ML17194A464

From kanterella
Jump to navigation Jump to search
IE Insp Repts 50-010/81-20,50-237/81-37 & 50-249/81-29 on 811205-30.Noncompliance Noted:Failure to Prepare,Approve & Implement Procedures Including Checkoff Lists Covering Operating safety-related Instrumentation
ML17194A464
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 01/26/1982
From: Jordan M, Knop R, Robinson D, Tongue T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17194A462 List:
References
50-010-81-20, 50-10-81-20, 50-237-81-37, 50-249-81-29, NUDOCS 8202160485
Download: ML17194A464 (9)


See also: IR 05000010/1981020

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-010/81-20; 50-237/81-37; 50-249/81-29

Docket Nos,50-010, 50-237, 50-249

Licenses No. DPR-02, DPR-19, DPR-25

Licensee:

Commonwealth Edison Company

Post Office Box 767

Chicago, IL

60690

Facility Name:

Dresden Nuclear Power Sta.tion, Units 1, 2 and 3

Inspection At:

Dresden Site, Morris, IL

inspection Conducted:

Decembe~ 5-30~ 1981

Inspectors:

.,

I .

. . °'

.... _ r .... " i

*--'--*-***

T. M. Tongue

. '

_(_

...

M J. Jordan

      • .D~~=~

'***

.:' ~.

Approved By:

R. C. Knop, Chief

Projects Branch 1

Inspection Summary

:

. /~ -~

'*

Inspection on December 5-30, 1981 (Reports No.50-10/81-20; 50-237/81-37;

50:-249/81-29)

Areas Inspected:

Routine unannohnced resident inspection of Operation

Safety Verification, Monthly Maintenance Observation, Monthly Surviellance

Observation, Licensee Event Reports Followup, Plant Trips, Inspection during

long term shutdown, Preparation for Refueling, Independent Inipection, Pre-

paration for Guard Force Strike", and Headquarters and Regional Requests.

The inspection involved a total of 93 inspector-hours onsite by three NRC

inspectors including 20 inspector-hours during offshift.

Results:

Of the ten areas inspe~ted, there were no items of noncompliance

in nine areas.

There was one item of noncompliance (Severity Level IV -

Failure to have and to follow adequate procedures - Paragraph 7) in one area .

8202160485 820128

PDR ADOCK 05000010

G

PDR

.L

DETAILS

1.

Persons Contacted

Corporate

B. Lee, Jr., Executive Vice President

D. Galle, Operations Manager - Nuclear Stations Division

Station

  • D. Scott, Station Superintendent
  • R. Ragan, Operations Assistant Superintendent*

J. Eenigenburg, Maintenance Assistant Superintendent

  • D. Farrar, Administrative Services and Support Assistant Superintendent

J. Brunner, Technical Staff Supervisor

J. Wujciga, Unit 1 Operating Engineer

J. Almer, Unit 2 Operating Engineer

M. Wright, Unit 3 Operating Engineer

J. Doyle, QC Supervisor

D. Adam, Waste Systems Engineer

G. Myrick, Rad-Chem Supervisor

B. Saunders, Station Security Administrator

B. Zank, Training Supervisor

E. Wilmer, QA Coordinator

A.S.M.E

H. F. Jackson, ASME N Stamp Survey Team Chairman

The inspector also talked with and interviewed several other licensee

employees, including members of the technical and engineering staffs,

reactor and auxiliary operators, shift engineers and foremen, elec-

trical, mechanical and instrument personnel, and contract security

personnel. .

  • Denotes those attending one or more exit interviews conducted on

December 11, December 23, and December 30, 1981.

2.

Management Meeting.

A management me~ting between members of the Region III staff, and

Commonwealth Edison Corporate and Dresden Station staffs to discuss

concerns related to recent events at the Dresden Nuclear Power

Station.

The meeting was held on December 22, 1981, at the NRC,

Region III office in Glen Ellyn, Illinois.

The concerns were generally related to delays in pursuance of the

causes of events, lack of indepth investigation when events occur,

reluctance to declare affected systems inoperable when evidence

clearly indicates operability is unknown, and the need for some

- 2 -

form of verification that systems are properly returned to service

following maintenance, surviellance, etc.

Each of the concerns will

be treated as an open inspection item.

The meeting also included comments from the security section discus-

sing operational events that occur with no ready explanation, or

non-operational events that occur related to personnel causes with

potential malicious mischief.

