ML17201Q405

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SALP 8 Repts 50-237/89-01 & 50-249-89-01 for Feb 1988 - Jan 1989
ML17201Q405
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 01/31/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17201Q404 List:
References
50-237-89-01, 50-237-89-1, 50-249-89-01, 50-249-89-1, NUDOCS 8904180078
Download: ML17201Q405 (34)


See also: IR 05000237/1989001

Text

SALP BOARD REPORT

'

.

.

.

U.S. NUCLEAR REGULATORY COMMISSION

REGION I I I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

. 237/89001; 249/89001 .*

Inspecti~n Report Nos~

Commonwealth Edison Company

Name of Licensee.

Dresden Station

Name of Facility

February 1, 1988, through Jan~ary 31, 1989

Assessment Period

8904180078 8~~37

PDR

ADOCK 0

PNU

G.

SAlP 8

TABLE OF CONTENT~

I.

INTRODUCTION

II .. SUMMARY OF RESULTS

A.

Overview

B..

Other Areas of Interest

I I I. CRIT~RIA

IV,

PERFORMANCE ANALYSIS

v.

A.

Plant Operations

B:

Radiological Co0trols

C.

M~intenance/Surveillance

D.

Emergency Preparedness

E.

Security

F.

  • Engineering/Technical Support .

.

G.

Safety Assessment/Quality Verificat~on

SUPPORTING DATA AND SUMMARIES

A.

. Licensee Attivities

B. * Inspection Activities

C.

Escalated Enforcement Actions

D.

Confi~matory Action Letters (CALs)

E.

License Amendments Issued

F.

Review of Licensee Event Reports Submitted

by the Licensee

Page

1

3

3

3

4

6

6

9

. 11

No.

15

17 .

18

21

27

27

28

30

30

31

31

_,,.

'*

.:.

  • .**:

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is ~n

integrated NRC staff effort to collect available observations and data

on a periodic basi~ and to evaluate licensee performance on the basis

of this information.

The program is .supplemental to normal regulatory

processes used to ensure compliance with NRC rules and regulati-0ns.

SALP is intende.d to be sufficiently diagnostic to provide a rational

basis for ~llocating NRC resources and to provide meaningful feedback

to the licensee's management regarding the NRC 1s assessment of their

facility's performance in each functional area~

An NRC ~ALP Board, composed ;f ihe staff members listed below, met on*

  • March 22, 1989, to review the observations and data on performance,

and to assess licensee performance in accordance with the guidance

in NRC' Manual. Chapter 0516,

0 Systerriat i c Assessment of* Licensee

Performance.

11

The gUi da.nce and eva 1 uati on criteria are summarized in.

Section III of this report.

The Board's findings a'nd recommendations

were forwarded to.the NRC Regional Administrator for approval and

issuance.

This repor~'is the NRC 1 s asses~ment.of the licensee's safety perfdrmance

at the Dresden Station for the period February 1,

1988~ through

January 31, 1989.

SALP Board for Dresden Station SALP 8 assessment was composed of:.*

Name

  • H. J. Miller
  • C. E. Norelius
  • W. L. Forney

E. M. McKenna

G. c. Wright

    • L. R.

Greg~r

  • J. J. Har.risen
      • M. A. Ring
      • F. J. Jablonski
        • M. Phillips

M. Schumacher

J. Creed

  • D. R. Muller
  • B. I-. Siegel
  • S. G. DuPont*

Tit 1 e

SALP.Board Chai~man, Director, Division

of Reactor Safety (DRS)

Deputy Regional Administrator

Deputy Director, Division of Reactor Projects,

(DRP)

Chief, Reactor. Projects Branch 1 (DRP)

Chief, Operations Branch (DRS)

-Chief, Reactor Programs Branch {DRSS)

Chi~f. Reacto~ P~ojects Section lB (DRP)

Chief, Reactor Projects Section 3B (DRP)

Chief, Maintenance and Outage Section (DRS)

Chief, Operational Programs Section (DRS)

Chief, Radiological Efflu~nts and Chemi~try *

Section (DRSS) *

.

.

Chief, Safeguards Section (DRSS)

Director of Project Directorate III-2, NRR

Project Manager, NRR

Dresden Senior Resident Inspector

,<J

Name

D. *E. Miller

T. J. Plosk.i

D. E. Jones

W. J. Kropp

T. Vandel

J. Holmes

D. Funk.

R. B .. Landsman

  • Denotes voting members.

Title

Senior Radiation Specialist (DRSS)

Emergenty Preparedness Specialist (DRSS)

Project Inspector, Sectioh lB (DRP)

Rea~tor lnspector (DRS)

Reactor Inspector (DRS)

Reactor Inspector (DRS)*

Security Specialist (DRSS)

Reactor Engineer (DRP)

      • Voting M~intenance/Surveillance Only
        • Voting Engineering/Technical Support Only

2

"II.

SUMMARY OF RESULTS

A.

Overview

Overall, the licensee's performance was found to be acceptable

and improved since the last SALP assess~ent period.

Of the .

. seven functional areas rated, during this assessment peri6d

licensee performance in four areas improved; Plant Operations

from a Category 2 and improving rating to a Category 1 rating,

Emergency Preparedness from a Category 2 and improving rating

to a Category 1 rating, Security from a Category 2 to a

Category 2 and improving, and Maintenance/Surveillan_ce from a

Category "3 rating in Maintenance to a Category 2 rating.

All of

the remaining functional areas sustained Categoty 2 ratings with

an improving trend noted in Safety Assessment/Quality Verification.

  • .

.

-

.

.

Whi 1 e there has been performance* improvement, ; ncreased. management**

. attentio~ is needed in areas of identified weakness to.assure this

perform~nce is sustained.

For example, the NRC Ma{ntenance Team

Inspection (MTI) identified several areas requiring increased

management involvement, including:

the Electrical Preventive

Maintenance Program and the over a 11 trending of adverse system

equipment, and component performance.

The performance rat{ngs during the previous assessment period and

this assessment period according to functional area are given below:

Functional Area

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engi~eering/Techhical Support

Safety Assessment/Quality

Verification

N/R - Not Rated

8.

Other Areas of Interest

None;

3

Rating Last

Period

2

2

3/2

2

2 2*

N/R

Rating This

Period

  • Trend

1

2

2

1

2

Improving

2

  • 2

Improving

II.I. CRITERIA

Licensee pe~formance is assessed in selected functional areas.

Functional areas normally repres~nt areas signiffcant to nuclear

safety and the environment.

Some functional areas may not be assessed

because of little 6r no licens~e activities* or lack of meaniMgful

observations.

Special areas ~ay be added to highlight significant

observations.

The following. evaluation c~iteria were used to assess each functional

.area:

1.

Assurance of quality, including management involvement and

control;

2.

Apptoach to the resolutton of technical issues from a safety

standpoint;

3.

Responsiveness to NRC initiatives;

4.

Enforcement history;

5.

Operati9nal events (including response to, analyses of, reportfng

of, and corrective actions for);

6.

Staffing (including management); and

7.

Effectiveness of ~raining and qualification program.

Howev~r, the NRC is not limited to.these criteria and others may h~ve

been used where appropriate .

. On the basis of the NRC assessment, each functional area evaluated is

rated according to three performance categories.

The definitions of

these performance categories a~e as follows:

Category 1:

Licensee management attention and involvement are readily

evident and.place emphasis on superior-perfor~ance of nuclear safety

or safeguards ac~ivities, with .the resulting performance substantially

exceeding ~egulatory require~ents. Licensee resources are ample and

effectively used so that ~ high level of plant and persohnel

performance is being achieved.

Reduced NRC attention may be

appropriate.

Category 2:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are good.

The

licensee has attained a level of performance above that needed to meet

regulatory requirements.

Licensee resources are adequate and

.

reasonably allocated so th~t good plant and personnel performance is

being achieved.

NRC attention ma~ be maintained at normal levels.

4

  • .

.,

Category 3:

Licens~e managemeht attentioh to and involvement in

the performance of nuclear safety or safeguards activities are not

sufficient.

