ML17219A711

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Insp Repts 50-335/87-11 & 50-389/87-10 on 870622-26.Major Areas Inspected:Gaseous Liquid & Radwaste mgt,NUREG-0737 TMI Item II.F.1,Attachment 1 & 2 Implementation,Info Notices & Previous Followup Items
ML17219A711
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 07/15/1987
From: Gloersen W, Kahle J, Stoddart P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17219A709 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-2.F.1, TASK-TM 50-335-87-11, 50-389-87-10, IEIN-86-030, IEIN-86-042, IEIN-86-076, IEIN-86-30, IEIN-86-42, IEIN-86-76, NUDOCS 8707280012
Download: ML17219A711 (24)


See also: IR 05000335/1987011

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W,

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/87-11

and 50-389/87-10

Licensee:

Florida

Power and Light Company

9250 West Flagler Street

Miami, FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St. Lucie

1 and

2

License Nos.:

DPR-67 and

NPF-16

Inspection

Conduct

Inspectors:

4

o r

n

ne 22-26

1987

ate

gne

P.

G.

oddart

ate

S>gne

Accompanying Person

1:

.

B.

K hie

Approved by:

a

e,

Se

s

)e

Divis on of Radiation Safety

and Safeguards

Date

sgne

SUMMARY

Scope:

This special

unannounced

inspection involved an examination

on site in

the

areas

of gaseous

and liquid radwaste

management,

TMI/NUREG-0737 II.F.l.

Attachments

1

and

2

implementation,

Information

Notices,

and,

previously-identified inspector followup items.

Results:

One violation was identified - inadequate

procedures

for operation of

the waste

gas

system.

7O7P800i2

8707

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gDOCK ODO< po~

REPORT DETAILS

Persons

Contacted

Licensee

Employees

  • K. N. Harris, Vice President
  • J. Barrow, Operations

Superintendent

(Acting Plant Manager)

  • T. Dillard, Maintenance

Superintendent

  • B. Parks,

gA Performance

Monitoring Supervisor

  • R. J. Frechette,

Chemistry Supervisor

  • R. E. Cox, Effluents Supervisor,

Chemistry Department

  • D. H. Faulkner,

Chemistry

  • H. M. Mercer, Health Physics
  • C. F. Leppla,

I&C Supervisor

  • L. W. Pearce,

Operations

Supervisor

  • C. A. Pell, Technical

Supervisor

Other

licensee

employees

contacted

included

engineers,

technicians,

operators,

and office personnel.

NRC Resident

Inspectors

  • P. Bibb,
  • D. R. Brewer, Senior Resident

Inspector - Turkey Point

  • Attended exit interview

Exit Interview

The inspection

scope

and findings were

summarized

on June

26,

1987, with

those

persons

indicated in Paragraph

1 above.

The inspector described

the

areas

examined

and

discussed

in detail

the inspection

firidings.

No

dissenting

comments

were received

from the licensee.

One violation was

identified

in

the

area

of

gaseous

waste

management

(Paragraph

6).

Additionally, one inspector

followup .item was identified regarding

the

sampling

of particulates

and

iodines

in plant effluents

during

and

following an accident

(Paragraph

9).

The licensee

did not identify as

proprietary

any of the materials

provided to or reviewed

by the inspectors

during this inspection.

Procedure

Review (84723, 84724)

The inspectors

reviewed

selected

portions of the following

procedures.'rocedures

with the prefix "C" were Chemistry procedures.

Procedures

with

the prefix "1-C-" or "2-C-" were chemistry procedures

applicable to Unit 1

or Unit 2, respectively.

Procedures

prefixed

"1" or "2" only were

Operations

procedures.

1-C-64

1-C-65

1-C-66

2-C-66A

2-C-66B

1-C-67

1-C-68

1-C-69

1-C-70

Rev. 9,

10/31/86,

Calibration of the Liquid Waste

Discharge

Radiation Monitor

Rev. 8, ll/5/86, Technical

Specification

Calibration of the

Gaseous

Radwaste

Monitor

Rev.

13,

11/3/86,

Technical

Specification

Calibration of the

Plant Vent, Fuel Building Exhaust,

ECCS,

and Steam Line Monitors

Rev. 5,

10/31/86,

Technical

Specification

Calibration of the

General

Atomic Gas Liquid and Steam Line Process

Monitors

Rev. 5, 3/10/87, Calibration of the General

Atomic Gas,

Liquid

and

Steam Line Process

Monitors

Rev. 8, 7/11/86, Calibration of the Containment

Process

Monitor

Rev. 6, 7/11/86,

Calibration of the

Component

Cooling Water

Radioactive Monitors

(NMC)

Rev. 7, 7/11/86,

Calibration of the

Steam

Generator

Blowdown

Radiation Monitors (Victoreen)

Rev.

