent

power.

During the inspection period,

the plant went into and out of final

feed water temperature

reduction,

as operating conditions permitted.

Throughout this period,

the plant operated

at, full power (except for momentary

power reductions to support weekly bypass

valve testing

and control rod

exercises).

On Harch 26,

1994, with the reactor at

75 percent

power, Control Rod 06-39 failed to insert

when operators initiated

a scram signal locally

during control rod scram time testing.

Operators

reduced

power and manually

inserted this control rod.

The operators

then tested

the scram times of the

remaining

184 control rods to assess

their short-term operability.

The

licensee

conc'luded that degraded

diaphragms

in the control rod's

scram

solenoid pilot valves

(SSPV) contributed to the cause of the rod's failure to

insert.

At the

end of this inspection period, the plant was operating at 64

percent

power with control rod

SSPV refurbishment

in progress.

2

ONSITE FOLLOWUP TO EVENTS (93702,

92701)

2.1

Failure of Control Rod 06-39 to Insert Durin

Rod Scram Time Testin

2. l. 1

S stem Descri tion and Desi

n Basis

One of the reactivity control systems for the

WNP-2 reactor is the control rod

system.

The

WNP-2 reactor control rods are positioned

by hydraulics.

The

hydraulics

are controlled

by electro-pneumatics.

The electro-pneumatics

use

a

number of Automatic Switch Company solenoid operated

valves to perform the

rapid insertion

(scram) function of the

185 control rods.

The rod control

electro-pneumatic

system

has the three following means of rapidly inserting

(scramming) control rods into the reactor core:

(1) the

SSPVs which are

guality Class

1 components;

(2) the backup

scram pilot air solenoid valves,

which are guality Class

2 components;

or (3) the anticipated transient without

scram automatic rod insertion

scram air header

blowdown valves,

which are

guality Class

2 components.

The design basis of the reactivity control system is to provide sufficient

nuclear reactivity control devices

(control rods) to control the excess

reactivity in the core

and to provide for adjustments

of the control rods to

permit power generation.

The safety functions of the reactivity control

system,

that apply to this event,

are to provide sufficient excess

negative

reactivity to keep the reactor

shutdown,

thereby preventing fuel damage,

and

to provide sufficient rapid insertion of control rods

so that no fuel

damage

results

from any abnormal

operating transient.

2. 1.2

Event Descri tion

At 1:43 p.m.

(PST), Saturday,

March 26,

1994, with the reactor at 75 percent

power

and

WNP-2 licensed operators

conducting Control

Rod scram time testing

on

a

10 percent

sampling of control rods, control rod 06-39 failed to insert

when operators initiated

a scram signal locally.

Because

the positions of

Control Rod 06-39 switches

and valves

had

been verified as correct,

licensed

operators

concluded that the control rod had malfunctioned.

At 1:52 p.m., the

operators

manually inserted

Control Rod 06-39, de-energized

that rod's

electrical

components,

and declared

the rod inoperable

per

WNP-2 Technical

Specification

(TS) 3. 1.3. l.a. l.a.

The Shift Hanager notified supply system

management

of the malfunction;

however,

he did not notify the resident staff

of this failure or the entry into the Limiting Condition for Operation.

The Shift Hanager

documented

the failure of Control Rod 06-39 to insert in

Problem Evaluation

Request

(PER) 294-0235.

At 3 p.m., licensee

management

decided to perform scram time testing

on selected

control rods.

Later that

day, the Plant Hanager

(PH) concluded that scram testing of all

185 control,,

rods

was necessary

to gather data to assess

control rod operability.

Based

on that testing,

the

PH considered all the control rods operable,

with

the exception of Control Rods 54-47,

54-15,

30-31,

and 10-15, which were out-

of-specification slow on start of initial rod motion and

had

been fully

inserted.

Operators

had also fully inserted

Control Rod 30-03,

which could

not be scram time tested

due to a failed transponder

card located in the

testing circuitry.

The licensee

wrote emergency

work order

HS 28 to remove,

disassemble,

and rebuild

SSPVs

CRD-Y-117 and CRD-V-118 For Control Rod 06-39.

By approximately 6:00 p.m., the system engineer

determined that Control Rod 06-39 had failed to insert because

the Buna-N rubber diaphragms,

environmentally qualified components of SSPV CRD-V-118,

had thermally aged

and

failed due to embrittlement.

The system engineer characterized

the failure as

brittle cracking of the diaphragm with the crack going approximately

180 degrees

around the interior circumference of the diaphragm.

He noted that

the diaphragms of SSPV CRD-V-117 were flexible.

At 8 p.m., the licensee

concluded that the failure of the diaphragm could have caused

the rod not to

scram

by not exhausting

the air on the exhaust

diaphragm at

a rate greater

than the leakage of air into the diaphragm area.

At 3:58 p.m.,

on Harch 27,

1994, the repair of SSPV 'CRD-Y-117 and CRD-V-118

were completed

and the operators

declared

Control Rod 06-39 operable.

At

6: 17 p.m., operators

increased

reactor

power to 88 percent

and, at 8: 16 p.m.,

operators

completed

the scram time testing of all

185 control rods.

This issue will,be followed up in a special

inspection

(NRC Inspection

Report 50-397/94-15).

2.2

Core Fuel

Reload

Desi

n for 0 eratin

C cle

10

During routine inspection

associated

with outage preparations,

on February

25,

1994,

the resident

inspectors

learned that the licensee

was considering

changing the previously finalized batch size

(number of fuel assemblies)

and

reload design (fuel arrangement

and rod patterns)

for the next operating

cycle,

Cycle 10, which was scheduled

to begin in July 1994.

