ML17195A979

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Insp Repts 50-010/85-14,50-237/85-31 & 50-249/85-27 on 850816-28.No Violations Noted.Major Areas Inspected: Licensee Prompt & long-term Actions in Response to 850816 Loss of Offsite Power
ML17195A979
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 09/23/1985
From: Wright G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17195A978 List:
References
50-010-85-14, 50-10-85-14, 50-237-85-31, 50-249-85-27, NUDOCS 8510080518
Download: ML17195A979 (5)


See also: IR 05000010/1985014

Text

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Report Nos. 50-010/85014(DRP); 50-237/8503l(DRP); 50-249/85027(DRP)

Docket Nos.50-010; 50-237; 50-249

License Nos. DPR-02; DPR-19; DPR-25

Licensee:

Commonwealth Edison Company

P. 0. Box 767

Chicago, IL 60690

Facility Name:

Dresden Nuclear Power Station, Units 1, 2, and 3

Inspection At:

Dresden Site, Morris, IL

Inspection Conducted:

August 16 through August 28, 1985

Prepared By:

T. M. Tongue, Senior Resident Inspector

Dresden Nuclear Station

J. H. Neisler, Reactor Inspector

D. E. Miller, Reactor Inspector

Approved By:#.~.~~

Projects Section 2C

Inspection Summary

~

9/ 13/ <tS

DHe

Ins ection on Au ust 16 throu h Au ust 28, 1985 (Re ort Nos. 50-10/85014(DRP);

50-237/85031 DRP ; 50-249/85027 DRP

Areas Inspected: This special report is a summary of the loss of offsite power

event experienced on Dresden Unit 2 on August 16, 1985, a review of the

licensee's prompt and long term actions, and the NRC response.

The inspection

involved a total of 82 inspector-hours onsite by NRC personnel including 46

inspector-hours onsite during off-shifts.

Results: No violations were identified during the inspection .

8510080518 850927

PDR

ADOCK 05000010

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PDR

. '

DETAILS

1.

~ersons Contacted

Commonwealth Edison Company

D. Galle, Vice President and General Manager - Nuclear Stations

    • D. Scott, Station Manager
  • J. Wujciga, Production Superintendent

R. Flessner, Services Superintendent

T. Ciesla, Assistant Superintendent - Operations

R. Zentner, Assistant Superintendent - Maintenance

    • J. Brunner, Assistant Superintendent - Technical Services

R. Christensen, Unit 1 Operating Engineer

J. Kotowski, Unit 3 Operating Engineer

W. Pietryga, Unit 3 Operating Engineer for Recirc. Piping Replacement

J. Achterberg, Technical Staff Supervisor

S. McDonald, Radiation Chemistry Supervisor

J. Mayer, Station Security Administrator

W. Johnson, Chemistry Supervisor

P. Lau, Q.A. Supervisor

R. Stobert, Q.A. Inspector

J. Williams, Sr., Q.A. Inspector

NRC Personnel on Site

J. Keppler, Regional Administrator

N. Chrissotimos, Chief, Division of Reactor Projects Branch 2

W. Guldemond, Chief, Division of Reactor Safety, Operational Progress

Section and Regional Duty Officer

  • T. Tongue, Senior Resident Inspector, Dresden Nuclear Station*
    • J. Neisler, Reactor Inspector

S. Stasek, Resident Inspector, Dresden Nuclear Station

M. Jordan, Senior Resident Inspector, LaSalle County Station

G. Christoffer, Security Specialist

J. Belanger, Security Specialist

D. Miller, Radiation Specialist

  • Indicates those persons present at the Exit Meeting on August 28, 1985.
    • Indicates those persons present at the Exit Meeting on August 20, 1985.

The inspectors also talked with and interviewed several other licensee

employees, including members of the technical and engineering staffs,

reactor and auxiliary operators, shift engineers and foremen, electrical,

mechanical and instrument personnel, and contract security personnel.

2

. (,

2.

Event Description

On August 16, 1985, at 12:21 a.m., Dresden Unit 2 experienced a scram

from low reactor water level from about 70% power.

The trip resulted

from a loss of offsite power that caused a running 2B reactor feed pump

(RFP) to trip and the standby 2C RFP failed to start due to the loss of

power.

The associated auxiliary Buses 22 and 24 had failed to transfer

to the unit auxiliary transformer (UAT) TR21 source of power resulting in

the loss of RFP power.

When the scram occurred, the turbine-generator tripped causing a loss of

power to the UAT resulting in a complete loss of auxiliary power.

The

Unit 2 and 2/3 emergency diesel generators (E D/G) started as designed

and provided power to their respective Buses 24-1 and 23-1.

This

provided power to the ECCS and shutdown systems as necessary; however,

none were required during the event.

Containment Group I, II, and III isolations occurred and reactor pressure

was controlled through use of the isolation condenser and level was

controlled through use of the control rod drive system.

Other associated effects were a loss of power to in-plant radio

transmitters and some telephones including the nuclear accident reporting

system (NARS).

Power was also lost to various reactor protection system

(RPS) components, and the process computer alarm memory which resulted in

the loss of the event alarm history. The reactor building ventilation

system tripped and the standby gas treatment system,started as designed.

At about 12:45 a.m., the licensee declared a GSEP "Alert" and notified

appropriate personnel and agencies.