17, 3/11/87,

Processing

Aerated Liquid Wastes

1-C-72

. Rev.

22, 3/18/87,

Processing

Gaseous

Wastes

C-74

C-06

C-09A

C-46

C-47

C-48

1-C-62

2-C-62A

2-C-62B

2-C-62C

Rev. 6, 11/17/86, Particulate

and Iodine Filter Testing

Rev. 5, 10/24/86,

Control of Radioactive Calibration Sources

Rev. 5, 10/24/86,

Primary and Secondary

Grab Sample

Rev. 9, 10/10/86,

Determination of Gross Alpha Activity

Rev. 5, ll/18/86, Determination of the Average

Beta

Gamma

Energy

E-Bar of Reactor Coolant

Rev. 5,

1/14/86,

Operation

of the

Nuclear

Data

(ND)

6605

Computer

Based

Counting System

Rev.

11, 10/31/86,

Process

Monitoring System Operation

Rev. 4, 1/9/87,

General

Atomic Particulate,

Iodine and

Gas

(PIG)

Process

Monitor Operation (Unit 2)

Rev. 4, 2/20/87,

General

Atomic Single Stage

Gaseous

(SSG)

and

Steam Line Process

Monitor Operation

Rev. 4,

10/31/86,

General

Atomic Single

Stage

Liquid

(SSL)

Process

Monitor Operation

2-C-62D

Rev. 4,

10/9/86,

General

Atomic

Wide

Range

(WRGM)

Process

Monitor Operation

2-C-62F

Rev. 2, 10/27/86,

Remote Operation of the General

Atomic Process

Monitor System

1-C-63

Rev. 7, 7/ll/86, Calibration of the

Condenser

Air Exhaust

Process

Monitor

C-111

Rev. 5, 11/5/86, Collecting Initial Set of Post-Accident

Samples

and

Guidelines for Establishing

Post-Accident

Water

and

Gas

Inventory Control.

Rev. 3,

12/10/86,

Es tab 1 ishing

Remote

Analysi s

Counting

Laboratory

and Counting Procedures

for Accident Samples

The reviewed

procedures

appeared

to be adequate

and

had

been reviewed

and

approved

by plant

management

and

administrations

in accordance

with

Technical Specification requirements.

No violations or deviations

were identified.

4.

Audits

Techni cal Specification 6.5.2.8

requires

audits to

be performed of unit

actsvsties

under

the

cognizance

of the

Company

Nuclear

Review

Board

(CNRB).

In the area of radiological effluents,

the licensee

is required

to audit the radiological environmental

monitoring program and the results

thereof at least

once per

12 months,

the Offsite Dose Calculation Manual

and implementing

procedures

at least

once per 24 months,

and the Process

Control

Program

(PCP)

and

implementing

procedures

at least

once

per

24

months.

The inspectors

reviewed the following audits

and appraisals:

QAA-QAP-84-577:

Re-evaluation

of Quality Program

and

Followup of

State of Florida Division of Radioactive Monitoring Services,

6/18/84

QAA-QAS-ENR-85-1:

Radiological

Environmental

and

Radioactive

Effluent Technical Specifications,

4/22/85

QAA-QSL-OPS-86-240:

Solid Radioactive

Waste

(Spent

Resin Transfer),

4/10/86

QAA-QAS-OSD-86-1:

Offsite

Dose

Calculation

Manual,

Appendix E,

9/24/86

QAA-QAS-ENR-86-1:

Radiological

Environmental Monitoring, 9/25/86

QAA-QSL-OPS-86-475:

Liquid and

Gaseous

Waste

Management

Systems,

11/24/86

QAA-QSL-OPS-86-472:

Non-radiological

and Radiological

Environmental

Protection

(Technical Specification Sections '3/4.11, 3/4.12, 3.3.3. 1.

3.3.3.9, 3.3.3. 10,

and Chemistry Procedure

C-200

(ODCM), 12/16/86

QAA-QSL-OPS-86-488:

Inplant Radioiodine

and Monitoring and Secondary

Water Chemistry,

1/8/87

QAA-QSL-OPS-87-537:

Special

Audit of Chemistry Section performed

by

General

Physics;

June

1-19,

1987, 6/24/87

QAA-QAP-87-281:

Audit of State of Florida Division of Radioactive

Monitoring

The inspectors

reviewed the audits

and noted that appropriate

actions

had

been

taken or were being taken

on the findings identified in the reports.

No violations or deviations

were identified.

5.