The inspectors

assessed

this activity to understand

the causes

and potential

impact

on

operation.

The following is

a chronology of the issues that led to the apparent late

decision making in the finalization of the Cycle

10 reload design:

In July 1993, the

PH had

begun to question the supply system designing

core reloads,

assuming

a capacity factor of 60 percent,

when it appeared

that for WNP-2 power production to be economical

the plant

had to operate

at

a capacity factor of about

73 percent.

In October

1993, the licensee

received the fuel vendor's

recommended

fuel

design for Cycle 10.

This design

assumed

a 60 percent capacity factor

and the implementation of the reactor

power up-rate

(RPU) modification

which enabled

the generation of approximately

50 additional

megawatts of

electrical

power.

In November

1993, the licensee's

senior management

requested

authorization

from the Bonneville Power Administration

(BPA) to extend

Cycle 9 operation

from approximately April 16 to May 15,

1994,

because:

(I) some long lead time repair parts

may not be available for Refueling

Outage 9; (2) the

RPU license

change

had been submitted late

and

may not

be approved

by the

NRC within the current operating

schedule;

and (3) the

Refueling Outage

9 preparations

were

somewhat

behind schedule.

Also in

November

1993, at

a senior management

review group meeting

(SHRG), the

group questioned

the licensee's

fuel designers

about the adequacy of the

Cycle

10 design projecting that

WNP-2 would operate

at

a capacity factor

substantially greater

than the

assumed

73 percent,

which appeared

possible

since the plant had

been operating well.

The designers

subsequently

informed the

PN that the reload design

was adequate.

However, the fuel designer s were not cognizant that management

had

requested

an extension to Cycle 9 operation.

On January

15,

1994,

WNP-2 fuel designers

again determined that the

Cycle

10 reload design

was adequate.

~

On January

17,

1994, the

WNP-2 fuel designers

learned that management

had

requested

an extension to Cycle 9 operation.

~

On January

26,

1994, the

BPA authorized the licensee to extend

WNP-2

Cycle

9 operation to April 29,

1994.

On February

2,

1994, the licensee

announced that

BPA had requested

the

supply system operate

WNP-2 until April 29,

)994, to support regional

power needs.

On February

14,

1994, the supply system fuel engineers

determined that

the hot excess reactivity for Cycle 10, reload design,

was

a concern,

after having been

informed by the fuel vendor on approximately

-6-

February 7,

1994, that the hot excess reactivity for Cycle

11 was

a

concern.

~

On February

17,

1994, the supply system

met with the fuel vendor to

establish

a plan to address

these

concerns.

The plan included increasing

batch size from 156 to 164 assemblies,

delaying the delivery of 32 fuel

assemblies

scheduled

for delivery on February

23,

1994,

and revising the

previously submitted final energy notice.

Also,

on February

17,

1994,

licensee

senior

management

decided to defer the implementation of the

RPU

until Refueling Outage

11.

~

On Parch 4,

1994, the licensee

again

met with the fue'Is vendor

and

discussed

four reload design options that were being considered.

Each of

the four design options reverted to the original design

of, 156 fuel

assembles,

due in part to the deferral of the

RPU.

The licensee

subsequently notifi d the vendor of the selectioii of the final reload

design option and

had the remaining Cycle

10 reload fuel assemblies

shipped.

Based

on the above chronology, the inspectors identified that the causes

which

led to the licensee

considering

a change to the batch size

and reload design

for Cycle

10 were as follows:

senior management

failed to effectively

communicate their plans to the fuels engineers

to extend Cycle

9 operation;

the timeliness

and quality of the

RPU amendment to the facility operating

license

was lacking, which resulted

in the deferral of the modification and

potential for reanalysis;

the licensee

fuel engineers

did not perform a, timely

detailed analysis of the potential

impact of operating at substantially higher

capacity factors

and extending Cycle

9 operation;

and weak outage planning

implementation.

2.3

Conclusions

Poor communications

resulted in late decision

making with respect to core

reload design.

3

OPERATIONAL SAFETY VERIFICATION (71707)

3.1

Plant Tours

The inspectors

toured the following plant areas:

Reactor Building

Control

Room

Diesel

Generator Building

Radwaste

Building

Service Water Buildings

Technical

Support Center

Turbine Generator Building

Yard Area and Perimeter

k

3.2

Ins ector Tour Observations

3.2. I

0 eratin

Lo s

and Records

The inspectors

reviewed operating logs

and records

against

TS and

administrative control procedure

requirements.

3.2.2

Honitorin

Instrumentation

The inspectors

observed

process

instruments for correlation

between

channels

and for conformance with TS requirements.

3.2.3

f~lif

2

The inspectors

observed

control

room and shift manning for conformance with

10 CFR 50.54(k),

TS,

and administrative procedures.

The inspectors

also

observed

the attentiveness

of the operators

in the execution of their duties,

and the control

room was observed to be free of distractions

such

as nonwork

related radios

and reading materials.

3.2.4

E ui ment Lineu s

The inspectors verified valves

and electrical

breakers

to be in the position

or condition required

by TS and administrative

procedures

for the applicable

plant mode.

This verification included routine control board indication

reviews

and conduct of partial

system lineups.

TS limiting conditions for

operation

were verified by direct observation.

3.2.5

E ui ment Ta

in

The inspectors

observed

selected

equipment, for which tagging requests

had

been initiated, to verify that tags were in place

and the equipment

was in the

condition specified.

3.2.6

General

Plant

E ui ment Conditions

The inspectors

observed plant equipment for indications of system leakage,

improper lubrication, or other conditions that would prevent the system from

fulfillingits functional requirements.

