ML17199Z138

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Insp Repts 50-237/88-06 & 50-249/88-07 on 880318-0509. Violations Noted.Major Areas Inspected:Operational Safety Verification,Followup of Events,Ler Followup,Monthly Maint Observation & Monthly Surveillance Observation
ML17199Z138
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 05/25/1988
From: Ring M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
References
50-237-88-06, 50-237-88-6, 50-249-88-07, 50-249-88-7, NUDOCS 8806100050
Download: ML17199Z138 (13)


See also: IR 05000237/1988006

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Report Nos. 50-237/88006(DRP); 50-249/88007(DRP)

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Licensee:

Commonwealth Edison Company

P. 0. Box 767

Chicago, IL 60690

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Inspection At:

Dresden Site, Morris, IL

Inspection Conducted:

March 18 through May 9, 1988

Inspectors:

Approved By:

S. G. Du Pont

P. D. Kaufman

~-:*f-ri2/l~

M. AAfn9,v~~ ~

Reactor Projects Section lB

Inspection Summary

~~s-A~

~

Ins ection durin the eriod of March 18 throu h Ma

9, 1988

e ort

10s. 50-237 88006

P * 50-249 88007 DRP

Areas Inspected: Routine unannounced safety inspection* by the resident

.

inspectors on previous inspection findings; operational safety verification;

followup of events; licensee event reports followup; monthly maintenance

observation; monthly surveillance.observation; refueli~g activities;

verification of Temporary Instructions; SALP meetings; meeting with local

public officials; management meeting; and report review.

Results:

Of the 12 areas inspected, no violations or deviations were

identified in 9 areas; one violation was identified in the area of maintenance

observation (inadequate rigging procedure - Paragraph 5); one violation was

identified in the areas of surveillance observation (failure to follow HPCI

IST surveillance procedure - Paragraph 6). Additionallj, one violation was

also identified in the area of licensee event reports; however, in accordance

with 10 CFR 2, Appendix C, Section V.G.1, a Notice of Violation was not issued

(failure to have required number of instrument channels operable per trip

system - Paragraph 7).

8806100050 880525

PDR

ADOCK 05000237

DCD

DETAILS

1.

Persons Contacted

Commonwealth Edison Company

  • E. Eenigenburg, Station Manager

J. Wujciga, Production Superintendent

  • C. Schroeder, Services Superintendent

L. Gerner, Superintendent of Performance Improvement

T. Ciesla, Assistant Superintendent - Planning

  • D. Van Pelt, Assistant Superintendent - Maintenance

J. Brunner, Assistant Superintendent - Technical Services

  • J. Kotowski, Assistant Superintendent - Operations

R. Christensen, Unit 1 Operating Engineer

G. Smith, Unit 2 Operating Engineer

  • E. Armstrong, Regulatory Assurance Supervisor

W. Pietryga, Unit 3 Operating Engineer

J. Achterberg, Technical Staff Supervisor

R. Geier, Q.C. Supervisor

D. Sharper, Waste Systems Engineer

D. Adam, Radiation Chemistry Supervisor

J. Mayer, Station Security Administrator

D. Morey, Chemistry Supervisor

D. Saccomando, Radiation Protection Supervisor

  • E. Netzel, Q.A. Superintendent
  • R. Stols, Q.A. Engineer

The inspectors also talked with and interviewed several other licensee

employees, including members of the technical and engineering staffs,

reactor and auxiliary operators, shift engineers and foremen, electrical,

mechanical and instrument personnel, and contract security personnel.

  • Denotes those attendina one or more exit interviews conducted on

May 9, 1988 and informally at various times throughout the inspection

period.

2.

Review of Previous Inspection Items (92701)

a.

(Closed) Open Item (237/85015-01):

Local Leak Rate Test (LLRT)

procedure requires revision to incorporate correct methodology

when summing the maximum pathway leakage rate for two valve

isolation systems.

The licensee issued corporate directive

NSDD-S19, Revision 1, dated April 2, 1987, for all stations to

follow and ensure uniformity in the way that ILRT calculations

are performed.

