ML17284A794

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Insp Rept 50-397/98-21 on 980830-1010.No Violations Noted. Major Areas Inspected:Operations & Engineering
ML17284A794
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 10/27/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17284A793 List:
References
50-397-98-21, NUDOCS 9811030099
Download: ML17284A794 (21)


See also: IR 05000397/1998021

Text

ENCLOSURE

U.S.'UCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

License No::

Report No.:

. Licensee:

Facility:

Location:

Dates:

Inspector(s):

Approved By:

50-397

NPF-21

50-39?/98-21

Washington Public Power Supply System

Washington Nuclear Project-2

Richland, Washington

August 30 through October 10, 1998

S. A. Boynton, Senior Resident Inspector

J. E. Spets, Resident Inspector

W. B. Jones, Senior Reactor Analyst

G. A. Pick, Acting Chief

Project Branch E

Division of Reactor Projects

ATTACHMENT:

Supplemental Information

98ii0300'PV 'F81027

PDR

ADOCK 05000397

6'DR

0

EXECUTIVE SUMMARY

Washington Nuclear Project-2

NRC inspection Report 50-39?/98-21

This information covers a 6-week period of resident inspection with input from a senior reactor

analyst.

~Oerarione

During a walkdown of the service water supply to the System A residual heat removal

pump room cooler, the inspectors determined that the locking device to an isolation

valve was unattached, contraiy to plant procedures.

Since the valve was found in the

correct position, no safety impact would have resulted.

This failure to properly lock the

valve is a violation of minor significance and is not subject to formal enforcement action

(Section 02.1).

~En ineerin

~

The manual startup and shutdown of the reactor core isolation cooling system for level

control, following the March 1998 main steam isolation valve closure, challenged the

operators.

The proceduralized method to control reactor vessel level by diverting

reactor core isolation cooling flow through the test return line could not be accomplished

because of valve design deficiencies. The method used to maintain the reactor core

isolation cooling system test return line isolation valves decreased

the reliability of the

system and challenged the containment isolation function since the valves may not have

closed against high differential pressure.

Unresolved Item 50-397/98005-05, involving

exclusion of the reactor core isolation cooling test return line valves from the scope of

the maintenance

rule, was determined not to be a violation of NRC requirements

(Section M8.1).

Re ort Details

Summa

of Plant Status

The plant operated in Mode 1 at full power for the duration of the inspection period.

I

I. 0 erations

02

Operational Status of Facilities and Equipment

02.1

En ineered Safe

Feature S stem Walkdowns

a.

lns ection Sco

e 71707

, The inspectors walked down accessible portions of the following systems:

Standby Service Water System A

Emergency Diesel Generators (Division I, II, and III)

Standby Gas Treatment (SGT) System A

Containment'Atmosphere

Control Systems A and B

b.

Observations and Findin s

The material condition of the systems was generally very good with some minor

deficiencies identified for the emergency diesel generators.

Those deficiencies were

brought to the attention of the control room supervisor for appropriate action,

Configuration of the systems was verified to be in conformance with Mode 1

requirements, with the exception that Valve SW-V-24A, standby service water isolation

valve to the Train A residual heat removai pump room cooler, was not locked as

required; however, the valve was in the correct position (open) with the locking chain

hanging from the m'anual handwheel.

Technical Specification (TS) Surveillance

Requirement 3.7.1.3 requires manual valves in the standby service water system to be

verified in their correct position every 31 days, unle'hey are locked, sealed, or

~

otherwise secured in their position. Procedure 1.3.29, "Locked Valve Checklist,"

Revision 29, requires Valve SW-V-24A to be locked open to satisfy TS 3.7.1.3.

Noting that Valve SW-V-24A was open, the inspectors determined that the actual safety

significance of the unlocked valve was low. A nonsafety-related flow switch associated

with service water flow to the room cooler provides annunciation in the control room

under low flow conditions.

Since operators routinely opera;e the standby service water

system, any low flow would have resulted in an alarm and alerted the control room

operators.

Thus, qualitatively, the risk significance was considered to be low. A

potential consequence

of the valve being mispositioned would be the inability to

maintain long-term operability of Residual Heat Removal System A because of high

pump room temperatures

following a design basis accident.

This finding was essentially identical to a poor valve locking practice documented in

NRC Inspection Report 50-397/97-12.