Annunciators

were observed to

ascertain their status

and operability.

3.2.7

Fire Protection

The inspectors

observed firefighting equipment

and controls for conformance

with administrative procedures.

3.2.8

Plant Chemistr

The inspectors

reviewed chemical

analyses

and trend results for conformance

with TS and administrative control procedures.

The licensee

continued to

operate with elevated

reactor water conductivity.

The licensee controlled

reactor conductivity at less

than 0.15 micro Siemens

by frequent condensate

filter demineralizer

changeouts.

3.2e9

Radiation Protection Controls

The inspectors periodically observed radiological protection practices to

determine whether the licensee's

program was being implemented

in conformance

with facility policies

and procedures

and in compliance with regulatory

requirements.

The inspectors

also observed

compliance with radiation work

permits,

proper wearing of protective

equipment

and personnel

monitoring

devices,

and personnel

frisking practices.

Radiation monitoring equipment

was

frequently monitored to verify operability and adherence

to calibration

frequency.

3.2. 10

Plant Housekee

in

The inspectors

observed plant conditions

and material

and equipment

storage to

determine the general

state of cleanliness

and housekeeping.

Housekeeping

in

the radiologically controlled area

was evaluated

with respect to controlling

the spread of surface

and airborne contamination.

3.2.11

~Securit

The inspectors periodically observed security practices to ascertain that the

licensee's

implementation of the security plan was in accordance

with site

procedures,

that the search

equipment at the access

control points was opera-

tional, that the vital area, portals were kept locked

and alarmed, that

personnel

allowed access

to the protected

area

were

badged

and monitored,

and

the monitoring equipment

was functional.

3.3

En ineered

Safet

Features

Malkdown

The inspectors

walked

down selected

engineered

safety features

(and systems

important to safety) to confirm that the systems

were aligned in accordance

with plant procedures.

During the walkdown of the systems,

items such

as

hangers,

supports,

electrical

power supplies,

cabinets,

and cables

were

inspected

to determine that they were operable

and in a condition to perform

their required functions.

Proper lubrication and cooling of major components

were also observed for adequacy.

The inspectors

also verified that certain

system valves were in the required position by both local

and remote position

indication,

as applicable.

The inspectors

walked down accessible

portions of the following systems

on the

indicated dates:

~Sstem

Diesel Generator

Systems,

Divisions 1, 2,

and 3.

Dates

Harch

24

0

-9-

Hydrogen Recombiners

Low Pressure

Coolant Injection

Trains "A," "B," and

"C"

Low Pressure

Core Spray

High Pressure

Core Spray

0

Reactor

Core Isolation Cooling

Residual

Heat

Removal

(RHR),

Trains "A" and

"B"

March 24

March 8,

24

March 8,

24

March 8,

24

March 8,

24

March 8,

24

Standby

Gas Treatment

Standby Liquid Control

Standby Service

Water

125V

DC Electrical Distribution,

Divisions

1 and

2

March 24

March 24

March 25

February

23,

March 8

250V

DC Electrical Distribution

3.4

Conclusion

February

23,

March 8

The inspectors

concluded that the systems

were in good order

and aligned in

accordance

with plant procedures.

4

SURVEILLANCE TESTING (61726)

The inspectors

reviewed surveillance tests

required to be performed

by the

TS

on

a sampling basis to verify that:

(1)

a technically adequate

procedure

existed for performance of the surveillance tests;

(2) the surveillance tests

had

been

performed at the frequency specified in the

TS and in accordance

with

the

TS surveillance

requirements;

and (3) test results satisfied

acceptance

criteria or were properly dispositioned.

The inspectors

observed

portions of the following surveillances

on the dates

shown:

Procedure

Descri tion

Dates

Performed

7.0.0

Shift and Daily Instrument

March

11

Checks

7.4.1.3.2

'ontrol

Rod Drive Scram Time

Harch 28-30

Test with Auto Scram Timer

-10-

The inspectors

concluded that the surveillances

were performed

and documented

properly.

5

PLANT MAINTENANCE (62703)

During the inspection period,

the inspectors

observed

and reviewed

documentation

associated

with maintenance

and problem investigation activities

to verify compliance with regulatory requirements

and with administrative

and

maintenance

procedures,

required quality assurance/quality

control

involvement,

proper use of clearance

tags,

proper equipment alignment

and use

of jumpers,

personnel

qualifications,

and proper retesting.

The inspectors

verified that reportability for these

maintenance activities was correct.

The inspectors

witnessed

portions of the following maintenance activities:

Descri tion

Dates

Performed

DH-3901,

Replace

Fire Damper

ROA-FD-7

February

22

EF-3501

Install Strain

Gages

and Perform

March

16

MOVATS Testing for SW-V-75A

DV-0901, Repair

and Overhaul

FP-P-1

HT-1601,

Replace

Diaphragms for Scram

Pilot Valve Solenoids

March 28

Narch 29-31

In addition to the above maintenance

observations,

the inspector reviewed the

in-process

and completed

work package for fuel pool Cooling

Pump FPC-P-lA per

Haintenance

Work Order FL-9801.

The inspectors

noted that this work was

originally scoped to replace the leaking mechanical

seal.

The inspectors

reviewed the past work history to ascertain

the quality of work that was

performed.

The inspectors

noted that in April 1993

Work Order AR6375 was performed

on

this

pump to replace

the existing

pump seals

and

add

a vent to the

pump

casing.

This procedure

also aligned the

pump.

However,

2 months after this

work was complete,

the

pump exhibited excessive

seal

leakage

again

and was

caution tagged "for emergency

use only."