Reports

(84723,

84724,

80721)

a ~

Effluent Reports

Technical Specification 6.9.1.7

requires

the

licensee

to

submit

within

60

days

of January

1

and

July

1 of each

year,

routine

Radioactive

Effluent Release

Reports

covering

the operation of the

unit during

the

previous

six

months of operation.

The reports

include

a

summary of the quantities of radioactive material

released

from the unit as outlined in Regulatory

Guide 1.21.

Additionally,

reports

that

are

submitted

60

days after January

1 of each

year

include

an

assessment

of radiation

doses

due to the radioactive

liquid and gaseous

effluents released

from the unit or station during

the previous calendar year.

The inspectors

reviewed the Semiannual

Radiological Effluent Release

Report for the period July 1,

1986 through

December

31,

1986.

The

review included

an examination of the liquid and

gaseous

effluent

release

data

as .well

as

dose estimate

data.

Selected

data from this

report and previous reports

are presented

in Table 1.

The inspectors

noted that quantities of gaseous

radionuclides

released

during

1984

through

1986 were significantly higher than other Region II operating

pressurized

water reactors

(PWRs).

Additionally, the quantities of

radionuclides

released

in liquid form during the

same

time period

were higher than

most of the other

Region 'II PWRs.

Although these

radionuclide

releases

were higher

than the

average

PWR releases

in

Region II, the radiation

doses

from the primary effluent pathways

were

below

the limits specified

in

40

CFR

190,

Environmental

Radiation Protection

Standards for Nuclear Power Operations.

The

inspectors

noted

that

the

reporting

requirements

for the

Semiannual

Effluent Release

Report

as specified

by the Technical

Specifications

and

the licensee's

Offsite

Dose

Calculation

Manual

(ODCM) had

been

met.

The inspectors

discussed

the reporting of zero

values

in the

semiannual

reports

and

noted that

Zeros

should

be

defined in the reports

as

below the minimum detectable

limits of the

counting system.

Additionally, the inspectors

discussed

the reported

statistical

counting

errors

in

measurements

"reported

in

the

semiannual

report

and noted that more information should be provided

to justify the total statistical

error associated

with the effluent

measurements.

b.

Environmental

Reports

Technical Specification 6.9. 1.8 requires

the licensee

to submit prior

to Hay

1 of each year

a Routine Radiological

Environmental

Operating

Report

covering

the

operation

of the unit during the

previous

calendar

year.

The

inspectors

reviewed

1985

and

1986

Annual

Radiological

Environmental

Operating

Reports for omissions,

obvious

mistakes,

anomalous

measurements,

and

observed

biases.

The

inspectors

noted that the report included summaries,

interpretations,

and

information

based

on trend

analysis

of the results

of the

radiological

environmental'urveillance

activities for the report

period.

The

1986

environmental

samples

showing positive results

which were not consistent

with past

measurements

were attributed to

the

Chernobyl

incident since

the

samples

were collected during the

time the

plume passed

the affected area.

The

. licensee

concluded

that

the

levels

of radiation

and

concentrations

of radioactive

materials

in environmental

samples,

representing

the highest

potential

exposure

pathways

to members of

the public, were not increasing.

No violations or deviations

were identified.

6.

Radioactive

Gaseous

Effluent Process,

Treatment,

and Effluent Systems

(84724)

The inspectors

reviewed the licensee's

programs,

procedures,

and equipment

provided for the collection, processing,

treatment,

and release

to the

environment of radioactive,

or potentially radioactive

gases.

The waste

gas

processing

system at Plant St. Lucie

1

and 2'as

provided for the

maintenance

and control of the primary coolant cover gas

system.

In the

original design of the waste gas-processing

system,

waste

gas

was "bled"

from the

cover

gas

system

to

a

surge

tank,

from which the

gas

was

periodically

pumped

to

a series

of three

waste

gas

decay

tanks.

The

system

was designed

to retain or "holdup" waste

gas for an average of 30

days, after which the gas,

from which short-lived noble gases

had decayed

to

a

stable

non-radioactive

gaseous

form,

was

discharged

to

the

environment at

a substantial-ly

reduced radioactivity level.

A number of adverse

factors

were encountered

at the St. Lucie facilities

which have

made the

use of the designed

operating

mode of the waste

gas

processing

system impracticable.

The following factors were noted:

The design

volume capacity of the installed waste

gas

decay tanks

was

inadequate

to accommodate

the volume of waste

gas actually generated.

Each tank

was

144 ft'n volume and

had

a design operating pressure

of 150 psig,

or

about

10 atmospheres.

