ML17251A390

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Insp Rept 50-244/88-22 on 881017-1120.Violations Noted.Major Areas Inspected:Station Activities,Including Operational Safety Verification,Plant Operations,Surveillance Testing, Maint,Radiological Protection & Physical Security
ML17251A390
Person / Time
Site: Ginna Constellation icon.png
Issue date: 12/07/1988
From: Cowgill C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17251A388 List:
References
50-244-88-22, NUDOCS 8812150080
Download: ML17251A390 (22)


See also: IR 05000244/1988022

Text

U.S'.

NUCLEAR REGULATORY COMMISSION

REGION I

Report

No.

50-244/88-22

Licensee

No.

DPR-18

Priority

Category

C

Licensee:

Rochester

Gas

and Electric Corporation

49 East Avenue

Rochester,

New York

Facility

R.

E. Ginna Nuclear

Power Plant

Location:

Ontario,

New York

Inspection

Conducted:

October

17 through

November 20,

1988

Inspectors:

Approved by:

C.

S. Marschall,

Senior Resident

Inspector,

Ginna

N.

S. Perry,

Resident. Inspector,

Ginna

t

C.

.

ow

Chief, Reactor

Projects

Section

1A

Date

~Summar

A~Id. II

I <<I

A

Id

ties including plant operations,

operational

safety verification, surveillance

testing,

maintenance,

radiological protection,

physical security, written reports,

periodic and.special

reports,

action

on previous inspection findings, loss of

security surveillance capability,

housekeeping,

equality

Assurance

program imple-

mentation,

intra-company

communications,

licensee

control of modifications,

con-

tainment temperature

profiles,

and surveillance activity review.

d

Results:

Two violations were identified;

one concerning failure to perform safety

evaluations

as required

by 10 CFR 50.59 (section

3) and another concerning failure

'o

maintain

a radiation area

locked (section 2.e).

An additional

example of fail-

ure to adhere

to procedures

is discussed

(section 2.c).

Discovery of an inatten-

tive guard by the, Senior Resident

Inspector is discussed

(section 2.f).

Two pre-

viously identified inspector followup items were closed (se'ction 5).

Licensee fai lu're to perform safety evaluations

has

been

an

NRC identified concern

for more than twenty months,

and is indicative of a programmatic

weakness

in the

control of station modifications.

The additional

example of procedural

nonadher-

ence indicates

a licensee inability to take effective immediate corrective'action

for a previously identified deficiency; other examples

were contained

in inspection

reports 50-244/88-05,

88-15,

88-16 (multiple examples)

and 88-19.

'Appropriate

and

timely.action by an operator

prevented

a plant transient,

and is indicative of safe

and effective control of plant operation.

Several

minor weaknesses

related to

personnel

safety were identified during

a maintenance'ctivity

which was, overall,

carefully controlled.

Efforts to improve plant cleanliness

culminated in opening

the Auxilliary Building to access

in street clothing and construction for a con-

taminated

storage building, intended to allow further improvement in plant clean-

liness,

began

on November 7,

1988.

~,-.i2 i 500<0 88i207

PDR

ADOCK 05000244

PDC

DETAILS

1.

Persons

Contacted

During this inspection period,

inspectors

held discussions

with and inter-

viewed operators,

technicians,

engineers

and supervisory

level personnel.

The following people

were

among those contacted:

"S. T. Adams,

Technical

Manager

J. C..Bodine,

Nuclear Assurance

Manager

~R.

A'. Carroll, Training Manager

"E.

C. Edgar,

Manager of Planning

and Scheduling

D.

L. Filkins, Manager of HP

8 Chemistry

  • R. A. Marchionda, Director of Outage

Planning

'T. A. Marlow, Superintendent,

Support Services

"J.

T. St. Martin, Corrective Action Coordinator

"R.

C. Mecredy,

General

Manager,

Nuclear Production

  • A. G. Morris, Maintenance

Manager

"T. R.. Schuler,

Operations

Manager

L.

F. Smith, Operations

Supervisor

"S.

M. Spector,

Superintendent,

Ginna Station

J.

A. Widay, Superintendent,

Ginna Production

  • R.

E.

Wood, Superv'isor,

Nuclear Security

'Denotes

persons

present at exit meeting

on November 28,

1988.

2.

Functional

or Pro

ram Areas Ins ected

Review of Plant

0 erations

(71707)

The plant operated at full power throughout the inspection period.

On

November 4,

1988

a. worker's outer clothing accidentally caught

on the

Cable Tunnel fire system's

manual pull station.