Upon disassembly of FPC-P-1A per

Maintenance

Work Order FL-9801 in March of

1994, the licensee

noted that the bushing

was broken,

the seal

sleeve

was

worn, the mating ring was worn (indicating contact with the bushing),

foreign

material deposits

were found on the mating ring,

and the drive bands

and

retainer of the seal

had

become grooved.

The licensee

determined that these

deficiencies

should not have occurred after only 2 months of operation.

The

licensee

replaced

each of the failed components

under the supervision of the

system engineer

and

a vendor representative.

The licensee preliminarily

indicated that improper assembly

and alignment of the

pump resulted

in the

premature failure of the sealing

components.

The licensee

had not yet

determined

the root cause of this failure.

The inspectors will evaluate

the

root cause

when completed

by the licensee.

No violations or deviations

were identified.

6

ENGINEERED SAFETY FEATURES

WALKDOWN (71710)

The inspectors

performed

a detailed

walkdown of control

room heating,

ventilation,

and air conditioning

(HVAC).

This walkdown included both trains

of the emergency control

room chillers and detailed reviews of the low

pressure

core spray system

and Train A of the

RHR system.

The inspectors

examined

the system lineup procedures

to ascertain

whether they

matched plant drawings

and the as-built configuration.

The inspectors

verified that:

hangers

and supports

were

made

up properly, aligned correctly,

and

had sufficient hydraulic fluid levels;

housekeeping

was adequate;

insulation

and lagging was in-place

and maintained;

valves were installed

correctly, properly maintained,

locked

as appropriate,

and that local

and

remote position indications

were functional

and indicated the

same values;

flammable materials

were properly stored;

major system

components

were

properly labeled,

lubricated,

cooled,

and

no leakage existed;

instrumentation

was properly installed

and functioning; instrument calibration dates

were

current;

support

systems

were operational;

and breaker positions at local

electrical

boards

and indications

on control boards

were consistent.

With the

assistance

of licensee

personnel,

the inspectors

examined the interior of

breakers

and electrical cabinets.

In addition, the inspectors

assessed

licensee

procedure

PPH 2. 10.3,

Revision 21, "Control Cable

and Critical

Switchgear

Rooms

HVAC," to ascertain

whether the procedure

was adequate for

the system to perform its intended safety function.

The

inspectors'bservations

and findings are discussed

in the following paragraphs.

6. 1

Back round

LER 93-31 identified that the safety related control

room

HVAC would not

prevent temperature

in the control

room from exceeding

104 F.

The licensee

event report

(LER) states

that

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> into a design basis

event,

the control

room temperature

would reach approximately 107'F.

This concern

appeared

to

raise environmental qualification and control

room habitability questions.

The

LER primarily addressed

inadequate

cooling due to the degraded

cooling

capability of the service water system.

Because of the concerns

raised in the

LER, the inspectors

concluded that the control

room

HVAC required closer

scrutiny.

In addition, the inspectors

reviewed previous

NRC inspection reports to

determine if previous

commitments

and problems

had

been satisfactorily

implemented.

NRC Inspection

Report {IR) 50-397/90-05

(Haintenance

Team

Inspection)

indicated that the control

room chillers had been disassembled

and

inoperable for a period of 27 months.

The inspectors

had noted that redundant

seismic category I and environmentally qualified control

room emergency

chillers were required to be operable

per license condition

21 of the

WNP-2

-12-

operating license.

However,

IR 50-397/90-05 states

that the licensee

initially rationalized that corrective actions for the inoperable

equipment

"should not be pursued

at the crisis level" because

they were not specifically

addressed

in the TS.

The inspectors

were also concerned

because

in

IR 50-397/90-05,

neither

a justification for continued operation

(JCO) nor an

operability assessment

OA were performed for the degraded chillers.

The

licensee's

response

to the inspection report indicated that

a JCO and

an

OA

had

been performed.

In addition, the licensee

stated that, in the future,

JCOs

and

OAs would be performed for degraded

equipment

and that, for

safety-related

equipment,

that

was not addressed

in the TS, reasonable

allowed

outage times

(AOT) would be determined.

The control

room emergency chillers

were returned to service in January of 1991.

6.2

Control

Room Chiller 0 erabilit

During the inspector's

walkdown of the control

room emerg

ncy chillers,

two

deficiency tags

were observed

on the chiller s which appeared

to indicate

excessive

delays

in repairing Chiller CCH-CR-18.

One deficiency tag dated

February 4,

1993,

stated that the motor trips

on overload.

The other tag,

dated April 19,

1993, stated that the temperature controller indicates

zero

and that it will not control cooling properly.

The inspectors

were concerned

that the control

room chiller may have

been

inoperable for 13 months.

The inspectors

discussed

these deficiencies with the system engineer

(SE), his

supervisor,

and the systems

engineering

manager.

The licensee

indicated that

they were aware of these deficiencies;

however, their repair

had

been deferred

several

times.

The inspectors

asked if a prompt

OA (POA) was issued for

either of these deficiencies.

The licensee

stated that

a formal

POA had not

been performed,

but would now be completed.

The inspectors

also questioned

whether

a JCO had been developed for the degraded

condition.

The licensee

replied that

a

JCO had

been developed.

However,

when the inspectors

requested

a copy of this JCO, the licensee

presented

the inspectors

with a copy of the

JCO written in Hay 1990 that addressed

the previous inoperability of the

chillers discussed

in paragraph

6. 1 of this inspection report.

No specific

AOT appeared

to be addressed.

