ML17223B037

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Insp Repts 50-335/90-28 & 50-389/90-28 on 901023-1119. Violations Noted But Not Cited.Major Areas Inspected:Plant Operations,Maint & Surveillance Operations,Safety Sys Insp, Special Repts,Nonroutine Events & Followup of Insp Findings
ML17223B037
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 12/18/1990
From: Crlenjak R, Elrod S, Michael Scott
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17223B038 List:
References
50-335-90-28, 50-389-90-28, NUDOCS 9012270012
Download: ML17223B037 (29)


See also: IR 05000335/1990028

Text

~A,IA AEQUI

Wp0

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos:

50-335/90-28

AND 50-389/90-28

Licensee:

Florida Power

5 Light Co

9250 West Flagler Street

Niami,

FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St. Lucie

1 and

2

License Nos.:

DPR-67

and

NPF-16

Inspection

Conducte

.

Inspectors.

~

~/

AN. A.

Approved By;

R.

V. Cr

Divis.ion

ctober

23 - November

19,

1990.

/> /< f~

od,

Se

d'or

esi

t Inspector

Dat

Sig ed

P/8F~

t, Resi ent Ins

or

Date Signed

/z )8

FQ

enjak, Section Chief

Date

ign

of Reactor Projects

Scope:

SUMMARY

This routine resident

inspection

was

conducted

onsite in the

areas

of plant

operations

review, maintenance

observations,

surveillance

observations,

safety

system inspection,

review of special

reports,

review of nonroutine events,

and

followup of previous inspection findings.

Results:

No violations or deviations

were identified during the reporting period.

For

Unit 2, the licensee

conducted

part of a normal

outage this inspection period.

For the period,

Unit

1

had

a

normal

at-power

run with

a 'controlled

shut

down/restart for required Control

Element Assembly testing.

9012270012

901219

PDR

ADOCK 05000335

8

PDR

REPORT

DETAILS

Persons

Contacted

Licensee

Empl oyees

D. Sager,

St. Lucie Site Vice President

  • G. Boissy, St. Lucie Plant Manager

J. Geiger,

Vice President,

Nuclear Assurance

B. Guilbeault, Director, Nuclear Materials

Management

  • J. Barrow, Operations

Superintendent

J. Barrow, Fire Prevention

Coordinator

R. Church,

Independent

Safety Engineering

Group Chairman

  • H. Buchanan,

Health Physics

Supervisor

C. Burton, Operations

Supervisor

  • D. Culpepper, Site, Juno Engineering Supervisor
  • R.

Dawson,

Maintenance

Superintendent

  • J. Dyer, guality Control Supervisor
  • R. Englmeier, Site guality Manager

R. Frechette,

Chemistry Supervisor

C. Leppla,

ISC Super visor

G. Madden, Licensing Engineer

  • L. McLaughlin, Plant licensing Superintendent
  • B. Parks, guality Control Superintendent

L. Rogers, Electrical Maintenance

Supervisor

N. Roos,

Services

Manager

C. Scott,

Outage Supervisor

D. West, Technical Staff Supervisor

J. West, Mechanical

Maintenance

Supervisor

W. White, Security Supervisor

  • G. Wood, Reliability and Support Supervisor

E. Wunderlich, Reactor Engineering

Super visor

Other

1 icensee

employees

contacted

included

engineer s,

technicians,

operators,

mechanics,

security force members

and office personnel.

  • Attended exit interview

Acronyms

and initialisms used

throughout this report are listed in the

last paragraph.

-2.

Review of Plant Operations

(71707)

Unit I began

the inspection

period at power.

The unit was shut

down

on

October

27 to test

20

CEAs

.

While shutdown,

the licensee

investigated

potential

problems with TCBs

and the main turbine.

The unit was started

up

on October

29

and

ended

the inspection

period at

power - day

20

on

1 ine.

Unit 2 began

and ended the inspection period in a refueling outage.

'1

During this inspection" period,

NRC examiners

participated in the licensed

operator requalification testing

conducted

from October

29 to November 9.

a.

Plant Tours

b.

The

inspectors

periodically

conducted

plant tours to verify that

monitoring

equipment

was

recording

as

required,

apipment

was

properly tagged,

operations

personnel

were

aware of plant conditions,

and plant housekeeping

efforts were

adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

mre

properly

established,

critical clean

areas

were being controlled in accordance

with procedures,

exc ss

equipment or material

was stored properly,

and combustible materials

and debris

were disposed of expeditiously.

During tours,

the irxpectors

looked for the existeme

of unusual

fluid leaks,

piping vibrations,

pipe hanger

and seisaic restraint

settings,

various

valve and breaker positions, equipaent caution

and

danger

tags,

comporent

positions,

adequacy

of fire fighting

equipment,

and

instrument

calibration

dates.

Soae

tours

were

conducted

on backshifts.

The frequency of plant tocrrs

and control

room visits by site aranagement

was noted to be adequate.

The inspectors routinely conducted partial

walkdowns of ESF,

ECCS

and

support

systems.

Vclve, breaker,

and switch lineups

and equipment

conditions

were

randomly verified both locally and in the control

room.

The followiog accessible-area

ESF system walkdowns were

made

to verify that

system

lineups

were in accordance

vith licensee

requirements

for operability

and equipment material conditions

were

satisfactory:

Unit 2

CCW platform, Unit

1 "A" and

B'DGs, Unit 2

LPSI

pumps

(both aid-nozzle

and

SDC modes),

Unit I ECCS spaces,

and

Unit 1 cable spreading

rooms.