NUREG-0017, "Calculation of,

Releases

of Radioactive

Materials

in Gaseous

and Liquid Effluents

from Pressurized

Water Reactors

(PWR-GALE-CODE) provided for a 10-day

fill time and

a 10-day holdup period before release.

The licensee,

in the

FSAR, calculated

average total fill and holdup time to be 30

days.

In practice,

the licensee

found the fill and holdup'imes to

be

on the order of two to four days, primarily as

a result of higher

than anticipated

generation of disassociated

gases

and system air and

gas inleakage.

Both Units

1

and

2 also experienced

a higher than

normal

degree of

fuel

failure.

Fuel

failure resulted

in

higher

than

normal

concentrations

of fission products

and

gaseous

radioiodine in the

waste

gas

system

discharges

and

in

releases

from other

plant

discharge

paths.

Concentration

of these

gases

in the pressurized

waste

gas

decay

tanks

and related

systems

resulted

in increased

occupational

exposures

to plant workers.

The presence

of higher than

normal defective fuel at St. Lucie also

. resulted

in higher-than-normal

releases

of noble

gas

and iodine

fission

products

from other

gaseous

discharge

points within the

facilities.

The auxiliary building normal ventilation exhaust

system

and

the

containment

purge

exhaust

became

sources

of effluents

comparable

to,

and often larger

than

releases

from the waste

gas

system.

In April of 1984, plant management

decided to discontinue

the use'f the

waste

gas

decay

tank

system

in favor of direct

discharge

to the

environment

from the waste

gas

surge

tank to the plant vent.

The initial

action to implement this change

was to enter

changes

in the required valve

positions

in the

Control

Room

Locked

Valve Deviation List."

Unit 2

procedures

for waste

gas

system operation

and for waste

gas

system valve

lineup

were

revised

appropriately

to reflect

the

revised

mode of

operation.

However, the corresponding

procedures for Unit

1 had not been

revised

as of the date of this inspection.

Technical Specification 6.8. 1.a provided that written procedures

shall

be

established,

implemented

and maintained for radioactive waste

processing

systems

such

as

the waste

gas

system.

The failure to revise Operating

Procedures

1-0530020,

Waste

Gas

System

Operation,

and

1-0530021,

Controlled

Gaseous

Batch

Release

to Atmosphere,

to reflect existing

operating

conditions

was identified

as

an

apparent

violation of

NRC

requirements.

The licensee

was notified, both prior to and at the exit

meeting, that this omission

was considered

to be

a violation of Technical Specification 6.8. l.a, inadequate

procedures.

(Opened) Violation 50-335/87-11-01,

Inadequate

Procedures for Operation of

Waste

Gas

System.

Cl

Operation of the waste

gas

system in the

mode described

above, that is,

bypassing of the waste

gas

decay tanks

and release directly from the surge

tank to the

environment

through

the plant vent,

was

reviewed

by the

inspectors

relative to compliance with the Plant Technical Specifications

and Appendix I to

10 CFR 50,

Numerical

Guides for Design Objectives

and

Limiting Conditions for Operation

to

Meet the Criterion

"As

Low as

Reasonably

Achievable" for Radioactive

Materials in Light-Mater-Cooled

Nuclear

Power Reactor Effluents.

The inspectors

and licensee

representatives

discussed

calculations of air

doses

to unrestricted

areas

resulting from plant operation.

It was stated

that the difference in air doses

between operating the gas

decay tanks in

the holdup mode or in the bypass

mode was the difference

between

2.41 mrad/yr

and

3.47 mrad/yr,

or approximately

1 mrad/yr,

based

on

releases

from Units

1 and

2 combined in calendar year 1985.

Technical Specification 3. 11.2.4 requires that appropriate

portions of the

gaseous

radwaste

treatment

system

be used to reduce radioactive materials

in gaseous

waste prior to discharge

when the projected

gaseous

effluent

air doses

due to gaseous

effluent releases

from the site, to unrestricted

areas,

when

averaged

over

31

days,

would

exceed

0.2

mrad for

gamma

radiation

and 0.4 mrad for beta radiation.

Licensee calculations

appeared

to

show that releases

per unit per 31 day period resulted in air doses of

less

than

0. 15 mrad for combined

beta

and

gamma radiation.

Since

these

values

were

less

than

the

action

levels

specified

in Technical

Specification

3. 11.2.4,

the bypassing of the waste

gas

decay tank portion

of the gaseous

radwaste

system

appeared

to be acceptable.

Licensee

representatives

acknowledged

that their review of waste

gas

system operation

had identified the capacity

and number of waste

gas

decay

tanks provided in the original design

as inadequate

to permit operation in

accordance

with the design

concept of operation.