The licensee's

POA determined that Chiller CCH-CR-18 would trip off and not

perform its intended function under the present

degraded

condition if service

water temperature

was less

than

55~F.

On Harch 23,

1994, the licensee

immediately

noted that service water temperature

was at 52~F and declared

Chiller CCH-CR-18 inoperable.

Due to the licensee's

POA, the inspectors

concluded that Chiller CCH-CR-18 had

been inoperable for many months.

This

condition appears

to indicate

a repeat of the untimely correction of the

degraded

condition of the chillers

and poor management

oversight in pursuing

corrective actions similar to that discussed

in paragraph

6. 1.

10 CFR 50,

Appendix 8, Criterion XVI, requires

measures

to be established

to assure that

conditions

adverse

to quality such

as failures, malfunctions, deficiencies,

deviations,

defective material

and equipment,

and nonconformances

are promptly

identified and corrected.

Contrary to this requirement,

conditions

adverse to

quality concerning control

room Chiller CCH-CR-18, which is safety related

and

-13-

required

by the

WNP-2 operating license,

were not promptly corrected.

Because

deficiency tags dated

February 4,

1993,

and April 19,

1993, indicated that

Chiller CCH-CR-1B was in a degraded

condition for over

1 year,

the failure to

provide prompt corrective actions is

a violation of 10 CFR 50, Appendix B,

Criterion XVI (Violation 397/9412-01).

6.3

Potential for Nitro en Introduction into the Control

Room

A control

room operator aid identified that the liquid nitrogen tank, that is

used for safety relief valve operation

and inerting of the drywell, is located

near

one of the control

room ventilation intake structures.

The plant was

presently configured for intake from near this location.

The operator aid

also stated that the control

room may have

an oxygen deficient atmosphere

during

a design basis accident.

The nitrogen tank is not

a quality Class

I

category

component.

The licensee

postulated

the failure of this nitrogen tank

and intake of large

amounts of nitrogen into the control

room.

The inspectors

noted that

IN 89-44,

"Hydrogen Storage

on the Roof of the Control

Room,"

alerted the Supply System of the concerns for having nonoxygen

gas supplies in

close proximity of the control

room intakes.

The licensee

had previously evaluated this condition

and determined that

control'oom habitability problems

due to a failure of the nitrogen tank was

highly unlikely.

The licensee

concluded that this potential

was not

reportable

and

was not outside the design basis of the plant.

The inspectors

walked down the control

room intake structure

and noted that the closest

intake to the nitrogen tank was approximately

100 feet away.

Based

on this

observation

and the licensee's

evaluation,

the inspectors

accepted

the

licensee's

conclusions.

The inspectors

noted that the licensee's

review of IN 89-44 appeared

to be

cursory.

The supply system's

operating

experience

review of the information

notice only addressed

the location of hydrogen tanks

and required

no further

action.

The supply system's

review did not recognize the significance of

improperly located nitrogen tanks,

nor its consequences.

Although the

previous paragraphs

indicate that this poor review had

no safety significance,

this item emphasizes

the need for improved reviews of industry experience.

6.4

Procedural

Inade uacies of PPH 2. 10.3

During the inspectors'alkdown

of the control

room

HVAC system,

the

inspectors

used

PPM 2.10.3 to determine if adequate

direction for controlling

this system existed

and if personnel

adhered to the procedure.

The inspectors

noted the following apparent

problems with the procedure:

~

Final Safety Analysis Report,

Section 9.4. 1.5. 1, indicates that the only

operator action necessary

to operate Train

B of the control

room chillers

is to take the Chiller CCR-P-1B switch in the control

room to AUTO, at

which point the system will operate

automatically.

It further states

that

some

manual

valve manipulation is necessary

to operate Train A of

the emergency chillers.

The inspectors

were concerned that the latest

-14-

deviation to

PPM 2. 10.3 directed

manual manipulation of valves for

operation of Chiller B and that

a safety evaluation per

10 CFR 50.59

had

not been performed for this change.

The inspectors

discussed

this

concern with the SE.

The

SE stated that the manual

valve manipulation

was not needed for system operability,,but

was needed for "fine tuning"

of the system during routine operations.

~

Step 4.5 of PPM 2. 10.3 states

that the chillers must

be run for at least

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> before checking the oil.

LER 93-31 states

that the control

room

will exceed

104'F

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> into an accident.

The inspectors

were

concerned that checking for proper lubrication

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after the highest

heat load

may not be adequate

to ensure operability of the system during

accident conditions.

The

SE stated that the oil check after 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of

operation only applied during routine operation or when the chiller was

being operated for preventive maintenance

purposes.

~

In two instances

Step 5.5(19) refers the operator to use indication

on

Gage

WCH-PI-6B to control pressure.

The licensee

stated that the

intention of this step

was to refer to Chiller CCH-PI-6B.

The licensee

revised

PPM 2. 10.3 to correct this error.

On page

39 of the breaker lineup sheet,

the position for Switch

WMA-

FN-52B indicates

"ON/OFF."

There is no amplifying instruction to

determine

when this breaker

should

be

ON or OFF.

The licensee

was

evaluating this item on the lineup sheet to determine if a change is

necessary.

~

Breaker lineups for WMA-EHC-51B, 52B,

and

53B listed the required

position

as

"ON/LOCKED OFF(+)."

The (+) or amplifying instruction at the

bottom of the page indicated that the position of these

breakers

should

be

"OFF" in May through

September

and

"ON" in October through April.

On

March 18,

1994,

the inspectors

noted that the actual position was

"LOCKED

OFF."

The inspectors

noted that Paragraph

5.9,

Step

1, states

that these

should

be

"LOCKED OFF" during Modes 1, 2,

and 3.