Several

thousand

gal'lons

of firewater was sprayed into the area resulting in a ground

on

a non-

safeguards

480 volt bus.

The control

room received the fire alarm, but

fire brigade

members

were unable to verify no fire existed within ten

minutes,

therefore

an Unusual

Event was declared.

The Unusual

Event was

terminated

twelve minutes later when it was determined

no fire existed.

On November

11,

1988 Flow Instrument (FI) 465,

sensing

steam flow in the

"A" Steam Generator,

failed high.

A Steam

Flow/Feedwater

Flow mismatch

was created

since

FI 465 was the controlling steam flow channel

at the

time.

The operator

immediately placed

feedwater

control in manual,

pre-

venting

a plant transient;

he selected

the alternate

channel

of flow

indication for th'e 'A'team Generator,

and restored

feedwater control

to automatic.

Early on November

15,

1988,

an electrical fire in onsite security equip-

ment caused

a. temporary loss of security surveillance capabilities

(see

section 2.i and Inspection

Report 50-244/88-24).

Later on November

15,

1988,

the Senior Resident

Inspector

discovered

a

guard inattentive to duty at an observation

post (see

section 2.f).

0 erational

Safet

Verification (71707)

On

a daily basis,

inspectors

observed shift turnover

and conduct of

operations

in the control

room.

Proper c'ontrol

room staffing was main-

tained

and control

room access

was controlled.

Operators

were attentive,

responsive

to plant parameters

and conditions,

and adhered

to approved

procedures'for

ongoing activities.

Control

room log books were reviewed

to obtain information concerning activities and out-of-service

equipment

and use of overtime

was audited for compliance with licensee

and regula-

tory requirements.

On

a weekly basis,

the inspectors

checked

an Engineered

Safety

Feature

System train for operability.

The following were verified: accessible

valves in the flow path in proper position; proper

power supply and

breaker alignment,

and appropriate

MOVs deenergized.

Additionally,

trains were inspected for leakage,

lubrication, cooling and general

con-

dition.

The inspectors

regularly toured all accessible

areas

of the plant and

observed

general

conditions of,the plant and equipment, potential'fire

hazards,

control of activities in progress,

control of housekeeping

and

the presence

of potential missile hazards.

Biweekly the inspectors

reviewed the sampling program,

the problem iden-

tification systems,

and

one safety-related

tagout for proper implementa-

tion.

In addition, the inspectors verified correct lineup of a portion

of, the containment isolation

system

and proper posting of required

notices.

No conditions adverse

to safety were identified.

Monthl

Surveillance Observation

(61726)

Inspectors

observed portions of surveillance test procedures

to verify

test instrumentation

was properly calibrated,

approved

procedures

were

used,

work was performed

by qualified personnel.,

Limiting Conditions for

Operation

were met,

and the system

was correctly restored

following

testing.

The following surveillance activity was observed:

Periodic Test (PT)-2.7,

Revision 42, "Service Water System", effec-

tive date

September

12,

1988,

observed

November 3,

1988.

During performance of PT-2.7,

the inspectors

observed

Results

and Test

- personnel

had unlocked valves to be manipulated during the surve'illance

at the start of the procedure;

the procedure

does not provide guidance

for locking or unlocking the valves.

In the body of the procedure

the

Results

and Test personnel

are required to sign

a step

as completed which

verifies certain valves are locked.

Since the valves were unlocked near

the beginning of the procedure,

the personnel

incorrectly signed the step

with the valves unlocked.

The inspectors

brought this to the attention

of department

and plant management.

Department

management

has already

addressed

the problem by meeting with Results

and Test personnel

and

discussing

the unacceptable

practice of. unlocking the valves at the be-

ginning of a procedure.

Additionally, procedures will be changed

to

describe specifically when to unlock and lock valves.

Licensee control of this surveillance activity was considered

adequate

to insure operability.

Monthl

Maintenance

Observations

(62703)

The. inspectors

observed

portions of various safety-related

maintenance

activities to determine

redundant

components

were operable, activities

did not violate Limiting Conditions for Operation,

required administra-

tive approvals

and tagouts

were obtained prior to initiating work, ap-

proved procedures

were

used or the activity was within the "skills of

the trade",. appropriate

radiological controls were implemented,

igni-

tion/fire prevention controls were properly implemented,

and equipment

was properly tested prior to 'returning it'o service.

Maintenance

(M)-38. 1 "Repair or Replacement

for W-2 switch

1B, Boric

Acid Transfer

Pump" revision 7, effective date August 12,

1988,

observed

November 9,.1988.

