ML17265A206

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Insp Rept 50-244/98-02 on 980303-12.Violation Noted.Major Areas Inspected:Circumstances Surrounding 980303 Event in Which Pressurizer Pressure Increased to Set Point of Power Operated Relief Valve
ML17265A206
Person / Time
Site: Ginna Constellation icon.png
Issue date: 03/31/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17265A204 List:
References
50-244-98-02, 50-244-98-2, NUDOCS 9804070230
Download: ML17265A206 (10)


See also: IR 05000244/1998002

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

License No.

DPR-18

Report No.

50-244/98-02

Docket No.

50-244

Licensee:

Rochester Gas and Electric Corporation (RGRE)

Facility:

R. E. Ginna Nuclear Power Plant

II

Location:

1503 Lake Road

Ontario, New York 14519

Inspection Period:

March 3-12, 1998

Inspectors:

Herb Williams, Senior Operations Engineer, DRS (Lead)

~ Steve Dennis, Operations Engineer, DRS

Peter Drysdale, Senior Resident Inspector

Clyde Osterholtz, Resident Inspector

Approved by:

Richard J.

Conte, Chief

Operator Licensing and

Human Performance

Branch

Division of Reactor Safety

9804070230

98033i

PDR

ADQCK 05000244

6

PDR

EXECUTIVE SUMMARY

R. E. Ginna Nuclear Power Plant

NRC Inspection Report 50-244/98-02

This special inspection reviewed the event that occurred on March 3, 1998, in which the

'ressurizer pressure increased to the opening set point of a power-operated

relief valve

(PORV).

The instrument and control (ISC) calibration activities being performed before the event

were found to have been well coordinated with the operating crew.

Operator response to

the event was good after they became aware of the pressurizer pressure

increase.

There was ample time and indications of the pressure increase to allow operators to correct

the problem before the pressure increased to the point of the PORV opening.

The event

was caused by the failure of the operators to adequately monitor panels and respond to

alarms.

The failure to notice and respond to the'alarms and indications is a violation of

NRC requirements.

'(VIO 60-244/98-02-01)

RGRE management

response was quick to initiate troubleshooting of'the instrumentation

and controls, but appeared slow in reviewing the human performance aspects of the event.

RG5E investigations and corrective actions were not completed at the end of this

inspection.

The investigation included a Human Performance Evaluation System (HPES)

evaluatio'n.

The results of these activities will be reviewed in a follow-up inspection.

There were no adverse consequences

associated

with this event.

The safety importance

of the transient was that it was an unnecessary

challenge to the PORV, which could have

resulted in a small break loss of coolant accident had the PORV and its associated

block

valve failed to close.

Re ort Details

Plant Status and Back round

The plant was operating at 100% power.

On March 3, 1998, pressurizer pressure

increased to the opening setpoint of a power-operated relief valve (PORV). The pressure

increase started because

of a malfunction in the pressurizer heater control circuit during an

instrumentation calibration.

In response to this event, Region

I dispatched two inspectors to join with the resident

inspectors

in reviewing the event for underlying causes

and safety consequences.

I. 0 erations

01

Conduct of Operations

01.1

0 erator Res

onse

93702

a.

~Scc

e

The inspectors evaluated the significance of the event, the performance of plant

systems,

and the actions of reactor operators. Interviews were conducted with

instrument and controls (IKC) technicians and reactor operators involved in the

event.

a

A sequence

of events on March 3, 1998, is given in at the end of this report.

b.

Observations and Findin s

The Control Operator (CO) placed the pressurizer pressure control switch back in

automatic at 0802 hours0.00928 days <br />0.223 hours <br />0.00133 weeks <br />3.05161e-4 months <br /> as directed by the IRC calibration'procedure

and monitored

plant parameters to ensure there were no perturbations following the switch

movement.

At 0805, after observing proper response from pressurizer pressure

controls, the CO gave a briefing to the Head Control Operator (HCO) and left the "at

the controls" area to go to the restroom.

The HCO acknowledged the CO turnover

and returned to working on administrative duties at his desk in the "at the controls"

area.

These duties included performing containment leakage calculations, logging

data and entering data into the new computer log record system.

The Control Room foreman (CRF) was also performing duties in the control room at

a desk directly behind the HCO. The Shift Supervisor (SS-SRO) had previously left

the control room for a meeting.