The licensee's *performan~e does not significantly exceed

that needed tp meet minimal regulatory requirements.

Licensee

resources appear to be strained or not effectively used.

NRC

attention should be increased above nor~al levels.

The SALP report may include an appraisal of the* performance. trend in a

functional area for use as a predictive indicator if near-te~m

performanc*e is of interest.

Licensee performance during the last

quarter of the assessment period shou'd be exa~ined to determine

whether a trend exists.

Normally, this performance trend should only

b~ used if both ~ definite trend is discernable and continuation of

the trend may result in a change in performance rating.

The trend, if used, is defined as:

  • Improving~

Lic~nsee performance wai determined to be improving near

the close of the assessment period.

Declining:

Licensee performance was dete~mi~ed to be declining near

the close of the assessment period; and the.licensee had ncit taken

. meaningful steps ~o address this patte~n.

5

IV.

PERFORMANCE ANALYSIS

A.

Plant Operaticins

1.

Analysis

Evaluation of this functional area was.based on the. results

of nine inspections ccinducted by th~ resident and regional

insp~ctors and an emergency operating procedure (EOP) inspection

conducted by Region I.

Enforcement history in this functional area was good and indicated

an improvement in performance.

Two Severity Level IV violations

were identified durihg this assessment period compared with

one Seve~ity Level III and two Severity Level V violatitins

identifi.ed d~ring the previous assessment period.

During the

previous ass~ssment period, the Severity Level III violatio~ and

one of th~ Seve~ity level V violations w~re due to personnel*

errcirs; however, during this assessment period, no violations

due to personne 1 errors occurred.

One of the Severity Leve 1 IV

violations during this .assessment period was associated with*

outage activities. This activity was not evaluat~d in this.

functional area, but in the outage functional area during the

previous assessment period.

During this a~sessment period only one reactor scra~ occurred,

compa~ed with ten during the previous two*assess~ent periods~

indicating a significant improvement* in perfofmante.

With regard to this functional area, there was a positive trend

in both the total number of licensee ~vent.reports (LERs) issued

and the number att~ibuted to personnel error~ During this

assessme-nt period 11 LERs were issued that were attributed to

operations; of these 6nly 2 were attributed to personnel error.

During the previous assessment period, seven LERs were attributed

to personnel error.

Management attention and effort directed toward the reduction of

operational events was very good and significantly successful

. in reducing th~ number of scrams.

In addition to a reduction

    • in the total number of reactor scrams, Dresden set a world

record for~ dual~unit boiling-water reactor (BWR) of 403 days

without a ~cram on either unit.

In July 1988, manag~ment

applied the lessons learned from the scram reduction program to

engineered safety feature (ESF) actuations.

Thfs ~ffort resulted

in ~-reduction in ESF ~ctuations from seven du~ing the first

half to fou~ durin~ the second half of the.assessment pe~iod.

The operating staff demonstrated e~cellent professionalism in

the control room and efficient supervision of plant activities

durin~ routine opera~ions and two refueling and maintenance

.6

outages.

The operating staff was directly and extensively

involved in the licensee's ongoing detailed control room

design review (DCRDR) program and the control room lighting

and ventilation modification.

The licensee has been successful

in achieving a black-board concept by reducing the total number

of annunci~tor alarms for both unit~ from an a~erage of 16

alarms per month during the previous period to only 2 per ~orith

  • during the last half 6f-this assess~ent period.

Since August

1988, complete black-board c6nditions (zero annunciator alarms)

were achieved on each unit on several occasions.

Another

noticeable impro~ement was teamwork between the facility

department~. During the previous assessment period, the lack

of effective teamwork was noted as a major contributor to the

generally low morale and operational performance.

During the

curre~t Unit 2 .refueling outage, both the operations and

maintenance departments demonstrated superior teamwork.

This

was demonstrated by repair of the main service water system

isolation val~es. The service water system at Dresden is a

fully cross-connected system, and, as su~h, required both units

to be in an outage dufing the replacement of the isolation valves

and the development of an a1ternate cooling path to provide fuel

pool and shutdown cooling for both units.

The coordination and

planning efforts of onsite and corporate organizations resulted

in a well-controlled and trouble-free evolution that was completed

in a timely and safe manner.

Teamwork among operators was

also evidenced by performance during EOP inspection simul~tor

drills; notwithstanding problems identified with the procedures,

operators placed the plant in a known safe, stable condition

following simulated upsets.

Outing this assessment period, both units demonstrated significant

  • improvements in plant operations ind safety.

Unit ~ had a

forced-outage rate of 0.1% and was available 78.9% of the tim~,

and Uriit 3 had a forced-outage rate of'0.0% and was available

71.5% of the time.

During the previous assessment period,

Unit 2 had a forced-outage rate of 8.5% and was available 61.0%

of the time, and Unit 3 had a forced-outage rate of 24.0% and

was available 75.3% of the time~ During this assessment period,

the facility experienced several deratings affecting availability

during the summer months because of the extreme drought and

severe temperatore conditions.

In addition to the improved

performance associated with the forced-outage rates and

availabilities~ the facility completed two continuous runs ~f.

dual-unit operation that lasted 156 and 111 d~ys. During the *

assessment period, two events occurred that were initially* *

classified as significant~*. Both of these ev~nts, the failure

of MSIVs to close during special testing and the Unit 2 excessive

drywell temperatures, were subsequently assessed by either a NRC

augmented or special inspection as having low safety significance.

Additionally, in the previous assessment period, there*were 12

safety system failures compared with 6 during this assessment.

Housekeeping conditions within the plant were good throughout

this period with a steady improving trend.

The control room

  • also was subjected to a modification pr6gram that included

7

~ainting and color~cotje shading of panels to aid operators

in system identification ..

Management's inv~lvement in ensuring* quality in plant operatioris

was evident and good during this assessment period.

Management

inv6lvement has improved significantly compared with the previous

asses~m~nt period during which a Severity Level III violation

was identified that was attiibut~ble to the lack of effective

management involvement in routine operational activities.

During this assessment: period, two events occurred that were

. attributable to inadequate administrative controls: 'high

temperatures in the Unit 2 drywell and the inoperability of

the Regulatory Guide 1.97 primary oxygen monitor.

The high

temperatures in the Unit 2 drywell resulted from the use of

in~dequate operating procedures.

In both cases, management

aggressively reviewed the events and took immediate corrective

actions.

Frequent tontrol room observations and ~lant walkdowns

by management and supervisory staff, including attendance at

plan-of-the-day meetings and participation in. le~sons-learned

. and root-cause-analysis meetings, have resulted in effective

assurance of quality in plant operation a~d performance:

These

actions have reduced operational events, personnel errors, and.

inoperability of control room equipment, instrumentation, and

annunciators.

.

.

.

.

Managers take a conservative approach from a safety standpoint

- when. reiolvihg technical iisues and classifying operational

events such as the voluntary inoperability of _the high pressure

coolant injection system to conduct plahned preventive

maintenance.

The licensee has been very responsive to NRC. initiatives ..

Outing this assessment period, the licensee met frequently

with the.NRC to discuss improvement programs and task forces

responding to NRC initiatives,

An example of th~ resolution

of technical issues was the successful resolution during this

assessment period of NRC Diagnostic Evaluation Team (DET)

concerns related to plant operations.

.

Staffing for plant operations was very good with no violations

related to overtime requirements. *This was a specific problem

noted during the previous assessmerit period, resulting in a

violation regarding control of overtime.

The stafffng of t:he

operations department was maintained at an efficient level.

During this assessment period, the licensee added a nuclear*

station operator (NSO) to the contr~l room staff increasing

th~ control room staff to four NSOs, two shift foremen (SF), a.

  • shift engineer (SE),_ and a shift control ro6m engineer (SCRE).

8

Management was also directly involved in operator qualification.

Several

improvem~nts that resulted in an overall increase in

the quality of training were initiated during this assessment

period.

Both of two senior reactor operator (SRO) replacement

. candidat~s passed examinations during this as~essment period.

2.

Performance Rating

The licensee's performance is rated. Category 1 in.this area.