Overall,

removal

and replacement

of the'witch was

a carefully controlled

process.

However,

several

minor weaknesses

were observed during the

process'se

of "N/A" for procedure

signoff was inconsistent

in completing the

procedure.

Step 3.4 which requires

a Special

Work Permit

be obtained,

if required,

was marked "N/A" without specific guidance to do so.

Step

5.6,. restoration of wires

on the

new switch provides this step

be marked

"N/A" if the previous

step to remove the wires was not performed;

Main-

tenance

management

indicated

use of "N/A" was considered

acceptable

for

any procedure

step containing the words "if" or "or".

Review of main-

tenance

procedures

revealed

several

steps

containing the words "if" or

"or" where the*use of "N/A" was not intended

by the licensee.

Use of

"N/A" without providing the specific circumstances

which allow its use

fosters interpretation of procedures

by the

end users;

as

a result,

con-

trol of the maintenance activity is not assured.

The use of "N/A" with-

out specific guidance is considered

a weakness

in the licensee's

control

of safety-related

maintenance.

Removal of the control switch was accomplished

without checking switch

terminals for'oltage.

Although the .electricians

wore leather gloves

when possible,

removal

and restoration of the wires terminated

on the

switch was accomplished without a glove due to the nature of the work.

The switch was tagged out as required

by procedure;

however

a recent

instance of electricians at Ginna beginning work on the wrong ventilation

motor illustrates

the benefit of insuring

no voltage is present prior

to commencing work on electrical

equipment.

The inspectors

were sur-

prised to learn that senior station

management

and

some electricians

were

unaware of work on the wrong ventilation motor, which involved 480 volt

equipment

and the potential for loss of life.

The inspectors will moni-

tor licensee efforts to improve timeliness of dissemination

of informa-

tion important to safety.

guality Control

(gC) signoffs were not used consistently

in the procedure.

A gC signoff was

used to insure all wires

on the switch were properly

labelled prior to removal.

However,

no gC signoff was evident to verify

wires were placed

on the proper terminals during restoration.

The

gC

inspector

and the electrician performing the'aintenance

noted the

need

for the signoff; the electrician .stated his intent to submit

a procedure

change

to incorporate

gC verification of wire restoration.

Licensee control of these activities was adequate

to ensure

component

operability.

h

Radiolo ical Protection

Review (71707)

During this inspection period,

the resident

inspectors periodically

verified

RWPs were

implemented properly, dosimetry

was correctly worn

in controlled areas

and dosimeter

readings

were accurately

recorded,

access

control, at entrances

to high radiation areas

.was adequate,

per-

sonnel

used contamination

monitors

as required

when exiting controlled

areas,

and postings

and labeling were in compliance with regulations

and

procedures.

During

a tour of the Auxiliary Building basement

on November 9,

1988,

the inspectors

discovered

the gate barricading the area

behind the Re-

fueling Water Storage

Tank

(RWST) unlocked.

A survey dated October-4,

1988- indicated radiation levels less

than

500 mrem/hr. general

area

and

smearable

contamination

less

than

1400 dpm/100

sq

cm.

Administrative

procedure A-l.1,

Locked Radiation Areas, revision

19, effective March

'5,

1988,

step 3.4.6 requires

each

locked high radiation wi 11

be locked

to prevent unauthorized

entry except while individuals are inside .or

surveillance is maintained at the gate.

At the time of discovery,

the

gate

had been

unlocked for approximately twenty-four hours.

This is apparently

an isolated

instance;

the inspectors routinely verify

barricades

are locked as

a part of plant tours

and

have not previously

"identified an unlocked b'arricade during this

SAL'P period.. Upon noti-

fication, the licensee

immediately surveyed'the

area

found unlocked,

8

confirmed the area*was

not actually

a high radiation

and locked the bar-

ricade.

The licensee

also determined

the door was not intentionally left

unlocked.

Initial corrective actions

planned

included frequent

checks

of high locked radiation area

doors to insure

none are unlocked, adjust-

ment or replacement

of springs

and general

inspection of the door found

unlocked.

Long term corrective actions

planned include

a feasibility

study for installation of local alarming devices

and general

inspection

of all locked high radiation doors.

As described

in

10 CFR 2, Appendix C, section V.A., as

amended

on October

14,

1988,

no Notice Of Violation (NOV) will be issued for this violation

since it is considered

an isolated

instance,

corrective action

has

been

initiated,

and the violation has minor safety or environmental signific-

ance.

