ML17284A429

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Mgt Meeting Rept 50-397/88-23 on 880607.Major Areas Discussed:Enhancement to Programs in Response to SALP & Safety Sys Insp Conducted in 1987 & Concerns Re Number of Personnel Errors & Near Misses During Beginning of 1988
ML17284A429
Person / Time
Site: Columbia 
Issue date: 06/23/1988
From: Caldwell C, Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17284A428 List:
References
50-397-88-23-MM, NUDOCS 8807130441
Download: ML17284A429 (35)


See also: IR 05000397/1988023

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

No.

Docket No.

License

No.

Licensee:

Facility Name:

Meeting at:

50-397/88-23

50-397

NPF-21

Washington Public .Power Supply System

P.

0.

Box 968

Richland,

Washington

99352

Washington Nuclear Project

No.

2 (WNP"2)

Region

V Office

Meeting Conducted:

June 7,

1988

Prepared

by:

W. Caldwell, Project

nspector

Approved by:

P.

H

Johnson,

Chief

Rea

r Projects

Section

3

~Summar:

Da e

S gned

</zan/gp

Date Signed

A Management

Meeting was held on June 7, 1988 to continue the dialogue

between

Region

V and the Supply System

on items of mutual interest

and recent

enhancements

to programs in response

to the Systematic

Assessment

of Licensee

Performance

(SALP) and the safety

system functional inspection

(SSFI) that were

conducted in 1987.

In addition, the meeting participants

discussed

concerns

regarding the

number of personnel

errors

and near misses that have occurred at

WNP-2 since the beginning of 1988.

8807130441

88062~

PDR

ADOCK 05000~97

6

PNU

DETAILS

Mana ement Meetin

Partici ants

NRC Partici ants

J.

B.

B.

H.

D.

F.

R.

A.

R.

P.

M.

B.

J.

L.

F.

A.

P.

H.

C. J.

C.

W.

A.

D.

G.

N.

Martin, Regional Administrator

Faulkenberry,

Deputy Regional Administrator

Kirsch, Director, Division of Reactor Safety

and Projects

Scarano,

Director, Division of Radiation Safety

and Safeguards

Zimmerman, Chief, Reactor Projects

Branch

Blume, Regional

Counsel

Crews,

Senior Reactor

Engineer

Wenslawski, Chief,

Emergency

Preparedness

and Radiological

Protection

Branch

Johnson,

Chief, Reactor Projects

Section

3

Bosted,

Senior Resident Inspector

Caldwell, Project Inspector

Toth, Reactor Inspector

Cook, Public Affairs Officer

WPPSS Partici ants

D.

W. Mazur,

Managing Director

G.

D. Bouchey, Director, Licensing

and Assurance

A.

L. Oxsen, Assistant

Managing Director - Operations

J.

P.

Burn, Director, Engineering

C.

H.

McGilton, Manager,

Operational

Assurance

Programs

C.

M. Powers,

WNP-2 Plant Manager

L. T. Harrold, Manager,

Generation

Engineering

Bonneville

Power Administration

R.

F. Mazurkiewicz, Chief, Operations

Branch

D.

L. Williams, Nuclear Engineer

State of Washin ton Ener

Facilit

Site Evaluation Council

C. Eschels,

Chairman

W. Fitch, Executive Secretary

~Back round

On June 7, 1988,

a management

meeting

was held at the Region

V Office with

the individuals identified in paragraph

1 in attendance.

The purpose of

the meeting

was to continue the dialogue

between

Region

V and the Supply

System

on items of mutual interest

and recent

developments

in program

enhancements

in response

to SALP and the safety system functional

inspection

(SSFI) that were conducted in 1987.

Recent

NRC concerns

have focused

on several

areas

since the beginning of

1988.

These

concerns

were concentrated

on personnel" performance errors,

clearance

order/system

lineup deficiencies,

engineering

design errors,

weaknesses

in documenting/reporting

plant problems,

performance of root

cause

analysis of events,

management

awareness

of plant problems,

and

follow through

on commitments.

Repetitive personnel

errors

and clearance

,order deficiencies

which have

impacted plant operations

or resulted

in

near misses

have

been of particular concern.

Examples

included:

a.

Operations

personnel

errors

January

18 - Nisoperation of safety/relief'alves

resulted

in an

actual

low reactor pressure

vessel

level following a normal

shutdown.