When events of this sort occur, the

NRC expects a determination of individual security significance,

plus a review for trends identifiable from a security standpoint.

It is believed that this will require coordination between security

and operations departments.

Examples identified were the recent Unit 3 emergency diesel generator,

emergency fuel cutoff valve found shut and safety related instrument

valves were found in inc.orrect positions.

This matter was discussed

prior to this meeting with CECo corporate security personnel. It was

pointed out that the NRC is also independently reviewing such events

for trends.

This is open inspection item 50-237/81-37-01 and

50-249/81-29-0i.

'

Representatives from the Division of Resident and Projects Inspection

expressed concern that delays in review of events can result in con-

fusing or conflicting information that eventually can compound the

investigation of a problem.

One *recent example cited was the.Unit 2/3

and Unit 3 Emergency Diesel generator cooling water pump problems,

where delays in agressive solution seeking contributed ~o confusing

information and a prolonged NRC investigation.

This .is open inspec":'

tion it~m 50-237/81-37/02 and 50-249/81-29-02.

It was pointed out that licensee investigations of events should be

conducted in sufficient depth to identify generic or related applic-

ability.

An example discussed was the recent Unit 3 scram with a

short period that resulted from an inadvertent control rod double

notch withdrawal.

The investigation addressed only that event; but

should have been expanded .to look at a similar event under different

reactor conditions, e.g., a newer cor~, a more reactive control rod,

and possibly greater than a two notch withdrawal.

This is open

inspection item 50-237/81-37-03 and 50-249/81-29-03.

Another point of concern was ?n apparent reluctance ~r resistance

of licensee.personnel to declare a system inoperable*when evidence

clearly points out that damage has occured to the system or when

there is doubt that the function can meet it's design criteria.

Examples pointed out were the recent events when pipe hangers and

supports were found damaged on the Unit 2 and 3 HPCI steam lines and

the 2B CCSW system, and water was identified in the HPCI steam lines.

This is open inspection item 50-237/81-37-04 and 50-249/81-29-04.

The final item of concern discussed was the need for some means of

verification that a system or component has been properly returned

to service following surviellance or maintenance, etc.

The licensee

- 3 -

has addressed this matter in the tag out system for safety related

equipment per the T.M.I. Task Action Plan. *However, there is an

apparent need for verification of system changes when the tag out

system is not used such as surviellances.

A recent example is the

instrumentation valves found mispositioned where a verification of

the valve positions following the reference leg back fill could have

prevented the event.

This is open inspection item 50-237/81-37-05

and 50-237/81-29-05.

Following some discussion, the licensee representatives expressed

concern about some of the recent events at Dresden and acknowledged

the concerns of the NRC.

The response to the open items will be reviewed during a future

inspection.

3.

Operational Safety Verification

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during the

period of December 5-30, 1981.

The inspector verified the operability

.of selected emergency systems, reviewed tagout records and verified

proper return to service of affected components.

Tours of Units 2-3

reactor buildings and turbine buildings were conducted to observe plant

equipment conditions, including potential fire hazards, fluid leaks,

and excessive vibrations and to verify that maintenance requests had

been initiated for equipment in need of maintenance.

The inspector by

observation and direct interview verified that the physical security

plan was being implemented in accordance with the station security p1an.

The inspector observed plant housekeeping/cleanliness conditions and

verified implementation of radiation protection controls.

During the

period of December 5-30, 1981, the inspector walked down the accessible

portions of the Unit 2 HPCI, 2B. LPCI, 2B Core Spray, Unit 3 HPCI, 3A

LPCI, 3B Core Spray systems to verify operability.

The inspector also

witnessed portions of the radioactive waste system controls associated

with radwaste shipments and barreling.

These reviews and observations were conducted to verify that facility

operations were in conformance with the requirements established under

technical specifications, 10 CFR, and administrative procedures.

No items of noncompliance were identified.

4.

Monthly Maintenance Observation

Station maintenance activities of safety related systems and components

listed below were observed/reviewed to ascertain that they were conducted

in accordance with approved procedures, regulatory guides and industry

codes or standards and in conformance with technical specifications.

- 4 -

The following items were considered during this review:

the limiting

conditions for operation were met while components or systems were

removed from service; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; functional testingand/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities o/ere accomplished by

qualified personnel; parts and materials used were properli certified;

radiological controls were implemented; and, fire prevention controls

were implemented.