Plant Operations

Review

The

inspectors

periodically

reviewed shift logs

ard

operations

records,

including data

sheets,

instrument traces,

and records of

equipment malfunctions.

This review included contre1

room logs

and

auxiliary logs, operating

orders,

standing

orders, jmper logs

and

equipment tagout records.

The inspectors routinely observed operator

alertness

and

deoeanor

during plant tours.

They observed

and

evaluated

control

reom staffing, control

room access,

and operator

performance

during routine operations.

The inspectors

conducted

random off-hours iaspections

to assure

that operations

and security

performance

remained

at acceptable

levels.

Shift turnovers

were

observed

to verify that

they

were

conducted

in accordance

with

approved

licensee

procedures.

Control

room annunciator

status

was

verified.

Except as noted below,

no deficiencies

were observed.

'I

During this inspection

period,

the inspectors

reviewed the following

tagouts

(c'learances):

1-)0-98

Unit

1 TCB 7,

2-10-146

2B Bus Load Test Circuit Breaker,

and

2-10-327

breaker 2-93102,

2A CEA NG set.

Special

test

procedure

OP

2-0410026,

Rev 0, Differential Pressure

Testing of Notor Operated

Valves,

was partially performed

on Unit 2

on October

10.

The procedure satisfied certain

GL 89-10 requirements.

Appendix A of the procedure controlled the testing of SDC valves

HCV

3657

and

FCY 3306.

The procedure

required

no temporary

changes

to

correct errors

and functioned well in the

hands

of the operations

'taff.

The valves

operated

satisfactorily under

1B LPSI

pump full

flow operation.

The licensee

monitored

HCV 3657 characteristics

with

Novats test equipment.

On October

25, prior to taking the

)A startup

transformer

out of

service for PN, the licensee

conducted TS-required starts of the Unit

1

EDGs.

The

)A

EDG started

within 10

seconds

but the operator

thought that

1B

EDG took 12.6

seconds

to attain

60 Hertz.

Per the

applicable

TS,

EDG start timing for this condition was not required;

the

TS

had

been recently

changed

to

r equire

timed

EDG fast starts

twice

a year instead of monthly.

Prior to 1987,

the

)A

EDG frequency

meter in the control

room was

replaced with a meter dissimilar to those serving the other

EDGs.

No

similar meter

was available at the time.

The

1A EDG meter pointer

rest position

was at the low Hertz end of the scale.

The

1B

EDG

meter pointer rest position

was at the high Hertz end of the scale.

The remainder of the meters

in both units and the simulator were the

same

as the

1B meter.

EDG start timing was normally accomplished

by

the control

room operators

using these

meters

and

a stopwatch.

The operator first started

and timed the

1A EDG.

During the IB EDG

start,

the operator

simply forgot the meter difference

and waited an

extra overshoot to stop the stopwatch.

When timed by other utility

personnel,

the

1B

EDG performed correctly.

After the operators

determined

that

1B

EDG

was

operating

correctly,

the

lA startup

transformer

was taken out of service.

The

human factors

problem of frequency

meter

pointers

moving from

opposite directions only affects

the manual timing process.

When the

diesels

auto-start

due to

some

safety-related

signal,

the aeter

details

do not matter.

When timing is measured

by automatic timers,

these'eters

are

not used.

Part of the

human factors corrective

0

action

was to change

out the

1A meter in the control

room.

Since

no

meters

were available,

a

NPWO was written to exchange it with the

local

panel

meter.

At the

end of the inspection period, this action

was still pending.

During

a Unit

1

BAM station. tour, three

degraded

and rusted

pipe

hangers

were observed.

They were pointed out to, the operations staff

who issued

repair

NPWOs.

The hanger

condition did not jeopardize

safety-related

systems.

During

a Unit

1

ECCS area tour, several

indications of boric acid

leakage

were observed:

Boric acid build up was noted

on the shaft seal

area of the

1B

Containment

Spray

pump.

The spray

pump

had slight buildup

of acid during the last unit startup with no evident

leakage

during operation.

The acid

had yet to be cleaned

since that time

and

more

accreted

over the 'intervening

approximate

3 months.

The

buildup

was

due

to very slight leakage

at the'nitial

startup

of the

pump;

as

the

pump

came

up to

speed,

the

mechanical

pump seal

ceased

to leak.

A NPWO was existing from

the,startup

of the unit.

When questioned

about about the leak

rate,

Operations

re-opened its dialogue with the engineering

group regarding acceptable

leak rates for such mechanical

seals,

had the

seal

area

cleaned

of boric acid,

and ran the

pump to

verify the above observed

leakage

phenomena.

Boric acid buildup and standing moisture were noted in the drip

pan

beneath

the

1C

HPSI

pump.

Operations

had the drip pan

cleaned

of boric acid residue

and

was to monitor the area for

points of leakage.

Mechanical

maintenance

had

a

NPWO

on

a

suspect

valve,

V 3867,

that

would

be

pursued

on

a higher

priority basis.

1R 335,389/90-18

discussed

impeller-cavitation-induced

erosion of the

1A

CCW pump.

A proposed

corrective action in a licensee evaluation

report

was to review operating

procedures

for any needed

changes

to

preclude

pump run out.

One

pump supplying two

CCW trains,

as during

an outage,

was of prime interest.

During a Unit 2

CCW platform area tour

on October 25, the 2A CCW pump

discharge

pressure

was

60 to

65 psig

vice the

110-psig

normal

operating

pressure.