February

13 - Erratic operation of the turbine bypass

valves

(following a manual

scram)

caused

level excursions

and masked

a

diversion of water through the reactor water cleanup

system to

the condenser

(a path not previously

known to exist).

February

14 - Control

room and equipment operator errors in

restoring

the reactor building heating

and ventilation

(HVAC)

system resulted

in building overpressurization

and rupture of

the roof.

March

12 - Control rod 46-51

was unknowingly mispositioned

from

step

48 (full out) to step

36 while taking rod drive stall flow

measurements.

April 30 - Main steam isolation valves

(MSIV) closed following a

reactor

shutdown

due to failure to adequately

anticipate plant

conditions

(underestimated

rate of pressure

drop).

May

1 - Approximately 9600 gallons of reactor coolant were

drained to the suppression

pool

due to improper control switch

operation while realigning Residual

Heat

Removal

(RHR) Train

B

from shutdown cooling to suppression

pool cooling mode.

May 12 - A resin spill (and consequent

Unusual

Event) occurred

due to two open valves in a sample line.

b.

Clearance

order/system

lineup deficiencies

Nay 3 - An electrician unknowingly worked on an energized

4160

VAC potential transformer

drawer

due to a tagging error.

Nay 6 - Reactor building vent fans automatically tripped

on

actual

high reactor building pressure

due to closure of

ventilation exhaust isolation valve during surveillance

.(operators

did not check the consequences

of pulling fuses for

testing).

II'ay

16 - An electrician

was flash burned while working on an

energized

bus for a tower makeup

pump (load side of breaker

was

energized

since motor was

powered from an alternate

source).

May 17 - Two condensate

valves

opened

when power was restored

after

a Division I bus outage which resulted in draining about

200 gallons of condensate

into a feedwater heater

where

two

mechanics

were working.

c.

Maintenance

personnel

errors

February

4 - Instrumentation

and control (I&C) personnel

initiated a reactor

scram while performing

a surveillance test

(technicians

tested

a second trip channel without asking

operators

to reset the channel

already tripped).

May 25 - Electricians

improperly installed

a design

change

on

No.

1 diesel

generator

(found during post-modification testing);

local start switch would not function because

one wire had been

incorrectly determinated.

April 1 - Two fuel bundles fell over onto the refueling floor

after uprighting of shipping container

due to the failure of

mechanical

maintenance

personnel

to attach securing brackets.

April 11 - A mechanic

stepped

on

a new fuel bundle while

preparing the bundle for inspection.

In the area of engineering

design effectiveness,

a number of concerns

were

identified by the

SSFI team,

the resident inspectors,

and the licensee.

These

concerns

related to inadequacies

in the design data base,

weaknesses

in the design

review process,

and possible

weaknesses

in the design

organizational

structure

(one manager for every

30 - 35 engineers).

Additional concerns

identified during 1988 related to weaknesses

in

documenting/reporting

plant problems

and follow through

on timely

completion of commitments.

In particular,

nonconformance

reports

(NCRs)

were not initiated on the fuel assembly that was stepped

on nor on recent

motor operated

valve

(MOY) problems.

In the case of the

MOYs, not issuing

an

NCR resulted in plant management's

not being fully aware of the extent

of problems with MOYs.

A recent licensee

event report

(LER 88-06) also

did not disclose that operating

crews did not understand

the severity of

the transient

described

and did not identify corrective actions to prevent

future backflow of reactor water through the feedwater

system.

With

regard to follow through

on commitments,

the Supply System stated in LER

87-24 that,

"Engineering efforts already in progress

to upgrade Electrical

Wiring Diagrams to top-tier status will be expedited."

However, this

effort was apparently discontinued in December

1987 and remained

on hold

thereafter

due to realignment of priorities.

The meeting

convened at 10:00 a.m.

Mr. Martin opened the meeting

by stating that these

meetings

have

been

useful in maintaining communications

and minimizing misunderstandings

between

the

NRC and the Supply System.

0

Mr. Mazur began the Supply System's

presentation

by discussing

the purpose

of the visit and by briefly describing recent performance

enhancements

and

prospective

organizational

changes

at MNP-2.

After introductory remarks,

Supply System representatives

made

presentations

on the following subjects:

Organizational Initiatives

Mr. Oxsen presented

the agenda

and discussed

recent

management

and

organizational initiatives.