The licensee's performance was rate.d Category 2 in the

previous assessment period.

3.

Recommendations

None.

s:

Radiological Controls

1.

Analysis

Evaluation of this functional area was based on the results

of three inspections by regional specialists and observations

by the resident inspectors.

Enforcernent history improved during this assessment period;

One Severity Level JV violation was identified compared with

two violati6ns with possible escalat~d enforcement ramificati6n

du~ing the previous assessment period.

The violation. failu~e

to analyze ehvironmental sam¢les in 1986, reflected management.*

laxhy.but not programmatic breakdown.

-

Staffing remai~ed generally adequate.

Professional staff

stability ~ai improved and overall experience level has increas~d.

The chemistry and health physics functions were ~eparated into

two groups each reporting independently to the Assistant

Superintendent Technical Services.

Technicians no longer

rotate between the two groups and new*technicians are being

trained to supplement both groups.

All technicians are involved .

in a continuing training *program and will .be annually recertified

in their specialities~ Training for cohtract radiological

workers and technicians appears to need improvement based

on radiological performance problems occurring during the

most rec~nt o~tage:

. Management involvement in. ensuring quality was generally good

although supervisory weaknesses were noted during the outage

that.occurred near.the end. of the assessment.period.

Thi~

weakness was evidenced by an event involving internal

9

..

contamihation of three men performing work on Unit 2 feedwater

check valve.

Reduction of outage duration may have been a

factor in this event and the lessened adherence by workers to

good health physics practices.

Good performance was noted in

licensee audits and responses, including the area of primary

chemistry which was assigned to an auditor who is well _

quilified by eduction, expe~ience, and training.

Cdrporate

  • support and ~ssist~nce for the radiatibn protection program

remained.strong.

~he li~ensee's responsiveness to NRC i~itiatives was generally

good .. Licensee actions concerning the contamination survey

program, the investigation of events involving contamination

of personnel, and the.radwaste handling and packaging facilities

have re~ulted in

itjentif~able improvements in these areas.*

The licensee's approach to resolving radfol~gical technical

issues was generally timely and sound.

The total station

dose for 1988 (about 1405 person-rem) exceeded the station

goal (1260 person~rem) owing to unforeseen work ~uch as drywell

electrical cable repair and MSIP.

The dose was higher than

typical US BWRs but r~asonable because it included two major

r~fueling and maintenance outages.

Improvements during this

assessment period included the use of control rod drive shields

and removal/installation machines, ~nd increased use of mock-ups.

. The ALARA program appeared to be adequately implemented for

high dose rate, high dose, and critical path outage work:

However, for other radiologi~al work, adequate notice was not

always provided to ALARA personnel and therefore, extensive*

ALARA reviews were not always made.

Also, tool equipment, and

staging requirements are not always included in ~ainte~ance

procedures to ensure that wor~ performed in radiological areas

is efficiently performed.

Personal contamination events have

continued to decrease, and are no longer excessive.

The extent

of contaminated areas was considered low.

No unplanned liquid or gaseous releases were reported, Through

licensee efforts, the volume of radwa~te generated this period

has been reduced as has the backlog of radwaste awaiting

packaging and shipping.

However, contaminated soil from

past years remains onsite with no disposition established.

The.re were no transportation incidents.

Results of the radiological confirmatory measurements were

very good with only 1 disagreement in 75 comparisons made on

. six routinely used measurements* and one Post Accident

measurement.

2.

Performance Rating

The licensee's performan~e is rated Category 2 in this area.

The licensee's performance was rated Category 2 in the previous

assessment period.

10

3.

Reco1T111endations

None.*

C.

Maintenance/Surveillance

L

Analysis

Evaluation of this functional area was based on the results

of eight routine inspections perfonned by the resident inspectors,

three routine inspections by regional inspeetors, a special NRC

augmented inspection team (AIT) inspection, and a maintenance

team inspection (MTI)~ Maintenance and surveillance were

.separate functional areas in the previous assessment period, but

have been combined as one functional area for this asse~sment.

Enforcement history indicated a decline in performance.

Three

Severity Level iV and one Severity Level V violations were

identified during this assessment period.

No violations were

identified in the chemistry area.

The MTI identified two

additional violations but had not determined the severity

levels during this assessment.

During the previous assessment

period, there weie no violations in the maintenance area and one

deviation in the *surveillance area .. However, two of the Severity

Level IV violations issued during this assessment period were

addressed during the previous assessment period.

Additionally~

the increase i.n the total number of violations refletted the

increased attention to this functional area by the resident

and regional inspectors.

Only one surveillance specified by the Technical Specifications

was missed during this assessment period compared with three .

during the previous period.

The licensee detected a deficiency

in the scram testing pro.cedure for Unit 2 that invalidated the

previous scram insertion timing data for five control rod drives

(CRDs).

The licensee imnediately .revised the procedure and

retested the affected CRDs.

The affected CRDs were within the

required Te~hnical Specification insertion times and had n6

resulting safety significance.

During this assessment peri-0d, one operational event was* attributed

to ~ither maintenah~e or surveillance activities compared with

eight during the previous assessment period.

The Unit 2 main

steam isolation valves (MSIVs) failed to close during a special

test. This event .resulted in the only forced outage relating*.

to Unit 2.

The NRC initiated an AIT and issued.a Confirmatory

Action Letter (CAL) relating to the licensee's corrective

actfons. The AIT detennined that the event was of minor safety

. significance and that the root-cause of the MSIVs' failure to

close was the excessive friction forces induced by overadjustments

of the tightness of the Chevron-type valve packing.

11

During this assessment period-, the licensee issued 21 LERs

felated to this functional area compared with 30 during the

pievious as~essment period.

During the previous assessment

period, 22 LERs attributed to component or equipment failure

indicated a weak preventive maintenance program~ During this

assessment ~eriod 15 LERs attributed t6_tomponent or_eq~ipment

failufes indicated a slight improvement in the effectiveness of

preveniive ~ainten~nce. Additionally, ~ix failures of the hi~h

pressure coolant injection (HPCI) system were identified duri~g

the previous assessment period compared with only one failure

during this period.

There were no reactor scrams attributed to

surv~illance or maintenance attivities during this assessment

period compared with six during the previous assessment period.

During the-previb~s assessment period, sev~ral weaknesse~ were

observed in the maintenance. area including incomplete maintenance

improvement and preventive maintenartce prog~ams, the number of

reactor icrams caused by maintenance errors, and the number of

plant oil and water leaks.

Specific problems noted were:

problems with the root-cause and failure analysis, the trending

of component faiiures, the lubrication and oil analysis, and the

number of failures associated with the HPCI and feedwater systems.

During this assessment period, the lic_ensee was very responsive

to NRC concerns to identify and correct programmatic and

procedural defic1eni:ies in this functional area by initiating

a M~intenance Improvement Program (MIP).

These actions resulted.

in noticeable improvements in plant perfor~ance, reliability,

and safety.

A noticeable improvement was the implementation of

the Model

Syst~m concept.

On the basis of a time series analysis

  • (TSA), the HPCI system was selected for improvement betause of*

its importance arid historical high failure rate.

During this

assessment period, the HPCI system performance improved with

only one failure.

Another significant improvement was the

intre~sed reliability and safety of the station emergency*

diesel generators, which during the previous assessment peri~d;

had a tumulative unavailability factor of 4.5% comp~red-with

0.5% during this assessment .period.

Development of the new

inservice testing (IST) progfam issued on April 15, 1988, was

in exam~l~ of another noticeable improvement.

The program

resolved concerns identified during the 1987 NRC DET.

The MTI found that management was vigorously involved with

the MIP.* The current eff~ctiveness of the MIP was due, in part,

to the periodic assessments.by corporate evaluators and subsequent

implementation of corrective actions at the station.

Other

examples of management's effectiveness intluded the establishment

of a clear long-range maintenan_ce plan, "Conduct of Maintenance

Program," the upgrading of systems that were performing poorly,

and overall improvements in maintenance procedures.

Improvement

was rioted by the reduced number of LERs, low forced-outage rate,

12

and increased reliability of systems.