The directive correctly addresses the proper

method to be used when ~ressurizing between two isolation valves

which are tested simultaneously.

The isolation system's leakage

rate is equal to the measured leakage rate.

The licensee is

currently in the process of revising procedure DTS 1600-1, "LLRT

of Containment Isolation Valves", which will incorporate this NSD

directive.

2

b.

(Closed) Open Item (237/85015-02):

ILRT Procedure Revision required

to incorporate correct as-found methodology into Type A test results.

The licensee issued corporate directive NSDD-S19, Revision 1, dated

April 2, 1987, to ensure uniformity in the way that ILRT calcula-

tions are performed.

The directive correctly addresses the proper

methodology to be utilized in calculating the as-found and as-left

Local Leak Rate Test results to determine an as-found Type A test

results.

The licensee is currently in the process of revising

procedure DTS 1600-7,

11Primary Containment ILRT

11

, which will

incorporate this NSD directive.

No violations or deviations were identified in this area.

3.

Operational Safety Verification (71710 and 71707)

The inspectors observed control room operations, reviewed applicable logs

and conducted discussions with control room operators during the period

from March 18 to May 9, 1988.

The inspectors verified the operability of

selected emergency systems, reviewed tagout records and Verified p~oper

return to service of affected components.

Tours of Units 2 and 3 reactor

buildings, refueling floor and turbine buildings were conducted to

observe plant equipment conditions, including potential fire hazards,

fluid leaks, and excessive vibrations and to verify that maintenance

requests h~d been initiated for equipment in need of maintenance.

The inspectors, by observation and direct interview, verified that the

physical security plan was being implemented in accordance with the

-

station security plan.

The inspectors observed plant housekeeping/cleanliness conditions and

verified implementation of radiation protection controls. During the

inspection, the inspectors walked down the accessible portions of

systems to verify operability by comparing system lineup with plant

_drawings, as-built configuration or_present valve lineup lists; observing

equipment conditions that could degrade performance; and verified that

instrumentation was properly valved, fun~tioning, and calibrated.

The inspectors reviewed new procedures and changes to procedures that

were implemented during the inspection period.

The review consisted of

a verification for accuracy, correctness, and compliance with regulatory

requirements.

These reviews and observations were conducted to verify that facility

operations-were in conformance with the requirem~nts established under

technical specifications, 10 CFR, and administrative procedures.

a.

Unit 3 operated continuously for 172 days until March 27, 1988, at

1:58 a.m., when the generator was taken off-line to begin the unit_'s

tenth refueling outage .

b.

Unit 2 exceeded its previous record for days of continuous

operation.

The previous Unit 2 record of 163 days was established

between January 11 and June 21, 1984.

Unit 2 has also passed the

3

recently set station record of 172 days set by Unit 3 in

March, 1988.

The unit continues to operate on day 200 of

continuous operation.

No violations or deviations were identified in this area.

4.

Followup of Events (93702)

During the inspection period, the licensee experienced several events,

some of which required prompt notification of the NRC pursuant to 10 CFR

50.72.

The inspectors pursued the events onsite with 11censee and/or

other NRC officials.

In each case, the inspectors verified that the

notification was correct and timely, if appropriate, that the licensee

was taking prompt and appropriate actions, that activities were conducted

within regulatory requirements and that corrective actions would prevent

future recurrence. The specific events are as follows:

a.

On March 24, 1988, Dresden Units 2 and 3 lost offsite communications

including the ENS, at 4:54 p.m.(CST). *The loss of offsite communiCa-

tions was due to the phone box located approximately 5 miles from the

plant, being struck by an auto.

Internal communications, including

with the.Chicago Load Dispatcher, was maintained. The dispatcher

made the required notification to the NRC via commercial tele-

communications.

All communication networks were returned to

operation at 5:21 p.m.

b.

Unit 3 commenced an orderl~ shutdown at 6:25 p.m., on March 26,

1988, for the planned 10th cycle refueling outage.

The outage is

planned to run through June 26, 1988.