He identified that the last operating

cycle was marred

by too many personnel

and performance

problems.

Mr.

Oxsen stressed

the

need for more management

involvement and personnel

accountability in the conduct of activities at MNP-2.

He stated that

these

enhancement

efforts should result in fewer

human errors, better

design products,

and

a safer

and more reliable plant.

Personnel

Performance

Issues

Mr.

Powers discussed

recent problems in the area of personnel

performance.

He category ized the performance

errors

and discussed

other items

such

as

inadequate

clearance

orders that led to some of

the recent events.

Mr. Powers detailed the

new discipline policy in

response

to poor performance

and outlined proactive

items designed

to

provide positive reinforcement to aid performance.

This presentation

was followed by a series of questions

to further understand

the

licensee's

enhancements.

Mr. Oxsen

summarized

the initiatives by

stating that the Supply System is unhappy with past performance

and

Mr. Mazur

emphasized

the fact that management

is

trying to penetrate

and improve existing attitudes of personnel.

Mr. Martin responded

to these initiatives by stating that correcting

the problems

leading to inadequate

clearance

orders

should

be

a

number

one priority.

He also identified that the

NRC has

become

increasingly concerned

over the negative trend in operations

personnel

performance.

In particular, the February 13,

1988 reactor

water level excursions

and the

May 12,

1988 resin spill events

have

raised

concerns

about the knowledge levels of some operators.

In

addition, there

has

been

an apparent

lack of penetrating

management

involvement and ability to turn around the operating crews'ttitudes

and performance.

Mr. Martin stated that

he sensed that no one

approach

would produce

a change in performance.

Instead,

he

suggested

that

a combination of items

may be necessary

to bring about

an effective change in attitudes.

Design Issues

Mr. Burn provided

an outline of the internal

and external

evaluations

that had been performed

on engineering

and des'ign issues

during the

last 12 months.

These evaluations

were performed primarily due to

deficiencies identified during the SSFI conducted

by, Region

V in

August 1987.

Additional concerns

were raised

by the

NRC in February

1988 as

a result of an inadequate

anticipated transient without scram

(ATWS) design

change that was being installed in the plant.

Mr. Burn

identified that

a re-review of design'ackages

implemented during

refueling

outage

(R-3)

had

been

performed

as

a result of these

internal

and external

concerns.

He identified that

no safety

problems

were found during these

reviews.

Nr. Burn also discussed

the "Engineering

Improvement Plan" that is being

implemented to make

enhancements

to the design

program.

Mr. Powers followed by

providing a description of the plant modification request

(PMR)

implementation

improvement program.

He stated that it was believed

that the enhancements

to these

programs

would minimize the

possibility of inadequate

design

changes

reaching the plant for

implementation.

Nr. Mazur summed

up these

program changes

by

identifying that

a

QA audit would be performed prior to the end of

1988 to evaluate

the effectiveness

of the changes.

Mr. Nartin responded

to these

enhancements

by stating that

engineering

is

a full partner with operations

in conduct of

activities

and must share

the responsibility for plant operations.

He reiterated

Nr. Burns'oncern

that the Supply System engineering

department

must get over its construction mentality.

Nr. Martin also

stated that the Supply System must delve into problems,

before they

identify themselves

at

a significant level.

He also suggested

that

the Supply System look at the single-unit Region

V utilities and talk

to them individually about engineering

program enhancements.

QA/QC Initiatives

Nr. Bouchey presented

the

QA/QC initiatives that were being

instituted to enhance

the effectiveness

of the quality programs.

In

particular,

a number of program

improvements

and management

enhancements

have

been planned,

such

as the issuance

of a

new policy

statement

on quality and

an increased

level of management

participation in quality matters.

Nr. Martin stated that

QA needs

to be more aggressive

in identifying

problems.

He stated that the test will be to see if QA has

a hand in

identifying future significant issues

before they identify

themselves.

Nr. Martin stressed

the concern that problems

need to be

identified to the appropriate

levels of management

at an early enough

time so that they can

be properly dealt with.=

He noted that

sometimes it may be necessary

to raise the issue prior to finding

proof that it is

a bona-fide problem.

Mr. Martin also stated that if

the Supply System could wait until problems are self-revealing,

then

they would not need organizations

such

as

QA.