The MTI found the quality.

of the motor-operated valve (MOV) procedures and the writers

guide for procedures to be strengths.

Additionally, several

attributes of the preventive maintenance program were considered

to be very good, such as the trending of instrument setpoint

drift, overall preventive .maintenance of the security systems,

the MOV program, and activities asso~iated with the safety

relief valves.

However, *the team also f6urid several areas

it considered weak and still in need of increased management

involvement.

These areas were preventive maintenance for

250-vdc motor control centers and 4.16-kV circuit breakers,

establish~ent of additional effective maintenance performance

indicators, completiori of system walkdowns for establishing

as-built conditions, compilation o1 usable machinery histories,

~nd establishment of an effective trending program.

Maintenance staffing appeared adequate as evidenced by the.

manageable size of the maintenance wo~k request backlog~ Based

  • on a .review of licensee records, the inspectors determined that

open non outage Corrective Maintenance Work Requests (CMWRs)

decreased from about 1300 in January 1988 to 938 on January 2~,

1989.

There had bee~ a decreasing trend throughout most of the

year.

Development of the MOV team concept was an excellent

example of the use of maintenance staff to effectively complet~

maint~nance activities .. The aggressive management of the

backlog of maintenance work requests, the lbw number of forced

outages du~ to equipmerit. failures, and the overall plant

forced-outage rate indicated that the overall performance of

maintenance at Dresden wa~ good.

The backlog o~ maintenance

work requests was considered low and manageable.

The number of

work requests affecting activities in the control room was ~lso

considered low and manageable.

Ai noted in the Plant

Operations section, the number of forced outages due to

equipment failure was small and the overall forced-outage rate*

of 1ess than 0.1% was ve~y good.

The mechanical and instrumentation maintenance staffs were

considered effective, but the electrical maintenance staff

appeared weak.

Staffi~g levels and qualification~ were adequate

to implement the routine chemistry programs.

The management

for the chemistry group was extensively reorganized during this -

period, and the chemistry supervisor now reports directly to an

assistant superintendent.

The technicians ho longer perform

both radiation protection and chemistry functions .. The

techhicians were all qualified under American National

Standards Institute Standard Nl8.l-1971.

Mainten*ance training and the qualification program for the

station maintenance staff were considered very effective.

MOV

teams received excellent training and acquired a high level of

expertise.

The use of a maintenance personnel qualification

matrix, mockups, and photographs of the actual work.area and

components contributed to this effectiveness.

13

The licensee's quality control organization was effective in

identifying problems in mechanical and instrument maintenance

acti~ities, but was less effective in electrical maintenance.

Because of the inconsistent use of the deficiency identification

program, the licensee was not totally eff~ctive in ensuring that

plant material deficiencies were identified.

The inconsistent

use of the program aiso placed an additional burden on the

maintenance staff be~ause a high percentage of ~ork requ~sis

were duplfcated and there was~ general inability to fully

assess the material condition of various systems and equipment.

This was considered a weakness in both the identification and

trending of plant material defici~ncies, even though no actual

concern about the operability of the systems and equipment *

existed.

Licensee manageme~t involvement in en~urihg qualit~ in the area

of chemistry was miXed .. The water chemistry program conformed

with the Electri~ Power Research Instit~te (EPRI) BWR Owners

Chemistry Guidelines, and licensee data indicated that water

chemistry variables were under good control.

The makeup water

system is being rebuilt to improve the quality and quantity of

makeup water.

The.1i~ensee injects hydtogen into the Unit 2 *

primary water to improve water chemistry.

However,

th~s program

appeared deficient in that the licensee had not been able to*

optimize the hydrogen flow to balance cdrrosiveness against

increased radiation .. levels (ALARA) because the electrochemical

potential (ECP) m6nitor (which estimates corrosiv~ness) was .ndt

operational and had not been for about two year~. The licens~e

~as planning to install a ne~ monitor, but it will not be

operational for ~bout another 18 months.

The. licensee's response to NRC initiatives. in the chemistry.

area was good.

The licensee has been receptive to the_NRC

nonradiological confirmatory measurements program and is *

impr6ving the quality assurance/quality tontrol (QA/QC)

program in the laboratory.

The laboratory facilities were recently refurbished, and

state-of-the-art instrumentation, including four computer-controlled

ion chromatographs for low-level trace materials analyses have

been added.

The quality of the nonradiological confirmatory

measurements co~parisons declined with only 11 of 26 initial

analyses in agreement (42%), compared with the previous year's

rate of 89% agreement.

The disagreements appeared to be due

mainly to deficiencies in the procedures for preparatio~ of.

calibration and check standards, which the licensee corrected

in a timely manner.

The licensee achieved all agreements in

seven split samples compared with Brookhaven National

Laboratory.

14

2.

Performanc~ Rating

The licensee's perfo~m~nce is rated Category 2 in this area.

The licensee's performance was rated Category 3 in.the

maintenance fun ct i ona l area and. Category 2 in the* su.rvei 11 ance

  • functional area in the previous asiessment period.

3.

Recommendations

None.

D. * Em~rgency Prepar~dness *

1.

. Analysis

Evaluation of this funct~orial area was based on t~o inspectioris

conducted by regional inspectors. These inspections were an

exe~~ise observation and a routine inspection of the p~ogra~.

During this assessment period, enforcements history.improved in

that no violations of NRC requirements were identified,

compared with one violation identified during the previous

assessment period.

Management involvement in ensuring quality was good.

An indepth

evaiuation of the onsite program in May 1988 by corporate staff

and several emergency planning.specialists from other nuclear

stations identified a number of progr~mmatic improvements.

These improvements were complete or underway by the end of this

assessment period.

The principal improvement resulting from

this self-evaluation was the tomplete rewrite and expansion of

the emergency plan implementing procedu~es (EPIPs), which* are

scheduled for completion in the next SALP period.

The licensee's approach to resolving technic~l issues was good,

T~e station's tracking system was used effectively to track

.progress on items identified during NRC inspections, the

corporate evaluation of the program, ~uality assu~ance audits,

and drill critiques. All required emerg~ncy preparedness

drills, ~quipment tests, and supply inventories were completed

as scheduled during this assessment period.

A complete ~et of

upgraded EALs has b~en developed as part c:if a long-te~m project

to correct inconsistencies i~ the organization and interpretation*

of EALs in use at all of the licensee's nuclear station~.

.

Another potential problem was resolved with the de~elop~ent and

successful ~ompletion of surveillance procedures for the

Technical Support Center's ventilation and radiation monitoring

system.

The emergency response organization has re~ained well staffed,

with nc:i individual holding multiple positions.

Primary and

15

support- positions remained well defined.

Successful, quarterly*

off-hours drills demonstrated that the licensee was able to

augment onshift personnel in a timely manner.

A part-time

interi~ emergency planning c~ordinator was appointed to manage

the program while the regular coordinator was unavai]a~le because

of a lengthy illness. A full-time aide was ap~ointe~ after the

regular coordinator returned to work in the Spring of 1988.

The onsite emergency preparedness training program has remained

clearly defined.

Recordkeeping was improved during this

assessment period.

Lesson plans and oth~r training materials

were being revised as a result of the ongoing EPIP revision

project.

lnterviews with a small sample of members of ~he

emergency organization indicated some minor weaknesses

concerning emergency preparedness training for persons who

cou.ld be assigned .to inplant repair teams;_however, the' overall

performance during these intervtews and the March 1988 exercise

indicated that training of the on~ite emergency response

organization was good.

The licensee's respons~veness to NRC initiatives has generally

been good.

The 1988 scenario addressed the items identified

during the previous exercBe.

One Emergency Ac-tion Level (EAL}

was adequately revised to resolve a relatively longstanding

co~cern regarding t~e notification of State and NRC offtciils

. in the event of an onsite fire.

Onshift personnel activated the emergency plan* on ~ight

occasions during 1988.

All situations were properly

classified, State and NRC -0fficials were always notified within

the regulatory time limits.

Licensee evaluatioris of r~cords

generated during these activations were well done.