At the time, the

pump was supplying both A and

B

trains.

The

inspector

discussed

this

near

run

out condition with the

operations

staff.

The

ANPS in charge

of the unit had previously

throttled

pump flow to 9,000

gpm to stay

below

a

known

CCW heat

0

'5

exchanger

design

flow limit of 10,500

gpm.

He was

unaware of any

other

imposed limits.

Neither -engineering

nor the technical

support

staff had yet provided operations

a not-to-exceed

pump flow value to

prevent

pump

run out or impeller cavitation.

On October

27, the

operations

department

issued

a night order indicating that

CCW flic

should

be limited to 10,000

gpm until the flow question

was resolved.

Subsequently,

technical

support

personnel

considered

that the

CCM

heat

exchanger

limiting flow of 10,500

gpm

would probably

be

sufficient to prevent impeller damage.

They planned to transmit

a

formal answer to the operations staff.

According to FPL drawing 2998-4182,

the

pump head curve,

pump run cut

occurred

during

a vendor's test at 11,000

gpm

pump flow with 65 feet

NPSH,

135 feet discharge

head

(approximately

58 psig),

and

75

F water

temperature.

The inspector

concluded that the 10,500

gpm limit waald

preclude

pump run out.

Unit

1

was

shut

down

on October

27 to conduct

NRC-.required

CEA

testing.

Hajor procedures

in use for the shutdown were:

OP 1-0030128,

Rev 7, Reactor

shutdown,

and

OP 1-0030125,

Rev 22, Turbine Shutdown - Full Load to Zero Load.

Trainees

from the ongoing operator licensing class

performed reactor

and t'urbine control duties

under the close supervision of licensed

operators.

The

shutdown

was

performed

smoothly.

Following the

shutdown,

several

surveillance

procedures

and minor

SNOW repairs mre

performed prior to the

CEA test.

The

20

suspect

CEAs were tested

during full-length withdrawal

at@

insertion per

NPWO 17969/61

and LOI-0-40, Rev 0, Testing of "Origisal

Design" Type 81 Control Element Assembly.=-

Additionally, coil current,

traces

were recorded.

The test results

were satisfactory.

During the

CEA testing,

a

new computer-controlled

device,

a "sticky

gripper monitor", developed

by the site

18C department

was plugged

into

the circuit for first time

evaluation

of its

sensing

capabilities.

Its output controls

were not attached

to the

CEA

controls.

This device will function,

on

a per

CEA basis, similar to

the Unit 2 ACTM circuits that detect

CEA drive upper gripper sticking

and lock the lower gripper,

thus reducing the occurrence

of dropped

CEAs during startups.

The

new device's

sensing circuits

seemed to

function well.

While attempting to return Unit

1 to power operation

on October 28,

the

main turbine high pressure

end vibration probe indicated higher

than

normal vibration at

the

number

one

bearing.

The licensee

removed

covers

from the area

around

the bearing

and took main shaft

runout

readings

while operating

the turning

gear

to verify an

instrumentation malfunction..Power

ascension

was

resumed

on the 29th

and full power was attained

on the 31th.

The posting of required notices to workers

was reviewed

by the

NRC

HP

staff during this inspection period with no adverse findings.

During the

inspection

period,

Unit

2 was to enter

a reduced

RCS

inventory condition to support

the

SG

nozzle

dam

removal while

returning from the refueling outage.

The evolution was scheduled for

October

31 at 5:30 a.m.

The following items were checked. for this

evolution:

J

Containment

Closure Capability - Instructions

were

issued

to

accomplish this; personnel

and tools were stationed.

RCS Temperature

Indication - Cables

were connected

to four CETs

for temperature

display in the control

room.

RCS

Level Indication - Independent

RCS wide

and

narrow range

level

instruments

were

operating~ and providing control

room

indication.

The Tygon tube loop level

gage in the containment

was

manned

during level

changes

and

checked

every

two hours

during static conditions.

A licensed

operator

was assigned

to

monitor control

room indication throughout mid-nozzle operation.

K

RCS Level Perturbations

- When

RCS level

was altered,

additional

operational

controls

were

invoked.

At plant daily meetings,

operations

routinely made

announcements

to not

even consider

performing

work that might effect

RCS level

or shut

down

cooling.

RCS Inventory Volume Addition Capability -

One HPSI

pump and

a

second

LPSI

pump were available for RCS addition.

No charging

pumps

were to be available for this mid- nozzle evolution.

RCS Nozzle

Dams - Instructions were issued for their removal.

Vital Electrical

Bus Availability, - All required vital busses

were available for the evolution.

No vital bus work was to be

performed during the reduced

inventory condition.

Non-vital bus

2Bl was repaired during mid-nozzle.

That this bus did not power

anything associated

with the evolution had

been

checked

by three

.separate

SROs.

On

November ll, Unit 2 was in mode

5 following refueling.

While

performing

safeguards

time

response

testing, 'n

I8C technician

depressed

the group

5 pushbutton

instead of the group

3 pushbutton.

This actuated

equipment

and alarms not anticipated

by the operators.

The operating

crew immediately notified the

I&C personnel

of the

unexpected

actuations

and verified that shutdown cooling had not been

affected.

All the erroneously

selected

equipment actuated

properly

unless

out of service or already operating.

Testing

was terminated,

safeguards

was reset,

and

the

equipment

restored

to its pre-test

condition.

No plant equipment

damage

had occurred

and the licensee

promptly notified the

NRC.