He further noted that

opinions

and intditions are worth hearing

because

often they are

correct.

Nr. Martin summed

up the NRC's concerns

by stating that he

sensed

that the Supply System

has the capability to make

QA more

effective.

Balance-of-Plant

System Survey

Mr. Powers

presented

a brief description of the balance of plant

system

survey that was instituted to assess

systems for

susceptibility to wiring deficiencies

such

as those

found in the

reactor building overpressure

event that occurred

on February

13,

1988.

He described

the criteria that were established

as guidelines

for the survey and summarized

the results of the effort.

The results

found, in general,

were that systems

were adequately

tested

and

had

performed

as designed.

The remaining actions to be performed

by the

Supply System

wer'e to execute

the technical

support center

(TSC)

ventilation interlock verifications and complete the control switch

verifications

on 8 switches that

had similar installations to the

reactor building supply and exhaust

fans.

Refueling Outage Status/Restart

Program

Mr. Powers

provided

a brief description of the restart evaluation

process

and its results.

He identified the work that had

been

completed

and the remaining

items to be worked prior to startup.

Issues

assessed

within the restart evaluation

process

were stated

to

include the status of 27 functional

programs,

the operability of

balance-of-plant

systems,

management

review of deferred maintenance

tasks,

and more rigorous documentation of plant readiness

for

restart.

Mr. Powers also stated that the results of the restart

evaluation

would be presented

to Supply System

managers

upon

completion.

SALP

Mr. Powers

completed his portion of the agenda

by identifying the

scram frequency reduction efforts that were initiated in response

to

the

1987

SALP recommendations.

The primary focus of this effort was

to strengthen

performance

requirements

and emphasize

procedure

compliance.

In addition,

such things

as divisionalization of

surveillance

procedures

had

been

implemented to reduce the potential

for working on the wrong train while performing surveillances.

Mr. Martin suggested

that it may be worthwhil'e to contact the

Institute for Nuclear

Power Operations

( INPO) and other organizations

to det'ermine

what efforts have already

been

performed in the area of

scram reduction.

Conclusions

Mr. Mazur concluded

the Supply System's

presentation

by emphasizing

that

he would maintain strong vigilance on the work load,

management

involvement,

and organizational -strength of the Supply System.

He

stated that efforts would concentrate

on the proper establishment

of

priorities, that "not enough

time"- to perform. activities would not be

a valid excuse,

and that the threshold for questioning faulty work

would be decreased.

He stressed

that

he would open

up minds

and

attitudes

to the necessity for constructive self-criticism.

Mr.

Mazur identified that .he was promoting

an exchange

program between

the Supply System

and the Swedish State Power'Board.to

exchange

information and personnel.

He also identified that

he was initiating

an effort to increase

the operational

experience of the Corporate

Nuclear Safety. Review Board.

Mr. Mazur stated that these additional

initiatives were being established

to enhance

and expedite the

quality of Supply System activities.

Mr. Mazur sumarized

the Supply System's

problems

as

an inability to

work as

an effective team

and to be self-critical.

In the attempt to

satisfy everybody,

he felt that they had satisfied

nobody.

Selected

slides

from the licensee's

presentations

are enclosed

with this

report.

~C1

1

R

1

In closing, Mr. Martin responded

to the Supply System's

presentation

by

summarizing

the

NRC's concerns.

He restated

the need for additional

management

emphasis

on personnel

performance

and attitudes, for raising

issues

to appropriate

management

at an early stage,

and for optimizing gA

effectiveness.

In addition,

he also stressed

the need for the proper

allocation of resources

to make effective changes

(e.g.,

management

involvement),

and

a commitment to excellence

in training (e.g., simulator

upgrades

and adequate

operator instruction).

Mr. Martin stated that

enhancements

appeared

to be well thought-out for the majority of the

programs,

but that operations

performance

needs

to be turned around

by

more direct action

and management

involvement.

The meeting adjourned at 4:00 p.m.