The March 1988 utility-only exercise involved a hi~h-quality

scenario that was challehging and addressed the few

deficiencie~ that were identified during the previous

exercise.

Overall performance during the exercise was good,

with only a few w~aknesses identified.

These included a poor

demon~tration of collecting, bagging and labeling of smear

samples, and s~owness in the evaluation and iricorporatiori of

meteorological information into the protective action

decisionmaking process.

Although these weaknesses are not

normally indicative of good performance, the high-quality and

challenging scenario that played a role in identifying these

program deficiencies reflect strong management initiatives t6

enhance their response capabilities.

2.

Performance Rating

The licensee's performance is rated Category 1 in this area.

The 1 i cen se-e 1 ~-performance was rated Category 2 and improving

in the previous assessment period.

16

3.

Recom~endations

None.

E.

Security

1.

Analysis

Evaluation of this functional area was based on the results

of two routine inspections and one reactive inspection conducted

by regional physical security inspectors and by the resident

inspectors' routine observations of security activities.

"The enforcement hi story represented an improvement i f'.I the

licensee's performance.

Two S~verity Level IV violations

were identified during.the a~sessment period.

Bot~ violation~

occurred within the {irSt half of the assessment period.

One

Severity Level III and two Severity Le~el IV violations were

noted during the previous assessment period.

One violation.

during this assessment period was issued for the failure to

ensure positive access control, and the second violation was

issued for.the failure to conduct an adequate ingress search.

Although the security ~anagement staff initiated effective

and timely corrective actinhs, the violati6ns reflected

~eakriess in the licensee's program.

Security events reported under 10 CFR 73.71 were properly*

identified and analyzed.

~bwever, a generic concern with the

nonconservative reporting of loggable events remains open at

the corporate level .. The licensee had one reportable security

event during ~he* assessment period which involved the failure

of an individual .to declare a weapon during ingress screening.

Management involvement in assuring quality has improved during

this assessment period.

This was demonstrated by the licensee's

development and successful. implementation of both a perforMance

indicator program and preventive maintenance program.

Management

was actively involved in root-cause analysis and the mbnitoring

of performance trends and, as a result, there were very few

outstanding security issues.

However, several weaknesses in

"the area of access control e~isted throughout the period.

.

.

.

The pr~vious.assessment was critical of the adequacy of the

annual quality assurance security audit.

Thi~ issue.has been

resolved.

The lastannual audit was both thorough and

performance based.

Respbnsiveness to.NRC concerns ~as developed i~to a strength

of the security pr6gra~. Enforcement i~sues, licensing matters,

and inspection findings were addressed in a timely manner and

r~solved in a technically competent fashion.

Communications

- 17

with NRC Region III staff have been frequent and effective,.

and the Security Director has developed an awareness of issues

of regulatory interest.

Although an allegati6n of excessive

overtime was substantiated, the licensee efficiently and

effectively addressed NRC concerns.

Staffing was ~ppropriate. Although the security cbntractor

was changed during -this assessment period, the transition was

well planned and coordinated with no adverse security affects.

Positions and responsibilities within the licensee and contract6r

security organization ~ere well defined.

The licensee added an

additional position to the training staff.

The individual is

responsible fo.r collecting, analyzing, and disseminating security

data.

The analysis has enhanced the proactiveness of the

security program through the early identificatibn of potential

prob 1 ems.

The licensee's security force was adequately supervised and

triined.

Generally, the licensee's proced~ral guidance for

the security for~e was sufficiently detailed to ensure that

personnel ar~ knowledgeable of their responsibilities.

The

training and qualification program used by the licensee was

. considered acceptable and met the 1icen~ee's commitments.

The tacticil contingency traihing program developed in r~sponse

to the upcoming regulatory effectivene~s review exceeded the

licens~e's commitment.

2..

Performance Rating

The licensee's peiformance was rated Category 2 with ah

improving trend in this area.

The licensee's performance

was rated Category 2 in the previous assessment -period.*

3.

Recommendations

None.

F.

Engine~ring/Techhical S~pport

1.

Analysis

Evaluation of this functional area wa$ ba~ed on the results

of four rout.ine inspections by regional inspectors, several

inspections by the resident inspectors, a Maintenance Team

Inspection (MT!), a Region I team inspection of EOPs ahd an

NRR special team inspection to review licensee corrective

actions regarding the safety system outage modification

inspection (SSOMI).

Enforcement history during this assessment period declined

slightly. Three Severity Level IV violations were identified

18 .

'

)

during this assessment period compared with two Severity Level IV

violations identified during the previous assessment period.

The three ~i6lation~ reflected a weakness in the implementation

of the fire protection program.

Three design-error LERs

attributabl~ to this area were issued during this assessment

period* compared to nine duririg the previous assessment ..

Manag~ment involvement to ensure quality was mixed .. Management

and the e~gineering staff have taken sigriificant actions to

improve quality and saf~ty. During this assessme~t period,

the Jicensee initiated a system engineering concept that led

to the use of, in addition to system engineers, operations

department personnel as cognizant individual~ for each system.

The new concept has been effective in developing teamwork and

in promoting the exchange of information between the oper~ting

and technical depart~ents. The effectiveness of the sy~tem

engin~ering concept has not been totally ~ffective because of

the relatively recent implementation and the less than full

usage of the concept.

The licensee has corrected a weakness identified in the previous

assessment period dealing with the timeliness of support for

modification work as evidenced by the fact that most of the

engineering ~a~ completed several mbnths-before the outage.

In addition, most of the deficiencies identified during the

SSOMI were resolved.

Adequ~te planning _and assign~ent of

priorities were evident throughout the ~curse of the cor~ective

~ction programs that addressed the deficienci~s in drywell

structural steel connections, embedded plate_ anchor straps,

and flued head anchor structures.

Exampl~s of less tha~ adequate perfor~ance in~ol~ed commercial

grade dedication and fire protection.

The dedication of

commercial-g~ade components for safety~r~lated applications

consisted mainly of a review of purchasing specifications

and the use of vendors' certificates of conformance.

The

engineering staff was not identifying critical. characteristics

for component~ installed~ nor were appropriate receipt insp!ction

requifements specified.

Similafly, activities associated with

the fire protection area have b~en weak.

For example,

administrattve controls for comb~stible. materials and for

cutting and welding were not eff~ttive. The latter resulted*

in a fire in the Unit 3 drywell expansion gap.

The licensee's approach to the identification and resolutiori

of technical issues was mixed.

In most cases, the licensee

used conservative approaches to resolve pciteritially safety-

significant problems.

When specific problems arose, the

licensee conducted comprehensive reviews.to determine generic

appli~ability. An example of this was the eff6rt im~lemented

at Dresden as a result of the grounding fault identified at

19

Quad Cities.

The engineering and safety evaluations prepared

for most modifications were thorough* and technically sound.

The licensee's action to correct the swing bus transfef design

deficiency was technically ~cceptable. Engineering and

technicil support staff provided prompt, technically complete

res6lution of issues su~h as integranular stress cor~osjon

cracking (IGSCC), high drywell temperature, and the main

steam isolation valves failures.

.

Although most of the root-cause determinations by the engineering

staff have been effective, the total effectiveness of root-cause

. determinations still needs improvement.

As previously stated,

the MTI team identified two Deviation Reports (DVRs) regarding

the 4.16 kV breakers and the 250 volt DC system in which the

failure to adequately-address the ro6~ causes resulted in a*

failure to resolve potentially significant prob)ems.

Because of

the inconsistent documentation of initial failu~e conditions,

many of the failure evaluations may not'be valid. -During its

  • -inspection, the EOP team found deficiencies associated with the

control of procedural deviations from the BWR Owners Group

guidelines and the Dresden-specific guidelines without apparent

documented justification.

Most of these deficiencies were noted

because engineeiing calculations supporting the procedural

assumptions were lacking.

These deficiencies were subsequently

reiol~ed when c6rporate engineering staff provided the engineering

justificitioris and as such, are considered to be programmatic in

nature.

The EO~ team also concluded that the actual performance

of the procedures would mitigate the ~lant upset conditions and

place the plant in a known safe, stable condition.