The local operator aid

also states this requirement.

The licensee

stated that the breaker

was

in the correct position but that the procedure

was in error.

The error

was introduced during the latest revision of the procedure.

The licensee

initiated

a procedure revision to correct this error.

~

On page

40 of the breaker lineup sheet,

the procedure lists the required

positions for Switches

WRA-EUH-52, 53,

54,

and

56 as

"ON/OFF(+)."

There

is no explanation of the (+) on this page.

The licensee

stated that

there should

have

been

an amplifying instruction stating that the breaker

should

be

"OFF" in May to September

and

"ON" in October through April.

The inspectors

noted that all of these

breakers

were in their correct

position.

Although none of the above procedure errors involved inoperability of the

system,

the inspectors

were concerned that the procedure

reviews were not

adequate.

The licensee

stated that each of the errors that the inspectors'

-15-

identified was introduced during the latest revision

and after each of the

breakers

had

been properly positioned.

The inspectors

noted,

however, that

PPH 2. 10.3

had recently

been verified and validated,

indicating that the

verification and validation process

was of poor quality.

The failure to

provide the appropriate

gage designation for Chiller CCH-PI-68 and the failure

to provide appropriate

breaker lineup sheets

in Revision

21 of PPH 2. 10.3 was

an example of a violation of 10 CFR 50, Appendix 8, Criterion

V

(Violation 397/9412-02).

6.5

Procedure

Com liance Issues

With PPM 2. 10.3

The inspectors

noted

a number of instances

in which the emergency chillers or

control

room ventilation components

were set improperly or misaligned

as

required in

PPM 2. 10.3:

~

Step 5.5(7)e requires

the operator to ensure that the Temperature

Control

Point, located

on the local panel called the temperature

control module,

is set

6 increments

from the

"RAISE" position.

The inspector

found that

the actual setting

was at

4 increments

from the "RAISE" position.

~

Step 5.5(7)e requires

the operators

to ensure that the Maximum Load

Adjustment (also located

on the local panel) is set at 69 percent.

The

inspectors

noted that the actual setting

was at 90 percent.

~

Step 5.5(8) requires

the operators

to ensure Chiller SW-TIC-118 is set at

75'F.

The inspectors

noted that the actual setting

was at 70OF.

~

Step 5.5(9) requires the operators

to ensure Chiller WMA-TIC-118 is set

between

744F and

76OF.

The inspectors

noted that the actual setting

was

at 69OF.

~

Paragraph

4.9, in the precautions

and limitations section of PPH 2. 10.3,

requires that the setpoints of the temperature

controllers of the control

room to be set

as follows to meet the Final Safety Analysis Report

commitments of normal control

room temperatures:

WMA-TIC-12Al

74 to 76 degrees

WMA-TIC-1281

74 to 76 degrees

WMA-TIC-12A2

WHA-TIC-1282

70 to 72 degrees

70 to 72 degrees

WHA-TS-12A

Knob A- 71 to 73 degrees,

Knob 8- 69 to 71 degrees

WHA-TS-128

Knob A- 71 to 73 degrees,

Knob 8- 69 to 71 degrees

Contrary to Paragraph

4.9, all of the setpoints for the above controllers were

set improperly,

some

by as

much

as

5 degrees.

The licensee

stated that

-16-

control

room operators

adjusted

these setpoints without,referring to the

procedure.

The operators initiated

PER 294-0236 to address this condition.

This

PER appeared

to indicate that the operators

did not consider precautions

and limitations to be mandatory steps

in a procedure.

The inspectors

noted

that licensee

administrative

procedures

did not support this conclusion.

The inspectors

discussed

all of the

above incorrect settings

and misalignments

of the

HVAC systems with the SE.

The

SE stated that the operators

mispositioned

these controllers

during various operations

on the system

apparently without regard to returning these

HVAC systems

to the required

standby or normal positions of PPM 2. 10.3.

Operations

management

discussed

the above items with the operations staff and posted operator aids to prevent

recurrence.

The failure to follow PPM 2. 10.3 in setting the setpoints for the

above listed controllers

was

an example of a violation of 10 CFR 50,

Appendix B, Criterion

V (Violation 397/9412-02).

6.6

Other Material Deficiencies

Deficiency Tag 0093789 dated

November 6,

1993, states

that

LOW REFRIG.

PRESS.

annunciator

alarms at 1.5 psig.

The

SE stated that

a maintenance

work order had already

been

issued.

The inspectors

found oil leaks inside the local panel for the Control

Room

B chiller.

The

SE wrote

a deficiency tag

upon the

inspectors'otification.

Temperature

Gage TI-69B had

a broken glass

cover with a deficiency tag

dated October

19,

1993.

The licensee

had already initiated

a maintenance

work order.

The inspectors

found that Valve SW-V-862 had

a loose handwheel.

The

SE

stated that this would be corrected during the next routine walkdown.

The position indicator for Chiller CCH-V-3A did not indicate valve

position properly.

The

SE initiated a deficiency tag to document this

item.

The inspectors

noted that

a U-bolt nut was loose

on the drain connection

for Chiller CCH-RY-2A.

The

SE stated that maintenance

would correct this

deficiency.

The inspectors

noted that

a temperature

indicator (TI) and cap were

missing from the top of Chiller A.

However, this TI was found on

Chiller

B.

The

SE stated that the TI was necessary

only for

troubleshooting

and was left in place

on the chiller for which the

troubleshooting

had

been performed.

The

SE also stated that the cap for

the connection

needed to be replaced.

-17-

~

The inspectors

found damaged

and split electrical

conduit

on emergency

Chiller A.