Work requests were reviewed to determine status of outstanding jobs

and to assure that priority is assigned to safety related equipment

maintenance which may affect system performance.

The following maintenance activities were observed/reviewed:

.Unit 3

3A Standby Liquid Control. Pump

Emergency Diesel Generator

Semi-annual Maintenance *

3B LPCI Heat Exchanger.

No items of noncompliance were identified ..

5.

Monthly Surveillance Observation

The inspector observed technical specifications required surveillance

testing on portions of Unit 2 HPCI Valve Operability and Core.Spray

Operability and verified that testing was performed in accordance with

adequate procedures, that limiting conditions for op~ration were met,

that removal and restoration of the affected components were accom-

plished, that test results conformed with technical specifications

and procedure requirements and were reviewed by personnel other than.

the individual conducting the test, and that any deficiencies

identified during the testing were properly reviewed and resolved

by appropriate management personnel*:

No items of noncompliance were identified.

6.

Licensee Event Reports Followup

The licensee reported finding two safety related pressure switch

isolation valves shut related to low pressure core spray permissive

alarm and isolation condenser initiation on December 14, 1981.

On

,

December 15, 1981, the licensee reported finding a pressure transmitter

(PT) isolation valve shut and it's test connection open, related to the

anticipated transient without Scram (ATWS) system that would have pre-

vented the 2B recirc pump from tripping and one ARI valve would not

have opened if an ATWS event had occuired.

Normal scram functions

were not affected. .All of the valves identified, were on the same

- 5 -

instrument racks (2202-5&6) and licensee personnel stated that they

believed the valves were left in the wrong position when the reactor

vessel level reference legs were back filled following a scram on

December 13, 1981.

The back fill was done with a modified procedure *that had not received

proper review and approval.

At the request of the NRC, the licensee conducted a check of the

position of all safety related instrument valves and test connections

.on December 16, 1981.

The check of these valves revealed two addi-

tional pressure switches valved out.

One was for the 2B LPCI heat

exchanger differential pressure indication used to minimize a release

of radioactive material from LPCI to theCCSW systems and the other

was a high pressure turbine inlet pressure switch that had no auto-

matic control function.

The cause of these valves being mispositioned

is unknown, however, it is .evident that had a procedure been followed

properly, these valves would not have been mispositioned.

This is not in accordance with Technical Specification 6.2.A requiring

_detailed written procedures including applicable check off lists pre-

pared, approved, and adhered to for instrumentation operation which

could have an affect on the safety of the plant, and for surviellance

and testing requirements.

This is considered noncompliance

(50-237/81-37-06) (50-249/81-29-06).

The licensee reported that the fire deluge system had automatically

activated in the Unit 2 HPCI room on December 23; 1981.

This resulted

in the HPCI being inoperable due to water in the lube oil.

This was

later found to have been caused by welding in the HPCI room that

caused.a smoke detector to activate the deluge system.

During the

process of conducting the required surviellances, the 2B Electromatic

safety/relief valve failed to operate.

This required an orderly

reactor shutdown per Technical Specifications.

The cause of the

Electromatic S/R valve failure was an inadequately suspended wire on

the pilot solenoid junction box that prevented contacts from making

up allowing the solenoid to properly energize.

This problem was

promptly corrected by taping the cable up with other cables.

After

the HPCI oil was changed, the reactor was started up. on December 24,

1981.

During the startup, the HPCI and the 2B S/R valve were tested

satisfactorily.

The licensee also inspected the 2D S/R valve pilot

solenoid and found no problems.

In subsequent discussions-with the-

Ass.istant Superintendent for Maintenance, he committed to have the

remainder of the electromatic S/R valves on Units 2 and 3 inspected

for similar problems.

This is an open inspection item (50-237/81~37-07)

and (50-249/81-29-07).

The licensee will submit appropriate events

reports.

With respect to LER 50-249/81-40/0lT-0~ a regional inspector arrived

onsite on December 2, 1981, in response to the event.

The inspector

noted that no Technical Specifications had been violated and that

the observed notch worths had not exceeded those predicted in the

-

6 -

CRDA analysis.

From discussions with Tech Staff personnel and the

Nuclear Fuel Services Department, the inspector concluded that the

high control rod notch worths would be expected near the top of the

core at low power, end of life conditions due to insu.f f icient voiding

and excessive fuel depletion in the lower portions of the core.

The

corrective actions proposed by the licensee were addressed in a man-

agement meeting at the Region III office on December 22, 1981.