Additionally,

the licensee aggressively upgraded the EOP program a~d the

Unit 2 control room and simulator to acc6mmodate human factors.

The licensee's responsiveness toNRC initiatives was good.

The onsite engineering a~d technical support staffs were

instrumental in helping the licensee provide prompt responses td

technical, safety, and licens~ng concerns.

The engineering and

technical support staffs also demonstrated good responsiveness

dufing the failure of the main steam isol~tion valves (MSIVs)

to close and*the high.drywell temperature event.

The staffing of the onsite engineering and technical support

groups is consider-e.d to be adequate.

In response to problems

identified in the previous periods, the licensee has increased

the engineeririg and technical staffs.

In addition, the

technical staff was reorganized and a system engineering

co~cept was implemented as previously discu~sed. Onsite

engineering personnel have increased their involvement either

by performing more evaluations, such as that of the failure of

the MSIVs to close, or by performing parallel evaluations, suc.h

as that of the high drywell temperature event.

Although this *

indicates an improvement over the practices noted during previous

20

as~essments, the licensee continues to rely almost exclusively

on outside engineering consultants w~thout positive oversight

control for many of the complex ~ngineering evaluations;

including all aspects of design and analysis of plant

modifications.

This r~liance on contracto~s without technical

Oversight appears to have coritributed to the 4-month deJay in-

recognizing modification deficiencies ~n the flued head anchor

  • structures.

Th~re appeared to be a lack of technical involvement

between the licensee's BWR engineering- staff and consultants

performing the design and analysis work.

The effectiveness of the training and qualification of personnel

in this functional area was adequate.

Observations of

modification installation and testing and discussiohs with

technical personnel showed that an adequate level of knowledge

to perform their assigned tasks had been attained.

When

complex engineering activities were undertaken, licensee

engineering personnel often referr~d the~e activities to

outside contr~ctors.

2.

Performance Rating

The 1icensee's performance is rated Category 2 in this area.

The licensee's performancewas rated Category 2 during the

previous assessment period.

3.

Recommendations

None.

G.

Safety Assessment/Quality Verification

1.

Analysis

This is a new functional area and inco~porates many of the

activities reported under the functional a~eas of quality

programs and.administrative controls affecting quality and

licensing activities in previous repo~ts. Evaluation bf this

functional area was based on the result~ of routine inspections

conducted by the resident and regional inspectors, an emergency

bperating procedures (£0~) inspection, and a maintenance team

inspection.

In addition, NRC staff revie~ of licensee submittals

and requests for amendments to the operating license.were

considered.

Enforcement hfstory in this functio~al area was good with only

one Severity Level IV violation. *This is an improvement compared

with a Severity Level III and Severity Level Vin the similar

functional area during the previous assessment period.

The

v~olatioh no~ed during thi~ assessment period was associated

with inadequate auditing *Of the EOPs.

During the NRC EOP

21

inspection, the team found that the results of the initial

quality assurance revfew of the ~OPs were not incorporat~d

into the final EOP product and that subsequent audits were

not performed.

This .was the only violation associated with

the EOP~, .and it was promptly corrected.

Manigement has taken significant actibns to improve quality and

safety.

In respohse tb problems identified in the previous

assessment period, the 1.icensee iniiiated the Dresden Station.

lmpr6vement Plan (DSIP) during this assessment period.

The

DSIP was instrumental in providing viable goals and actions.

The DSIP consolidated management efforts ~nto a singular

.

direction for station improvements by delineating responsibilities,

accountability, actions, and progr~ss trending.

M~ny of the

improvements, such as reduced reactor scrams and ESF actuations,

~ffective inservice testing (!ST) programs; time serie~ analyses

of system performanc~, motor operator overhaul program, and

facility improvements, were directly affected by the DSIP.

The DSIP also was instrumental in improvihg performance such

as safety system failures, forced..:outage rates due to component

failures, and entry into limiting conditions for operation.

These actions a~d improvements have met the licensee's commitments

in response to the NRC DET findings to improve quality and

safety.

The licensee's response to the NRC initiatives

associated with the EOPs was also considered to be good

as evidenced by its prompt correction of the identified

short- and long-term concerns during this assessment.

Management's high level of attention and com~itment in the

area of training *and qualification has resulted in significant

improvements and changes in the lic~nsee's program.

These-

included increased simulator training, increasing the

plant~specific knowledge of classroom and simulator instructo~s.*

and use of the tea~ concept during simulator training.

Most

noticeabl~ was ~he licensee's approach to realism during simulator

training by requiring notification prior to the SE's respon~e.

The licensee also has increasingly emphasized training by

requir1ng 100% attendance and implementing required makeup

. training for any training that was missed.

The simulator al~o

has been extensively upgraded to ensur~ that it. reflects the

"as-built" condition of the plant.

The licensee's responsiveness to NRC initiatives was prompt and

timely for bulletins, generic lette~s. special inspecti6ns~ and

non-:obligatory surveys and studies. *The corporate office and

  • station made their most knowledgeable people available to assist

the NRC and its contractors.

Only a few longstanding* regulatory

issues remain that can be attri.butable to the licens~e. The

licensee has greitly reduced the number of these issues during

~his assessment period.

An example of this is the resolution of

approximately 380 inspection findings within ~he last 2 years

22

and the reduction of the outstandin[ findings to a manageable

100 items.

Although the licensee has, on occasion, requested

time extensions for responding to regulatoty actions, it has

ge~erally been to allow for the opportunity to produce~ better.

prod~ct than allowed by the ori~inal schedule.

During the assessment period, the licensee anticipated several

regulatory initiatives and maintained an awareness of operational.

experience in the industry.

This was indicated by the licensee's

prompt evaluation of a 10 CFR Part 21 associated with Power

Converiion Company battery chargers used at the Commanche Peak

facility and the rapid issuance of an operating directive based

on the industry study of neutron flux oscillations: Additionally,

the *licensee was prompt in addres~in~ NRC initiatives at other

facilities, such as the Vermont Yankee neutron flux os~illation

  • and the Pilgrim reactor neutron building vacuum breakefs.

Another example was the r~cent concern with the torus to reactor

  • building vac~um breakers at the Pilgrim facility .. The licensee

actively responded to information relating to the instrument air

problems associated with.the v~cuum breakers by forming a task

force.

Because of this, ~he l~censee was abl~ to rapidly

address the concerns of the NRC before a bulletin was issued.

The licensee has also used experience gained by various site

visits to other facilities.

Based upon these experiences, the

licensee initiated several i~provements such as, a recorded

morning status repott to minimize inquiries into the control

room, an area status map used within the plant to _indicate the

location of import~nt equipment and radiological conditions,

and the application of a floor sealant that has reduced

decontamination efforts.

There are still some weaknesses in

incorporating experiences outside the Dresden Station.

One

example is the failure to perform effective preventi~e

maintenance on 4.16kv breaker~ in light of recent problems

identified at Quad Cities by the NRC and the licensee.

The licensee has performed a significant number of self-

ass~ssments (16) during this assessment period .. The li~e~see

also participated in several Institute for Nuclear Power

Operatiori (INPO) assisted evaluations and initiated a self SALP

type concept conducted by an outside independent tonsultant.

The licensee also conducted a sec6nd safety system functional.

inspeciion (SSFI) of the Unit 2 high pressure coolant injection

(HPCI) system which increased reliability of the HPCI system.

Anothe~ self-assessment r~sulted in imp~6ved reliability and

safety of the station emergency diesel generators.

During this assessment period, the offsite nuclear safety

organization met with Dresden management every quarter arid

reviewed the ~ffectiveriess of corrective actions associated

with nonrouti~e e~ents. These reviews have been effective in

evaluating the licensee~s cor~e~tive actions.

Onsite safety

reviews have alSo resulted in correcting many long:--term .

deficiencie's at the facility by directing the control room and

  • . .-: -

panel modifications, reducing the occurrence of reactor scrams

23

a~ a result of past problems, ah~ providing a preventive

maintenance program for security equipment and components.

These reviews have also in addressed and resolved many of the

deficiencies that had been identified at other facilities.

