ML17244A521
| ML17244A521 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 05/08/1979 |
| From: | Depew L ROCHESTER GAS & ELECTRIC CORP. |
| To: | |
| Shared Package | |
| ML17244A520 | List: |
| References | |
| MOR-790430, NUDOCS 7905220227 | |
| Download: ML17244A521 (10) | |
Text
OPERATING DATA REPORT DOCKET NO.
50 244 DATE
~ay 8, 1979 COMPLETED BY LEWIS DEP
~ OPERATING STATUS 1
- 1. Unit Name:
GINNA STATION U
- 2. Reporting Period:
- 3. Licensed Thermal Power (MWt):
- 4. Nameplate Rating (Gross MWe):
- 5. Design Electrical Rating (Net MWe):
- 6. Maximum Dependable Capacity (Gross MWe):
- 7. Maximum Dependable Capacity (Net MWe):
490 470 TELEPHONE 1-716-546-27pp Ext. 291-205, at Ginna Low Power Physics Testing after refueling-were completed and Unit placed on line 4-3-79 for power physics testing and continued operation.
- 8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level to Which Restricted, If Any (Net MWe):
- 10. Reasons For Restrictions, If Any:
This Month Yr.-to-Date Cumulative
- 11. Hours In Reporting Period
- 12. Number of Hours Reactor Was Critical
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Gcncrator On-Line
- 15. Unit Reserve Shutdown Hours
- 16. Gross Thermal Energy Generated (MWH)
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical Energy Generated (MWH)
- 19. Unit Service Factor
- 20. Unit AvailabilityFactor
- 21. Unit Capacity Factor (Using MDC Net)
- 22. Unit Capacity Factor (Using,DER Nct)
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Months (Type, 719 696.09 22.91 656.5 2,879 1,682.17 22.91 1 617.25 856,560 287,845 272,664 91.3%
91.3%
80.69%
80.69%
0%
2 263 416 760 836 722 230 56.17%
56.17%
53.37%
53.37%
0/
None Date and Duration of Each):
83,033.45 62,884.59 1 569.42
- 61 195.88 8.5 81 193 330 26 334 076 24 923 268 74.06%
74.07%
66.765%
66.765%
10%
- 25. If Shut Down At End Of Rcport.Period, Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operation):
~
INITIALCRITICALITY 7
INITIALELECTRICITY COMMERCIALOPERATION
- Cumulative Data Commencing-January 1,
1975 Forecast Achieved 49 dd (RLVa I/76) 7 V905 aaO Z<7
0 l()
2 )+
P>>
L AVERAGE DAILYUNIT POWER UNIT hIONTH P
DAY AVERAGE DAILYPOWER LEVEL (hIWe-Net) 19 DAY,AVERAGE DAILYPOWER LEVEL (MWe-Net) 451 17 18 450 450 DOCKET NO.. 50 244 UNIT N1 @irma Statio DATE Ma 8
1979 COMPLETED BY LEWIS DEPEW TELEPHONE 1-716-546-2700 Ext. 291-205, at Gonna 10 12 13 14 15 16 94 242 339 352 430 445 450 442 450 450 450 450 451 20 21 22 23 24 25 26 21 28 29 30 31 449 450 451 450 450 450 450 452 452 451 452 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month..
Compute to the nearest whole megawatt.
40 87 (RCV, 1/78)
E f
~ri
4 DOCKET NO.
Nl Ginna Station UNIT SHUTDOWN AND POWER REDUCTIONS COMPLETED BY LEWIS DEPEW REPORT hlONTH TELEPHONE
0 Ext. 291-205, at Ginna No.
Date 0
I-0 I
o o X n ~
CV c0 oe tY e s-0 c u 0
ou7 c 0n Licensee Event Report 5
Ew-0 e
IA 0 u7 cO u7 c
Q u0 (J
Cause 8 Corrective Action to Prevent Recurrence 790210 790409 S
62.5
=512 A-B HH, VALVEX Low power,physics testing was completed after refueling, unit placed on the line on 4-3-'79 for continued physics testing and power operation.
Annual overhaul of "A" Condensate Pump still in progress, "B" Conden-sate
'Pump Discharge. Valve position limited 'condensate pressure and feedwater flow.
790411 5.5 A
EB RELAYX Hain transformer cooling fan relay failure.,
F: Forced S:
Scheduled 49.89 tRKV 8/78)
Reason:
A-Equipment Failure (Explain)
B-hlaintenancc or Test C-Refueling D-Regulatory Restriction E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain) hlethod:
1-hlanual 2-hlanual Scram.
3-Automatic Scram.
4-Other (Explain) 4 Fxhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)
Exhibit 1 - Same Source
4 NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
0-2 UNIT Ginna Station Unit b'1 DATE COMPLETED BY LEWIS DEP MONTH A ril 1979 TELEPHONE 1-716-546-2700 Ext. 291-205, at Ginna Low power physics testing were completed and unit was placed on the line on April 3.
Turbine tests and physics testing were completed as power was escalated.
At 98% power, the condensate bypass valve
- opened, power was reduced to 92%.
The low condensate pressure was due to the "A" condensate pump still undergoing annual overhaul and the discharge valve of the "B" condensate pump was not in the full open position due to a faulty position indicator.
On,Apiil 11, a
relay on the main transformer fan coolers failed, load reduction was started and terminated when the fan coolers were reinstalled.
Operation at 92% continued due to condensate pump maintenance.
49 I'23 0/78)
'4 s
0 GINNA STATION MAINTENANCE REPORT FOR APRIL, 1979 During April, normal inspection and minor maintenance was performed.
Major safety related maintenance included:
1.
Replacement of a faulty bistable on Overpressure Protection Channel 452.
2.
Replacement of a bad batch board on Boric Acid Flow Channel 110.
3.
Replacement of a damaged valve diaphragm on the containment radiogas/particulate monitor pump return to containment.
4.
Repair to the flow control valve FCV llOA for the normal flow path from the Boric Acid Tanks to the Reactor Coolant System.
5.
Replacement of a leaking 3 1/2" long piece of pipe adjacent to FCV llOA.
In addition, the check valve next to this piece of pipe was also replaced as a preventive measure.
4
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