Major activities scheduled to

be performed during the outage include:

Feedwater Regulating Valve

Modifications; LPRM Replacements; SRM/IRM Dry Tube Replacements;

Standby Liquid Control (ATWS) Modification; 250 Volt Battery/Rack

Changeout; Unit 3 and 2/3 Dies~l Generator Stub Shaft ~edification;

and 125 Volt Battery Discharge Test.

As part of the pre-planned shutdown, the licensee elected to take

the High Pressure Coolant Injection system (HPCI) out-of-service

at 6:30 p.m., on March 26, 1988, with Reactor power at 91%, to

perform a HPCI Overspeed Test per Dresden procedure DOS 2300-2.

The purpose is to test the operation of the HPCI turbine overspeed

trip.

The Resident Inspectors and Region III had been previously

informed of this preplanned event on March 24, 1988.

The licensee

made the required ENS call at 6:33 p.m (CST) on March 26, 1988, to

declare the HPCI system inoperable, which put the licensee in a 24

hour LCO Action Statement to be shutdown and Reactor Pressure

reduced to 90 psig. Reactor Pressure was reduced to less than 90

psig at 7:39 a.m., on March 27, 1988, and Reactor Mode switch was

placed to shutdown at 11:37 a.m., the same day ..

c.

During a plant walkdown on December 2, 1987, to followup on

.

discrepancies found during a licensee conducted Quality Assurance

Safety System Functional Inspection (SSFI) oh the Unit 3 Diesel

4

d.

Generator in May 1987, Sargent & Lundy (S&L) identified that the

Starting Air System piping for both Unit 2 and Unit 3 Diesel

Generators was supported from platform handrails inside the diesel

rooms.

S&L informed the licensee at approximately 10:20 a.m., on

March 29, 1988, that the Starting Air System piping did not meet the

FSAR piping design stress requirements.

However, even though the

piping was attached to the handrails, it was analyzed to still be

operable.

This piping is utilized to store and deliver sufficient

air to start the diesels under all conditions.

S&L is in the

process of making the required design changes for both units so the

piping will meet FSAR requirements.

On April 7, 1988, at 5:57 p.m.(CDT), with Unit 2 operating at

approximately 92% power, the "2A" Reactor Recirculation pump

tripped.

Control room alarms indicated that the trip occurred from

high differential current which caused a generator lockout. Prior

to the Recirc pump trip, the. "Recirc M/G A Generator Differential

Current High" alarm was continually comirig in and was being

investigated by.the shift.

While attempting to manually control reactor water level, flow and

position indication of the

11 2A" Feedwater Regulating valve indicated

that the valve would not fully close when given a full closed signal

from it's controller. With the valve remaining stuck at 15% open,

reactor level increased to 53 inches before the

11 2A" Feedwater

Regulating valve was isolated from the control room.

Disassembly of.

the 2A Feedwater Regulating valve disclosed the reason for ~he val~e

not going full-close was that two bolts, and a seat assembly hold

down clamp from a Reactor Feedwater Pump Isolation Check Valve, were

found lodged between the plug and seat. Examination of the 2A FRV

stem and plug revealed a crack in the seal weld between the stem and

the plug.

The licensee replaced the stem and the valve was returned

to service at 1:35 a.m., on April 10 9 1988.

In addition, the

licensee has performed testing of all three Reactor Feed Pump (RFP)

Discharge Check Valves and could not verify which check valve the

hold down clamps originated from.

After discussions with the NRC *

Region III Office, the licensee is evalu~ting the situation to

determine whether all three feedwater discharge check valves should.

be disassembled to verify which valve. is operating in a degraded

condition.

The licensee has currently disasembled the "2C RFP

discharge check valve and found no missing hold down.clamps.

The

valve manufacturer (Crane), in addition to licensee personnel from

the Quad Cities Station, were at the Dresden Station to examine the

  • "2C" valve and discuss recolTD'Tiendations about the seat assembly hold

down arrangement.