Accordingly,

a formal response

to this violation is not required.

NO VIOLATION (50-244/88"22-01).

Ph sical Securit

Review (71707)

During this inspection period,

the resident

inspectors verified x-ray

machines

and metal

and explosive detectors

were 'operational,

Protected

Area (PA) and Vital Area (VA) barriers

were well maintained,

access

con-

trol during security turnover was adequate,

personnel

were properly

badged for unescorted

or escorted

access

and compensatory

measures

were

implemented

when necessary.

During an inspection of the inside p'erimeter

fence

on November

15,

1988,

a guard in an observation

post

was observed

leaning against

the wall

while seated.

He remained motionless

as the inspectors

walked across

the guard's field of vision and tried to attract the guard's attention

by waving at him.

As the inspectors

approached

the post,

the guard was

coincidently interrogated

by radio,

and began.to

move about

as

he re-

sponded

to the radio.

When licensee

management

was notified of the in-

cident,

the guard

was immediately relieved of his post

and

an investiga-

tion was initiated.

The inspector determined that the post was

a security program

enhancement

and not a compensatory

measure for inoperable

equipment.

Corrective action,

including disciplinary measures

and retraining of the

guard,

were timely and appropriate.

Review of Written

Re orts of Nonroutine Events

(90712)

Written reports

submitted to the

NRC were reviewed to determine

whether

details

were clearly reported,

causes

properly identified and corrective

actions appropriate.

The inspectors

also determined

whether

assessment

of potential

safety consequences

had been properly evaluated,

g'eneric

implications were indicated,

events

warranted onsite follow-up, reporting

requirements

of 10 CFR 50.72 were applicable,

and requirements

of 10 CFR 50.73

had been properly met.

The. following L'ER was reviewed

and found to be satisfactory

(Note: date

indicated is event date):

88-009,

September

30,

1988,

"Inadequate

Fire Barrier Inspection

Procedure Identified Only Through Breaches

Causing Partial

Breaches

To Go Undetected".

No unacceptable

conditions were identified.

Review of Periodic

and

S ecial

Re orts (90713)

Upon receipt, periodic

and special

reports

submitted

by the licensee

pursuant to Technical Specifications 6.9. 1 and 6.9.3 were reviewed

by

. the inspectors.

This review included the following considerations:

re-

ports contained

information required

by the

NRC; test results

and/or

supporting

information were consistent

with design predictions

and per-

formance specifications

and reported

information was valid.- Within this

scope,

the following report was reviewed

by the inspectors:

Monthly Operating

Report for October

1988.

The report

was considered

adequate

to meet regulatory requirements,

Loss of Onsite Securit

Surveillance

Ca abilit

(71707)

On November

15,

1988 at 3:54 A.M., operators

received

an alarm indicating

loss of security Uninterruptible

Power Supply.

A guard, called to re-

spond to the alarm,

reported

heavy

smoke

from security electrical

equip-

ment.

Station Fire Brigade personnel

responded

at 3:56 A.M. and secured

electrical

power to security switchgear,

extinguishing the fire at 4:04

A.M.

Removing power from security switchgear

also caused

loss of all

onsite security surveillance

functions; the security shift supervisor

immediately stationeg

guards

to provide compensatory

measures

for loss

of surveillance capability and called the day shift in early as

a con-,

tingency measure.

Alternate

power was restored

to security electrical

equipment

and compensatory

security measures

were terminated at 5:31 A.M.

\\

Follow-up by the licensee,

vender representative,

and

NRC revealed

the

fire detection

system for the area

was poorly designed.

Although the

licensee will correct the design deficiency it was pointed out that the

licensee relies

on fire brigade

members to manually actuate

the

system

if required.

Auxiliary operators

and security guards

make

up the fire

brigade;

questioning

by the resident

inspectors

revealed

operators

and

guards

received

adequate

training

on manually actuating fire systems.

Licensee

actions during the event were adequate,

appropriate

and per-

formed within a reasonable

amount of time.

~Hk

(7

7 7)

Major portions of the Auxiliary,and Intermediate

Buildings were opened

to access

in street clothes

on October 31,

1988.

All floor areas,

walls

and equipment

from the floor to 8 feet above the floor are clean unless

otherwise

posted.

Additionally, floors and walls are being painted

and

the licensee

is evaluating lighting in various areas

for potential

im-

,provements.

A new Auxiliary Building addition is currently under construction just

south of the Auxiliary Building.

