ML17279A472

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Monthly Operating Rept for June 1987.W/870709 Ltr
ML17279A472
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 06/30/1987
From: Hutchison L, Powers C
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC
References
NUDOCS 8708190265
Download: ML17279A472 (3)


Text

OPERATINB DATA REPORT WNP-2 01-Jul-87 DOCKET: 50-397

2. REPORTINB PERIOD! Jun-87 OUTAGE ~ ON-LINE HOURS 720
3. UTILITY CONTACT! LEONARD HUTCHISON (509) 377-2486
4. LICENSED THERMAL POWER (MWt) a 3323 S. NAMEPLATE RATING (GROSS MWe)! 1200. 9 6- DESIGN ELECTRICAL RATING (NET MWe>! 1100
7. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe) a 1140
8. MAXIMUM DEPENDABLE CAPACITY (NET MWe> a 1095 IF CHANGES OCCUR ABOVE SINCE LAST REPORT, GIVE REASONS!

10 POWER TO WHICH RESTRICTED, IF ANY (NET MWe) a 1 i. REASONS FOR RESTRICTIONS, IF ANY!

MONTH YEAR CUMULATI VE

12. REPORT PERIOD HOURS 720 4343 22303 2
13. HOURS REACTOR CRITICAL 176.3 2424 3 16131 '
14. RX RESERVE BHTDWN HRB 0.0 0 0 340.4 15 HRS GENERATOR ON LINE 52. 4 2250.9 15411 8 16 UNIT RESERVE SHUTDOWN HOURS 0.0 0 0 381.7 17 GROSS THERMAL ENERGY (MWH> 83299 5188171 38869351 18 GROSS ELECTRICAL ENERGY (MWH) 15560 1726090 12945360 19 NET ELECTRICAL ENERGY (MWH) 14276 1666193 12436164 20 UNIT SERVICE FACTOR 7. 3X 51. 8/ 69. 1%
21. UNIT AVAILABILITYFACTOR 7. 3X 51.8/ 70.8%

22 UNIT CAPACITY FACTOR (MDC NET) 1. 8/ 35 OX 50.9X

23. UNIT CAPACITY FACTOR (DER NET> 1 BX 34.9% 50 7/
24. UNIT FORCED OUTAGE RATE 58. 2/ 10.3% 8.0%

25 FORCED OUTAGE HOURS 73 1 258 3 1333 5

26. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE DATE DURATION)a 27 IF CURRENTLY SHUTDOWN ESTIMATED STARTUP DATE!

8708190265 870630 PDR ADOCK 05000397 R PDR

DOCKET NO.

NIT NNlE WNP-2 DATE 7/1/87 IJlIT SIUTDOl'tNS / REDUCTIONS COWpLETEO By LB Hutchison BEGAT PERICO JUNE 19 87 TELEPIGNE mmth, year BD. 177'Pif TEIOIIs TiiNSII KTlliU 1%I%BI al l ma 87-04 4/10/87 S 583. 75 C RC FUELXX REFUELING OUTAGE CONCLUDES

'7-05 6/25/87 S 10.73 B HA HECFUN GENERATOR WAS REMOVED FROM GRID TO PERFORM OVER-SPEED TESTS ON TURBINE 87-06 6/26/87 F 17.63 A 87-18 EB TRANSF REACTOR SCRAMMED AT 40K POWER FROM TGV FAST CLOSURE RPS TRIP AS A RESULT OF TURBINE TRIP CAUSED BY TR-Nl AUXILIARY TRANSFORMER SUDDEN PRESSURE RELAY ACTUATION. THE RELAY WAS REPLACED AND PLANT WAS RESTARTED WITH TR-Nl OUT OF SERVICE FOR FURTHER EVALUATION.

87-07 6/27/87 F 26. 32 A 87-19 EB TRANSF REACTOR SCRAMMED AT 58K POWER FROM TGV FAST CLOSURE RPS TRIP AS A RESULT OF TURBINE TRIP CAUSED BY TR-N2 AUXILIARY TRANSFORMER SUDDEN PRESSURE RELAY ACTUATION. THE CAUSE OF THE TR-Nl AND TR-N2 SUDDEN PRESSURE RELAY OPERATION WAS TRACED TO AN INSTALLED TEST SWITCH WHICH CAUSED MISOPERATION OF THE RELAYS. THE RELAY WAS REPLACED AND PLANT RESTARTED WITH THE SUDDEN PRESSURE RELAY DYPASSEI FOR FURTHER EVALUATION.

87-08 6/28/87 F 29.13 A 87-20 EB CKTBKR REACTOR SCRAMMED AT 54'X POWER DUE TO A SPURIOUS LOSS OF MG SET POWER TO RPS BUS A. ANOTHER HALF sony i SCRAM ALREADY EXISTED ON THE OPPOSITE RPS CHANNEL (B) DUE TO A LEAKING RPS OIL PRESSURE SWITCH.

THE SPURIOUS LOSS OF POWER FROM THE MG SET WAS THE RESULT OF A BINDING IN UV RESTRAINT COIL IN EPA hKT}KO SySTDi g COMPOM=lL}T BREAKER SUPPLYING THE "A" RPS BUS. THE COIL WAS ADJUSTED AND TESTED TO VERIFY PROPER OPERATION F-Forced A-Equi.p Failure F-Admin 1-Manual Exhibit F h H AND THE OIL PRESSURE SWITCH .

S-Schcd 0-Maint or Test ~ G-Oper Error 2-Manual Scram REPLACED PRIOR TO PLANT RESTART.

C-Refueling H-Other 3-Auto Scram 0-Aegula tory Restriction 4-Continued Data Entry Sheet E-Operator Training 5-Reduced Load Licensee Event Report h License Examination 9-Other (LER) File (NUBEG-Oldl)

DOCKET NO.

'HNP-2 DATE COMPLETED IlY LB Hutchison MONTH DAY AVERAGE DAILYPOP/ER ~(EL DAY AVERAGE DAILYPOWER LEVEL (MR~et} (MR~et) 0 0 1 17 49 45 105 168 44 228 l5 INSTRUCTIONS On this form, Hst the average daily unit power level ht MVe '%et for each day in the reporting month. Compute to the nearest whole megawatt.

These Ggures vrill be used to plot a graph for each reporting month. Note that when maxbnum depettdable capacity s used for the net electrical rating of the. unit, there may be occasions when ~ daily average power btvei ex~

100% Une (or the restricted power level line). In such cases, the average daily unit power output sheet should be the footnoted to explaht the apparent anomaly.

P I