ML17227A412

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Insp Repts 50-335/92-05 & 50-389/92-05 on 920225-0323. Violations Noted.Major Areas Inspected:Plant Operations, Maint,Surveillance,Fire Protection Review,Review of Nonroutine Events & Followup of Regional Office Requests
ML17227A412
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 04/16/1992
From: Butcher R, Elrod S, Lesser M, Schin R, Michael Scott
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17227A410 List:
References
50-335-92-05, 50-335-92-5, 50-389-92-05, 50-389-92-5, NUDOCS 9205120083
Download: ML17227A412 (25)


See also: IR 05000335/1992005

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.IN.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/92-05

and 50-389/92-05

Licensee:

Florida Power

5 Light Co

9250 Nest Flagler Street

Miami,

FL

33102

Docket Nos.:

50-335

and 50-389

License Nos.:

DPR-67

and

NPF-16

Facility Name:

St. Lucie

1 and

2

Inspection

Conducted:

Februar

25 - March 23,

1992

I

Inspectors

r

, Senior

Ress

ent

nspector,

St. Lucie Site

M.

.

cott,

esi ent

nspector

D

eS

ne

II,/1Z.

at

Signed

u c

,

en>or

es)

ent

nspector,

Tur ey Point Site

e

gne

~. Lesser,

Se

or Resident

Inspector,

Nor h Anna Site

c

D

e

S gne

Approved by:

R.

P. Schin,

roject

ine

.

Lan ss,

Se

ion

C ief,

Division of Reactor Projects

Da

e Si

ned

z-

D te

igned

SUMMARY

Scope:

This routine resident

inspection

was

conducted

onsite in the

areas

of plant

operations

review,

maintenance

observations,

surveillance

observations,

fire

protection

review,

review of nonroutine

events,

followup of regional office

requests,

and followup of previous inspection findings.

Results:

This inspection

found that the licensee

operated

the

two units in

a routine

manner with obvious

regard for safety.

Minor events

occurring during the

period,

such

as

a loss of circulating water

pump

and

an

emergency

diesel

generator failure during testing,

received

prompt responses

consistent with the

9205120083

920022

PDR

ADOCK 05000335

9

PDR

event.

Maintenance

controls

were appropriate

for the various

maintenance

activities.

Followup inspection

to Service

Water Inspection

335,389/91-201

produced

enforcement findings which were issued with this report.

Within the areas

inspected,

the following violations were identified:

VIO 335,389/92-05-04,

Inadequate

Test of Intake

Cooling

Water

Pump,

paragraph

7d.

VIO 335/92-05-05,

Failure to Test Certain Valves quarter ly as

Required

by

the Inservice Test Program,

paragraph

7e.

Within the areas

inspected,

the following unresolved

item was identified:

URI 335,389/92-05-06,

Evaluation of whether

or

not Air Controls -for

Component

Cooling

Water

Temperature

Control

Valves

should

be Safety

Related,

paragraph

9e.

Within the areas

inspected,

the following non-cited violation was identified:

NCV 335,389/92-05-03,

Inadequate

Training Materials,

paragraph

7c.

Within the areas

inspected,

the following non-cited deviation

was identified:

NCD 335,389/92-05-02,

Failure to Maintain Submersible

Valve gualifications

as Described in the Final Safety Analysis Report,

paragraph

7b.

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

D. Sager, St. Lucie Plant Vice President

G. Boissy, Plant General

Manager

J. Barrow, Fire/Safety Coordinator

H. Buchanan,

Health Physics

Supervisor

C. Burton, Operations

Manager'.

Church,

Independent

Safety Engineering

Group

R. Dawson,

Maintenance

Manager

R. Englmeier,

Nuclear Assurance

Manager

R. Frechette,

Chemistry Supervisor

J. Holt, Plant Licensing Engineer

C. Leppla,

Instrument

and Control Supervisor

L. McLaughlin, Licensing Manager

G. Madden, Plant Licensing Engineer

A. Menocal,

Mechanical

Supervisor

T. Roberts, Site Engineering

Manager

L. Rogers, Electrical Supervisor

N. Roos,

Services

Manager

C. Scott,

Outage

Manager

M. Shepherd,

Operations

Training Supervisor

D. West, Technical

Manager

J. West, Operations

Supervisor

W. White, Security Supervisor

D. Wolf, Site Engineering Supervisor

E. Wunderlich, Reactor Engineering Supervisor

Chairman

Other

licensee

employees

contacted

included

engineers,

technicians,

operators,

mechanics,

security force members,

and office personnel.

NRC Employees

S. Elrod, Senior Resident

Inspector,

St. Lucie Site

M. Scott, Resident

Inspector,

St. Lucie Site

M. Lesser,

Senior Resident

Inspector,

North Anna Site

R. Butcher, Senior Resident

Inspector,

Turkey Point Site

R. Schin, Project Engineer, Division of Reactor Projects

  • Attended exit interview

Acronyms

and initialisms used

throughout this report are listed in the

last paragraph.

2.

Review of Plant Operations

(71707)

Unit 1 and Unit 2 began

and ended

the inspection period at power - days

91

and 473 of continuous

power operation, respectively.

During the inspection

period,

a number of

INPO personnel

were onsite for

two weeks conducting evaluat'ion activities.

During the inspection

period,

both the cognizant

NRC Region II Project

Branch Chief and the Deputy Director of the

NRC Region II Reactor Projects

Division visited the site.

a 0

Plant Tours

The

inspectors

periodically conducted

plant tours to verify that

monitoring

equipment

was

recording

as

required,

equipment

was

properly tagged,

operations

personnel

were aware of plant conditions,

and plant

housekeeping

efforts were

adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

were

properly

established,

critical clean areas

were being controlled in accordance

with procedures,

excess

equipment

or material

was stored properly,

and combustible materials

and debris

were disposed of expeditiously.

During tours,

the

inspectors

looked for the existence

of unusual

fluid leaks,

piping vibrations,

pipe hanger

and seismic restraint

settings,

various valve

and breaker positions,

equipment caution

and

danger

tags,

component

positions,

adequacy

of fire fighting

equipment,

and

instrument

calibration

dates.

Some

tours

were

conducted

on backshifts.

The frequency of plant tours

and control

room visits by site management

was noted to be adequate.

The inspectors

routinely conducted

partial

walkdowns of ESF,

ECCS,

and support

systems.

