ML17195A764

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Notice of Violation from Special Insp on 850216-0328
ML17195A764
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 04/18/1985
From: Norelius C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17195A763 List:
References
50-237-85-10, 50-249-85-09, 50-249-85-9, NUDOCS 8505020610
Download: ML17195A764 (2)


See also: IR 05000216/2003028

Text

Commonwealth Edison Company

Dresden Nuclear Power Station

Appendix

NOTICE OF VIOLATION

Docket No. 50-237

Docket No. 50-249

As a result of a special inspection conducted during the period of February 16

through March 28, 1985 at the Dresden Nuclear Power Station, and in accordance

with the General Policy and Procedures for NRC Enforcement Actions (10 CFR

Part 2, Appendix C), the following violations were identified:

1.

Technical Specification 3.5.C.1 states in part that "the HPCI subsystem

shall be operable whenever the reactor pressure is greater than 90 psig

and irradiated fuel is in the reactor vessel."

Technical Specification Definition 1.0.0 defines Operability for a

subsystem to include all auxiliary equipment that are required for the

subsystem to perform its function(s), are also capable of performing

their related support function(s).

Contrary to the above, on February 22, 1985, the service water to the

High Pressure Coolant Injection (HPCI) System room cooler was found

valved out.

The licensee determined that this situation had existed for

approximately 29 to 38 days.

Therefore, this resulted in the room cooler,

and by definition, HPCI, to be considered inoperable for that period of

time.

A technical evaluation conducted by a licensee contractor showed

that the HPCI would be functional for a period of time sufficient to take

alternative actions.

This is a Severity Level IV violation (Supplement I).

2.

Technical Specification 3.7.2 states in part, that primary containment

integrity shall be maintained at all times when the reactor is critical

  • or when the reactor water temperature is above 212° and fuel is in the

reactor vessel.

Contrary to the above, on March 2, 198S, the lice~see found a torus water

sample line open.

This allowed for a direct flowpath for torus water from

primary containment to secondary containment via the reactor building floor

drain sump.

It should be noted that this leakage path would still have

been in existence during an accident situation and would have allowed for

a calculated flow rate of approximately 40 gpm maximum, unless one loop of

the core spray system was intentionally isolated to prevent it.

The licen-

see subsequently determined that the valves had been open for a period of

approximately five shifts.

This is a Severity Level IV violation (Supplement I) .

8505020610 850418

~DR

ADOCK 05000237

PDR

Appendix

2

3.

10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings"

requires that activities affecting quality shall be prescribed and accom-

plished by appropriate instructions, procedures, and drawings.

10 CFR 50 Appendix B, Criterion XIV, "Inspection Test and Operating

Status", requires that measures be established for indicating the oper-

ating status of .... systems and components of the nuclear power plant

such as by tagging .... to prevent inadvertent operation.

Commonwealth Edison Company, Topical Report CE-1-A, "Quality Assurance

Program for Nuclear Generating Stations", implements 10 CFR Appendix B.

Dresden Operating Surveillance Procedure DOS 6600-5, "Bus Undervoltage and

ECCS Integrated Functional Test for 2(3) Diesel Generator", Prerequisites,

Step 13, calls for an equipment line up in accordance with the attached

loadlng and Caution Card check lists.

Contrary to the above, while preparing to conduct Dresden Operating Sur-

veillance, DOS 6600-5, "Bus Undervoltage and ECCS Integrated Functional

Test for 2(3) Diesel Generator", on the Unit 2 emergency diesel generator

on February 16, 1985, mislabeling and misapplication of the Caution Cards

resulted in the removal of the ability of the Unit 3 low pressure emergency

core cooling systems to respond under a loss of off site power condition

if they had been called upon.

The condition existed for about four and

one half minutes while the Cnit was at full power and it was recognized

and corrected through the prompt response of control room management per-

sonnel.

It is recognized that the low pressure emergency core cooling

systems could have responded as designec as long as offsite power was

available.

This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, you are required to submit to this

office within thirty days of the date of this Notice a written statement or

explanation in reply, including for each item of noncompliance:

(1) corrective

action taken and the results achieved; (2) corrective action to be taken to

avoid further noncompliance; and (3) the date when full compliance will be

achieved.

Consideration may be given to ex~ending your response time for good

cause shown.

Dated

C. E. Norelius, Director

Division of Reactor Projects