In the previous instance, the locking chain

remained attached to the valve handwheel and the manual adjustment knob, but a

significant amount of slack existed in the valve locking chain, which could have allowed

1

-2-

the locking chain to be unsecured.

The unlocked valve in this instance demonstrates

that there is an inherent vulnerability in the locking method for the emergency core

cooling system pump room cooler inlet isolation valves.

Specifically, the use of the

manual adjustment knobs on the motor operators as anchor points has not assured

locking of the valves, in that a small amount of slack in the locking chain allows for the

chain to be readily removed.

The failure to properly lock Valve SW-V-24A in

accordance

with Procedure 1.3.29 constitutes a violation of minor significance and is

not subject to formal enforcement action.

The licensee did not identify any cause for the unattached locking chain; however, since

the valve was found in the correct position and since flow had continued to the room

cooler, the licensee did not suspect tampering.

To prevent recurrence, the anchor point

of the locking chains on each of the emergency core cooling system pump room cooler

service water isolation valves was moved to the valve yoke. The corrective action was

found to be appropriate to address the concern.

~ C.

Conclusions

During a walkdown of the service water supply to the System A residual heat removal

pump room cooler, the inspectors determined that the locking device to an isolation

valve was unattached contrary to plant procedures.

Since the valve was found in the

correct position, no safety impact would have resulted.

This failure to properly lock the

valve is a violation of minor significance and is not subject to formal enforcement action.

08

Miscellaneous Operations Issues (92901)

08.1

Closed

Violation 50-397/96327-01013:

operational mode change with equipment

inoperable

I

On June 2, 1996, operators entered Mode 2 with a train of the control room 'emergency

filtration syster;

'., superable.

The licensee relied provisions contained in the ACTIONS

section of a Limiting Condition for Operation when entering Mode 2. Entry into a Mode

while relying upon provisions in the ACTIONS section violated TS 3.0.4. The corrective

actions consisted of discussing the event with operating crews and modifying specific

procedures controlling mode changes to require an electronic global Iog search for

mode change restrictions.

The inspectors reviewed the training attendance

log and subject training and found that

the target audience and subject training presented were adequate for the issues.

The

inspectors also reviewed Procedure 1.3.40, "Outage Mode Change or Refueling Activity

Readiness

Evaluation," Revision 11; and Procedure 3.1.2, "Reactor Plant Startup,"

Revision 43, and found that steps were added to require an electronic global log'search

for mode change restrictions.

The inspectors also reviewed several other plant

procedures to determine if similar changes were required.

The inspectors did not

identify any other procedures requiring similar changes.

-3-

Closed

Violation 50-397/96327-01023:

various surveillances inappropriately deferred

until after mode change

In June 1996 on three separate occasions, operators failed to meet TS surveillance

requirements required for the mode entered.

Specifically, the TS surveillance

requirements not met were associated with: (1) turbine throttle valve closure, (2) rod

block monitor channel checks, and (3} average powe

~ange monitor downscale rod

block channel functional test and fixed neutron flux upscale trips. The corrective actions

included:

(1) consisted of training for operations, licensing, and compliance personnel;

(2) voiding an inaccurate TS interpretation; (3) reviewing other TS interpretations for

inaccuracies; (4) assessing

generic impacts; and (5) performing plant modifications.

The inspectors noted that, when the license implemented the Improved TS, the scope of

some corrective actions changed.

The inspectors reviewed training attendance

records

and training information and found that the target audience and subject training

presented were adequate for the issues.

The inspectors found that the licensee voided

TS'Interpretation 94-06, which had provided an inaccurate interpretation of TS and that

the licensee had identified and voided several other TS interpretations that were no

longer needed.

The inspectors reviewed the assessment

of generic impacts and

considered the assessment

thorough as demonstrated

by the items reviewed and the

resulting. type and number of required surveillance procedure changes.

The inspectors

also found the Technical Evaluation Request 96-0177-0, Equivalent Change Evaluation

TER 96-0177, and screening for licensing basis change were adequate for the

corrective action design changes.

Closed

Violation 50-397/96327-01033:

inadequate startup procedures

On June 12, 1996, the licensee changed modes without testing of the containment

function of specific reactor core isolation cooling (RCIC} valves.

The corrective actions

consisted of discussing the event with operations crews, clarifying startup procedure

requirements regarding RCIC testing, establishing a iield in the maintenanc,.ork order

software to display mode change restrictions which apply to a work order, and

establishing an administrator position for outage-associated

equipment testing.