Valve, breaker,

and switch lineups

as well as

equipment

conditions were randomly verified both locally and in the

control

room.

The following accessible-area

ESF

system

and

area

walkdowns

were

made to verify that system lineups were in accordance

with licensee

requirements

for operability

and

equipment material

conditions

were satisfactory:

Unit 2

EDGs,

Unit I and

2 SFPs,

Unit I and

2 SFP

pumps

and heat exchangers,

and,.

Unit 2 Control

Room ventilation.

On

March

9,

1992,

while touring the Unit I B-train

4160 Volt

switchgear

room, the inspector

observed

that the

18

ICW breaker

had

been

removed from its switchgear

housing

and

was sitting unrestrained

in front of other safety-related

switchgear.

Based

on nuclear

industry

concerns

regarding

seismic qualification of safety-related

switchgear

with breakers

in racked-out

or

removed condition,

the

licensee

was informed that the

removed

breaker

should

be restrained

to prevent possible safety-related

switchgear

damage

during

a seismic

event.

The licensee

initiated

REA 92-104,

requesting

engineering

evaluation

of circuit breaker

seismic

loading/qualification

in

various positions

other than fully installed.

This issue will be

tracked

as

IFI 50-335,389/92-05-01,

Seismic gualification of Racked

Out Circuit Breakers.

At 9:30 p.m.

on March

14, Unit 2 control

room operators

recognized

a

loss of

RTGB annunciator

panels

H, J,

K, L,

M, and

N due to lit

annunciators

becoming

very dim and

no annunciator

lights

on these

panels

lighting brightly when

checked.

Operators

entered

ONOP

2-0030137,

Partial

or Complete

Loss of Annunciators,

Rev.

1.

The

ONOP

was written in the

two

column

EOP format

and did contain

guidance for operators;

including checking all alarm panels for the

extent

of the malfunction,

referring to

an

Annunciator

Summary

procedure

to assess

the

impact of the lost annunciators,

increased

monitoring of the

RTGB,

and

implementing the

Emergency

Plan per EPIP

3100022E,

Classification

of

Emergencies.

The

EPIP

required

declaration

of

an

Unusual

Event

based

on

a loss of indication or.

alarm panels

which, in the opinion of the NPS/EC,

would significantly

impair accident

or emergency

assessment.

An unusual

event

was not

declared.

(The

inspector

later

reviewed

the

approximately

240

'nnunciators

lost with an

NPS

who described

why he also would not

have declared

an Unusual

Event.)

The

ONOP also directed operators

to

check annunciator

power supplies

and contact the

18C staff.

At 10:48

p.m.,

ISC personnel

manually

bypassed

the power supply inverter (and

its logic) and restored

the annunciator

panels to operation

on backup

120 volt ac

power.

IKC personnel

subsequently

replaced

the failed

annunciator

power supply inverter and logic assembly.

Shop

testing

of the failed

power

supply

assembly

revealed

a

previously

unseen

failure mode.

A 12 volt regulator

had failed,

causing

28 volt unregulated

dc voltage to be introduced into the

12

volt regulated

dc voltage

sensor

card.

The voltage

sensor

card

failed, causing

the

two power supply switching relays to chatter

as

they switched

back

and forth between

the normal

(120 volt ac through

the

power supply assembly)

and alternate

(125 volt dc through

the

inverter)

power sour ces.

This caused

the related

alarm lights in the

control

room to

become

very dim.

ISC determined

that

a similar

failure to

a different power supply assembly

could cause

the loss of

virtually all control

room annunciators.

For long term corrective

action,

I&C initiated

an

REA requesting

modification of the

annunciator

power supply to limit such

a failure to

a specific group

of annunciators.

Also,

the

licensee

labeled

the

power

supply

inverter

bypass

switches

(located

inside

cabinets

in the

cable

spreading

room)

and

issued

a temporary

change

to

ONOP 2-0030137

on

March

19.

This temporary

change

gave operators

instructions

on when

and where to operate

the

power supply inverter bypass

switches.

The

inspector

walked

down the temporary

change with an operator'nd

found

that

the

bypass

switches

were clearly labeled,

but were

located

inside different cabinets

than

those listed in the temporary

change.

The

inspector

gave

this

information

to the

NPS

on shift for

correction of the temporary

change.

On March

15,

the

2B1 circulating water

pump failed.

Prior to the

failure, the

pump

had

been restarted

at 9:05 a.m. following the

2B1

main condenser

water box post-cleaning

return to service.

Subsequent

power ascension

was

stopped

at

90 percent for turbine valve testing

at

10:20

a.m.

At 1: 15

p.m.

operations

noticed

the main turbine

generator

megawatt output decreasing

and main condenser

back pressure

increasing.

Approximately two minutes later,

the operators

noticed

the

2B1 circulating

pump current

reduced

from the normal

220 to 270

ampere

range

to

130

amperes.

The control

room operators

began

a

downpower

and dispatched

other operators

to observe

the pump.

The non-licensed

turbine operator

and

an

SRO found that the

2B1

pump

had

an overheated

shaft

and gland area.

The area

was visibly warm.

The

pump

was shut

down at approximately

1:20 p.m.

Plant

power

was

stabilized at 85 percent at this time.

At 1:40 p.m.

on the

same

day,

a non-licensed

operator

observed that

the

2A MFP

had lost

some

amount of lubricating oil.

The reservoir

was

down about

5 gallons

when checked,

and oil was visible around

and

dripping from the

coupled

pump bearing.

Oil- was

added

to the

reservoir,

the

mechanical

maintenance

staff

was

called,"

and

the

predictive maintenance staff was called for an oil sample.

As

a conservative

measure,

at 2: 10 p.m., plant

power

was further

reduced

to approximately

70 percent

in case

there

was

a problem with

the

MFP.

The plant could not

be maintained

on line at this

power

should

a

MFP trip because

the

MFPs were only 60 percent

capacity

pumps,

however power was not reduced

below 70 percent

due to shutdown

margin restraints

and the

4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

LCO time restraints

of TS 3. 1.3.6,

Regulating

CEA Insertion Limits.

If the

MFP

had tripped

from 70

percent

power,

the operators

planned

to quickly reduce

power to keep

the plant on line and temporarily enter the

TS

4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

LCO.

Subsequent

2A MFP observation,

evaluation,

and oil sample laboratory

results

revealed

no

probable

pump problems.