The licensee initiated

engineering

studies

(in

CY

1987)

to determine

means

or

methods

for

improving the design of the gaseous

waste treatment

system.

Engineering

solutions were expected

to be implemented at

a later date to be determined

based

on the outcome of the ongoing engineering studies.

In addition to the engineering

studies

noted

above,

the

licensee

has

undertaken

to improve the integrity of the fuel

by new fuel design

and

"reconstitution" of fuel assemblies.

Unit

1 was refueled in February

and

March of 1987, with the Unit

1 core currently

composed entirely of Exxon

fuel.

After a preliminary run at full power, Unit

1 was shut

down and all

fuel

re-examined

using ultrasonic

nondestructive

testing

methods,

and

underwater

video

camera

visual

inspection

techniques.

Several

fuel

defects

were

found

and the defective fuel

rods

were

removed

from fuel

bundles

and

replaced

with pre-tested

rods.

Fuel

bundles

were

then

returned

to the

core

and Unit 1

was returned

to power.

The licensee

referred

to

the

process

of

replacing

individual

fuel

rods

as

"reconstitution".

Prior to refueling, Unit

1

had

a level of defective

fuel that resulted

in abnormally high noble

gas

releases

from the plant.

After refueling, initial operation

indicated that noble gas releases

were

substantially

decreased

over

previous

experience;

however,

after

approximately

20-21

days

of operation,

noble

gas

releases

increased

rapidly over

a short

period of time.

The

subsequent

inspection

and

reconstitution

of the fuel resulted

in returning operational

noble

gas

effluent

levels

to

"freshly

refueled"

levels.

Operation

since

reconstitution

has

been

at

noble

gas effluent levels

approximately

a

factor of ten lower than during the previous fuel cycle.

Several

other factors were being studied

or implemented during the current

fuel cycle.

Fuel

is

now being fabricated

using

an approximately three

inch-long solid zircalloy cap at the lower end of each fuel rod.

Fuel

pellet conditioning prior to loading

was being

used to reduce

moisture

content,

which was suspected

to have

been

a factor in earlier fuel failure

mechanisms.

Bringing the

reactor

to

power at

a

slow

ramp

was

also

believed to result in a lower incidence of fuel failure.

During licensee

reviews of the offsite dose effects of plant effluents, it

was observed that the release

of gaseous

radioiodine in containment

purges

contributed

a large fraction of the projected

organ

doses

to individuals

in unrestricted

areas.

The original

design of the

containment

purge

system

provided high efficiency particulate air

(HEPA) filtration of the

exhaust

gases.

Engineering

studies

indicated

that

space

limitations

prevented

the addition of charcoal

adsorbers

to the existing

system.

Since particulates

had not been

an operational

problem at St. Lucie

1 and

2,

the

licensee

elected

to modify the existing filter installation to

permit

replacement

of the

HEPA filters with charcoal

adsorber

modules

which would provide

two inches

of activated

impregnated

charcoal

in the

space

previously allotted

to

HEPA filters.

This modification

was

calculated to reduce offsite iodine organ

doses

due to containment

purge

discharges

by a factor of approximately

10.

Doses

were further reduced

by

instituting a reduction in number of containment

purges

performed annually

as part of an overall plant effluent reduction

program.

The licensee's

10 CFR 50.59

review of the modification

was

reviewed

and "appeared

to be

acceptable.

One violation was identified.

Liquid and

Gaseous

Process

and Effluent Radiological

Monitoring

and

Sampling

System

(84723,

84724)

The inspector

reviewed the licensee's

program for monitoring and sampling

of radioactive

liquid and

gaseous

process

and effluent streams.

The

inspector

observed

the operation

of the

process

and effluent monitors

during

a tour of the facilities.

All monitors were operating at the time

of the inspection

and

appeared

to be functioning properly.

Calibration

and

maintenance

records

and

documentation

of

NBS traceability

of

calibration sources

were reviewed

and appeared

to be satisfactory.

The

NUREG-0737 high range effluent radiation monitors were reviewed during

the inspection

(Paragraph

9).

It was noted that Unit 1 uses

an Eberline

SPING-4 for effluent

stack .monitoring

and

sampling

of noble

gases,

0

radioiodines,

and particulates

and that Unit 2 used

a

GA (General

Atomics)

system

which included

a wide-range

gas monitor with a separate

skid for

particulate

and

iodine sampling.

Installations at both Units

1 and

2

appeared

to be acceptable

and were consistent with NUREG-0737,

Item II.F. 1

requirements.

All monitors

appeared

to be operating at the time of the

inspection.

No violations or deviations

were identified.

Liquid Radioactive

Waste

Systems

(84723)

The inspector

reviewed the liquid radioactive waste

system operation.