The licensee

plans to issue

an

LER

concerning

the event.

c.

Technical Specification

Compliance

Licensee

compliance with selected

TS

LCOs was verified. This included

the

review

of

selected

surveillance

test

'results.

These

verifications were accomplished

by direct observation of monitoring

instrumentation,

valve positions,

and switch positions,

and by review

of completed

logs

and records.

Instrumentation

and recorder traces

were observed for abnormalities.

The licensee's

compliance with LCO

action

statements

was

reviewed

on

selected

occurrences

as

they

happened.

The inspectors

verified that related plant procedures

in

use

were adequate,

complete,

and included the most recent revisions.

d.

Physical

Protection

The,.inspectors

verified by observation during routine activities that

security program plans were being implemented

as evidenced

by: proper

display of picture badges;

searching

of packages

and personnel

at the

plant entrance;

and vital area portals being locked and alarmed.

Overall,

the licensee

supported

the Unit 2 outage activities well

and

maintained Unit 1 in an operational

condition.

)

3.

Surveillance Observations

(61726)

Various

plant

operations

were verified to

comply with selected

TS

requirements.

Typical of these

were confirmation of TS compliance for

reactor

coolant chemistry,

RWT conditions,

containment

pressure,

control

room ventilation

and

AC and

OC electrical

sources.

The

inspectors

verified that

testing

was

performed

in

accordance

with

adequate

procedures,

test instrumentation

was calibrated,

LCOs were met,

removal

and restoration

of the affected

components

were accomplished

properly,

test results

met requirements

and were reviewed

by personnel

other than

the individual directing the test,

and that any deficiencies

identified

during the testing

were properly reviewed

and

resolved

by appropriate

management

personnel.

The following surveillance tests

were observed:

OP 2-0410050,

Rev 16,

HPSI/LPSI Periodic Test,

was performed

on the

2A

LPSI

pump.

It was

being returned

to service following system drain,

multiple system entries into other parts of the system,

and system refill.

System venting, which had recently

been

a problem on Unit 1, successfully

eliminated trapped-air-related

water

hammer

problems.

Pump operation

was

satisfactory.

Several

control

room flow meters for this system indicated

erratically and were flagged for additional

sensor venting.

MP 2-0960152,

Rev 4,

2B Safety Battery Performance

Test,

was performed

on

October

23 under

NPWO 8336/62

using the three-hour rating of 637 A.

The

procedure,

which had

been significantly modified by TC following a recent

field evaluation,

worked quite well.

The computer-controlled

load bank

and data recorder,

and the

2B battery its'elf, also functioned well.

The

test concluded with the performance of MP 0960164,

Rev 5,

125

VDC System

Monthly Maintenance.

Following The Unit

1

shutdown

on October

27,

operators

were

observed

performing

OP

1-1210051,

Rev

10,

Wide

Range

Nuclear

Instrumentation

Channels

Functional Test.

The functional test

was satisfactory.

Prior to conducting

CEA tests

on October

28,

operators

conducted

RPS

testing

per

OP

1-1400059,

Rev

17, Reactor

Protection

System - Periodic

Logic Matrix Test.

Due to its nature, this test also required tripping of

the

TCBs numerous

times.

Conduct of testing

was satisfactory,

however

TCB

3 tripped

open

unexpectedly

and

TCB

7 failed to close.

The operator

properly stopped

the test until

TCB performance

was resolved.

Following

TCB evaluation,

the test

was

completed satisfactorily.

Specific

TCB

problems are discussed

in paragraph

4 below.

Prior to conducting Unit 2

ATWS tests

on November 18, operators

conducted

RPS testing

per

OP 2-1400059,

Rev 13, Reactor Protection

System - Periodic

Logic Matrix Test.

Conduct of testing

was satisfactory

and the

TCBs

functioned properly.

Re-performance

of portions of the

18-month

ESF test,

per

OP 2-0400050,

Rev. 8, Periodic Integrated

Test of the

Engineered

Safety Features,

was

observed

on

November

10-11.

This test contained

several

sub-tests

and

verified plant

response

to

a

loss of offsite power followed by

ESF

-actuation;

load tested

the

EDGs; and tested

a number of specific equipment

interactions,

some

during the loss-of-offsite-power test

and

some under

other conditions.

The test

had been routinely conducted at the beginning

of refueling

outages

so that

unexpected

failures

could

be efficiently

evaluated

and corrected prior to

post-outage

unit restart.

The retest

was scheduled

as

a

more efficient maintenance

post-test

than individual

equipment tests.

At the

end of the 24-hour

EDG test run, the

EDGs were required to be

restarted within 5 minutes to demonstrate

hot start capability.

During

the October

2-3 test,

the

EDGs

had run well during the 24-hour test

run

but were still at post-run idle speed

vice stopped

when restarted.

They

responded

proper ly for the condition

by accelerating

to operating

speed

and then loading, but the surveillance

requirement

was not satisfied.

The

EDGs were subsequently

overhauled

as

planned.

The 24-hour test run and

hot restart

were repeated

during the November

10-11 safeguards

test.

The

EDGs ran wel'l again

and restarted

properly.

IR 389/90-24,

paragraph

7, discussed

DC vice AC HFA relays

being installed

in certain

ECCS control valves.

If throttled after

an

ESF actuation,

the

valves

would re-open

when the control

was

released.

Since the

A train

relays

had

been

restored

to design,

valve throttle function for A train

valves

was tested

and confirmed during the

safeguards

retest.