No upward

trending

bearing

temperatures

were observed.

Vibration analysis

indicated

no

changes

in

pump vibration.

Oil sample

analysis

indicated

no oil

degradation.

The initial conclusion

drawn

was

that

pump

had

experienced

some

minor,

unexplained

transient.

Further analysis

would follow.

At 9:30 p.m., after the laboratory results

were

digested,

power

was

increased

to around

90 percent,

the

maximum

achievable

with the

missing

2B1 circulating

pump

and resulting

condenser

back pressure

limitations.

The circulating

pump

was carefully disassembled

to understand

its

failure mode.

The shaft

had cracked or cracked

and rewelded itself.

The shaft sleeve

on which the

packing

rode

had

been

heated

to the

point that portions of it had

been welded to the packing gland.

The

affected

parts

were

removed

to the licensee's

materials

laboratory

for further evaluation.

At the

time of discovery,

the

licensee

thought that sufficient water lubrication and cooling was available

to the

pump packing

area

based

on feedback

from the non-licensed

operator

who

had started

the

pump at 9:05

a.m.

The licensee

is

continuing their review and root cause determination.

Plant Operations

Review

The

inspectors

periodically

reviewed shift logs

and

operations

records,

including data

sheets,

instrument traces,

and records

of

equipment malfunctions.

This review included control

room logs

and

auxiliary logs, operating

orders,

standing

orders,

jumper logs,

and

equipment tagout records.

The inspectors

routinely observed

operator

alertness

and

demeanor

during plant tours.

They

observed

and

evaluated

control

room staffing, control

room access,

and operator

performance

during routine operations.

The inspectors

conducted

random off-hours inspections

to assure

that operations

and security

performance

remained

at acceptable

levels.

Shift turnovers

were

observed

to verify that they

were

conducted

in accordance

with

approved

licensee

procedures.

Control

room annunciator

status

was

verified.

Except

as noted below,

no deficiencies

were observed.

During this

inspection

period,

the

inspectors

reviewed

tagout

(clearance)

2-2-86 - 2B

EDG for PMs.

Due to a need to reduce

condenser

tube fouling rates

and reduce the

overall

environmental

effluents,

the

licensee

has

obtained

an

EPA

,permit for use of

a chemical

agent to reduce

clam growth in the

plants'ntake

structures

and condensers.

The chemical

agent

would

be

an adjunct to the existing use of hypochlorite.

Hypochlorite has

had

a minimal effect

on the clams,

oysters,

and bivalves for which

the

chemical

agent

was targeted.

On March 4,

1992,

a contractor

began

injection of the

chemical

agent

into the Unit

1

intake

structures.

The injection period lasted

approximately

10 days.

The

trial period will be

18 months in duration with injections occurring

every

2 to 3 months.

The posting of required notices to workers

was reviewed

and was noted

to be satisfactory.

Technical Specification

Compliance

Licensee

compliance with selected

TS

LCOs was verified. This included

the

review

of

selected

surveillance

test

results.

These

verifications

were accomplished

by direct observation

of monitoring

instrumentation,

valve positions,

and switch positions,

and by review

of completed

logs

and records.

Instrumentation

and recorder traces

were observed for abnormalities.

The licensee's

compliance with LCO

action

statements

was

reviewed

on selected

occurrences

as

they

happened.

The inspectors

verified that related plant procedures

in

use were adequate,

complete,

and included the most recent revisions.

Because

during the inspection period,

the

2B

EDG had

been

placed out

of service for PMs

and subsequently

returned

to service,

the

2A

EDG

was started

on February

27 for an idle start operational

check per

TS 3.8. 1. l.b.

The

2A EDG's

2A1

( 16 cylinder)

engine established

the

required fuel rack position for 450 rpm on the idle start test while

the

2A2 ( 12 cylinder) engine accelerated

to 900 rpm, carrying the

16

cylinder engine to the

same

speed - the engines

were coupled via the

common generator

between

them.

Appropriate annunciation lit.

The speed

adjusting

Bodine brand motor on the

2A2 engine's

governor

was

found missing

a brush.

This left the motor inoperative

and

locked in its last operating

position,

which had

been at its high

speed

stop.

Due to the Bodine motor problem,

the governor

was at its

high fuel rack stop (which would produce

900 rpm).

This position was

fortuitous

in that,

had

the

2A

EDG received

an

emergency

start

signal,

the generator

would have

loaded with required

emergency

bus

loads.

The screwed-on

brush

cap that held the brush spring

and brush against

the motor commutator

had loosened.

The brush

and cap were found atop

the governor

housing just beneath

the motor.

Speculation

was that

the externally threaded

cap

had

loosened

because

of diesel

running

vibration.

Work instructions

were

issued

and

implemented

that

evening

(February

24) to check tight all Bodine motor brush caps.

Oue to loss of governor control, the

2A EOG was declared

inoperable.

The

2B

EDG

was

started

on

February

28 within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,

per

TS 3.8.l.l.b,

A special

report is due from the licensee within 30

days.

By the

end of the inspection

period,

the licensee

had obtained

a

telecon

from the governor vendor for a fix on the Bodine motors.

The

vendor indicated that currently the motors were being sold with a dot

of

RTV in the brush-cap-to-motor-body

joint to inhibit vibration

induced

loosing of the brush

cap.

At the

end of the inspection,

the

licensee

had received on-site

review committee

approval

for repair

instructions

to apply

a

dab of

RTV to the exterior of the screwed

joint.

,The remaining

brush

caps

were subsequently

verified to

be

tight.

The resident

inspectors

were collecting information regarding

the specific event for consideration

as

a generic issue.

Physical

Protection

The inspectors verified by observation

during routine activities that

security program plans were being implemented

as evidenced

by: proper

display of picture badges;

searching of packages

and personnel

at the

plant entrance;

and vital area portals being locked

and alarmed.

Observed

operator

deportment

and actions

during the recovery

phase of the

Unit 2 2B1 circulating water

pump loss were commendable.

Followup actions

on the transient

experienced

by the

2A NFP were thorough.

Staff actions

were timely in their support of plant operations.

3.

Survei1 l ance Observati ons

(61726)

Various

plant

operations

were verified to

comply with selected

TS

requirements.

Typical of these

were confirmation of TS compliance for

reactor coolant chemistry,

RWT conditions,

containment

pressure,

control

room ventilation,

and

AC

and

DC electrical

sources.