At 0808 pressurizer pressure

began to increase from 2235 psig, unnoticed by the

HCO and CRF, and continued to increase until at 0816 it reached 2335 psig and a

power-operated

relief valve (PORV)-430 opened.

During that time period, operators

did not observe and/or acknowledge

a plant process computer system (PPCS) alarm

denoting a high pressure warning for pressurizer pressure,

main control board

indication denoting pressurizer backup heaters energized, and instrumentation

showing increasing pressurizer pressure.

The six PPCS alarms that came in were

annunciated

by a one second audible alarm and a small blinking red light in the

upper right corner of the three PPCS monitors located in the control room. The

overhead annunciator for pressurizer high'pressure

at 2310 psig did not alarm

apparently due to an ongoing malfunction in the automatic pressurizer pressure

control system.

An annunciator did alarm at 2335 psig when the PORV opened.

Interviews with operators. confirmed that the reactor coolant system (RCS) pressure

increase went unnoticed until the PORV opened and the main control board alarms

came in. Also, operators were fully aware of the IRC calibration in progress.

Responding to the overhead annunciator, the HCO by 0817 had placed pressurizer

pressure control in manual and adjusted pressure until the backup heaters were

deenergized.

The CO returned from the restroom and was the first operator to observe that PPCS

had alarmed denoting high pressurizer pressure

and the PORV had opened and

reclosed.

The CO informed the other operators of the indications and continued to

monitor plant parameters

as required.

The HCO placed manual pressurizer spray in

service to lower pressure

and by 0822 pressurizer pressure was restored to 2235

psig.

Pressurizer pressure control remained in manual to commence

evaluation/troubleshooting

of the event.

The operators followed up their immediate

response

by referencing procedure AP-PRZR.1, "Abnormal Pressurizer Pressure," to

ensure all appropriate actions had been taken.

RGS.E Ginna Station Procedure 0-6, Revision 63, "Operations and Process

Monitoring," step 5.3.3.1, requires that operators acknowledge all computer alarms

and take appropriate actions.

Station Procedure A-52.11, Revision 8, "Conduct of

Activities in the Control," requires that on-shift operators maintain awareness

of

pertinent plant instrumentation.

Reactor operators did not respond to PPCS alarms

in a timely manner, nor did they monitor control board indication adequately as

required by these procedures.

The operators'ailure to adhere to these procedures

is a violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures

and

Drawings."

Conclusions

The IRC calibrations were well coordinated with the operators prior to the event.

Operators had alarms, indications, and time to respond to the pressurizer pressure

increase before the PORV opened.

The event was due to operator failure to monitor

the control boards and respond to alarms in accordance with established

procedures.

This was a violation of NRC requirements.

{VIO50-244/98-02-01)

After the control board alarms came in, the operators took prompt and effective

actions to reduce pressurized

pressure

and stabilize the plant.

I

01.2

Licensee Event Review 93702

a.

Ins ection Sco

e

The inspectors reviewed the appropriateness

of internal facility notifications, event

analysis, and corrective actions.

Also, the inspectors discussed the event with

RG &E management.

b.

Observations

and Findin s

RG&E management

response was quick to direct troubleshooting the instruments,

but appeared to be slow in reviewing the human performance aspects of the event.

The licensee initiated an ACTION Report (98-0334) on March 3rd and started on

HPES review on March 5th.

Initial troubleshooting indicated that the Pressurizer

Pressure

Defeat Switch P/429A had malfunctioned.

The licensee's review was still

in progress at the end of this inspection.

The results and corrective actions will be

reviewed in a future NRC Inspection.

It was evident to licensee management

soon after the event that operators

responded

inadequately to the plant computer alarms and had not monitored

pressurizer pressure

on the main control board.

However, a prompt review of the

human performance aspects was not initiated until 24-hours after the event

occurred.

Also, it appeared that RG&E management

did not assure that operator

performance was appropriately remediated in a timely manner to assure that

operator attentiveness to main control room indications met management

expectations.

C.

Conclusions

RG&E management

response was quick to address the plant equipment technical

aspects of the pressurizer pressure transient, but apparently slow to address the

inadequate

human performance aspects of the event.