The

SE wrote

a maintenance

work order to document

and correct

this deficiency.

~

The inspectors

found that Chiller CCH-V-43 had

a loose

handwheel.

The

SE

stated that the handwheel

would be tightened during the next routine

system walkdown.

~

The inspectors

found that the end connection

downstream of Chiller

CCH-'-63

was not capped

as

shown

on the system print.

The licensee

determined that,

since the valve was shut

and

no leaks were apparent,

this item had

no safety significance.

The

SE stated that the cap would

be replaced.

6.7

Drawin

Oeficiencies

The inspectors

found that downstream of Valves

SW-V-8S6A and 865B, there are

two valves not shown

on the drawing,

one labeled

"instrument isolation valve

PSllA/B" and the other "isolation drain valve PSllA/B."

The

SE stated that

the

WNP-2 policy was not to show the details of drain

and isolation valves for

pressure

switch lines

on top tier drawings.

The inspectors

found that,

on page

36 of the valve lineup sheet,

Chiller CCH-

V-13A was listed

as closed;

however,

the drawing required the valve to be

open.

The

SE submitted

a drawing change

request to correct this problem.

6.7

Conclusions

The inspectors

concluded that the licensee did not monitor the control

room

HVAC systems

and procedures

in necessary

detail to ensure

long-term

operability and prompt corrective action of potential

problems.

Several

previous inspection reports

noted that system engineers,

and the licensee

as

a

whole, did not appear to perform walkdowns of the systems with the necessary

frequency or at the requisite level of detail to ensure

a quality. condition of

the safety systems.

The licensee

committed in their 1993 Systematic

Assessment

of Licensee

Performance

response

to perform system walkdowns with

teams,

which included the system engineer,

a design engineer,

an equipment

operator,

and

a maintenance

craftsman.

The licensee

stated that these

team

walkdowns

had

been

done for the control

room

HVAC systems,

but that these

teams did not look in sufficient detail to identify and correct the type of

problems identified by the inspectors.

Although many of the

inspectors'bservations

appeared

to be minor in nature,

the number of

inspectors'indings

appeared

to -indicate that strong

management

attention is required to

improve total

system performance.

The inspectors

discussed

these

conclusions

and all of the above observations

with the

PH,

who acknowledged

the

inspectors'omments.

-18-

7

FOLLOWUP ON CORRECTIVE ACTIONS FOR VIOLATIONS (92702)

The inspectors

reviewed records,

interviewed personnel,

and inspected

plant

conditions relative to licensee

actions

in response

to previous violations:

7. 1

Closed

Violation

50-397 93-18-01

Control

Rod Drive

H draulic

Control Unit Accumulators

Re laced without a Substitution Evaluation

During

a previous inspection period, the inspector

noted that, during

replacement of the control rod drive hydraulic control unit accumulators,

the

mechanics

encountered

numerous

delays

and problems.

The inspector

then

questioned

the licensee's

planning process.

The inspector

noted that the

licensee

had treated this task

as

a one-for-one substitution rather than

a

design

change,

despite

the

new accumulators

being

made of stainless

steel

rather than the previously used

carbon steel,

having

a larger outside

diameter,

and having

a different operating pressure

and temperature.

The

inspector further noted that

a

SE was not performed per licensee

PPH 1. 17.2,

"Procurement

Engineering

Reviews."

Licensee corrective actions

included:

(1) properly performing

a substitution evaluation,

(2) reviewing

a

representative

sample of past work by the individuals involved in the

violation, (3) counseling of the individuals involved,

and

(4) performing

a

program review of the procurement

process.

The inspector

reviewed

documentation

associated

with the licensee's

corrective actions

and determined

them to be satisfactory.

7.2

C'losed

Violation

397 9318-10

As-Found Testin

not Performed for

Local

Leak Rate Testin

LLRT

During a previous inspection period, the inspector

observed

portions of the

Type

C testing for the

LLRT of valves

RHR-Y-16B and

17B.

The inspector

questioned

whether as-found

LLRTs were performed prior to any adjustments

of

the valve.

The

LLRT coordinator informed the inspector that such testing

was

not required.

The licensee

determined that as-found

LLRTs were required

by

licensee

procedures.

Licensee corrective actions

included:

(1) counseling

individuals performing/planning/coordinating

LLRTs, (2) performing

as found

LLRTs for subsequent

valve repairs,

(3) and issuing directions for proper

verbal

communications.

The inspector

reviewed documentation

associated

with

the licensee's

corrective actions

and determined that the licensee's

actions

were satisfactory.

7.3

Closed

Violation

397 9318-12

Pressure

Test Performed with

Uncalibrated

Pressure

Ga

e

During a previous inspection period, the inspector

noted that the licensee

was

using

an uncalibrated

pressure

gage during performance of an air pressure test

of the

head gasket

assembly

on

a cy'linder of Diesel Generator

2.

The

licensee's

corrective actions

included revising

PPH 1.5.4,

"Control of

Heasuring

and Test Equipment

Transfer Standards,"

to more clearly delineate

the requirements

for use of calibrated

equipment.

In addition, the

maintenance craft personnel

were trained

on the

new requirements.

The

~

~

4

inspector

reviewed the licensee's

procedure revision

and training records

and

determined that the licensee's

corrective actions

were satisfactory.

7.4

Closed

Violation

397 9324-02

Uncontrolled Combustible

Li uids Left

in Vital Area

During

a previous inspection period, the inspector

noted that, following a

repair of an oil leak in the

RHR A pump, licensee

personnel left a 5-gallon

bucket of oil in the

pump room but had not obtained

a Transient Combustible

Permit

as required

by

PPM 1.3. 10, "Fire Protection

Program."