The inspectors

verified that

testing

was

performed

in

accordance

with

adequate

procedures,

test instrumentation

was calibrated,

LCOs were met,

removal

and restoration

of the affected

components

were

accomplished

properly,

test results

met requirements

and

were reviewed

by personnel

other than

the individual directing the test,

and that any deficiencies identified

during

the testing

were properly reviewed

and

resolved

by appropriate

management

personnel.

The following surveillance tests

were observed:

a.

OP 2-2200050,

Rev 38,

Emergency

Diesel

Generator

Periodic Test

and

General

Operating Instructions,

28

EDG

b.

OP 2-2200050,

Rev 38,

Emergency

Diesel

Generator

Periodic Test

and

General

Operating Instructions,

2A EDG.

The

2A EDG test is discussed

in paragraph

2.c of this report.

c.

OP

1-2200050,

Rev 61,

Emergency

Diesel

Generator

Periodic Test

and

General

Operating Instructions,

lA EDG

d.

OP 1-0700050,

Rev 37, Auxiliary Feedwater

Periodic Test,

lA pump

e.

OP

2-0030150,

Rev 33,

Secondary

Plant Operating

Checks

and Tests,

Section

8. 1.4,

Turbine Valves.

During the turbine governor valve

tests

on

February

24,

paragraph

8. 1.4.k

(OP

2-0030150),

the

indicating lights

on the control

board did not react

as predicted.

The

DEH

"open" light did not extinguish

when three

of the four

governor

valves

went closed

(on the fourth valve,

the light went

out).

ISC personnel

indicated that the

"open" light was

operated

by the

snap-lock

valve position switches.

Often during long runs

between

operation of the valve position switches,

the switches

have frozen

due to corrosion buildup.

This

was described

as

an industry-wide

phenomenon.

I&C had

an operations-written

NPWO to repair

the

affected

switches.

Additionally, ISC had

been working with vendors

toward

potentially

replacing

the

snap-lock

switches

with

magnetic/reed

switches.

A

REA

was

to

be

submitted

to site

engineering

on the subject.

Not addressed

by the

procedure

were

the alternate

methods actually

used

by

operations

to verify valve

closure.

An

SRO

and

a

non-licensed

operator

were at the valves

when

they were cycled to

observe

proper operation.

Valve test lights

on the vertical

DEH

control

board

changed

state.

Also, the digital

readout

ceased

downward trending at 0.6 to 2.0 percent

closed (this indicated closed

but due to cold calibration of the valve position indication absolute

zero indication did not occur with the valve hot).

A change to this

procedure

was instituted to

add

the alternate

means

of verifying

valve closure.

f.

OP

1-0700050,

Rev

37, Auxiliary Feedwater

Periodic Test,

1B

pump.

During the surveillance of the

1B

AFW pump, it was observed that one

of the motor's

louvered exit covers

was installed with the louvers

opening

upward.

Since there

was

no rain catch or lip above this

cover, this would tend to invite rain water entry when the

pump was

not operating.

Subsequent

review showed that,

due to construction of

the motor housing,

water would only enter the shielding

shroud

and

still would not gain direct entry to the motor windings or bearings.

Standing

water in the internal

shroud

volume would tend to induce

rust

degradation

of the

shroud.

The

louver installation

was

subsequently

corrected.

The surveillances for this period were fully'acceptable

with the exception

of the

2A EDG.

4.

Maintenance

Observation

(62703)

Station

maintenance

activities involving selected

safety-related

systems

and

components

were

observed/reviewed

to ascertain

that

they

were

conducted

in accordance

with requirements.

The following items

were

considered

during

this

review:

LCOs

were

met;

activities

were

accomplished

using

approved

procedures;

functional

tests

and/or

calibrations

were

performed prior to returning

components

or systems

to

service;

quality

control

records

were

maintained;

activities

were

accomplished

by qualified

personnel;

parts

and

materials

used

were

properly certified;

and

radiological

controls

were

implemented

as

required.

Work requests

were

reviewed

to determine

the

status

of

outstanding

jobs

and

to

assure

that

priority

was

assigned

to

safety-related

equipment.

Portions

of

the

following maintenance

activities were observed:

a.

NPWO 7162/63

RPS

"C" subchannel

Low Level

S/G Failed Surveillance

1-1400050

b.

NPWO 7185/64

Unit 2 Annunciator

Power Supply Logic Housing Failure

c.

NPWO 4733/61

Repack

Charging

Pump

1C

d.

NPWO 4633/66

4160

V Switchgear

2B3 (SB) Feeder to Bus

2AB.

Per

NPWO

instructions,

the feeder

breaker

from the "B" side safety

4160 Volt

switchgear

was

removed

and replaced

in a routine manner.

The removed

breaker

would

be

overhauled

by

a

vendor

as

had

the breaker that

replaced it.

A spare

breaker

was

overhauled

and readied for this

pre-outage activity.

The effort was part of attempt to complete the

Unit

2

4160 Volt breaker

nine-year

overhaul

cycle.

The

feeder

breaker

was

not carrying

any load at the

time of the transfer.

Operations

personnel

who racked

the

breakers

out

and in utilized

procedure

OP 2-0910023,

Rev 5, Transfer Electrical

Alignment on the

4160V and

480Y Load Center

2AB Buses.

The replacement

breaker tested

sati sfactorily.

e.

NPWO 4610/61

Dragon Valves Model Numbers

10615

and 10905,

Inspect

for Loose Packing Nuts

f.

NPWO 2729/62

Dragon Valves in ECCS

Rooms

NPWOs e.

and f. above, for Dragon valves,

were followed this report

period

due to

an event

found during the last report period

and

discussed

in report

335,389/92-04.

Several

of the safety-related

vent

and drain valves in the Unit

1

ECCS

room were found with their

packing retaining

nuts

less

than

hand tight.

Based

on tightening

instructions

provided

by the vendor,

these

NPWOs direct checking the

tightness of the nuts in both units.

The

observed

maintenance

activities

were satisfactory

and controlled

appropriately.

5.

Fire Protection

Review (64704)

During the course of their normal tours,

the inspectors

routinely examined

facets of the Fire Protection

Program.