B train

valve relays

were scheduled for replacement

when plant conditions allowed.

They will be individually retested.

The

surveillance

program

observations

were

satisfactory

for this

inspection

period with the licensee

responding

appropriately to various

test results.

4.

Maintenance

Observation

(62703)

Station maintenance'activities

involving selected

safety-related

systems

and

components

were

observed/reviewed

to

ascertain

that

they

were

conducted

in accordance

with requirements.

The following items

wet e

considered

during this review:

LCOs were, met; activities were accomplished

using

approved

procedures;

functional

tests

and/or calibrations

were

performed prior to returning

components

or systems

to service; quality

control records

were maintained; activities were accomplished

by qualified

personnel;

parts

and

materials

used

were

properly certified;

and

radiological controls

were

implemented

as

required.

Mork requests

were

reviewed to determine

the status of outstanding

jobs

and to assure

that

priority was

assigned

to safety-related

equipment.

Portions

of the

following maintenance activities were observed:

NPNO 7165/61

required

replacement

of type

AGC fuses

on

CEDM coil power

programners

for all Unit

1

CEDHs. It also required marking of the fuse

holder

caps with a paint stripe to allow visual verification of the cap

being fully shut.

LER 335/90-08

had reported multiple drops of a

CEA

because

of a loose fuse holder cap.

The work was performed

on October

28

prior to the

special

CEA tests.

The

new fuse holder

cap markings

indicated

cap status quite effectively.

Troubleshooting

and repair of Unit

1 TCBs

3 and

7 was observed following

their failure during the

RPS logic matrix test

on October 27.

The

TCB 3 undervoltage trip coil had

burned out, which occasionally

occurs to normally-energized

equipment.

That accounted for the

TCB

tripping.

The undervoltage trip unit was replaced

per

NPNO 5027/61.

Post

replacement

adjustment

and

testing

was

accomplished

per

EHP-63.01,

Rev 2, Periodic Haintenance

of Reactor Trip Switchgear

and

Breakers,

section

8.2,

the quarterly

TCB inspection.

Several

required

gC witness points addressed

critical performance

elements.

'1

10

TCB

7 was troubl.eshot,

replaced,

and the

new breaker

inspected

per

NPWO 5028/61.

One of two TCB 7 closing latch springs

had

come loose

from the

two bars it normally attached

to.

These

springs

held the

latch in tension

arid provided

the

energy to

snap

open

the

main

contacts

when the

TCB tripped open.

Since that portion of the

TCB

would be repaired- only by the vendor,

a replacement

TCB was obtained

from stores,

tested,

and installed

per

1-EMP-63.01,

Rev 2, section

8.3, the

18-month

TCB inspection.

This section also included all the

steps

and required

QC witness points of section 8.2 mentioned

above.

It was

observed

that the springs for the failed TCB were wound alike

but those for the

replacement

were

counter-wound.

Licensee root

cause investigation

developed initial verbal information that the two

springs

should

be counter-wound for electrically-operated

TCBs

and

that the two springs

must

be installed in a specific configuration.

Approved

vendor

manual

8770-3561

did not discuss

this but it was

confirmed in

a vendor letter dated

November 2, 1990.

The licensee

promptly

determined

that all

TCBs

in

use for both units

had

counter-wound

spr ings except Unit

1

TCBs 2, 6, and newly-installed

7

which had reversed

springs.

A vendor representative

restored

these

three

TCBs to design

on November

12 per

NPWOs 5047/61,

5048/61,

and

5049/61.

The

licensee

was

auditing

GE's facility to'etter

understand

the root cause.

Initial licensee

review determined

that

TCB spring failure was not a

safety

concern at St.

Lucie because

the failure would occur only

while the

TCB was opening

and would not prevent proper opening - the

safety function of St. Lucie TCBs was to open upon

demand.

Following

the

inspection

period,

the

vendor

documented

in letter

JMA90130,

dated

November

27,

1990, that if one spring were to come off, the

other would also

come off and the breaker would no longer close.

The

inspector

concluded that this spring failure mode is self-identifying

prior to the

TCBs being relied upon for reactor protection.

NPMO 8330/62

provided, work control for the

PM inspection

and

bearing

replacement

of the

2A HPSI motor.

During post-maintenance

functional

motor testing,

the licensee

discovered

a potential vibrational

problem.

NPMO 5467/62

permitted

the reliability group to conduct

more extensive

vibrational testing,

which indicated that the replacement

bearings

were

less

than optimum.

The babbitt type bearings

were replaced

a second

time

at the end of the inspection period.

Other maintenance

items are discussed

in the paragraph

below.

5.

Outage Activities (62703)

The inspector

observed

the following overhaul activity during the ongoing

Unit 2 outage:

NPbS 3638/62

provided

work control for repairs

to

V 3227,

the

2A1 loop

injection check valve,

per

GMP-Ol,

Rev 0, Disasseahly,

Inspection,

and

11

.

Reassembly

of Plant

Check

Valves.

The inspectors

observed

valve disk

sanding.

The contractor

involved

was

" utilizin'g 'a

FPL-provided

Dexter

machine for the work.

The valve

and

a sufficient adj'acent

area

had

been

tented for ALARA considerations

during the sanding.

The health physics

aspects

and

overall

job control

were

good.

The

licensee

provided

machinist support in the manufacture

of sanding

caps

used

on the machine.

FPL mechanical

maintenance 'provided

continuous

engineering

supervisory

coverage for this

as well as other valve repairs

being performed

by this

contractor.