At

that time the licensee was requested to review its overnotching

history and take appropriate measures to prevent recurrence.

Since

the timing and contact condition of the single notch control switch

is under investigation, the LER remains open.

One item of noncompliance was identified.

7.

Plant Trip*s

Following the plant trips on Unit December 13, 1981, the inspector

ascertained the status of the reactor and safety systems by obser-

vation of control ro6m indicators and discussions* with licensee

personnel concerning plant parameters, emergency .system status. and

reactor coolant chemistry. The inspector verified the establishment

o*f proper communications and reviewed the corrective* actions taken

by the licensee.

All systems responded as expected, and the plant was returned to

operation on December 14, 1981.

No items of noncompliance were identified.

8.

Inspection During Long Term Shutdown

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during the

period of December 5-30, 1981.

~he inspector verified-su~veillance

tests required during the shutdown were accomplished, reviewed tagout

records, and verified applicability of containment integrety.

Tours

of Unit I accessible areas, including exterior areas were made to make

independent assessments of equipment conditions, plant conditions,

r~diological controls, safety, and adherence to regulatory requirements

and to verify that maintenance requests had been initiated for equipment

in need of maintenance.

The inspector observed plant housekeeping/

cleanliness conditions, includiffg potential fire hazar_ds, and* verified

implementation of radiation protection controls.

The inspector by

observation and direct interview verified that the physical secur1ty

plan was being implemented in accordance with the station security plan.

No items of noncompliance were identified.

9.

Preparation for Refueling

The inspector verified that technically adequate procedures were ap-

proved for the upcoming refueling of Unit 3.

The specific procedures

- 7 -

reviewed were those refueling procedures that had been revised or

modified during 1981.

Other procedures had been reviewed for the

Unit 2 refueling that took place in early 1981.

The inspector also

veiified that the licensee's 10 CFR 50.59 safety evaluation of the

reload core showed that no unresolved safety questions existed.

However, the inspector did verify that Technical Specification changes

were submitted for NRR approval of the change in fuel vendors (Exxon

vie General Electric) and the Exxon analytical models and methodology.

In correspondence reviewed, it was found that the licensee has .ex-

pressed concerns about a timely review and approval in order to

prevent a delay in the planned restart of Un~t 3.

The inspectors also reviewed the licensee's program for overall outage

control.

No items of noncompliance were identified.

10.

Independent Inspection

On December 8, 1981, an ASME survey team conducted a recertification

audit for renewal of the licensee's NA and NPT certificates (N-Stamp).

These certifications authorize the licensee to conduct ASME Code

related work on nuclear systems and to handle materials used for

nuclear grade work.

Licensee personnel and the ASME survey team

leader cordially invited the Resident Inspectors to participate in

the review.

During the review, several minor discrepencies were

identified and immediately corrected.

The licensee passed the *audit

and the review board is recommending that the National board recertify

the licensee.

The Station Superintendent agreed to provide the

Resident Inspectors with a copy of the report.

Due to the interest of the NRC in ASME Code work, the report information

will be treated in the same manner as INPO reports.

No items of noncompliance were identified.

11.

Preparation for a Guard Force Strike

The inspectors verified that the licensee was prepared to implement

their contingency plan in the event of a strike by the security guards.

A potential threat of a strike occurred on December 11, 1981, when the

unionized guard force, held a strike vote which resulted in favor of

continuing to work.

This issue was also followed by Region III Security

Specialists.

No items of noncompliance were identified.

12.

Headquarters and Regional Request

The Senior Resident Inspector conducted interviews with six licensed

Reactor Operators and Senior Reactor Operators, relavent to specific

corporate instructions and their training on the subject.

These were

- 8 -

  • --

the result of allegations received pertaining to Dresden, Quad-Cities,

Zion, LaSalle stations and Commonwealth Edison Corporate Office.

The

results will be forthcoming under a special investigation report.

13.

Meetings, Training, and Offsite Functions

During this inspection period, the Resident Inspectors attended a

Resident Inspectors' seminar on December 15-18, 1981, at the Region_III

Office in Glen Ellyn,. Illinois.

The Resident Inspectors were also absent from the site on annual leave

for a total of 12 inspector days during the report period~

14.

Exit Interview

The inspector met with licensee representatives (denoted in Paragraph 1)

throughout the month and at the conclusion of the inspection on December 30,

1981 7 and summarized the_ scope and findings of the inspection activities.

- 9 -