Normally the inspectors

reviewed

transient fire loads,

flammable materials

storage,

housekeeping,

control

of hazardous

chemicals,

ignition source/fire risk reduction efforts, fire

protection

system surveillance

program, fire barriers,

and fire brigade

qualifications.

The fire protection

program

seemed

to be working well during this period.

6.,

Onsite Followup of Events

(Units

1 and 2)(93702)

Nonroutine plant events

were reviewed to determine

the need for further or

continued

NRC response,

to determine

whether corrective actions

appeared

appropriate,

and to determine

that

TS were being met

and that the public

health

and

safety

received

primary consideration.

Potential

generic

impact and trend detection

were also considered.

The events

discussed

in paragraph

2 (annunciator

problems, circulator pump

failure,

and

EDG failure) were

handled

promptly with active

management

overview.

7.,

Followup of Inspector Identified Items (Units

1 and 2) (92701)

a.

(Closed - Units

1 and

2)

URI 335,389/91-201-01,

Pre-operational

Test

Review.

This

URI identified

several

ICW

system

pre-operational

test

anomalies.

The licensee

reviewed

the following discrepancies

to

ensure that system capabilities

were

known:

10

Inconsistences

were found in flow and differential pressure

data

at different points in the test

although

the system

alignment

was apparently

the

same.

The

licensee

attributed

this to modulation

of temperature

control valves during the test which may have changed

the system

parameters.

Since

the intent of this portion of the test

was to

obtain

system flow characteristic

data for modeling

purposes,

the

parameter

changes

were found not to be significant.

The

inspector

had

no further questions

on this point.

Minimum acceptable

flow was not maintained at all times during

the test.

The licensee

evaluated

this

and determined

that the intent of

the stated

minimum flow was to approximate

expected

flow rates

and that operation

below this value did not affect the test.

The inspector

had

no further questions

on this point.

The pre-operational

test did not establish travel stops

on flow

control valves to prevent

pump runout.

The licensee

determined

that travel

stops

were

used at

some

point

during

the

pre-operational

testing

phase

and

not

documented

as

such.

The licensee

could not determine

exactly

when

and

why they were

used other than to address

the concern

with pump runout which apparently

developed

during the testing.

The

licensee

recently

implemented

modifications that control

runout flow by use of orifices and negated

the requirements for

FCV travel

stops.

The inspector

had

no further questions

on

this point.

Valve settings for the backup source of lubrication water to the

ICW pumps were not established.

't

The licensee

referenced

FSAR section 9.2. 1 which stated that the

backup

source

of lubrication (domestic

water

system)

was only

required during initial

ICW pump startup

[when the

ICW system

would

be

empty]

and

was

not

needed

for restart

of

a

pump

following loss of offsite power.

The licensee

determined that

valve settings for the domestic water system were not required.

The inspector

had

no further questions

on this point.

There

were significant differences

in differential

pressures

recorded for

ICW strainers.

The licensee

attributed differences

to strainer cleanliness

or

gauge

reading

inaccuracies

and

concluded

that the differences

did not affect the test results.

The'nspector

had

no further

questions

on this point.

11

The inspector

concluded

that

the licensee

adequately

reviewed

the

anomalies

and that they did not significantly affect the

outcome of

the pre-operational

test.

b;

(Closed

-

Units

1

and

2)

Deficiency

Item 335,389/91-201-01,

~

Incomplete

and Inaccurate

FSAR Discussions.

The inspector

reviewed

the following discrepancies

regarding

FSAR

discussions

of the

ICW system:

Valves NY-21-2 and MV-21-3 were described

in the

FSAR as having

been

upgraded

(Unit 1) or qualified (Unit 2) for submersible

service

yet

were

subsequently

determined

during

inspection

91-201 not to be qualified for submersible

service.

The

license

provided

some

evidence

in the

form of memos,

requisition

forms,

motor test

recor'ds

and material

receipts

which suggested

that submersible

qualified motors

may have

been

installed at

some point several

years

ago.

The licensee

could

not,

however,

provide positive documentation.

Nevertheless,

the

licensee

had cooeitted to install submersible qualified

NOVs and

controls

did

not exist

or

were

not effective

to

ensure

submersible

qualification

was maintained.

In this case,

the

licensee

deviated

from a written commitment in that the valves

were

not maintained

as qualified for submersible

service

as

stated

in the

FSAR.

The licensee

subsequently

determined

that the valves

were not

required to be qualified for submersible

operation

on the basis

that

a flooding event

and

a design

basis

accident

occurring

simultaneously

was

not within the plant design

basis.

The

inspector

reviewed

the licensee's

draft 50.59 evaluation while

on site

and the final versions after they were issued,

and did

not identify any further concerns.

The licensee

indicated that

they

planned

to correct

the

FSAR.

This deviation

from

a

commitment

is not being cited

because

subsequent

operational

philosophy regarding

hurricanes

and

subsequent

modifications to .

Unit

1

ICW pumps to delete

the water lubricating

system

have

negated

the safety significance.

(2)

CCW temperature

control

valves

TCV 14-4A and

14-4B fail open

upon loss of in'strument air but were not described

in the Unit

1

FSAR

CCM section.

The licensee

provided the inspector with sections

of the

FSAR

which adequately

described

valves

TCV 14-4A and

14-4B (sections

7.3.1.3.2

and 9.2.1.5,

table 9.2-2,

and figure 9.2-1).

The

inspector

had

no further questions

on this point.

IN

12

(3)

ICW

valves

FCV

21-3A

and

38

isolated

the

non-essential

lubricating water header

upon SIAS but were not described

in the

FSAR.

(5)

The licensee

provided

the inspector with

FSAR table 7.3-2

and

figure 9.2-1a,

which described

valves

FCV 21-3A and 21-38.

The

inspector

had

no further questions

on this point.

The

FSAR incorrectly

referenced

a

deleted

section

which

described

recirculation

operation

between

the

discharge

and

intake canals for biofouling control.

The licensee

pointed out that recirculation

was proposed at one

point in time and actual modifications

had

been initiated, but

subsequently

terminated.

FSAR

drawings 9.2-1b

and

9.2-1e

accurately depicted

the as-built status.

The inspector reviewed

the

licensee's

currently

proposed

FSAR correction.

The

inspector

determined

that this error

did not

represent

a

significant concern.

The

FSAR did not

include

aspects

of the

sel f-lubrication

modification on the

2A

ICW pump.