Th~ licensee ~emonstrated an active ?pproach tb identifyihg and

~esol~ing technical issues. from a ~af~ty standpoint.

Exam~les

of this were the rapid development of an investigation team

during the Unit 2 MSIVs failures and the timely r~solution

of the problem.

During this event, the licensee sought and

received assistance from their onsite and offsite engineering

including the manufacturers of the components involved or

suspected to be

involv~d with the event.

The

lit~nsee provided

prompt notification to other facilities of the failure and *

cause of the failure of the MSIV eve~t thrbugh the INPO

notification reportin~.systems.

During this assessment period, NRR issued seveh Technical

Spetification (TS) amendments for both Unit 2 and Unit 3.

Additionally, six safety evaluations were issued on vario.us

safety-significant ~ssues. The most important of these lic~nsing

  • issu~~ and TS amendments included those peftaining to

10 CFR 50,

Appendix R exempt~on retjuests~ rel6ad submittals; IST reliefs;

emergency core cooling system (ECCS) o*perability requirements;

Regulatory Guide. i.97; and diesel generator testing.

The

licensee a~d its contractors demonstrated a clear undirstanding

of the compl~x technical and safety issues associated with these

  • licensing and regulato~y actions .. Although the technical

.. approaches were generally sound and comprehensive, management's

att~ntion to the resolution rif th~se issues has not resulted in*

consistent performance in accordance with regul~tions.

On the

_positive side, most notably the fire protection (Appendix R)

exemption and the reload submittals, a high level of management

attention resulted in strong performance .. The licensee did

an excellent job of discussing issues in a clear and complete

manner in its reload submittals and of acknowl~dging previous

safety evaluation report (SER) topi~s. The Appendix R revi~w

involved complex issues of protection for safe shutdown

components and systems that were located in many separate

areas of several buildings throughout the plant. The licensee

promptly responded to NRC requests for additional iriformation

or clarif1cation by providing answers that were complete and

demonstrated good attention to the issues.

The good technical

support for these exemption requests and the smooth interaction

with the*NRC was evidence that manage~ent was continuously

i.nvolved at a high level~ During the*previous ~ssessment

period, this was noted as a weakness in management inv6l~em~nt.

By contrast, for other reviews such as the anticipated transient

without* scram (ATWS) rule, alternate safe shutdown, flued heads,

24

and. monitorin~ of de voltage systems; the initial submittals

did not contain a clear and compl~te discussion of the issues.

These submittals required additional information.

Sevetal of

these issues ~ave taken more than a reasonable time to resolve,

which indicates tha~ additional management involvement is still

needed to provide consistent licensing performance for _all

issues.

.

.

Management's support of quality assurance (QA) activities was

evident.

The licensee's site QA organization is professionally

organized and staffed.

As was noted in the pr~vious a~sessment

period, the licensee'.s QA organization is committed to the

evaluation of operational activities by having QA engineers

maintaining senior reactor operator (SRO) licenses_ This, in

addition to station management's involv~ment, has tesulted in

an overall improvement in plant performance.

QA engineers

provided extensive surveillance coverage (including off~shifts

and weekends) during both refueling outages, the dual-unit

outage for maintenance on the service water system, startup,

and plant operating periods.

Specifically noteworthy were QA

ve0ification activities in plant improvement programs, including

corrective actions associated with the findings of the NRC

diagnostic evaluation team, implementation of the DSIP, and

the IST program.

The site QA organization is functibnall~

inde~endent, asseitive, and effective in the identification and

r~solution of quality concerns such as those associated with a

~o~tractor, used at both the Quad Cities and Dresden facilities,

and a shipping concern associated with the transport of a sealed

source between the Zion and Dresd~n faciliti~s. In both of these

events, the site QA organization was instrumental in identifying,

resolving, and providing prompt notification of the concerns to

the NRC resident staff,

QA personnel were actively involved in

the licensee's process for id~ntifying and resolving problems.

Audits and surveillances were performance based.

Management and QA personnel were very active in reducing operational

events.

During the previous assessment period, the licensee

issued 58 licensee event reports (LERs) at a rate of 4.5 per

month.

During this assessme~t pe~iod, it issued 41 LERs at a

rate of 3.4 per month, an improvement of 1.1 LER per month

since the previous assessment period.

Significant improvement

in the reduction of the number of LERs attrtbut~ble to personnel

errors continued during this assessment period.

Of the LERs

issued, 24% (14 of 58) were attributed to personnel errof *

during the previous assessment period compared with 20% (8

of 41) during this.assessment period.

This trend has shown

continued improvement in personnel errors ov~r three ~onsecutive

periods.

The licensee was effective in determining the root cause of

several major events, including the failure of the Unit 2 MSIVs

25

and the high drywell temperature conditions.

However, the

licensee, as indicated in the Maintenance/Surveillance functional

area, has not been fully effective in all its analyses of

individual compon~nt failures.

Open, effective, and frequent communications existed between

the_li~ensee and the NRC.

Conference .calls and meetings to

discuss technical and administrative issues occurred ~n a

proactive environment.

The licensing staff continued to

maintain a high level of experience and competence:

The licensee also had a very effective me~hod of tracking the

DSIP and station performance ~hrough its monthly plant ~erformance

report.

The report trended over 100 performance indicators

within 13 site-specific functional areas.

The majority of these

trended NRC initiatives or station. performance improvement

programs.

The5e indicators were determined to be an effective

management tool in trending both the completion and effectiveness

of station goals and programs.

The licensee also effectively

communicated the goals of the DSIP, station performance trend~,

and industry ev~nts to station personnel tro~gh daily and

monthly update letters.

The daily update lett~r provided

summaries of industry-related events a~d notific~tions that

enabled plant personnel to provide feedbatk to management.

Additionally, plant personnel participated in the DSIP by

providing feedback on the progress of the correcti~e actions.

2.

Performance Rating

The licensee's performante is rated Category 2 with an

improving trend in this area.

Because this is a new area,

no rating is avail~ble for the previous assessment period.

3.

Recommendations

None.

26

V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities.

1. .**Unit 2

Dresden Unit 2 began.the assessment peri6d operating at.full*

power and set a licensee record of 205 dais for continuous

dual unit operation.

The unit experi~nced a few short outages

and power reductions for maintenance and testing activities,

equipment repairs, and load dispatcher request~. Unit 2 completed

its eleventh refueling outage, and ended the assessment period*

in routine power operation.

Unit 2 experienced five ESF ~ctuations and one reacto~ scram ..

The reactor scram occurred without rod motion and was caused by

  • persohnel. error.

The ~nit has not experiehc~d a reactor scram

from power for 460 days.

Significant outages and events that occurred during the

assessment period are sum~arized b~low.

Significant Outages and Events

a.

As ot March 12, 1988, Dresde~ Units 2 and*3 oper~ted

continuously for 156 days exceeding the previous licensee's

records for continuous dual unit operation of 141 day~ set

by Zion, and 132 days set by Quad-C1ties for.BWRs.

b.

On May 15, 1988, (after 205 days of continuous operation)

Unit 2 was sh~tdown for a scheduled. 10-day maintenante

outage.

An unexpected reactor scram occurred with no rod

movemerit~ and an unusual event (UE) was d~clared ai a

result of a loss of secondary containment.

The licensee

remained shutdown to conduct special tests on the MSIVs.

c.

During October 29, 1988; through February 19, .1989, Unit 2

was shutdown for a scheduled 15-week refueiing outage.

Major activities included torvs recoat; mechanical stress

  • improvement program reviews, recirculation piping

decontamination activities, cleaning of low press~~e

coolant injection (LPCI) heat excha~gers, and control rod

drive blade cleaning.

In addition, 42 modificatibns were

accomplished, including control room human factor modifications.

2.

Unit 3

  • Dresden Uriit 3 begari the assessment period oper~ting at maximum

flow and reduced loads as directed by the load dispatcher.

The

unit began its tenth refueling outage in March 1988 ~nd recom~enced

-Operating at slightly reduced power levels and adjusted power

27

... -_ .....