This was

a

violation of Technical Specification 6.8. l.g.

In addition, the inspector

noted that

a number of licensee

personnel

performed fire tours in this area

prior to the arrival of the inspector.

The inspector determined that fire

tours

may not have

been thorough.

Licensee corrective actions

included:

(1) counseling of the craft personnel

involved,

(2) performing training of the

appropriate craft personnel,

and (3) revising fire tour procedures

to more

clearly communicate

management's

expectations

for ensuring

proper

administrative controls for hot wor k, fire impairments,

and combustible

material.

The inspector reviewed documentation

associated

with the licensee's

corrective actions.

In addition,

the inspector

has performed frequent tours

of vital areas

over the last several

inspection periods

and

no further

violations were noted.

The inspector considered

that the licensee's

corrective actions

were satisfactory.

8

REFUELING OUTAGE 9 PLANNING AND OUTAGE PLANNING IMPLEMENTATION (62703)

The supply system

had originally scheduled

Refueling Outage

9 to begin

April 15,

1994;

however,

at the licensee's

request

the

BPA approved deferral

of the outage until April 29,

1994.

Some of the major wor k scheduled for

Refueling Outage

9 includes mechanical

stress

improvement of selected

reactor

vessel

nozzles,

the 10-year

ASME hydrostatic test of the reactor vessel,

an

integrated

leak rate test of the primary containment,

replacement

of selected

containment

supply and exhaust

purge valves,

core shroud weld inspection,

and

jet pump

beam replacement.

The inspector

assessed

the licensee's

procedures for outage planning, the

outage planning requirements

established

in these

procedures,

the outage

plan

and the licensee's

status of readiness

for Refueling Outage

9.

To assess

the

status of readiness

the inspector

reviewed selected

work packages

and the

status of work package

planning.

The inspectors

review of PPM 1. 16.8,

"Outage Management,"

which describes

the

structure

and functions of the

WNP-2 outage

management

process

used during the

annual refueling and maintenance

outage,

identified several

strengths

and

a

weakness.

The strengths

of this

PPM include effectively describing the

responsibilities of each

member of the outage organization,

establishing

criteria for the minimum numbers of operable

safety systems

for all aspects

of

planning

and scheduling

work during the outage,

and establishing

an outage

critique.

This

PPM appeared

weak because

is does not identify specific

guidelines

in which elements of outage

planning must

be completed.

The

-20-

failure to establish

these guidelines

could lead to poor outage planning

implementation.

For example,

the

PPH states

that the outage

manager will

develop

and implement

an outage

plan prior to the next major outage

and,

several

months prior to the start of the outage,

the site will be notified of

the scope freeze date.

Also, this

PPH does not establish

goals for

completing work packages

prior to the outage.

The inspector's

review of outage status

information provided by the licensee

on Harch 31,

1994,

noted the following:

approximately

415 of 3800 outage

tasks

(which did not include preventive

maintenance

tasks)

were ready to work;

the ready to work packages

appeared

adequate

in quality; approximately

725 of

the 3800 outage

tasks

were in the final stage, craft walkdown, of the planning

process;

approximately

125 of the 3800 tasks

had

been

added to the outage

scope

since January

3,

1994;

approximately

1000 of the

2000 work tasks

scheduled

to start during the first 2 weeks of the outage

were either ready to

work or in the final stage of the planning process;

and approximately

200 of

the 2000 work tasks

planned to start during the first 2 weeks of the outage

were missing

some of the repair parts.

The inspector

concluded

from the review of this information that the

licensee's

plan for the outage

had

been thoroughly developed;

however,

the

implementation of the plan warranted significant strengthening.

Less than

approximately

25 percent of the tasks for the outage

were planned

or in the

final stage of planning,

and

some parts

were not yet available

3 weeks prior

to the beginning of the outage.

The inspector considered

that

PPH 1. 16.8

omission of clearly defined implementation goals contributed to the

implementation

weaknesses.

'

ATTACHMENT 1

1

PERSONS

CONTACTED

  • V. Parrish, Assistant

Managing Director for Operations

  • H. Flasch,

Engineering Director

  • J. Swailes,

Plant Manager

G. Smith, Operations

Division Manager

  • H. Reddemann,

Technical

Services Division Manager

  • H. Honopoli, Maintenance Division Manager
  • J. Sampson,

Maintenance

Production

Manager

  • P. Bemis, Regulatory

Programs

Manager

  • H. Kook, Licensing Manager

D. Larkin, Engineering

Services

Manager

D. Whitcomb, Nuclear Engineering

Manager

J.

Benjamin,

equality Assessments

Manager

  • J. McDonald, guality Support

Manager

R. Barbee,

System Engineering

Manager

Nuclear Safety Assurance

Division Manager

  • C. Noyes,

Engineering

Programs

Manager

  • J. Huth, Plant Assessments

Manager

  • B. Hugo, Licensing Engineer

D. Williams, Bonneville

Power Administration

  • H. Davidson,

Licensing Support

Counsel

The inspectors

also interviewed various control

room operators, shift

supervisors

and shift managers,

maintenance,

engineering,

quality assurance,

and management

personnel.

  • Denotes attendance

at the exit meeting

on April 8,

1994.

2

EXIT MEETING

An exit meeting

was conducted

on April 8,

1994.

During this meeting,

the

inspectors

reviewed the scope

and findings of the report.

The licensee

acknowledged

the inspectors'indings.

The licensee

did not identify as

proprietary any of the information provided to, or reviewed by, the

inspectors.