The observed

work was satisfactory.

This particular valve

had

a minor leak (approximately 0.2

gpm, ref.

IR

335,389/89-16,

paragraph

10) during the entire previous fuel cycle.

The

leakage

had

caused

the

operational

staff

to

log

and

trend this

information.

Following identification

as

a leakage

source

during the

previous refueling outage,

'minor valve machining

had reduced

but had not

halted the leakage.

NPWO 3617/62 controlled

work on

V 1202,

one of three pressurizer

safety

reliefs.

During past

outages,

all three relief valves

had

been

removed

for testing or overhaul,

but this -outage

the licensee

only removed the

ASME Code

recoomended

sample

size of one.

The remaining

two valves

had

exhibited

no leakage

during the last

power operation

period.

V 1202 was

bench tested with zero

leakage

and the lift pres'sure

was within limits

during pressure

testing.

The valve was reinstalled after testing without

disassembly.

Procedure

MP-0017,

Rev

22,

Pressurizer

Valve Safety

Maintenance,

Appendix

C,

Flange

gasket

replacement,

was utilized to

reinstall.

the valve.

The initial pipe-flange-to-valve-flange

alignment

was slightly off after

snugging

of the

flange bolts;

the

procedure

requirements

were followed to measure

and correct the misalignment,

a lack

of parallelism, prior to torque application.

The parallelism between

the

piping and valve inlet flange

was required to attain proper spiral-wound

gasket crush

between

the flanges.

Health Physics

aspects

of this job were. good.

A HP technician monitoring

the contract

mechanics

performing

the

work was directing

changes

to

anti-contamination

dress.

Sufficient shielding

was installed to keep the

dose rate low.

The mechanics

were applying proper

HP practices.

An FPL

technical

support

engineer

was

present for at least part of the initial

flange

makeup.

Contractor

crew changes

occurred primarily due to heat

stress

reasons

rather than radiation exposure limit reasons'.

Turn over at

crew changes

was good.

NPWO 8045/62 controlled

work on the reactor incore instrumentation that

penetrates

the reactor

vessel

head.

Procedure

ISC 1400023,

Rev 1, Incore

Instrumentation

(ICI) Outage

Tasks,

was the instruction used during the

instrumentation

work.

The inspector

observed

removal of the bullet noses

and part of the clean

up of flanged joints connecting the cabling through

the vessel

head.

The flanges

were cleaned

and inspected

to ensure that

a

good seal

was attained at these

pressure

boundary joints.

The work, which

was performed in air fed hoods,

proceeded

smoothly with highly visible and

supportive supervisors

and

HP.

12

The ten bullet noses

were guides installed syometrically around the vessel

head to aid in the removal

and installation of the upper guide structure

on the vessel

head;

the

noses

were installed prior to the removal of the

UGS after reactor

shutdown.

The bullet noses

were not used during power

operation..

ADY MV 08-18B

had both its actuator

and its valve overhauled

during the

outage.

NPWOs

8532/62

and

1089/62 controlled

the work evolutions.

At

val've disassembly,

the inspector

inspected

the disassembled

valve parts

and

reviewed

the mechanic's

inspection findings.

The intended repair

actions

were appropriate

and conservative.

The disassembled

actuator

showed

no signs of wear and the overhaul activi.ty was well controlled.

Work process

sheet

5033

provided

work control for site construction

service

personnel

during retubing of the

2B

CCW heat'xchanger.

The

inspectors

observed

aspects

of the entire job, which took approximately

three

weeks.

The effort

was

well controlled with'isible

gC

and

supervisory

involvement.

The retubed

heat

exchanger

hydrostatic test failed.

No problems

were

found with the

new

tube

bundle.

However,

the test

identified

a

through-wall, weld defect in an existing bimetallic weld between the outer

shell

and the

ICW outlet tube sheet.

By the end of the inspection period,

the licensee

had evaluated

and repaired

the defect with the aid of the

heat

exchanger

manufacturer

and corporate

NDE specialist.

The

NCR 2-428

response

provided repair directions.

Hydrostatic, retesting

was planned.

The

above

outage

work was

performed with good

HP coverage,

visible

supervisor oversight,

and excellent work performance.

Design,

Design

Changes,

and Modifications (37700)

Installation of new or modified systems

were reviewed to verify that the

changes

were reviewed

and

approved in accordance

with 10 CFR 50.59, that

the

changes

were

performed in accordance

with technically

adequate

and

approved

procedures,

and that

subsequent

testing

and test results

met

acceptance criteria or deviations

were resolved in an acceptable

manner.

This review included selected

observations

of modifications

and testing in

progress

relating to

PCM 103-289,

which provided for installation of a

Unit 2

DSS to comply with 10 CFR 50.62

ATWS requirements.

The

PCM added

electronic circuit boards

to the existing safety-related

ESFAS cabinets.

These circuits will monitor

RCS pressure

and, if needed,

provide an action

signal to open newly-installed

load contactors

in series with each

CEA MG

set output circuit breaker.

This system

was designed to be independent 'of

and redundant

to the

RPS

and

was designed

to be diverse at the component

level.

Different manufacturers

or principles of operation

were used,

i.e.,

a contactor vice

a circuit breaker.

The

CEA

MG set output circuit

breakers

were

interlocked

to the

new load

contactors

such

that the

contactor

must

be

shut

before

the circuit breaker

could shut.

This

13

ensured

synchronizing

and loading functions

would

be

performed only by

circuit breakers.