The inspectors reviewed the training attendance

log and subject training and found that

the target audience and subject training presented were. adequate for the issues.

The

inspectors also reviewed Procedure 3.1.2, "Reactor Plant Startup," Revision 43, and

found that the testing requirements for RCIC were clarified. Duiing the review of the

method used to identify and track work items that impact the ability to change modes,

the inspectors noted that the corrective action originally specified was no longer

implemented.

Subsequently,

the inspectors found that the licensee had implemented an

adequate process for tracking work items that impact the ability to change modes.

Specifically, the licensee used a "Technical Specification Inoperable

Equipment/LCO/RFO Status Log" that contains an entry titled "Mode Change Allowed:

Yes

No

." The log was used to track all inoperable equipment and mode change

restrictions and was required to be reviewed by operations personnel prior to mode

change.

-4-

The inspectors found that the licensee did not establish measures

to ensure that a

postmaintenance/surveillance

administrator position would be established for

outage-associated

equipment testing as committed to in Letter 602-96-250.

However,

despite the fact that measures were not in. place to establish an administrator position,

the inspectors found upon review of licensee procedures that sufficient requirements are

in place to ensure that required postmaintenance

testing and surveillances are

performed prior to change in mode.

The two instances where the licensee failed to fullyimplement or appropriately change

regulatory commitments in accordance

with Procedure SWP-LIC-01, "Regulatory

Commitment Change Process," Revision 0, indicated a weakness

in the regulatory

commitment tracking system and commitment change process.

08.4

Closed

Violations 50-397/96327-01043 and -01053: missed recirculation loop flow

mismatch surveillance and missed average power range monitor channel check

surveillance

On June 13 and 14, 1996, the licensee, while in Mode 2, failed to verify at least once per

24-hour period that recirculation loop flow mismatch was within limits. Similarly on

June 21 and 23, 1996, the licensee, while in Mode 1, failed to perform required daily,.

average power range monitor channel checks.

The corrective actions for both violations

consisted of discussing the event with operating crews, modifying surveillance and

startup procedures, and reviewing other surveillance procedures to determine if similar

problems existed.

08.5

The inspectors reviewed the training attendance

log and subject training and found that

the target audience and subject training were adequate for the issues.

The inspectors

reviewed Procedure OSP-RRC-D701, "Jet Pump Operability and Recirculation. Loop

Flow Mismatch," Re'vision 2; Procedure 3.1.2, "Reactor Plant Startup," Revision 43; and

Procedure OSP-INST-H101, "Shift and Daily Instrument Checks (Modes 1, 2, and 3),"

Revision 11. The inspectors found that the procedure changes clarified the TS '.

requirements, added steps to perform required surveillances, clarified when

surveillances were to be performed, and improved the method of verification. The

inspectors noted that the procedure changes should ensure that the missed

surveillances are now captured by procedure.

In addition, the inspectors found that'the

licensee's review of other operations surveillance procedures for similar problems

resulted in proposed procedure changes.

I

Closed

Licensee Event Re ort LER 50-397/98-002-00:

reactorscram andtransient

because of failed closed main steam isolation valve

The licensee performance and regulatory compliance aspects of the subject report are

adequately documented in NRC inspection Report 50-397/98-05.

-5-

08.6

Closed

LER 50-397/98-003-00:

reactor scram while shut down because

of low reactor

water level.

The licensee performance and regulatory compliance aspects of the subject report are

adequately documented in NRC Inspection Report 50-397/98-05.

08.7.

Closed

LER 50-397/98-011-00:

emergency core cooling system pump room flooding

because of fire protection system pipe break.

The licensee performance and regulatory compliance aspects of the subject report are

adequately documented in NRC Inspection Report 50-397/98-20.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments

a.

Ins ection Sco

e 61726 62707

The following maintenance and surveillances were observed and/or reviewed:

Procedure 10.24.32, "PM Cal/Test - Rosemount DP Transmitters," Revision 9

(residual heat removal heat exchanger service water flow)

Procedure OSP-ELEC-M703, "HPCS Diesel Generator Monthly Operability

Test," Revision 4

Procedure ICP-CRD-X901, "HCU Scram Accumulator Pressure

Low/Leak

Detection - CFT/CC," Revision 0

Procedure MSP-SGT-8102, "Standby Gas Treatment System Unit B HEPA Filter

Test," Revision 2..

a.