Enclosure:

Slides

from the licensee's

presentations

ENCLOSURE

SELECTED SLIDES

FROM THE LICENSEE'S

PRESENTATIONS

NRC/SUPPLY

SYSTEM AGENDA

JUNE 7, 1988

WALNVTCREEK, CALIFORNIA

AGENDA

A OPENING

REMARKS

JB Martin

DW Mazur

B

PRESENTATION

BY SUPPLY

SYSTEM

I INTRODUCTION

II PERSONNEL

PERFORMANCE

III DESIGN ISSUES

~

Root Cause Assessment

Results

Integrated Plant Modification

Improvement Program

Design Engineering

Implementation Initiatives

IV QA/QC INITIATIVES

V BOP SYSTEM SURVEY

VI R3 STATUS/RESTART PROGRAM

Vll SALP

VIII CONCLUSIONS

C ISSUES OF CURRENT NRC INTEREST

~

Personnel Performance/Involvement

in

Recent Plant Problems

~

Engineering/Design Control

~

Documentation/Reporting of Plant Problems

~

Recent Limitorque MOV Problems.

D OTHER TOPICS OF INTEREST

E CLOSING REMARKS

AL Oxsen

CM Powers

GD Bouchey

JP Burn

GD Bouchey

CM Powers

CM Powers

CM Powers

DW Mazur

10

30

50

20

30

5

II.

P ERSONNEL

P ERFORMANCE

C.M. Powers

~

Categorization

of performance

lapses

~

Management

initiatives on

procedural

compliance.

~

Selected

corrective

actions

in each

category

~

Summary

PERSONNEL

PERFORMANCE

ISSUES

~

Categorization Of Performance Lapses

~

Individual Performance Errors

RHR valving

MSIV isolation surveillance error

Reactor vessel level/pressure control

Fuel handling

Control rod mispositioning

MSIYclosure

PERSONNEL

PERFORMANCE

ISSUES

(cont'd)

~

Inadequate Clearance Order Boundary Established

Reactor building overpressurization

Improper tagging on SM-4

Feedwater heater flooding

Electrical switchgear near misses

MANAGEMENTINITIATIVES

ON PROCEDURAL COMPLIANCE

~

Discipline policy and implementation directed

squarely at procedural compliance issues

Meted out fairlyand consistently

Escalating penalty for severity and repetitious

performance

Termination of employment for failure to support

our mission

. MANAGEMENTINITIATIVESON PROCEDURAL

COMPLIANCE (cont'd)

C

~

Plant management developing a "sense of

stewardship" in all employees

Increase management's

involvement in problem

.resolution

Better recognition of successes

and positive

feedback to individual contributors

Develop "quality circles" in each functional area to

identify and address morale problems

Develop pay-for-performance comp'ensation for

employees

MANAGEMENTINITIATIVESON PROCEDURAL

COMPLIANCE(cont'd)

~

Restructure

Bargaining Unit contract to support complete

right of selection

of foreman, control room operators,

and training

~

Reorganize

Maintenance

Department to apply stronger

control of work activities and better planning

~

Modify problem identification programs

to emphasize

potential problems

and implement dedicated

root cause

program

~

Institute other reorganization

initiatives to strengthen

planning capabilitites

and build stronger station

management

team

SELECTED CORRECTIVE ACTIONS (cont'd)

~

Reactor Vessel Level/Pressure Control

General Operating Procedures revised to direct

level management strategy when isolated

New procedure created to direct shift from normal

shutdown to hot standby

Upgrade simulator model to more accurately

followreactor inventory behavior

SELECTED CORRECTIVE ACTIONS (cont'd)

Operations Management to conduct simulator

crew evaluations and guidance sessions on level

management

Operations Management to "close ranks" on policy

and plant initiatives

Personnel performance issues are pursued and.

discipline used to reinforce expectations

Long-term design change is to install a small

capacity, motor driven feed pump

SELECTED CORRECTIVE ACTIONS (cont'd)

~

Inadequate

Clearance

Order Boundary

Suspended

all high voltage, switchgear,

and

transformer work

Conducted

electrical shop meetings

on ramifications

of near miss

Instituted a Clearance

Order review process

on

outstanding

R3 electrical switchgear work

SELECTED CORRECTIVE ACTIONS (cont'd)

Required component-by-component

testing for

de-energization

prior to work

. Identified known backfeed

circuits on switchgear

.Established

new independent

Clearance

Order

Control Group on all remaining

R3 work to ensure

work description

and Clearance

Order boundaries

are adequate

0

SELECTED CORRECTIVE ACTIONS (cont'd)

~

Valve Control in Radwaste

Reassess

adequacy

of procedure

controls on

deactivated

solid radwaste

system

interface with

liquid radwaste

operations

Ensure other deactivated

valves are adequately

isolated

Modify management

response

to Unusual

Event

declarations

Plant Manager or Assistant will respond

on all

unusual

events

plus affected department

manager

DESIGN

ERROR

ROOT

CAUSE

ASSESSMENT

BACKGROUND INFORMATION

~

Too many errors were being discovered

during design

implementation. Therefore, QA requested to do indepen-

dent root cause analysis

.