The

inspector

reviewed

ongoing

modification

and

quality control

activities,

sampled

wiring installations,

and

witnessed

several

post-installation

system tests.

Observations

included portions of:

Preoperational

Test

2-1400200,

Rev

0,

ASS

Preoperational

Test,

sections

12.2, 12.3,

12.4,

12.6,

and 12.7;

and

IAC 2-1400052,

Rev

17,

Engineered

Safeguards

Actuation System-

Channel

Functional Test.

Testing

personnel

consistently

discussed

the test

with control

room

operators,

including alarms that might be received.

Testing

was conducted

strictly per

approved written procedures.

A test

change specifically

demonstrating

that

each

combination of two input signals

could cause

both

train's outputs to the contactor

was approved prior to performance.

Test

personnel

found that

CIS

Group

B did not actuate

from containment

high

radiation.

This was traced

to a mislabeled wire, which was corrected

and

retested.

The design contractor will address

this issue to ensure that it

was not

a design error.

On

November l,.a

number of jumpers previously

installed to support this modification were remved.

At that time, the

existing

systems

were

retested

per

18C

2-1400052

to

demonstrate

operability.

On November

18, both

A and

B train were

shown to trip the

respective

load contactor

and circuit breaker from the

ESFAS cabinet in

the control

room.

7.

Evaluation of Licensee

Self-Assessment

Capability (40500)

The

inspectors

evaluated

the

licensee's

self-assessment

programs

to

determine

whether

they contributed

to the

prevention

of problems

by

monitoring and'valuating

plant performance,

providing assessments

arid

findings,

and

communicating

and

following

up

on corrective

action

recommendations.

Portions of this evaluation

were previously accoaplished

in several

IRs:

IR 335,389/90-04,

paragraphs

3 and 4, discussing

Engineering

Response

and Effectiveness

of the Nonconformance

Reporting Program;

IR 335,389/90-09,

paragraph

4, discussing

the

ISEG, the

FRG,

and the

Industry Operating Experience

Program;

IR 335,389/90-18,

paragraph

2, discussing Quality Assurance

Audits of

the Corrective Action Program;

and

IR 335,389/90-22,

paragraph

2,

discussing

Quality Verification

Activities, Performance Monitoring, And Quality Assurance Audits; and

Paragraph

3, discussing

Engineering

Self-Assessments.

14

These reports

discussed

several

improvements that could be implemented but

found

no serious

problems.

IR 335,389/90-04

also

closed

a

1988 IFI

concerning

inconsistent

root cause

analysis

of failures.

This closeout

reported

completion of a spectrum of corrective actions for the identified

weakness.

IFIs 335,389/90-09-07

and 90-09-08 were promptly addressed

by

the licensee.

Corrective action status for these

items is discussed

in

paragraph

8 below.

The corrective actions for a number of minor items

previously identified by the resident inspectors

were also considered

as

a

'easure

of sensitivity.

It was

concluded

that the licensee

has

had

an

aggressive

corrective action

program in most cases

and the licensee

has

conducted

audits

in the area,

identified enhancements,

and

implemented

them.

The inspectors

had

no further questions

at this time.

8.

Followup (Units

1 and 2) (92701)

a.

Followup of Inspection Identified Items

(Closed - Units

1

8

2) IFI 335,389/88-07-02,

Establish

a Program to

Trend Valve Stroke Items.

This IFI concerned

the

ASME Code Section

11 valve stroke time test

program controlled

by procedure

AP 0010132,

ASME Code Testing of

Pumps

and Valves.

This

item

was

discussed

in

IR 335,389/89-26,

paragraph

6.a.

Changes

to overall

program

represented

by

a

new

revision

12 to the above procedure

and

AP 0010125A, Surveillance

Data

Sheets

(Rev

18 for Unit

1 and

Rev

19 for Unit 2), provided sufficient

direction and control for closure of this item.

Per discussion

and

demonstration

with operations

and

technical

support staff, valve

stroke information was

been

tracked appropriately.

IR 335,389/90-15

had been issued in this inspection

area with no outstanding

items.

(Open - Units

1

5 2) IFI 335,389/90-09-07,'eaknesses

in the

ISEG

Corrective Action System.

Weaknesses

primarily consisted

of not having

a formal, aggressive

corrective action

system that required written responses

and tracked

the corrective actions.

This item was addressed

on site in completed

Open Item Notice 90-00500,

dated 7-3-90.

Completion

was signed off

on August 6,

1990.

Final reinspection will occur at a later time.

This item remains

open.

(Open - Units

1

5

2)

IFI 335,389/90-09-08,

Weaknesses

in

FRG

Administration.

Weaknesses

included

abbreviated

minutes,

minutes not signed

by the

person

chairing that meeting,

and untimely distribution of minutes.

This

item

was

addressed

on site

by completed

Open

Item Notice

90-00501,

dated

7-3-90.

Completion

was signed off on September

7,

1990.

Final reinspection will occur at

a later time.

This item

remains

open.

0

I

15

b.

Followup of Headquarters

and Regional

Requests

(Closed Units

1

& 2)

P2188-03,

Gamma-Metrics

Cable Assemblies

in the

Post Accident Neutron Monitoring System

May Leak.

This condition was reported

by Gamma-Metrics

to the

NRC on February

19,

1988

as

a potential

cable

assembly leak, at elevated

temperature,

'n metal

hose solder joints.

This might allow moisture to enter the

cable

and contact cable connectors - causing signal interference.

For Unit 1, tests

in

1988

showed that

both

A and

B train cable

assemblies

leaked but no authorized repair

had been developed.