Observations and Findin s

'I

~

The observed work activities were properly implemented in accordance with the

established instructions.

Where appropriate, operators properly entered and complied

with TS action statements.

A spot check of personnel qualifications found that

personnel implementing the maintenance activities were qualified. The inspectors also

reviewed operational logs associated with the SGT system testing and found that they

were inaccurate or not complete.

Following are several examples:

(1)

An October 7, 1998, 11:35 p.m. Iog entry indicates Fan SGT-FN-1B2 was

shutdown; however, there is not a previous entry for starting the fan.

-6-

(2)

An October 8 12:20 a.m. Iog entry indicates that Procedure MSP-SGT-B104 was

being performed when actually Procedure MSP-SGT-B102 was being

performed.

(3)

An October 8 2:08 a.m. Iog entry indicates Fan SGT-FN-1B2 was shutdown;

however, there is not a previous entry for starting the fan.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

Closed

Unresolved Item 50-397/98005-05:

condensate

storage tank return valves not

within scope of maintenance

rule

The NRC staff concluded that Valves RCIC-V-22 and RCIC-V-59 (RCIC test return line

valves) were not required to be within the scope of the maintenance

rule. This

conclusion was based on the licensee having implemented the actions identified with

Generic Letter 96-05, "Periodic Verification of Design-Basis Capability of Safety-Related

Motor-Operated Valves." Specifically the RCIC system was declared inoperable

whenever Valves RCIC-V-22 and RCIC-V-59 were open. This is in recognition that the

valves were outside the scope of their Generic Letter 89-10, "Motor-Operated Valve

Testing and Surveillance," program.

The licensee stated that Valve RCIC-V-59 was not

designed to be able to open against system operating pressure.

Thus, when

establishing the test return flow path, operators are expected to open Valve RCIC-V-59

prior to opening Valve RCIC-V-22, which would expose it to system operating pressure.

During the March 1998 reactor scram, the licensee suspected

that Valve RCIC-V-22 had

been opened prior to opening Valve RCIC-V-59, which resulted in Valve RCIC-V-59

binding. Generic Letter 89-10, Supplement 4, "Consideration of Valve Mispositioning in

Boiling Water Reactors," does not require establishing testing of valves for conditions

caused by operational errors from the control room.

However, the inspectors noted that the operation of the RCIC system during

the'arch

1998 eve'nt challenged the system reliability and the passive containment

isolation function of Valves RCIC-V-22 and RCIC-V-59. A study (AEOD/S97-02) of

RCIC system reliabilityfor the period 1987-1993 (conducted for the Reliability and Risk

Analysis Branch, Safety Programs Division, Office of Analysis and Evaluation of

Operational Data, U.S. NRC) identified that the failure probability of the RCIC system to

restart was twice that of the failure probability to initiallystart. The inspectors found that

the inability to establish recirculation flow through the test return line and subsequent

stai tup and shutdown of the system to control reactor vessel level unnecessarily

challenged the reliability of the RCIC system to support decay heat removal and short-

term cooling.

M8.2

Closed

Violations 50-397/97014-02

-03 and LER 50-397/97-009-00:

missed inservice

.

testing (IST) for Valve TIP-V-6, transversing incore probe purge check valve, and failure

to maintain containment penetration isolated with inoperable containment isolation valve

The violations and LER specifically addressed

the following issues:

(1) At the

completion of Refueling Outage R12 (July 4, 1997), surveillance testing in accordance

with the requirements of the IST program had not been performed on Valve TIP-V-6;

-7-

and (2) between July 18 and August12, 1997, while the unit was in Mode

1 with

Valve TIP-V-6 inoperable, the affected penetration was unisolated continuously and was

not under administrative controls as required by TS.

The corrective actions for Violation 50-397/97014-02 consisted of all associated

corrective actions identified in LER 50-397/97-009-00 in addition to several other

corrective actions. The licensee:

(1) modified the surveillance procedure for

Valve TIP-V-6 to clarify when local leak rate testing

results can be used, (2) reviewed

other IST procedures performed during the subject refueling outage to ensure all IST

program plan requirements were met, (3) tested Valve TIP-V-6 as required by TS

amendment,

(4) reviewed other IST procedures to determine if clarification of

acceptance

criteria was required, (5) trained control room personnel, and (6) modified

the startup checklist to include a step that requires the IST program lead's signature

verifying that all IST procedures, having a mode change impact, have been reviewed

prior to startup.