Construction

began

on November 7,

1988

and turnover to the licensee

is targeted for March 1,

1989.

The addition

will be

used

as

a contaminated

storage building where contaminated

tools,

equipment

and

shutdown

staging will be stored.

The residents will monitor construction

progress

and

use .of the

new

storage building in addition to the effect of opening

the Auxiliary and

Intermediate

Buildings on activities and

management

tours in future in-

spection reports.

ualit

Assurance

Pro

ram

Im lementation

(71707)

On November

9,

1988,

a guality Control

(QC) inspector

was monitored while

conducting surveillance of electricians

replacing

a control. switch for

the 'A'oric Acid Transfer

Pump (see

section 2.d).

At the conclusion

of the maintenance activity, the

gC inspector discussed

his observations

with the= electricians

performing the activity.

Significant obs'ervations

included lack of a

gC signoff in the procedure

to insure wires removed

were restored

to the correct terminals

and failure of the electricians

to check the switch for voltage prior to beginning work.

The

gC surveillance

was adequate

to assure quality of the maintenance

activity.

Intra-com

an

Communications

On October

31,

1988,

the licensee

began

use of a unique method to com-

municate important information to all plant employees.

The system uti-

lizes

a combination of 6 closed-circuit monitors located throughout the

plant,

a personal

computer

and high quality computer-generated

graphics.

The

new system will inform employees of cur rent work activities, assign-

ments, training, safety,

regulations

and other miscellaneous

information.

Any employee

can submit material for use

on the system;

however,

the

plant manager or either plant superintendent

must give final approval

before material is used.

The system is updated

several

times during the

day to keep information current.

The inspectors will periodically moni-

tor the system's

effectiveness

to communicate

messages

efficiently and

accurately

to station personnel.

Licensee

Control of Modifications (71707)

A history of licensee

weakness

in the area of 10 CFR 50.59 reviews

has

been

documented

in inspection reports

over

a period of more than

20 months;

a

Notice of Violation (NOV) contained in Inspection

Report 50-244/87-04

docu-

mented failure to perform

a

10 CFR 50.59 review of lead shielding;

inadequate

10 CFR 50.59 reviews were discussed

at the exit meeting for Inspection

Report

50-244/87-23;

an unresolved

item in Inspection

Report 50-244/88-08

documented

lack of reviews to meet the requirements

in 10 CFR 50.59;

Inspection

Report

50-244/88-15

documented

licensee failure to perform reviews of modifications

to the Condensate

Storage

Tanks

(CST) and Spent

Fuel

Pool

(SFP)

as required.

by 10 CFR 50.59;

and

an update of open

item 50-244/88-08-01

in Inspection

Re-

port 50-244/88-19

documented

licensee efforts to meet the requirements

of 10 CFR 50.59 were,

as yet, incomplete.

During 'this inspection period the inspectors

reviewed licensee

documents

in

response

to the

CST safety concerns

raised in Inspection

50-244/88-15,

10 CFR 50, Appendix B, section III requires,

in part,

measures

shall

be estab-

lished to assure

appropriate quality .standards

are specified

and included in

,design

documents,

and deviations

from such standards

are controlled.

The

guality Assurance

Manual

Ginna Station,

section

3. step 3. 1.3 requires

modi-

fications involving a change

to the facility as described

in the Updated Final

Safety Analysis Report

(UFSAR) have

a safety evaluation

in accordance

with

10 CFR 50.59..

10 CFR 50.59 requires,

in part, the licensee

shall maintain

records of changes

in the facility as described

in the safety analysis report

and of changes

in procedures

as described

in the safety analysis report,

and

these

records

shall include

a written safety evaluation

which provides the

bases for determination that the change

does

not involve an unreviewed safety

question.

Licensee

records for the addition of local level indication to the

'ST

were inadequate

because

they did not provide the bases for concluding:

(i) the probability of occurrence

or the consequences

of an accident or mal-

function of equipment

important to safety previously evaluated

in 'the

UFSAR

will not be increased;

or (ii) the possibility for

an accident or malfunction

of a different type than

any evaluated

previously in the

UFSAR will not be

created;

or (iii') the margin of safety

as defined in the basis for any tech-

nical specification will not be reduced.

Moreover, the technical

evaluation

did not state

these

conclusions

had bqen reached.

Nonetheles's,

on October

4, 1988, modifications were

made to the

CST to provide tank level indication

utilizing-tygon tubing.

This is

a violation (VIO 50-244/88-22-02).