Facility follow up actions will be reviewed in a future inspection.

(IFI 50-244/98-02-

02)

01.3

Safet

Si nificance 93702

.

a.

Ins ection Sco

e

The inspectors evaluated the increase

in risk and the safety consequences

of the

event of March 3, 1998, considering plant systems response

and operator actions.

b.

Observations

and Findin s

The safety importance of this event was that it unnecessarily challenged the PORV

and therefore, contributed to the probability of having a small break loss of coolant

accident.

This could occur if there were a combined failure of the PORV and its

block valve to close.

During this actual event, which was within the plant's design.

basis, one PORV opened for a short time and reseated without leaking.

There were

no adverse consequences.

C.

Conclusions

The PORV liftwas a design basis event with no adverse consequences.

There was

no significant increase

in risk. The event was an unnecessary

challenge to the

PORV.

E9

Review of Updated Final Safety Analysis Report {UFSAR)

The inspectors verified that the Pressurizer Pressure

Control System as described in

section 7.7.1.3.1 of the Ginna UFSAR was accurate.

V. Mana ement IVleetin s

X1

Exit Meeting Summary

RGSE was informed of the scope and purpose of this inspection at an entrance meeting on

March 5, 1998. An exit was conducted by telephone on March 12, 1998.

RGSE

acknowledged the findings identified during the inspection.

They noted that they were

considering the human performance aspects but had probably not communicated this well

to NRC staff during the early post event stages.

PARTIALLIST OF PERSONS CONTACTED

Rochester Gas 5 Electric

R. Mecredy

R. Marchionda

J. Widay

G. Wrobel

R. Smith

T. Harding

T. Laursen

A. Jones

G.

Cain

K. McLaughlin

J.

Banke

S. Stinson

K. Moynihan

K. Garnish

J.

Hamm

T. Fouts

Vice President,

Nuclear Operations

Production Superintendent

Plant Manager

Nuclear Safety S. Licensing Manager

Senior Vice President,

Energy Operations

Senior Licensing Engineer

Operating Experience Engineer

0'perating Experience Engineer

System Engineer

Shift Supervisor

System Engineer

ISC Foreman

IRC Technician

Control Room Foreman

Control Room Operator

Head Control Operator

INSPECTION PROCEDURES USED

IP 93702, Prompt Onsite Response to Events at Operating Power Reactors

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-244/98-02-01

50-244/98-02-02

VIO

Failure to monitor control room panels and attend to alarms

IFI

Review the licensee's event review'and corrective actions for

the pressurizer pressure transient.

EVENT DESCRIPTION

Alltimes on March 3, 1998

NOTE:

Times and values are approximate and based on computer alarm reports and

chart recorder interpretation.

0731

IRC technicians began calibration procedure CPI-TRIP-TEST-5.30, "Reactor

Protection System Trip Test/Calibration for Channel 3 Bistable Alarms."

0808

Pressurizer backup heaters energized; indicated by a red light illuminated on

main control board.

Pressurizer pressure

begins to increase from 2235 psig

as indicated on main control board instrumentation (indicators and recorder),

0810

Plant Process Computer System (PPCS) alarmed when pressurizer pressure

increased to 2260 psig. A total of 4 alarms were received, one for each of

the 3 remaining valid pressure channels and

1 for average pressurizer

pressure.

0812

PPCS alarmed when pressurizer pressure increased to 2285 psig.

0814

PPCS alarmed when pressurizer average pressure increased to 2310 psig.

Main control board overhead annunciator F-2, PRESSURIZER HIGH

PRESSURE, failed to annunciate at its set point of 2310 psig.

0816

Pressurizer pressure

increased to 2335 psig.

PORV 430 opened and

reclosed about two seconds later.

Main control board overhead annunciators

alarmed for PRESSURIZER HIGH PRESSURE, PRESSURIZER RELIEF TANK

(PRT) HIGH PRESSURE, and PORV OUTLET HIGH TEMPERATURE (expected

due to PORV lift). Pressurizer pressure initiallydecreased to 2315 psig and

began to rise after the PORV closed.

0817

Operators took manual control of pressurizer pressure,

deenergized

backup

heaters,

and began to reduce pressurizer pressure

using spray.

0822

Pressurizer pressure restored to 2235 psig.