The inspectors noted that Procedure OSP-TIP/IST-R701, "TIP Valve Operability-

Refueling Shutdown," Revision 1, was modified to clarify when local leak rate test results

could be used for purposes of the surveillance.

The inspectors found that testing had

been completed in accordance with Procedure OSP-TIP/IST-R701 on March 13, 1998..

Based on the number of IST procedure performances reviewed by the licensee, the

inspectors concluded the licensee performed an appropriate review.

In addition, the

inspectors determined that the licensee

review of IST program plan procedures for

clarity was satisfactory, based on the identification and modification of ten IST

procedures that required clarification of requirements.

The inspectors reviewed training provided to control room personnel on IST program

issues during requalification Cycle 98-2 and found it to be adequate.

The training was

provided to "enable the control room staff's adequate

review of performed IST

procedures."

However, the inspectors did not find measures

established to ensure that

IST program training would be provided to control room personnel in the future. The

lack of continuous training does.not appear to be a significant problem because of the

implementation of other corrective actions.

The inspectors reviewed Procedure 3.1.1, "Master Startup Checklist," Revision 24, and

found that the licensee modified the procedure to require the IST program lead's

signature after the lead had verified that all mode change requirements had been

completed related to IST.

The corrective actions for Violation 50-397/97014-03 consisted of an immediate

corrective action of isolating the subject penetration and a followup corrective action of

training licensing personnel on verbatim interpretation of TS. The inspectors found that

the penetration was isolated, as indicated, and that licensing personnel did receive

training on verbatim interpretation of TS. The corrective actions were appropriate for

the circumstances.

Closed

LER 50-397/97-007-00:

voluntary report of automatic start of emergency

diesel generators because of undervoltage condition

-8-

The licensee initiated this voluntary report when the Division I and II emergency diesel

generators automatically started because of a momentary bus undervoltage condition.

The root cause of the event was determined to be an internal fault in the Train C

circulating water pump motor. The internal fault momentarily dropped voltage on the

Division I and II 4160 Yac vital buses until the fault was cleared.

The emergency diesel

generator output breakers did not close as the buses continued to be powered from the

station startup transformer.

The corrective actions to address the failure of the

nonsafety-related circulating water pump were appropriate.

Closed

LER 50-397/98-00?-00:

inadvertent full scram and Division I emergency core

cooling safety injection

The licensee performance issues and regulatory compliance aspects of the subject

report are adequately captured in NRC Inspection Report 50-397/98-13.

M8.5

Closed

LER 50-397/98-008-00: 'inadvertent full scram during reactor pressure vessel

leak testing in Mode 4

The licensee performance issues and regulatory compliance aspects of the subject

report are adequately captured'in NRC inspection Report 50-397/98-13.

M8.6

Closed

LER 50-'397/98-009-00:

nuclear steam supply shutoff system, Groups 3 and 4.

isolations during testing

The licensee performance issues and regulatory compliance aspects of the subject

report are adequately captured in NRC Inspection Report 50-397/98-13.

III. En ineerin

EB

Miscellaneous Engineering Issues (92903}

E8.1

Closed

LER 50-397/97-003-00:

notification of noncompliance with TS

The response time testing for reactor protection system, emergency core cooling

system, and containment isolation system instrumentation did not comply with TS. The

licensee concluded that the root cause of the TS violations was inadequate change

management for regulatory requirements.

Specifically, the licensee revised its

rr.ethodoiogy for performing response

time testing of instrument~tion using the

provisions of Licensing Topical Report NEDO-32291. The methodology in NEDO-32291

was approved by the NRC staff and provides for a more qualitative assessment

of

instrument loop response time compared to the traditional quantitative testing prescribed

by TS. However, in implementing the provisions of the NEDO report, the licensee failed

to request a change to the instrumentation TS. As a result, the approved TS continued

'o require quantitative testing of instrumentation loop response time.