Polled several groups about problem PMRs plus looked at

recent PMRs with numerous FCRs-initial resulting list was

23 PMRs

Concentrated on errors that represented

incorrect techni-

cal information-not opinion preference, field interferences,

or administrative detail

~

Screening against established erior criteria resulted in the

eight PMFts (approximately 11 errors) which were analyzed

in detail for root causes

CONCLUSIONS

~

General

~

Difficultdata base and lack of elementary diagrams

~, Insufficient planning/scheduling

~

Management control in l&C/electrical (span of control,

adequate technical oversight by managers, etc.)

~

Errors concentrated

in I&C/electrical discipline, but

similar problems not ruled out in other disciplines

CONCLUSIONS

(cont'd)

~

Design Process

~

Improved up front communication/design criteria definition

~

Errors could be reduced. by creating "FOR CONSTRUCTION

ONLY"drawings

~

Engineering department system engineers not always

.

involved with all system changes

~

Lack of sufficient personnel feedback on problems, in-line

quality measurements,

and self-assessment

programs

CONCLUSIONS (cont'd)

~

Checking, Verifying, and Review Processes

~

Lack of up front communications/design

criteria definition

affects these functions also

insufficient time scheduled for thorough checking, review-

ing, and verifying

The necessary expertise has not always been selected for

~ these functions

There has been a lack of accountability associated with

reviewer signatures

Waiver of optional review steps has not received manage-

ment scrutiny

~

QA Overview

~

QA involvement too little and late

"ENGINEERING IMPROVEMENT PLAN"

~ Post SSFI/ARI Activities

~

Design engineering meetings

Checking/verifying changes

~

Rereview R-3 design packages

~

Q.A. Auditing upgraded

~

Generation. engineer internal evaluation

880435.45

PMR IMPLEMENTATIONIMPROVEMENT

PLAN

~

PMR Implementation Commitments from SSFI

1.

Process improvements

Focus on Closure of work-'OCS'

Partial implementation formalized

Preimplementation revews

Post implementation reviews

2.

Post Modification,testing/training

Clarified who is responsible for what (with regard to testing)

Mandatory use of appropriate PMT forms for each type of work

performed

3.

Implementation package review of selected

R-3 mod's

-10% sample of R3 work (significant impact)

Noted areas for improvement-documentation

. l3edicated function within technical staff

PMR IMPLEMENTATIONIMPROVEMENT PLAN (cont'd)

~

Additional Supply System Reviews Since SSFI

Supply System audit by Q.A.-¹88-434

Result - Similar issues as in SSFI

Conclusion - SSFI corrective actions still valid

Line verification effectiveness review'

Reaffirmed integrity of PMR process

Recommended

improvements:

- Generation Engineering (Design)

- Plant Technical (implementation)

- Purchasing and Materials Management

- Records Management and Plant Administration (close-out)

- Quality Assurance (Receipt inspection, QC and QA

processes)

- Maintenance (Testing Review)

SAFETY ASSURANCE AND QUALITY

INITIATIVES

(1)

Management Enhancement Initiatives

~

Organizational & Staffing

~

Training/Qualifications

~

Attitudes/Organizational Norms

Planning

~

Information and Feedback Systems/Communications

(2)

Program Improvements

~

Evaluation of Engineering Design Activities

~

QA/QC Program Improvements

~

Root Cause Assessment/Corrective

Action Programs

~

Nuclear Safety Assessment

Initiatives

~

Licensing/Regulatory Compliance Initiatives

BALANCE OF PLANT SYSTEM SURVEY

(Corrective Action Follow-Up to NCR 288-050)

~ Qbjective

~

Assess other systems for susceptibility to similar type

wiring deficiencies

~ Discussion

~

Safety related systems/components

are not considered

likelysubjects for similar wiring errors due to technical

specification surveillance tests that are routinely performed