A licensee

document dated October 25,

1988,

"Design and Modification Guide-

lines for the Condensate

Storage

Tanks (CST)" classifies

the

CSTs

as "safety-

related

non Seismic Category I" equipment.

The document also states: "It is

apparent that good commercial-grade

engineering

practices

should

be used for

activities which could affect the tanks.'he

attachments

to the tanks,

such

as copper tubing, commercial quality valves,

and tygon hose (to fulfill a

specific Appendix

R function) are considered

acceptable,

as standard

commer-

cial practice."

The document further states:

"Additions of attachments

do

have to be evaluated

to ensure

no adverse effect would occur

on the ability

of the

CSTs to meet regulatory commitments."

10

Although the licensee is apparently

aware of the importance of the

CSTs to

safety,

as the main source of water for the Auxiliary Feedwater

system,

(UFSAR,

section

10.5.2)

~

Service Mater,

a seismically qualified safety-related

source

of water,

can

be used to supply the Auxiliary Feedwater

system only after

a

normally locked closed

manual

valve and

a normally closed motor operated

valve

are

opened.

The

UFSAR states,

in part,

the Auxiliary Feedwater

system is an

Engineered

Safety Feature

because it provides

a secondary

heat sink for resi-

dual heat removal; it therefore provides core protection

and prevention of

reactor coolant release

through the pressurizer relief valves.

Licensee re-

view does not address

whether

use of good commercial-grade

engineering

prac-

tices meets

the requirements

of General

Design Criterion

(GOC) 34

Residual

Heat Removal,

which states,

in part, suitable

redundancy

in components

and

features,

and suitable interconnections,

leak detection,'nd

isolation cap-

abilities shall

be provided to assure

the system,,safety

function can

be ac-

complished,

assuming

a single failure.

Technical

evaluation for installation

of tygon tubing,

and installation of copper piping to provide water for the

station

laundry, for which a technical

evaluation

had not been provided at

the end of the inspection period, illustrate the licensee

remains

unable to

adequately

control modifications to the plant as described

in the

UFSAR and

as required

by 10 CFR 50, Appendix B, the Ginna Quality Assurance

Manual,

and

10 CFR 50.59.

Containment

Tem erature Profiles (71707)

Containment

temperatures

for the period June

1987 through September

1987 were

reviewed to determine

average daily containment

temperature.

Copies of page

9 of Surveillance

procedure

S-12.4,

RCS Leaka

e Surveillance

Record Instruc-

tions, containing individual and average

containment

temperatures

taken

each

shift, were obtained for all days during the period when average

containment

temperature

exceeded

100 degrees

Fahrenheit.

Peak average

temperature

of

111.23 degrees

Fahrenheit

was reached

on August 18,

1987.

A copy of a con-

trolled drawing showing the location of the containment

Resistance

Temperature

Detectors

used to obtain containment

temperatures

was provided by the licensee.

This information was provided to

NRR for its review.

The inspectors

had

no further questions.

Action on Previous

Ins ection Findin

s (92701)

'Clcised

Ins ector Follow-u

Item

83-03-01

.

Inspection report 50-244/88-03

documents

licensee

commitment to install Safety Injection (SI)

pump suction

gauges.

Engineering

Mork Request

4675 controls the installation of the gauges,

and is scheduled for completion during the

1989 refueling outage.

Installa-

tion of the gauges will be monitored

as part of the normal inspection

program.

This item is closed.

+Closed

Unresolved

Item

88-08-01

.

This item documents

licensee failure

to perform adequate

reviews

as required

by 10 CFR 50.59.

Section

4 of this

report'documents

a violation of the requirements

of 10 CFR 50.59;

licensee

actions to meet the requirements

of 10 CFR 50 '9 will be addressed

in response

to the violation, therefore this item is administratively closed.

6.

Exit Interview (30703)

At peribdic intervals during the inspection,

meetings

were held with senior

facility management

to discuss

inspection

scope

and findin'gs.

During this inspection period,

two violations were identified;

one concerning

~failure to perform safety evaluations

as required

by 10 CFR 50.59, for which

a Notice of Violation (NOV) was issued,

and another concerning failure to

maintain

a radiation area

locked, for which no

NOV was issued.

Inspectors

also noted

an additional

example of failure to adhere to procedures.

In addition, discovery of an inattentive guard

by the Senior Resident'nspec-

tor is discussed,

and two previously identified inspector followup items were

closed.

Based

on

NRC Region I review of this report and discussion

held with licensee

representatives,

it was determined this report does not contain information

subject to 10 CFR 2.790 restrictions.