NPWOs

'899/61

and

7056/61,

along with Gamma-Metrics certification letters

dated

March 8,

1990,

showed that the Unit

1 cable

assemblies

were

replaced

then the replacements

repaired

in February

and March, 1990.

Zero power adjustments

were subsequently

performed.

I&C Procedure

1-1240065,

Excore Neutron Flux Monitor quarterly,

demonstrated

power

calibration

on May 16,

1990, following Unit 1 restart from refueling.

For Unit 2, this

item is closed

as

Not Applicable.

Unit 2 used

General

Atomic Brand post accident

neutron monitors.

9.

Exit Interview (30703)

The inspection

scope

and findings were

summarized

on November 21,

1990,

with those

persons

indicated

in paragraph

1

above.

The inspector

described

the

areas

inspected

and

discussed

in detail

the inspection

findings listed

below.

Proprietary material is not contained

in this

report.

Dissenting

comments

were not received

from the licensee.

Item Number

Status

Description

and Reference

335,389/88-07-02

Closed

IFI - Establish

a Program to Trend

Valve Stroke Items,

paragraph

Ba.

335,389/90-09-07

Open

335,389/90-09-08

Open

335,389/P2188-03

Closed

IFI - Weaknesses

in the

ISEG

Corrective Action System,

paragraph

8a.

IFI - Weaknesses

in

FRG

Administrati on, paragraph

8a.

IFI - Gamma-Metrics

Cable Assemblies

in the Post Accident Neutron Monitoring

System

May Leak, paragraph

9.

10.

Abbreviations,

Acronyms,

and Initialisms

ACTH

Automatic

CEA Timing Module

AFAS

Auxiliary Feedwater

Actuation System

AFM

Auxiliary Feedwater

(system)

16

ALARA

ANPO

ANPS

ANSI

AP

ASME Code

ATWS

BAM

CCW

CE

CEA

CEDM

CEOMCS

CET

CFR

CIS

CWD

CWO

DPR

DSS

ECCS

EOG

EMP

ESF

ESFAS

FCV

FI

FPL

FRG

FSAR

FT

GE

GMP

gpm

HCY

HFA

HP

HPSI

I&C

ICW

IFI

IR

ISEG

JPE

JPN

LCO

LER

LOI

LPSI

As

Low as Reasonably

Achievable (radiation exposure)

Auxiliary Nuclear Plant

t unlicensed]

Operator

Assistant Nuclear Plant Supervisor

American National Standards

Institute

Administrative Procedure

American Society of Mechanical

Engineers Boiler and Pressure

Vessel

Code

Anticipated Transient Without Scram

Boric Acid Makeup (station, etc.)

Component Cooling Water

Combustion Engineering

(company)

Control Element Assembly

Control Element Drive Mechanism

Control Element Drive Mechanism Control

System

Core Exit Thermocouple

Code of Federal

Regulations

Containment Isolation System

Control Wiring Diagram

Construction

Work Order

Demonstration

Power Reactor

(A type of operating license)

Diverse

Scram System

Emergency

Core Cooling System

Emergency Diesel

Generator

Electrical Maintenance

Procedure

Engineered

Safety Feature

Engineered

Safety Feature Actuation System

Flow Control Valve

Flow Indicator

The Florida Power

& Light Company

Facility Review Group

Final Safety Analysis Report

Flow Transmitter

General Electric Company

General

Maintenance

Procedure

Gallon(s)

Per Minute (flow rate)

Hydraulic Control Valve

A GE relay designation

Health Physics

High Pressure

Safety Injection (system)

Instrumentation

and Control

Intake Cooling Water

[NRC] Inspector

Followup Item

[NRCj Inspection

Report

Independent

Safety Engineering

Group

(Juno Beach)

Power Plant Engineering

(Juno

Beach

Nuclear Engineering

TS Limiting Condition for Operation

Licensee

Event Report

Letter of Instruction

Low Pressure

Safety Injection (system)

e

e

MG

MOV

MOVATS

MP

MV

NCR

NDE

NPF

NPO

NPS

NPSH

NPWO

NRC

OI

ONOP

OP

PM

PSL

PWO

PWR

QA

QC

RCO

RCP

RCS

Rev

RO

RPS

SDC

SG

SI

SNPO

SRO

STA

TC

TCB

TS

UGS

VIO

17

Motor Generator

Motor Operated

Valve

Motor Operated

Valve Test System

Maintenance

Procedure

Motorized Valve

Non Conformance

Report

Non Destructive

Examination

Nuclear Production Facility (a typ

Nuclear Plant Operator

Nuclear Plant Supervisor

Net Positive Suction

Head

Nuclear Plant

Work Order

Nuclear Regulatory Comission

Operating Instruction

Off Normal Operating

Procedure

Operating

Procedure

Preventive Maintenance

Plant St. Lucie

Plant Work Order

Pressurized

Water Reactor

Quality Assurance

Quality Control

Reactor Control Operator

Reactor Coolant

Pump

Reactor Coolant System

Revision

Reactor [licensedj Operator

Reactor Protection

System

Shut

Down Cooling

Steam Generator

Safety Injection (system)

Senior Nuclear Plant [unlicensedj

Senior Reactor [licensed] Operator

Shift Technical Advisor

Temporary

Change

Trip Circuit Breaker

Technical Specification(s)

Upper Guide Structire (part of the

Violation (of NRC requirements)

e of operating license)

Operator

reactor)

I ~