The inspector

determined

that

a weakness

existed with promptly

closing out the design

change

package

in order to ensure that

the

FSAR is

updated.

The licensee

conducted

a review

and

determined this to be

an isolated

example.

Section

9.2.7

of the

FSAR incorrectly described

the

UHS by

discussing

only two of three intake pipes.

The inspector

found that

FSAR section 9.2.3

and figure 9.12-1b

describe

the three intake pipes for the

UHS.

(Closed

-

Units

1

and

2)

Deficiency

Item

335,389/91-201-02,

Inadequate

Training Materials.

Several

examples

of inaccurate

or incomplete descriptions

of the

ICW

System

were identified in training documents.

Examples

included the

following;

strainer

mesh sizes

were incorrect,

ICW self-lubrication modification

was

not

implemented

in all

training documents

in a timely manner,

documents incorrectly described

cross-connected

operation of the

ICW system,

documents

omitted unit 2 specific

TCV closure limits,

13

some setpoints

were inaccurate,

and

annunciator

listings did not match verbatim the control

room .

annunciator.

The inspector

reviewed

the deficiencies

and determined

that while

weaknesses

may exist for ensuring

accurate

training materials,

the

deficiencies

were minor in nature

and did not represent

a safety

significant

concern.

The inspector

reviewed

corrected

training

materials

including

an 'RCO Self Study Test

on Cooling Water Systems

(0704201)

and

a

SNPO

Lesson

Text on Component

Cooling Water System

0511016).

The inspector additionally determined that other training

material deficiencies

were being adequately

addressed.

It appears

that the licensee's

Administrative Procedure

AP005766,

Training

Resources,

Information

and

Material

Control,

was

not

followed in that review of plant modifications for incorporation into

training material

was not adequate

and resulted in the discrepancies.

This

NRC identified violation is not being cited

because

criteria

specified

in Section

VII.B of the

NRC

Enforcement

Policy

wer e

satisfied.

This is identified

as

NCV 335,389/92-05-03,

Inadequate

Training Materials.

(Closed - Units

1 and 2) Deficiency Item 335,389/91-201-03,

ICW Pump

C and Header Inoperability.

This item involved potential inoperability of the

C

ICW pump

due to

not

adequately

demonstrating

operability

of

the

pump

and its

associated

actuation circuitry.

The licensee

determined that the

C

ICW pump start feature

on SIAS was

not required to be tested

because

during condi tions when the

pump was

required

to

be operable,

the

pump would

be running

and would not

require

an auto start signal.

The inspector

questioned

the licensee

concerning

a Loss of Offsite

Power

actuation

signal

and

reviewed electrical

logic drawings

to

determine if the

C

ICW pump

was

adequately

tested.

The inspector

determined

that following a Loss of Offsite power,

the

C

pump would

trip and later

be

sequenced

back after the

bus

was energized

by the.

diesel

generator.

The logic associated

with this, including relays

and

contacts,

was

not

tested

at

any periodicity.

Technical

Specification surveillance

4.8. 1. 1.2.e.4 requires

in part that

a loss

of offsite power be simulated every

18 months

and that auto-connected

shutdown

loads

be verified to energize

through the load sequencer.

Test procedures

failed to adequately

demonstrate

the ability of the

C

ICW

pump

logic, to

perform

this

function.

This

is

VIO

335,389/92-05-04,

Failure to Adequately

Test the

C Intake Cooling

Water

Pump.

14

(Closed - Units

1 and 2) Deficiency Item 335,389/91-201-04,

Inservice

Testing

IST Deficiencies.

One concern

involved the testing of manual

valves

SB-21211

and

SB-21165.

The licensee's

IST program

dated

January

3,

1990

identified these

valves to be exercised

quarterly.

The licensee

subsequently

determined

that these

valves were not required

by

Section

XI to be in the program

and

never initiated testing

on

them.

The licensee

did not obtain prior

NRC approval

for this

change.

Prior approval

is

not required

as indicated

in the

response

to question

62 of the October

25,

1989

NRC letter,

Minutes of the Public Meetings

on Generic Letter 89-04.

The

concern

was that the licensee failed to update their IST program

and

inform the NRC'f the

change;

The inspector

reviewed

further guidance

in the referenced

letter (question

61) which

indicated that the

NRC staff should

have the current

IST program

being

implemented.

The inspector

determined that this example

represented

a weakness

in not maintaining

an accurate listing'f

all valves in the program.

However, in that these

valves were

never required

by the code to be tested

and were inadvertently

added

to the list, the licensee's

failure to promptly revise

their

program

does

not

represent

a significant

concern.

Additionally, the licensee

was able to show the inspector that

these

valves

were in fact exercised

on

a quarterly basis during

surveillance

testing of

ICW

pump discharge

check

valves

per

Administrative Procedure

1-0010125A,

Surveillance

Data

Sheets.

The licensee

planned to correct

the program.

The inspector

had

no further questions

on this point.

(2)

'A second

concern

involved the testing

frequency of the valves

TCV-14-4A and

14-4B

on Unit 1.

The licensee

had

been testing

the valves during cold shutdown.

The valves were classified

as

Category

B power operated

valves.

Code requirements

for testing

include stroke valve timing every three months.

The licensee's

IST

program

valve table specified

a test

frequency

of cold

shutdown

and referenced relief request

VR-35.

VR-35 requested

relief from timing the valve

and provided

a basis

indicating

that

measurements

of valve closure

times

are not practical.

VR-35 did not request

nor provide

a basis for testing the valve

at

the

reduced

frequency

of cold

shutdown.

Further,

YR-35

stated

that alternate

testing

would

be

done

on

a quarterly

frequency.

The licensee's

program

was

approved

on

an interim basis

on

,

October

17,

1990.

This granted relief to exempt valve timing

for the valves.

No approval

was granted for a

reduced

test

frequency.

The

inspector

concluded

that

the

licensee's

submittal

was

inconsistent.

The

NRC granted relief from valve timing.

Therefore,

the valves

were required

to

be tested

every three

15

months.

This is identified as

a violation of the requirements

of the l icensee

'

IST program,

Fai lure to Test

TCV-14-4A and

14-4B every three months.

This is VIO 335/92-05-05,

Failure to

Test Certain Valves quarterly

as Required

by the Inservice Test

Program.

The

inspector

reviewed

the licensee's

revised

submittal

of

October

23,

1991 which included revision

3 to relief request

VR-35.