Quad Cities has the same hold down seat assembly

clamps installed in their RFP discharge theck valves. fhe licensee

is presently waiting on the valve manufacturer's resolution prior

to disassembling any more RFP discharge check valves.

5

During the event, reactor water level was maintained by the

11 2B

11

Feedwater Regulating (Drag) valve.

The

11A

11 phase of the

Recirculation M/G set breakers and relays were satisfactorily

tested and some worn brushes on the generator were replaced.

The "2A

11 M/G set was returned to service at 3: 30 a .m., and the

Recirc pump was placed in service at 4:15 a.m., on April 8, 1988.

Unit 2 was increased in reactor power while monitoring the M/G

sets breakers and relays.

On April 14, 1988, the

11 2A

11 Recirc Pump was removed from service

at 5:03 a.m., in order to inspect the current transformer circuits.

A drywell entry was made at approximately 7:30 a.m., and revealed

a loose wire connection on the

11A

11 phase of the current transformer

on the

11 2A

11 Recirc Pump motor.

The licensee promptly repaired the

connection and the Recirc Pump was returned to service at approxi-

mately 12:05 p.m. on April 14, 1988.

e.

With Unit 3 shutdown in a refueling outage, the licensee received

a Group II Isolation at 4:41 a.m.(CDT), on April 12, 1988.

While

hanging an outage tag on Unit 3 Atmosphere Containment Atmosphere

Dilution/Containment Air Monitoring (ACAD/CAM) system a Group II.

Isolation unexpectedly occurred. The Group II Isolation was

apparently caused by loss of power to both Drywell High Radiation

sensors in both logic channels .. All systems functioned as designed.

The Unit 3 Reactor Building ventilation fans tripped, Standby Gas

Treatment system auto-started and all isolation valves, that were

not out-of-service for the refueling outage, closed pertaining to

the Group II isolation signal.

The outage was immediately cleared

and power restored to the Drywell High Radiation Sensors.

The 'Group

II isolation was reset at 4:51 a.m., Re~ctor Building ventilation

returned to normal, Standby Gas Treatment system secured and any

isolation valves required to be open were reopened.

f.

On April 26, 1988, at 7:04 p.m.(CDT), the Unit 2 Reactor Building

Vent automatically tripped on a spurious high radiation indication.

The operators took prompt action* and manually tripped the Unit 3

Reactor Building Vent and the

11A

11 train of Standby Gas Treatment

System operated as required.

The licensee performed a walk down of

the refuel floor and the secondary containment and did not discover

any abnormal indications.

In addition, the instrumentation power

supply was verified to be fully operable.

The Reactor Building Vent

system was returned to service at 7:36 p.m.

The licensee has not

been able to determine the cause of the spurious trip.

g.

With Unit 3 shutdown in a refueling outage, an unplanned Group II

and Group III Isolation occur'red on May 5, 1988, at 8:50 p.m. (CDT).

While taking the Analog Trip System (ATS) panel 2203-73A Division I

out-of-service to perform modification work inside the panel to*

install new reactor pressure and level instruments per modification

M12-3-84-108, an unexpected Group II and Group III Isolations

occurred.

The isolation signals were received when the first fuse

was being removed from the ATS panel.

When the fuse wa~ pulled,

power was lost to the panel. All systems functioned as designed.

6

h.

i.

Unit 3 Reactor Building ventilation fans tripped, Standby Gas

Treatment system auto-started and all isolation valves, that were

not out-of-service for the outage, closed pertaining to the

isolation signals. The outage was immediately cleared, the panel

re-energized, and the Group II and Group III isolation signals were

cleared.

The Reactor Building ventilation system wa~ returned to

norma 1, Standby Gas Treatment system secured at 9: 10 p.m., and any

isolation valves required to be open were reopened.

The licensee

is in the process of reviewing the entire modification package,

including wiring prints and schematic diagrams, to determine the

root cause.

On May 6, 1988, at 8:58 a.m (CDT), the Unit 2 Reactor Building

Ventilation system automatically isolated and the Standby Gas

Treatment system (SBGT) auto-started and operated as intended.