In

1986

and

1985, total plant releases

of liquid radioactive

wastes

to the

environment

were

4.96

curies

and

5.51 curies,

respectively.

Liquid

releases

in 1985-86 were responsible for more than

50K of the calculated

dose

to persons

in unrestricted

areas

as the result of plant operation.

Since February,

1986, the plant

has

had

a Quality Improvement

Team (QIT)

working to reduce the curie content of liquids released

from the plant.

Improvements

implemented

up to the

date of this inspection

included:

(a) optimization of recirculation through waste treatment demineralizers,

(b) reduction of high curie content input sources

such

as spent resin cask

dewatering,

(c) improvements

in filtration systems,

and (d) optimization

of demineralizer

resins for best

decontamination

factors

and capacity.

Improvements

being

considered

included

chemical

monitoring,

use

of

charcoal

pre-filtration to extend

demineralizer

capacity,

and

use of

roughing prefilters.

At the

same

time,

the parallel effort to reduce

gaseous

releases

by

improving fuel integrity was expected

to have

an effort in reducing curie

input to the liquid radwaste

system.

No violations or deviations

were identi-fied.

TMI/NUREG-0737 (25544)

a ~

NUREG-0737,

Item II.F.1, Attachment 1, described

the high-range

noble

gas

monitoring

system

that is required

to detect

and

measure

concentrations

of noble

gas

fission

products

in plant

gaseous

effluents

during

and following an accident.

These

monitors provide

the plant operator

and

emergency

planning agencies

with information

on plant releases

of noble

gases

during and following an accident.

The

inspectors

noted

that

an

Eber line

SPING-4 plant

vent stack

monitoring

system

was

used for Unit 1.

The

analogous

system

on

Unit 2 was

a General

Atomics Wide Range

Gas Monitoring System

(WRGM).

The microprocessors

on both systems

allowed the operator to readout

releases

directly in terms of uCi/cc.

The monitoring systems

were

located

on the roof of the auxiliary building in concrete

structures

which were in the

general

vicinity of the respective

plant vent

stacks.

Additionally, the inspectors

noted that

the calibration

procedure for these

noble gas monitoring systems

specified the use of

10

Cs-137

and

Ba-133 solid sources for the low, mid, and high ranges.

The General

Atomics Wide

Range

Gas Monitor (Unit 2) utilized three

detectors

to satisfy the range

requirements

specified in NUREG-0737.

The

low range detector utilized

a plastic scintillator, whereas

the

mid

and

high-range

monitors utilized solid-state

detectors.

The

Eberline

SPING-4 (Unit 4) utilized energy-compensated

GM tubes

to

accomplish

the

same task.

Based

on the review performed during this

inspection, it appeared

that

the

systems

met

the criteria of

NUREG-0737

Table II.1-1 for the

required

range

to monitor noble

gaseous

effluents during accident conditions.

NUREG-0737,'tem II.F.1,

Attachment

2 .described

the

sampling

and

analysis

requirements

of high-range

radioiodine

and particulate

effluents

in

gaseous

effluent

streams.

The

purpose

of the

requirements

was

to

provide

the

capability

to

determine

the

quantitative

release

of radioiodines

and particulates

under accident

conditions for dose calculation

and assessment.

NUREG-0737, II.F.1,

Attachment 2,

states

that

the

licensee

shall

provide

continuous

sampling of plant

gaseous

effluent for post-accident

releases

of

radioactive

iodines

and particulates

to meet

the

requirements

of

Table II.F.1-2.

The inspectors

reviewed

the licensee's

system for

sampling

and analysis

or measurement, of high-range

radioiodine

and

particulate effluents against

the sampling

requirements

outlined in

Table II.F.1-2 of NUREG-0737.

The

sampling

requirements

were

as

follows:

(1) representative

. sampling

per

ANSI

N13. 1-1969;

(2) entrained

moisture

in effluent stream

should

not

degrade

the

adsorber;

(3) continuous

collection of the

sample

whenever

exhaust

flow occurs;

and

(4) provisions for limiting occupational

dose to

personnel

incorporated

in sampling

systems,

in sample

handling

and

transport,

and in analysis of samples.

The inspectors

noted that one

inch stainless

steel

delivery lines

were

incorporated

into both

Unit

1 and Unit 2 systems.

The Unit 1 sample delivery lines were not

heat

traced

on exposed

surfaces.

Non-heated

sample delivery lines

could result in entrained moisture in the effluent stream which could

-degrade

the

adsorbers

used

for radioiodine

collection.