Further errors

were identified with the request in that

the

requirements

for check

.valve tasting

were incorrectly

referenced.

Additionally, it was not clear whether the licensee

considered

the valve to be power operated

or fail safe.

8.

Followup of Headquarters

and Regional

Requests

(92701)

During the

inspection

period,

a

survey

on

maintenance

backlog

was

performed for the

NRC Region II Office.

9.'eview of Component

Cooling Water Temperature

Control System (Part of the

Intake Cooling Water System)

(92701)

a ~

While reviewing Unit

1

ICW system operation,

the inspector

observed

that:

(a)

ICW TCVs I-TCV-14-4A and

B had

a failure mode that may not

have

been previously evaluated,

and (b) the air-operated

controls for

the temperature

control valves

may not have the proper qualifications

for the safety functions performed.

If instrument air were lost:

The temperature

control valves

themselves

and their spring-open/

air-close Bettis operators

were designed

to fail open,

and were

Seismic Category

I and safety-related.

The qualification status

of the remaining air-operated

control

components

would not matter.

If instrument air were not lost:

The temperature

control valves themselves

and their spring-open/

air-close

Bettis

operators

did

not

have

physical

stops

preventing them'rom'eing

shut to less

than

some

minimum

accident flow position.

Failure

modes of the air-operated

controls for the temperature

control valves did not appear to be analyzed.

The air-operated

controls for the

temperature

control

valves

were

considered

by the

licensee

to

be non-safety-related

and

non-seismic.

The Unit

1

components

were located in exposed

locations

on the

CCW platform.

16

b.

A detailed control

system audit followed.

The inspector

approached

the review by:

reviewing

FSAR requirements

and statements;

reviewing

system

modifications

and

associated

analyses,

either

planned

or

accomplished,

that were not in the

FSAR;

reviewing the

component

vendor

manuals for potential

design input; reviewing the physical

installation;

determining

what surveillance

or maintenance

program

elements

have

been

applied to these

components;

and determining if

these

components

are

being

used

to

accomplish

an

actual

safety-related

purpose.

c.

Control System Audit Results:

(1)

The

FSAR review basically

found that the only instrument air

failure discussed

was total loss of instrument air.

There'as

also

a failure

mode listed

where

one of the

two temperature

control valves

would fail to open (for undefined reasons).

The

temperature

control

valves

themselves,

and the attached

Bettis

brand operators,

were identified as safety-related

and qualified

for seismic

category I, but the Bailey valve positioner s, the

associated

pneumatic

TICs,

and the related

pneumatic relays

and

regulating valves

(reducers)

were not designed

as safety-related

or seismic.

Control

components

were

found to actually

be

non-safety-related

per

analysis.'2)

Plant

change

PCM 005-190,

not yet included

in the

FSAR,

was

reviewed.

The

PCN was

performed

on Unit

1 in the fall of 1991.

Its

main

purpose,

per

the plant

maintenance

staff,

was to

replace

obsolete

non-safety-related

control

components

with

newer

safety-related

control

components.

The

maintenance

department

focus

when requesting

this

change

was

on maintenance

and availability of parts,

having nothing to do with the system

safety analysis.

However,

the engineering

analysis

applied to

the modification stated

very strongly that these

were required

to

be safety-related

to function in the

case

of an accident

without loss of instrument air.

This analysis

included

a markup

of the

FSAR deleting

the statements

that the control circuits

were

not safety-related

and

adding

statements

that they were

safety-related

and

had to function following an accident.

This

analysis

applied to:

TICs, which produced

an air pressure

signal

representing

a

temperature

measurement

Air pressure

limiting relays

in the TIC signal

path, since

the

TCVs closed

on increasing air pressure

and these relays

established

the minimum TCV opening

(most closed position);

and

The

common air pressure

regulator that reduced

the supply

air to the operating air pressure

for the

TICs

and air

pressure limiting relays.

17

The

above

analysis

stated

that this installation

included

a

positive valve position stop going closed

and

a positive valve

position stop going open, with the valve operating

range

between

those

stops.

Thus,

the valves

were

open far enough for safe

shutdown flow yet restrained

from exceeding

pump runout flow.

This was found to be in error.

The minimum valve position stop

was not

a hard stop at all, it'as established

by the pneumatic

control

system air relay setting discussed

above.

While perhaps

open

enough for safe

shutdown, it was less

than

the minimum

system accident

(LOCA) flow. It was

based

on cavitation in the

pipe

and

downstream

of the valve

and

was

not

based

on safe

shutdown or accident flows.

(4)

(5)

The actions

taken

by the utility did not address

the presently

non-safety-related

Bailey positioners,

or Fisher

volume booster

relays,

or Fisher air reducer

valves

mounted

on

the

TCVs

themselves.

A future

PCM, also

based

on obsolete

equipment

upgrade,

is planned to address

them.

The vendor

manual

and physical

installation

review found that

both the TIC and the air relay. vendor manuals specified limiting

air pressures

significantly less

then the air supply pressure.

Both the original

and the newly-installed reducing valves vendor

manuals

required that, if components

downstream

could be damaged

by upstream

pressure,

then

a full flow relief valve must

be

installed.

There

were

no relief valves installed in this

new

design.

Interviews of instrumentation

and control staff personnel

showed

that TIC control

loop equipment

was

on

an

18 month inspection

and calibration cycle.

The inspector

concluded

from literature

and installation reviews

that

the utility has

been

depending

on non-safety-related

components,

that were installed in a manner contrary to vendor

manual

requirements

and did not

have

a specific failure mode

analysis,. to control the functioning of the safety-related

TCVs.

The non-safety-related

components

were not backed

up by physical

minimum valve position stops.

The engineering

evaluation of PCM

005-191

appeared

to

have

identified

a previously

unreviewed

safety

question

concerning

a previously

unrecognized

failure

mode.

d.

Subsequent

Licensee Actions

When the inspector inquired about further actions that would appear

to be warranted

upon the licensee

recognizing

the subject conditions

during

Summer,

1991,

the

licensee

subsequently

stated

that last

summer's

analysis

was in error,

though it had

been

signed

by a number

of engineers,

had

been

reviewed

by the Facility Review Group - the

18

technical

specification

onsite

safety

review

group,

and

the

modification had subsequently

been completed

on 'Unit 1.

New material

provided included

a special

study of the licensing

basis

and

a probabi listic risk assessment.