The ESF actuation occurred during post-maintenance testing of the

Unit 2 Reactor Building Vent Radiation Monitor.

The testing was

being conducted on the "B" Channel due to a replaced detector.

When the Health Physics person tripped the

11B

11 Channel to perform

the testing a full trip signal was generated.

Investigation into

cause of the event revealed that procedure DRP 2000-5, utilized to

perform this activity, contained a procedural deficiency.

The

procedure discrepancy resulted in jumpering out the incorrect

terminals for Channel. "A" the Upscale Trip function, instead of

the correct Channel "B" terminals, thus producing the automatic

isolation of the Reactor Building Ventilation system and auto-start

of SBGT.

The Reactor Building Vent system was returned to normal

and SBGT secured at 9:05 a.m.

The licensee issued a temporary

change to procedure DRP 2000-5 correcting the procedural discrepancy.

On May 9, 1988, at 4:30 a.m. (CDT), with reactor power at 72%,

the Unit 2 ~igh Pressure Injection System (HPCI) was declared

inoperable when the HPCI system failed during its scheduled monthly

surveillance.

Cause was attributed to the gland ~eal leak-off

(GSLO) pump which would trip off.shortly after starting. The

licensee determined that the GSLO motor needed to be replaced.

The licensee issued a work request to replace the GSLO motor and

commenced the required Technical Specifications LCO action statement

surveillances. All required surveillances were completed

sat is factor i l y.

No violations or deviations were identified in this area .

. 5. * Monthly Maintenance Observation (62703)

Station maintenance activities of safety related systems and components.

listed below were observed/reviewed to ascertain that they were conducted

in accordance with approved procedures, regulatory guides and industry

codes or standards and in confonnance with technical specifications .

7

The following items were considered during this review:

the limiting

conditions for operation were met while components or systems were

removed from service; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; functional testing and/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities were accomplished by

qualified personnel; parts and materials used were properly certified;

radiological controls were implemented; and, fire prevention controls

were implemented.

Work requests were reviewed to determin~ status of

outstanding jobs and to assure that priority is assigned to safety

related equipment maintenance which may affect system performance.

The following maintenance activities were observed/reviewed:

On April 29, 1988, the nonnal primary containment nitrogen makeup

inerting system was rendered inoperable when the liquid nitrogen storage

tank had to be isolated due to a broken 1 1/2 inch nitrogen common header

supply line to both Unit 2 and 3 primary containments.

Unit 3 was in a

refueling outage, and not affected by this event. Unit 2 was operating

at 83% reactor power when a mechanical maintenance person called the

control room to report the broken nitrogen makeup line.

The break

occurred while the mechanical maintenance department was perfonning

rigging activity in the Unit 3 Torus area in preparation for replacing

a valve.

During the rigging of a chain fall, the 1 1/2 inch (copper) nitrogen

makeup line was inadvertently encompassed by the support rigging,

resulting in a break in the normal nitrogen makeup flow path.

The only method of securing the nitrogen leak/break location was to

secure the liquid nitrogen tank; rendering it inoperable.

The licensee

entered Technical Specification 3.0.A., requiring a plant shutdown.

An Unusual Event was declared and the ENS call was made.

The licensee

began reducing power from 83% reactor power down to 66% reactor power*

before the licensee provided an alternate nitrogen makeup flow path to

the primary containment through the nitrogen purge vaporizer line.

The licensee terminated the Unusual Event on the same day, when the

alternate nitrogen flowpath was established. Repairs to the normal

nitrogen makeup line were completed on the same day, and returned to

service.

Further evaluation by the inspectors revealed that the rigging procedures

DMP 5800-3 and OAP 4-4 were insufficient in providing clear established

control requirements on what can be utilized as a support to which

lifting devices and loads can be applied.

The inadequate rigging

instructions is considered a violation of 10 CFR 50, Appendix B,

Criterion V (237/88006-0l(DRP); 249/88007-0l(DRP)).

One violation was identified in this area.

8

6.