After removing TR-12 from the 138 KV system, power was restored on those

buses and auxiliary power was restored to Unit 2 through TR-22 at 4:32

a.m.

This resulted in the licensee restoring normal power, securing the

E D/Gs and continuing with a normal plant cooldown.

When auxiliary power was restored to Unit 2, the "Alert" was down-graded

  • to an Unusual Event.

When the condensate system was restored to normal

for cooldown purpose the Unusual Event was secured.

3.

NRC Response

Upon receipt of the ENs notification that the site was in an

11Alert

11

condition, the Senior Resident Inspector and the site response team

reported to the site. In addition, the regional incident response center

was activated and the headquarters operations center was placed in a

standby condition.

Licensee activities were evaluated and observed for verification that

appropriate actions were carried out.

3

!

- I

" '

At the time of the event, two regional security specialists were on site

for a routine inspection and one witnessed the arc in the transformer 12

bus duct.

Her observation and passing of information on to appropriate

personnel was very helpful in identifying the location of the electrical

fault and reduced the time to restore auxiliary power.

Communications between the site, Region III and Headquarters were

established and maintained throughout the alert.

Throughout the event, licensee personnel showed a high degree of

competence in their actions in the control room and through evaluations

and directions given in the Technical Support Center. This was also

verified by regional personnel in the !RC and headquarters personnel in

the O.C. with respect to the accuracy and promptness of answering

questions on the event.

Subsequently, the Senior Resident Inspector followed the recovery

and return to power operation.

He also reviewed all associated

correspondence generated during the inspection from the licensee

and within the NRC and found no inconsistencies.

4.

NRC Review of Corrective Action

The licensee's investigation revealed that the cause of the failure of

Buses 22 and 24 to auto-transfer from transformer 22 to transformer 21

was due to the transformer 22 lockout relay contacts in the tie breaker

closing circuits being open.

These contacts only close when there is a

lockout condition in transformer 22 and since the fault was not in

transformer 22 there could be no auto-transfer to transformer 21.

Subsequent to the event, the lockout relays in the feeder breakers to

4160 volt Buses 21, 22, 23, and 24 were modified to permit the closing

circuitry in the breaker to auto-transfer from transformer 22 to

transformer 21 on any 138 KV Bus, section 3, differential conditions

instead of limiting auto-transfers to internal faults on transformer 22.

  • The inspector observed the post-modification test of the auto-transfer

of the 4 KV Buses from transformer 22 to transformer 21 as a result of a

simulated differential on the 138 KV Bus, section 3.

The auto-transfer

test was acceptable. In addition, the inspector reviewed ECN D-85E-08,

modification test procedure M12-2-85-10 and procedure DOP-8500-8,

Revision 0, dated October 1914, Bus 24-1 to Bus 34-1 Tie Breaker Operation.

Based on examination of the engineering change notice, modification test

procedures, work requests and test results, observation of the test of

the auto-transfer function test, and review of operating procedures for bus

transfer, the inspector determined that the licensee's corrective action

to prevent loss of power to safety-related electrical circuits on a

differential trip of the 138 KV Bus, section 3, was adequate .

4

5.

Radiological Aspects of Isolation Condenser Release Event

After the loss of offsite power at 12:21 a.m. about 90,000 gallons of

contaminated condensate storage water was fed to the isolation

condenser until 2:46 a.m. when the clean demineralized storage water

feed to the condenser was restored.

The condensate storage tank

is on emergency power; the clean demineralized storage is not.

The activity in the water was 1.1 E-5 microcuries per cubic centimeter

of cobalt 60.

Assuming all of the activity was released, the total

activity released was 3.7 millicuries.

The licensee roped off and controlled access to outdoor areas that

potentially could be contaminated, including the employee parking

lots.

When the release diminished, the licensee began surveying

the outdoor areas.

At about 7:00 a.m. the main parking lot was

released; no activity was found.

At about 10:00 a.m. the majority

of the remaining roped off areas were released.

Several puddles

inside the security fence, and near the Unit 2 turbine building,

showed detectable activity; these puddles were absorbed with floor

dry and put in containers.

A concrete pad beneath the isolation

condenser exhaust was found to be slightly contaminated.

The pad

was later decontaminated.

The licensee properly quantified the release and determined offsite

dose in accordance with technical specification requirements.

There

were no inplant airborne radioactivity or direct radiation problems.

The inspector asked the licensee to determine if there are alternate

methods of feeding clean water to the isolation condenser using emergency

power.

The licensee stated that the matter would be reviewed.

This will

be followed under existing open item No. 237/85005-03 and 249/85004-03.

No violations or deviations were noted.

6.

Open Items

Open items are matters which have been discussed with the licensee, which

will be reviewed further by the inspectors, and which involve some action

on the part of the NRC or licensee or both.

Open items discussed during

the inspection are discussed in Paragraph 5.

7.

Exit Interview

The inspectors met with licensee representatives on August 20, 1985 and

at the conclusion of the inspection on August 28, 1985. The inspector also

discussed the likely informational content of the inspection report with

regard to documents or processes reviewed by the inspector during the

inspection.

The licensee did not identify any such documents/processes

as proprietary.

The licensee acknowledged the findings of the inspection .

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