Following the NRC.staff's identification of the discrepancy between the WNW-2 TS and

licensee implementation of the NEDO report, the licensee requested and received

approval for a Notice of Enforcement Discretion to allow continued plant operation while

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIALLIST OF PERSONS CONTACTED

Licensee

D. Coleman, Regulatory Affairs Manager

F. Diya, System Engineering Manager

D. Giroux, System Engineering

V. Harris, Assistant Maintenance Manager

P. Inserra, Licensing Manager

S. Oxenford, Operations Manager

G. Smith, Plant General Manager

INSPECTION PROCEDURES USED

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92902:

IP 92903:

Closed

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support

Followup - Operations

Followup - Maintenance

Followup - Engineering

.ITEMS OPENED, CLOSED, AND DISCUSSED

50-397/96327-01013

(r'El 96019-01)

50-397/96327-01023

(EEI 96019-02)

50-397/96327-01033

(EEI 96019-03)

50-397/96327-01043

(EEI 96019-04)

50-397/96327-01053

(EEI 96019-05)

50-397/97138-01013

(EEI 96022-01)

'IO

operational mode change made with equipment inoperable

(Section 08.1)

VIO

various surveillances inappropriately deferred until after

mode change (Section 08.2)

VIO

inadequate startup procedures (Section 08.3)

VIO

missed recirculation loop flow mismatch surveillance

(Section 08.4)

YIO

missed average power range monitor channel check

surveillance (Section 08.4)

VIO

failure to perform reactor protection system response time

testing in accordance with TS (Section E8.3)

50-397/97138-01023

(EEI 96022-02)

50-397/97138-01033

(EEI 96022-03)

50-397/97138-01043

(EEI 96022-04)

50-397/97014-02

50-397/97014-03

50-397/97-003-00

50-397/97-004-00

50-397/97-004-01

-2-

VIO

failure to perform isolation system response

time testing in

accordance

with TS (Section E8.3)

VIO

failure to perform emergency core cooling system

response time testing in accordance with TS

(Section E8.3)

VIO

failure to obtain NRC approval for elimination of TS

requirement (Section E8.3)

VIO

failure to perform inservice testing of Valve TIP-V-6

(Section M8.2)

VIO

failure to maintain containment penetration isolated with

inoperable containment isolation valve (Section M8.2)

LER

notification of noncompliance with TS (Section E8.1)

LER

TS-required manual scram resulting from an indication of

eritry into Region A of the power-to-flow map

(Section E8.2)

LER

TS-required manual scram resulting from an indication of

entry into Region A of the power-to-flow map

(Section E8.2)

50-397/97-00 7-00

LER

voluntary report of automatic start of emergency diesel

generators because of an undervoltage condition,

(Section M8.3)

50-39?/9?-009-00,

LER

missedinservice testi

~g for Valve TIP-V-6(Se~"..;> M8.2)

50-397/98-002-00

50-397/98-003-00

50-397/98-007-00

50-397/98-008-00

50-397/98-009-00

LER

reactor scram and transient because of failed closed main

steam isolation valve (Section 08.5)

LER

reactor scram while shut down because of vessel low level

(Section 08.6)

LER

inadvertent full scram and Division I emergency

core'ooling

system injection (Section M8.4)

LER

inadvertent full scram during reactor pressure vessel leak

testing in Mode 4 (Section M8.5)

LER

nuclear steam supply shutoff system, Groups 3 and 4

isolations during testing (Section M8.6)

50-397/98-011-00

50/397/98005-05

-3-

LER

emergency core cooling system pump room flooding

because of fire protection system pipe'break

(Section 08.7}

URI

condensate

storage tank return valves not within scope of

maintenance

rule (Section M8.1)

LIST OF ACRONYMS USED

.CAR

. FSAR

IST

LER

NRC

PDR

RCIG

SGT

TS

VIO

WNW-2

Code of Federal Regulations

Final Safety Analysis Report

inservice testing

licensee event report

U.S. Nuclear Regulatory Commission

Public Document Room

reactor core isdlation cooling

standby gas treatment

Technical Specifications

violation

Washington Nuclear Project-2

SITE COVERAGE FOR Rl COUNTERPART MEETING - NOVEMBER 17-19, 1998

SITE

ANO

CALL

CNS

CPSES

DC

FCS

GG

PY

RBS

SONGS

STP

WAT3

WC

WNP-2

COYERAGE

Russ B 'ater

Howard Bund

Bill McNeill

Paula Gofdber

Paul Ga e

CliffClark

Claude Johnson

Dennis Schaefer

John Whittemore

Mike Run an

Rebecca Nease

Lee Ellershaw

Chuck Paulk