The

inspectors

noted that

the Unit 2 particulate

and iodine

sampling

system

(General

Atomics) consisted of an accident

sampling skid with

the capability to collect particulate

and iodine samples

via three

separate

shielded

sample

assembly

chambers

in parallel.

This system

allowed for the continuous

sampling of the stack effluents while one

of 'the

sampling

assemblies

was

exchanged

and

replaced

with a

new

charcoal

cartridge

and particulate filter.

The Unit

1 post-accident

particulate

and iodine sampling

system

(Eberline)

consisted

of one

sample

assembly

chamber.

The

licensee

used

procedure

C-110,

Collecting Initial Set of

'ost-Accident

Samples

and Guidelines for Establishing

Post-Accident

Water

and

Gas

Inventory Control,

Revision 5, ll/5/86, for the

post-accident

sampling, collecting,

and analysis of radioiodines

and

particulates.

The

inspectors

noted

that

the

procedure

did not

provide sufficient detail for the collection of

a post-accident

11

particulate

and iodine sample

and subsequent

delivery of that sample

to the analytical

counting

laboratory.

There 'ere

no apparent

provisions

to limit the

exposure

to chemistry

and radiological

controls

personnel

to, ensure

that

General

Design Criteria

(GDC)

19.

could be met for the retrieval

and analysis of plant effluent samples

during

an accident.

The licensee

indicated that the exposures

could

be limited by good practice techniques

when collecting, transporting,

and

measuring

post-accident

iodine

and particulate

samples.

The

licensee

agreed

that

a time/motion

and

exposure

study

should

be

documented

to show that the

maximum dose

expected for chemistry

and

radiological controls

personnel

assigned

to collect, transport,

and

, measure

post-accident

particulate

and iodine samples

from the plant

vent would be within GDC-19 criteria.

This item was identified as

an

inspector followup item.

(Opened)

Inspector

Followup

Item

( IFI)

50-335/87-11-02

and

50-389/87-10-01:

Review

time-motion

and

exposure

study

for

collection, transport

and analyses

of post-accident

particulate

and

iodine samples

from the plant vent.

No violations or deviations

were identified.

10.

Information Notices

(92717)

The inspectors

reviewed

a nd discussed

with licensee

representatives

IE

Information Notices

( IEN) 86-30,

"Design Limitations of Gaseous

Effluent

Monitoring

Systems,"

IEN 86-42,

"Improper

Maintenance

of Radiation

Monitoring Systems,"

and

IEN 86-76,

"Problems

Noted in Control

Room

Emergency Ventilation Systems."

The inspectors

noted that the Information

Notices

had

been

received,

distributed

to the applicable

engineering

group,

and that appropriate

actions

had

been

taken or were being taken.

The inspectors

had noted that

a request for engineering

assistance

(REA)

was initiated for IEN 86-30 concerning

the vulnerability of the Eberline

SPING-4 microcomputer to radiation fields

when the total integrated air

dose

was greater

than

1000 rads.

No violations or deviations

were identified.

(Closed)

50-389/84-07-01:

Controls over inlet valve from hot leg sample

line.

This item pertained to the lack of administrative controls over the

inlet valve from the hot leg

sample line of the post-accident

sampling

system

(PASS).

This valve is located in the pipe penetration

room and is

manually operated.

The concern

was that if this valve

was inadvertently

closed

and

the

pipe

penetration

area

was

inaccessible

following an

accident,

then

the

PASS

would not

be

capable

of obtaining

a reactor

ll.

Licensee Action on Previously-Identified Inspector

Followup Items

(92701)

12

coolant

sample.

The

inspector

reviewed

procedure

2-0010123,

Administrative

Control

of 'Valves,

Locks,

and

Switches,

Revision 23,

4/29/87,

and

noted that the procedure

provided directions to

keep this

valve in the

open position.

This item is considered

closed.

(Closed)

50-335/84-42-01:

Review of licensee

Chemistry

and Radiochemistry

Cross

Check

Program.

This item was concerned with the need to develop

an

intralaboratory

and inter laboratory

cross

check

program.

The inspector

reviewed

Chemistry

Department

Standard

Practices

and Policies

CD-SPP-1,

equality

Control

of Analytical

Results,

Revision 1,

12/29/86.

This

procedure

described

the

licensee's

cross

check

program

for both

intralaboratory

and interlaboratory analyses.

According to the procedure;

intralaboratory

radiochemistry

spiked

sample

analyses

(including liquid

and g'aseous

isotopic, particulate filter isotopic, gross

alpha gross beta,

and tritium) should

be conducted

semiannually,

while the interlaboratory

radiochemistry split sample analysis

program should

be conducted annually.

This program started

in 1985 with the licensee's

Turkey Point facility and

the St. Lucie Health

Physics

Counting laboratory.