Monthly Surveillance Observation (61726)

The inspectors observed surveillance testing required by technical

specifications and verified that testing was performed in accordance

with adequate procedures, that test instrumentation was calibrated,

that limiting conditions for operation were met, that removal and

restoration of the affected components were accomplished, that test

results conformed with technical specifications and procedure require-

ments and were reviewed by personnel other than the individual

directing the test, and that any deficiencies identified during the

testing were properly reviewed and resolved by appropriate management

personnel.

The inspectors witnessed portions of the following test activities:

While reviewing the Unit 2 High Pressure Coolant Injection (HPCI)

In-Service Testing (IST) surveillance results on April 4, 1988, the

licensee determined that the HPCI pump discharge flow exceeded the

r~quired Action Range high flow limit of 5325 gpm.

The flow observed

was documented to be 5450 gpm.

Since the pumps IST test results fell

into the Required Action Range the HPCI system was declared inoperable

on April 4, 1988.

The licensee appropriately entered the Technical

Specification LCO action statement, which is a 7 day LCO and made the

required ENS notification.

The licensee commenced testing the other

ECCS systems required by the LCO Action Statement, with the exception

of Core Spray and Low Pressure Coolant Injection systems, which were

successfully tested just prior to the HPCI system being declared

inoperable.

In addition, the licensee proceeded to conduct another

HPCI pump IST surveillance. During this test the HPCI pumps discharge

flow was observed to be 5000 gpm, which is within the IST Acceptable

Range.

Based upon these test results, the HPCI system was declared

operable.

Subsequently, upon further review and discussions of the first HPCI

surveillance test, it was discovered that the HPCI system should not

have been declared inoperable.

The licensee determined that the

operator in the control room performing the HPCI IST. surveillance

failed to properly adjust the position of the HPCI Flow Controller

setpoint from 5600 gpm to 5000 gpm pump discharge required by Dresden

Operating Surveillance procedure, DOS 2300-6, "Monthly HPCI System

Pump Test For the In-Service Test (IST) Program.

11

This apparently

caused the pump discharge flow to be in excess of the IST Acceptable

Range.

The licensee made an ENS call on April 5, 1988, retracting the

previous HPCI reportability call declaring HPCI inoperable.

The

licensee concluded that the HPCI system was never inoperable since the

discharge pump flow rate would have fallen within the IST Acceptable

Range if the operator had correctly followed procedure dur1ng the first

IST test.

The failure to adjust the HPCI flow controller to 5000 gpm, in accordance

with approved procedure DOS 2300-6, is a violation of 10 CFR 50,

Appendix B, Criterion V (237/88006-02(DRP)).

9

In addition, examination of the Unit 2 NSO Log Book for the 1500-2300

shift on April 4, 1988, revealed that an entry was made at 1755 hours0.0203 days <br />0.488 hours <br />0.0029 weeks <br />6.677775e-4 months <br />

denoting the completion of DOS 2300-6 surveillance.

However, the Unit 2

NSO Log Book did not contain documentation of the unacceptable HPCI pump

!ST results or the HPCI system being declared inoperable.

Dresden

Administrative Procedure DAP 7-5, "Operating Logs", requires that these

activities be recorded in the Unit Logs.

The residents were informed

that no entry was made because the HPCI system was declared inoperable

after the Unit 2 operator had received a turnover from the subsequent

shift. The Degraded Equipment Log did have an appropriate entry made

declaring the HPCI system inoperable. Also, the Shift Engineers log also

had the appropriate entry.

The residents informed the licensee that

maintaining proper logs, including NSO logs, and procedure adherence

should be reemphasized to the operating staff.

The residents review of this event found several administrative controls

which may have contributed in the operator error; suc*h as performing

several related HPCI surveillances and a recently issued temporary

change (88-2~76) to DOS 2300-6 with new specified pump flow ranges.

In addition, on further examination of Temporary Change 88-2-76, the

inspectors found that Appendix A to DOS 2300-6 contained information

permitting 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> to review and conduct further analysis of IST test

data if it fell outside the Acceptable Range.