. ~

rates in late June 1988 .. Unit 3 e~perienced no significant

outage~ until November 27, 1988, when it was shutdown for

equipment repairs.

The unit ended the assessment period

operating at normal power levels.

Unit 3 experienced seven ES~ actuations and one reactor. scram.

This reactor scram oc~urred above 15% power and was spuii~us and

unavoidable .. This reactor scram also ended a c6ntinuous 403 day

period without any scrams from pow~r from either unit, setting

a wo~ld record for du~l unit BWRs.

Significant outages and events that occurred during the assessment

period are summarized below.

Significant Outages and Events

~-

As 6f March 12, 1988, Dresden Un~ts 2 and 3 continuously

operated for 156 days, exceediog th~ previous litensee's

records for continuous dual unit operation of 141 days set

by Zion, and 132 days set by Quad-Cities for BWRs.

b .. During March 26 through June 24, 1988, Unit 3 ~perated

continuously for 172 days, until. it comm~nced an orderly

shutdown fo~ its planned tenth cycle refueling outage;

Major activities d~ring the refuelin~ outage included

feedwater regulator valve modifications, LPRM replacements,

SRM/IR dry tube replac~ments, and standby liquid control

system (ATWS) modificatibns.

c.

During November .27 through December 10, 1988, Unit 3 was.*

shutdown.fat a dual outage.

Major activities included

service water system maintenance of both units and the

installation of a temporary piping system for shutdown

cooling.

d.

On January 2, 1989, Unit 3 was shutdown because of a false

failure indication on two of the main. steam line radiation

monitor channels.

Repairs were performed and the unit was

returned to service .after approxi~ately 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br />,

R.

Inspection Activities

Thirty-five inspecti6n reports are discussed in this SALP report

(February 1, i988, through January 31, 1989) and are listed in

Paragraph 1 of this section, Inspecti6n Data.

Table 1 lists the

violations per functional area and severity levels.

Significant*

inspection activities are listed in Paragraph 2 of this section,

Special Inspection Summary.

28

'*.:

1.

Inspection Data

a.

Unit 2

Docket No.:

50~237

Inspection R~ports No.: 8704G, 88002 through 88019,

88021 thro~gh 88030, and 88002 through 89004. *

.b.

Unit 3

Docket No.: 50-249

Inspection Reports No.: 87039, 88002 through 88020,

88022 through 88031, 88200~ and 89002 through 89004.

  • Table 1

Number of Violations in Each Seve~ity Level

Functional Areas

Unit 2

III

IV

V

A.

Plant Operations

1 -

B.

Radiological Controls

c~

Maintenance/Surveillance -

1 1

D.

Emergency Preparedness

E.

Security

F.

Engineering/Technical

Support

G.

Safety Assessment/ .

Quality Verificition

TOTALS

Unit 2

III

IV

V

2

1 *

2.

Special Inspection Summary

Un,i t 3

III IV

V

1 -

1 -

Unit 3

III. IV

V

2 -

COMMON

.III

IV

V

-

. 1

1

1

2

... 2

1

Both

III

IV

V

8 -

a.

During February 16 through March 16, 1988, a followup

SSOMI was performed (Inspection Report No. 249/88006).

b.

Periodically from April 18 th~ough December 13, 1988,

a special ffre protection inspection was conducted

(Inspection Report Nos. 237/88010, 249/88012). *

29

c.

During May 31 through June 8, 1988, a ~pecial team inspection

of emergency operating ~rocedures was performed (Inspettion

Report Nos. 237/88012, 249/88014).

d.

During May 17-24, 1988, an AIT inspection of MSIV failures

was perf6rmed to ~evi~w the circumstances surrou~djng the

failure of all eight Unit 2 MSIVs. (Inspection Report

No. 237/88013).

e.

During February 22 through March 11, 1988, a SSOMI team

followup

inspectio~ was tonducted (Inspectibn Report

No. 249/88200).

f.

During December 5, 1988, through January 6, 1989, a biannual

inspection of activities associated with the NRC DET was

conducted (Inspection Report Nos. 237/88023, 249/88024).

g.

During January 23 through February 10, 1989, a MTI was

  • conducted (Inspection Report Nos. 237/88029, 249/88030).

C.

Escalated Enforcement Actions

1.

A notice of violation and proposed imposition of civil penalty

in the amount of $50,000 was issued to the licensee on.

February 11, 1988.

This action was based on two events in which

the licensee exceeded the speciffed time limits for two Te.chnical

Specifications associated with containment deinerting for

Unit 2.

Although escalation and mitigation factors of the

enforcement policy were considered, no adjustment to the base

civil penalty was deemed appropriate.

The licensee p~id the

$50,000 civil penalty.

T~is notice of violati6n was addressed

in a previous assessment per1od. (Enforcement Not1ce No. EN-88-007,

Enforcement Case No.

EA-87-207~ Inspection Report No. 237/87005).

2.

A pr6posed imposition of civil penalty in the amount of $150,000

was issued -0n April.28, 1988.

This action was based on violations

6f equipment qualificatio~ (EQ) requirements of 10 CFR 50.49.

The NRC

~taff submitted this action for the Commission'~ review

as part of SECY,:88-104, via memorandum dated April 27, 1988,

is still under review.

D.

Confirmatory Action Letters

A confirmatory action letter (CAL-RIII-88-012) was issued to the

licensee on May 18; 1988, regarding the failure of the MSIVs~ The

licensee was requested to take the necessary actions needed to ensure.**

that complete documentary evidence of the *~s f6und 1 condition of

30

  • *, ';,!

( ..

equipment being inspected is maintained, to ~rovide a st~p-by-step

troubleshooting program, and to*establish root-cause.

In addition,

the licensee was asked not to disturb any .components that offer

potential for being the root-cause, and to submit a formal report of

their findings, conclusions, ~nd causes within 30 days of the letter.

E.

License Amendments Issued

  • Amendment No.

98/93

94

99/95

100/96

101/97

102/98

103/99

104

De?cr1 pt ion

Date

Dfesel Testing

2/19/88

Unit 3 Cycle 11 reload

7/12/88

Security Plan

7/22/88

APRM/IRM Downscale Scram 8/24/88

ECCS Operability

. 10/26/88

R.G. 1.97 Changes

11/3/88 * *

Oxygen Conc~ntration

11/8/88

Unit 2 Cycle 12 reload

1/6/89

F.

Review of Licensee Events Reports Submitted by the Licensee

1.

Uhit 2 LER Nos.: 88001 through 88023

2.

Unit 3 LER Nos.: 88001 through 88018

Table 3

.

.

.

Collectively, 41 LERs wer~ issued in accordance with NUREG-1022

guidelines duriri~ this assessment, and are addressed in this

report.

There wer~_23 LERs reviewed for Unit 2, and 18 LERs*

reviewed for Unit 3, for this assessment per.iod.

Table 2

compares the cause codes associated with the LERs issued for

each unit.

Table 2

Cause Areas

Unit 2

Unit 3

Personnel Errors

6

2

Design Defici~ncies

1

2

External

0

0

Procedure Inadequacies

6

5

Equipment/Component

9

8

Other/Unknown

1

1

Totals

23

18

shows a cause code comparison of SALP i versus SALP 8. LERs ..

31

\\

i,

-!;

Cause Are.as

Personnel Errors

Design Problems

External Causes

Procedure Inadequacies

Equipment/Component

Other/Unknown

TOTALS

FREQUENCY (LERs/MO)

Table 3

. Dresden 2/3

(12-MO)

(13-MO) .

SALP

7

SALP

8 .

14 (24.1%)

8 (19. 5%)

9 (15. 5%)

3 ( 7.3%)

o ( o. o~~)

0 ( 0.0%)

6 (10. 3%)

11 ( 26. 8%) .

22 (38.0%)

17 ( 41. 5%)

_l {12.1%2

2 { 4.9%2

58 (100)

41 (100)

4.5

3.4

NOTE:

The above LER information wa~ derived frbm a review of

LERs performed by the NRC staff ~nd may not completely

  • coincide with the licensee's cause code assignments.

32