In 1986,

only the

Health Physics

Laboratory participated

in the program.

The licensee

was

planning to have the Turkey Point facility participate in the program for

1987.

All sample results that were reviewed

showed

good agreement.

This

item is considered

closed.

(Closed)

50-335/84-42-02:

Use of Standard

Filter

Paper

Geometry for

Ge(Li) Detector Calibrations.

This item was concerned

with the use of an

evaporated

standard

source

on

a metal

planchet- for filter paper

geometry

calibrations.

It was

noted

that

the filter paper

was utilized for

effluent process

streams

sampling

and in selected

process

monitors.

The

inspector

noted that the licensee

was

using vendor prepared

particulate

filter standards

and

no longer

used

the metal

planchets for calibration

purposes.

The inspector

noted

good agreement

between

the Health Physics

counting laboratory

and the Chemistry Departments

counting laboratory

when

using

the

vendor

prepared

particulate filter spikes.

This

item is

considered

closed.

(Closed)

50-335/84-42-03:

Review of Fe-55 verification testing.

The

inspectors

noted that the licensee

was in disagreement for Fe-55 analyses

of spiked

samples

prepared

by the

NRC Contract laboratory during 1984 and

1985,

however

they were in agreement

for a

1986 spiked

sample.

During

1986,

the

licensee

was

using Scientific Applications,

Inc.

(SAI) for

performing the

Fe-55 analyses.

As part of the licensee's

quality-control

program,

spike

samples

are

prepared

periodically by the licensee for the

contract

laboratory

to analyze.

The inspector

mentioned

that "blind"

spiked

samples

should

be sent to the contract laboratory.

This item is

considered

closed.

(Closed)

50-335/85-05-01:

Provide shielding study for sampling

panel for

containment

atmosphere

sampling

Unit 1

NUREG-0737 Post-accident

Sampling

System

(PASS).

The licensee

performed

an evaluation of expected

dose

rates

to which

an individual would

be

exposed

while obtaining

a Unit 1

PASS

Containment

atmosphere

grab

sample

under post-accident

conditions

13

(EP0-85-2037,

9/16/85

memo).

The analysis

indicated that

no additional

radiation

shielding

would

be

required

in order

to obtain

a

PASS

containment air grab

sample

during accident

conditions.

This item is

considered

closed.

(Closed)

.50-335/85-05-02:

Provide

approved

procedure

for

low

concentration

dissolved

hydrogen

measurement

method for NUREG-0737

PASS.

The inspector

reviewed procedure

1-C-112, Operation

and Calibration of the

Hilton-Roy Post-Accident

Sampling

System,

Revision 5, 4/17/85,

and

noted

that in Section 8.3

a procedure

change

had

been

made which formalized the

low concentration

dissolved

hydrogen

measurement

technique.

This item is

considered

closed.

(Closed)

50-389/85-05-01:

Provide results of test verifying accuracy of

dilution volume for Unit 2 containment air sample for NUREG-0737

PASS.

The

inspector

noted

that

the dilution volume for the

Post-accident

Sampling

System

(PASS)

Containment air sample

was

a calculated

volume that

had

not

been

experimentally

verified.

The

licensee

performed

a

verification test

to determine

the dilution volume

and

included this

information in procedure

2-C-113, Operation of the Combustion

Engineering

Post-Accident

Sampling

System,

Revision 5,

4/22/86.

This

item is

considered

closed.

po

TABLE 1

ST.

LUCIE NUCLEAR STATION

SEMIANNUAL EFFLUENT RELEASE

SUMMARY

1984 - 1986

Year

No. Abnormal Releases

a;

Liquid

b.

Gaseous

Liquid Waste

Released

(gallons)

Activity Released

(Curies)

a.

Liquid

1984

0

3.46x10'9855.00xlO'986

7.79x10'.

Fission

and Activation

3.86x10'roducts

5.5lx10~

4 96xlOo

2.

Tr itium

3'.

Gross Alpha

b.

Gaseous

1.

Noble Gas

2.

Halogens

3.

Tritium

4.

Gross Alpha

Dose Estimate

(mrem)

a.

Liquid

Whole-body

b.

Gaseous

1.

Whole-body

2.

Thyroid

4.42x10'.32xl04

5.40x10-'.10x10'

03x10

s

3.12x10-'.54x10-~

1.14x10'.50xlO'.02x10-'.03x104

9.80x10-'.62x10'.55x10-'.92xlO-'.87xlO-'.60xlOo

5.56x10~

3.10x10-"-

4.33x104

3.11x10-'.11x10'.06x10-'.llx10'.32x10-~

6.67x10'