This is contrary to the

NRC's position, which was transmitted to all Region III licensees on

September 4, 1987, by Mr~ A. Bert Davis.

The NRC does not allow any

time for analysis to determine whether the component can be considered

operable if the !ST test data falls into the Required Action Range.

The inspectors reviewed a memorandum from the Assistant Superintendent

of Operations, dated October 1, 1987, which delineated the NRC's policy

regarding entry into an LCO based on !ST surveillance results, which are

in the Required Action Range.

The licensee plans to incorporate this

change into the next revision of DOS 2300-6.

One violation was identified in this area.

7.

Licensee Event Reports Followup (90712)

.

. .

Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to determine

that reportability requirements were fulfilled, immediate corrective

action was accomplished, and corrective action to prevent recurrence had

been accomplished in accordance with Technical Specifications:

(Closed) LER 249/88005-00:

HPCI System Intentionally Made

Inoperable to Facilitate Pre-Planned Preventive Maintenance Testing.

The HPCI system was made intentionally inoperable at 1830 hours0.0212 days <br />0.508 hours <br />0.00303 weeks <br />6.96315e-4 months <br /> on

March 26, 1988, to facilitate performance of Dresden Operating

Surveillance (DOS) 2300-2,

11HPCI Overspeed Test".

In order to.

conduct the overspeed test the HPCI turbine must be uncoupled from

its driver equipment.

This testing was performed in a controlled

and pre-planned manner while Unit 3 was being shutdown for its

scheduled 10th cycle refueling outage.

10

. *

I

(Closed) LER 249/88006-00:

HPCI Areas Temperature Switches Exceeded

Technical Specification Limit Due to Instrument Setpoint Drift.

As part of the Unit 3 refueling outage surveillance testing was

performed on the HPCI Area temperature switches per Dresden

Instrument Surveillance (DIS) 2300-7. A total of 16 temperature

switches are located in four different areas of the HPCI pump room.

The switches are connected in four one-out-of-two-twice logic

channels.

There are two trip systems for the HPCI auto-isolation

system.

These tempe0ature switches are required to trip at less

than or equal to 290 F.

The as-found trip settings of 7 switches

were above the 200 F Technical Specification (TS) limit of Table

3.2.1. This TS table also states that four instrument channels

shall be operable per trip system. This requirement was not met

since only three instrument channels were operable. Temperature

switches 3-2370D and 3-2371D failed, resulting in the lOlD relay

being inoperable.

The failure to have the required number of instrument channels

operable per trip system is a violation of Technical Specification

Table 3.2.1. (249/88007-02(DRP)). This violation meets the tests

of 10 CFR 2, Appendix C, Section V.G.1; consequently, no Notice of

Violation will be issued and this matter is considered closed.

As corrective actions for this event the licensee has: recalibr5ted

all th0 temperature switches to within the station limit of 170 F

to 185 F; given Impell Corporation the authorization to search for

a suitable replacement switch per Action Item Report No.12-86-46

(249-200-88-03001); accelerated calibration frequency in order to

determine the optimum calibration frequency and inspection interval;

2 switches will be inspected (1) month following the Unit 3 -startup

from the 1988 refueling outage scheduled to be completed June 26,

1988, and two temperature switches from Unit 2 HPCI pump room will

be tested during a May 1988 maintenance outage to evaluate whether

an accelerated calibration frequency is required for Unit 2.*

Additionally, the licensee's industry~wide NPRDS search on the

United Electric Controls Company temperature switches revealed that

the unreliability of these switches has been limited to the Dresden

Station.

Of the 16 reported failures, 12 have been attributed to

setpoint drift.

One violation was identified in this area.

The violation met the

criteria.of 10 CFR 2, Appendix C and no Notice of Violation was issued.

8.

Refueling Activities (86700)

The inspectors witnessed several shifts of fuel handling operations while

the Unit 3 fuel assemblies were being unloaded from the reactor vessel

to the spent fuel pool. All 724 fuel bundles were unloaded from the

core between April 2 and April 7, 1988, which met the licensees outage

schedule.