The licensee

stated

that the text of PCM 005-190 would be rewritten.

Interviews

with licensee

engineers

found that

the

licensee

considered

the licensed

basis

of St.

Lucie to not include

a

seismic event coincident with a

LOCA - which would challenge

the

ICW system

from

a heat

removal

basis.

A seismic

event is

postulated

coincident with

a

need for safe

shutdown - which

would not require

more

than

normal

heat transfer to the

ICW

system.

The licensee

stated that it was

common nuclear design practice

to use air system relief valves

only if the components

did not

bleed air during normal operation - these all did normally bleed

air.

The licensee

stated

that there

are

no specific

standards

for

qualification of air-operated

control

components,

therefore

highly reliable commercial

equipment

was satisfactory.

e.

Conclusion

At this point, further review is required to determine if the

CCW

TCVs

should

be

safety-related

or

not.

This

matter

is

URI

335,389/92-05-06,

Evaluation of whether

or not air controls for

CCW

Temperature

Control Valves should

be safety related,

pending further

NRC review of basic requirements.

10.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on March 30,

1992, with

those

persons

indicated in paragraph

1 above.

The inspector described

the

areas

inspected

and discussed

in detail

the inspection findings listed

below.

Proprietary material is not contained

in this report.

Dissenting

comments

were not received

from the licensee.

Item Number

Status

Descri tion and Reference

335,389/92-05-01

open

335,389/92-05-02

closed

335,389/92-05-03

closed

IFI - Seismic gualification of Racked

Out

Circuit Breakers,

paragraph

2a.

NCD - Failure to Maintain Submersible

Valve

gualifications

as Described in the

FSAR, paragraph

7b.

NCV - Inadequate

Training Materials,

paragraph

7c.

19

Item Number

Status

Descri tion and Reference

335,389/92-05-04

open

VIO - Inadequate

Test of ICW Pump,

paragraph

7d.

335/92-05-05

open

VIO - Failure to Test Certain Valves

quarterly

as

Required

by the

Inservice Test Program,

paragraph

7e.

335,389/92-05-06

.

open

335,389/91-201-01

cl osed

URI - Evaluation of whether or not air

controls for CCW TCVs should

be

safety related,

paragraph

9e.

URI - Preoperational

Test Review, paragraph

7a.

335,389/91-201-01

closed

335,389/91-201-02

closed

335, 389/91-201-03

closed

335,389/91-201-04

closed

Deficiency Item - Incomplete

and Inaccurate

FSAR Discussions,

paragraph

7b.

Deficiency Item - Inadequate

Training

Materials,

paragraph

7c.

Deficiency Item -

ICW Pump

C and Header

Inoperability, paragraph

7d.

Deficiency Item - Inservice Testing

IST

Deficiencies,

paragraph

7e.

11.

Abbreviations,

Acronyms,

and Initialisms

AC

AFW

ANSI

AP

ASME

ATTN

CC

CCW

CEA

CFR

CWO

DC

DEH

DPR

EC

ECCS

EDG

EOP

EPA

EPIP

Alternating Current

Auxiliary Feedwater

(system)

American National Standards

Institute

Administrative Procedure

Code American Society of Mechanical

Engineers

Boiler and Pressure

Vessel

Code

Attention

Cubic Centimeter

Component

Cooling Water

Control Element Assembly

Code of Federal

Regulations

Construction

Work Order

Direct Current

Digital Electro-Hydraulic (turbine control

system)

Demonstration

Power Reactor

(A type of operating license)

Emergency Coordinator

Emergency

Core Cooling System

Emergency

Diesel Generator

Emergency

Operating

Procedure

Environmental

Protection

Agency

Emergency

Plan Implementing Procedure

20

ESF

FCV

FLO

FMEA

FPL

FRG

FSAR

GL

gpm

HX

Hz

ISC

ICW

IFI

INPO

IST

JPN

LCO

LOCA

LOI

MFP

MOV

MY

NCD

NCR

NCV

NEMA

NPF

NPS

NPWO

NRC

NRR

ONOP

OP

PCM

PM

pslg

PSL

QA

QI

RCO

REA

Rev

rpm

RPS

RTGB

RTV

RWP

RWT

SAMA PMC

SB

Engineered

Safety Feature

Flow Control Valve

ABASCO Standard Specification for an

FPL Project

Failure Modes

and Effects Analysis

The Florida Power

8 Light Company

Facility Review Group

Final Safety Analysis Report

[NRC] Generic Letter

Gallon(s)

Per Minute (flow rate)

Heat Exchanger

Hertz (cycle per second)

Instrumentation

and Control

Intake Cooling Water

[NRC] Inspector Followup Item

Institute for Nuclear

Power Operations

InService Testing

(program)

(Juno

Beach)

Nuclear Engineering

TS Limiting Condition for Operation

Loss of Coolant Accident

Letter of Instruction

Main Feed

Pump

Motor Operated

Valve

1

Motorized Valve

Non Cited Deviation

Non Conformance

Report

Non-cited Violation (of NRC requirements)

Nationa1 E1ectrical Manufacturers Association

Nuclear Production Facility (a type of operating license)

Nuclear Plant Supervisor

Nuclear Plant Work Order

Nuclear Regulatory Commission

NRC Office of Nuclear

Reactor Regulation

Off Normal Operating

Procedure

Operating

Procedure

Plant Change/Modification

Preventive

Maintenance

Pounds

per square

inch (gage)

Plant St. Lucie

Quality Assurance

Quality Instruction

Reactor Control Operator

Request for Engineering Assistance

Revision

Revolutions

per Minute

Reactor Protection

System

Reactor Turbine Generator

Board

A Type of silicone rubber

Radiation

Work Permit

Refueling Water Tank

Standard of Unknown Origin

Safety Train 8

~

'

21

SFP

SG

SIAS

SNPO

SRO

St.

TCV

TIC

TQR

TR

TS

UHS

URI

VIO

Spent

Fuel

Pool

Steam Generator

Safety Injection Actuation System

Senior Nuclear Plant [unlicensed] Operator

Senior Reactor [licensed] Operator

Saint

Temperature

Control Valve

Temperature

Indicator Controller

Topical equality Requirement

Temperature

Recorder

Technical Specification(s)

Ultimate Heat Sink

[NRC] Unresolved

Item

Violation (of NRC requirements)