The observed acti~ities were verified to be in accordance

with station procedures and Technical Specifications.

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During an inspection of these activities, the inspectors witnessed a

cont~act person, who had been performing ISi work on the reactor vessel

head, make an error with respect to not removing the rubber outer foot

wear prior to proceeding to the next step-off pad.

The licensee's fuel

handling foreman observed this event and took prompt effective corrective

action to curtail any possible further spread of contamination.

The

individual was specifically counselled by the foreman.

In addition, the

licensee stopped all ISI work on the reactor vessel head and provided

those individuals with further Radiation Protection guidance and training

the following day.

The resident inspectors view this event as a positive

trend by management and first line supervision involvement to assure

quality. *

Additionally, the licensee has i.ncreased usage of mock-ups, including a

model of the drywell and internals to reduce the man-rem dosage.

No violations or deviations were identified in this area.

9.

Verification of Multi-Plant Actions (Temporary Instruction 2515/93)

The inspectors verified by review of audit and surveillance docum~ntation

review that the licensee had adequately implemented the January 1980

Office of N~clear Reactor Regulation (NRR) request for licensees to

include Diesel Generator (DGJ fuel oil in their Quality Assurance (QA)

programs.

The review revealed that Dresden's QA Department performed both onsite

and offsite QA audits of DG fuel oil samples and analysis, receipt

inspections and active witnessing of fuel oil sampling .. The QA program

includes DG fuel oil as commercial purchased with safety related

standards which requires verification and analysis of receipt and

storage of DG fuel oil.

10.

SALP Meeting

The NRC met with the licensee at a public meeting at the Dresden facility

on May .2, 1988, to discuss the most recent Dresden Systematic Assessment

of Licensee Performance (SALP) 7 Board Report for the Dresden Nuclear

Plant covering the period January 1, 1987 through January 31, 1988.

11.

Management Meeting (30702)

On April 19, 1988, a meeting was held at the NRC, Region III office in

Glen Ellyn, Illinois. The meeting was between NRC and CECo Corporate and

Station Management to discuss Dresden Station Performance Improvement

results and receive NRC feedback.

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12.

Meeting With Local Public Officials (94600)

On May 2, 1988, the residents, members from the region and NRR met with

officials of Grundy County, including the Director of Emergency Services

and the Mayor of Coal City.

The purpose was to discuss the recent SALP

ratings, SALP process and the purpose of the resident inspectors.

13.

Report Review (90712)

During the inspection period, the inspectors reviewed the licensee's

Monthly Operating Report for March and April 1988.

The inspectors

confirmed that the information provided met the requirements of

Technical Specification 6.6.A.3 and Regulatory Guide 1.16.

14.

Viblations For Which a "Notice of Violation" Will Not Be Issued

The NRC uses the Notice of Violation as a standard method for fonnalizing

the existence of a violation of a legally binding requirement.

However,

because the NRC wants to encourage and support a licensee's_ initiatives

for self-identification and correction of problems, the NRC will not

generally issue a Notice of Violation for a violation that meets the

tests of 10 CFR 2, Appendix C, Section V.G.1.

These tests area:

(1) the

violation was identified by the licensee; (2) the violation would be

categorized as Severity Level IV or V; (3) the violation was reported to

the NRC, if required; (4) the violation will be corrected, including

measures to prevent recurrence, within a reasonable time period; and (5)

it was not a violation that could reasonably be expected to have been

prevented by the licensee's corrective action for a previous violation.

A violation of regulatory requirements identified during the inspection

for which a Notice of Violation will not be issued is discussed in

paragraph 7.

15.

Exit Interview (30703)

The inspectors met with licensee representatives (denoted in Paragraph 1)

on May 9, 1988, and infonnally throughout the inspection period, and

summarized the scope and findings of the inspection activities.

The inspectors also discussed the likely informational content of the

inspection report with regard to documents or processes reviewed by the

inspector during the inspection.

The licensee did not identify any such

documents/processes as proprietary.

The licensee acknowledged the

findings of the inspection.

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