ML17193B134
| ML17193B134 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 03/03/1981 |
| From: | Maxwell D COMMONWEALTH EDISON CO. |
| To: | |
| Shared Package | |
| ML17193B133 | List: |
| References | |
| NUDOCS 8103130358 | |
| Download: ML17193B134 (17) | |
Text
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OPERATING DATA REPORT OPERATING. STATUS.
1
- Unit Name :__.D_r...
e.-s.-de
.... n-.....I......................... -----------........-
- 2.
Re po rt i ng Period :*......-F..-e.-b.... ru
- . a;r;r-..y._..i...--1.... 9....
8-..1' _. ------------
- 3.
Licensed Thermal Power (MWt}:
700
- 4.
Namep'late Rating (Gross MWe) =---20_9 ___________ __
- 5.
Design Electrical Rating (Net MWe): 200
- 6.
Max imµm Dependable Capacity (Gross *-M.,..,\\.J-e.... }-: 0'"""5-. ----....-.---
DOCKET NO.
- 050-010 DATE March 3, 1981 COMPLETED BY D... c*. Maxwell tELEPHONE ca15) 942~2920 x...:550 NOTES
- 7.
Maximµm Dependable. *Capacity (Net :MWe):
197
- 8.
If Changes Occur in Capacity *Ratings -.(-1-tem_*_s_,_3 __
T,.,.h_r_o-ug_h_ 7) SinC:e Last Report, Give Reasons:
N/A
- 9.
Power Level to Which Restricted,.If Any (Net MWe) :-...:N:.:.i/..-A;:._ _________ _,_ _____ _
. 10.
Reasons For Restrictions, If Any::..;.*...;N~/:..;;A;;;..... ________ __;_..... ____ _..... _____....,...--'-
- 11.
Hours: in Reporting* Period
- 12.
Number of.Hours Reactor Was. Cr it ica 1 1 J.
Reactor Rese.rve Shutdown Hours
- 14.
Hours* Generator On-Line
- 15. *Unit 'Reserve. Shutdown Hours
- 16.
Gross Thermal. Energy Generated (MWH)
- 17.
Gross 1::1 ect r i ca 1 Energy.Generated (MWH) * *
- 18.
Net E*lectrical Energy Generated (MWH)
- 19.
Unit ~ervice Factor".
- 20~
Unit Avail~bil ity Factor
- 21.
Unit Capacity Factor {Using MOC Net) *.
This Month*
Yr-to-Date Curmtt.atlv.e.
. EXTENDED**
.*MODIFI.CATION *
- .ouTAGE'
- 22.
Unit 'Capacity F~ctor (Usin'g DER Net)
- 23.
Unit :Forced Outage Rate.
. 24 *. Shutd()Wns Scheduled Over Next 6 Months (-T-yp
.... e-.-,.-p-a-.t-e""",..-. -arid Duration *of Each):
N/A
- 25. *If Sh~ut Down At End Of.Report Pe.riod, Estimated Date of Startup: E~tended Modificatior:
Outage -
Shutdo'Wn'
- Until Jµne,. 1986
.. **8i~~l80;')$~{.......,**.....
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- . OPERATING DATA REPORT
- DOC KET N 0 *.--:::0"'"5.:.0-_,2:1"'3...,7_... __
DATE March 3, 1981 COMPLETED BY D. C. Maxwell TELEPHONE (815) 942-2920 OPERATING STATUS NOTES 1
- Uni t Name :__,,o'""r..,.e..... s_,,d""e.:.:.n_I=-r=--* ----------------------
- 2.
Reporting Period:..,....;;F~e~b_r_u~ar_y..,.....,.~1~9~8~1~*---------------,__,_,.
- 3.
Li~ensed Thermal Power (MWt}: 2 527
- 4.
Nameplate Rating (Gross MWe):
828
- 5.
Design Electrical Rating (Net-. -t1W_e_,)..... -.: _7_9_4_....__ ____ _
- 6.
Maximum Dependable.Capacity (Gross MWe) :812
- 7.
Maxi mum Dependab 1 e Capacity (N'et MWe) : 772
- 8.
If Changes Occur in Capacity Ratings..,.(-=-1"'"'te_m_s_3__,,T __ h_r_o_u_g_h 7) Since Last Report, Give Rea.sons:
- 9.
Power Level to \\~hich Restricted, If Any (Net MWe):* NA
- 10.
Reasons For Restrictions, If Any:
NA
-=--------------__.,..--
- 11.
- 12.
- 13.
- 14.
- 15.
- 16.
- 17.
- 18.
- 19.
- 20.
- 21.
- 22.
'23.
- 24.
Hours i~ Reporting Period Numbe.r of Hours Reactor Was Cr it i'ca 1 Reactor Reserve Shutdown Hours This Month Yr-to-Date 6_7_2 1.416 0
73.8 0
0 Hours Generator On-Line 0
69.4 Unit Reserve Shutdown Hours 0
0 Gross Thermal. Energy Generated (MWH) 0 74,675
~ross.Electrical Energy Generated (MWH) 0 22.045 Net Electrical Energy Generated (MWH)
-1,695 15,527 Unit *Service Factor 0
- 4.901 Unit Availability F~ctor 0
4.901 Unit Capacity Factor (Using.MDC Net)
- 0.
1.420 Unit *capacity Factor (Using D~R N~t) o 1.381 0~it Forced Outag~ Rate 0
0 Shutdowns Scheduled Over N.ext 6 Month_s *(Type', Date, and Duration of.Each):
C urou:la ti '.le.
94.656 73,211. 7 0
59,529.S 0
137,372,731 43,894,908 41,484,526 73.5 73.5 56.8 5-5. 2
- 12. 5' 25.. If Shut Down At End Of Report Period,: 'Estimated Date bf Startup: _______ _
. 1:*
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- 1.
- 2.
- 3.
- 4.
- 5.
- 6.
- 7.
- 8.
OPERATING DATA REPORT
(
OPERATING STATUS.
Unit Name: Dresden III*
Reporting Period: February, 198f Licensed The rma I _P_o_w_e_.r__,..( M_W._t.... )_:_2_5 __ 2_7 _____....._...__ __
Nameplate Rating (Gross MWe):
. aa8 Design Electrical. Rating (Net-MW-e'""fF"'*."'": -7_.9-4-.--------
Maximum Dependable Capacity (Gross _M.... W-e.-)_:_8_1_2 _____....__
DOC KET NO *.-0=5.... 0-.... 2""'4.. 9 ___ _
DATE March 3, 1981 COMPLETED BY. D. C. Maxwell TELEPHONE (815) 942-2920 NOTES Maximum Dependable Capacity (Net MWe):
773 If Changes Occur in Capacity. Ratings..... (_1,._t.... em-.s_3_T __ h_r_o_u_g_h 7) Since Las.t Report, Give Reasons:
- 9.
Power Level to \\.Jhich Restricted, If Any (Net MWe): N
-=-------------------~
- 10.
Reasons For Restrictions, If Any:
NA
---==---------------------------
- 11.
- 12.
- 13.
- 14.
- 15.
16 *.
- 17.
- 18.
- 19.
- 20.
- 21.
22..
- 23.
- 24.
Hours in R~porting Period Number of Hours Reactor Was Critical Reactor Reserve Shutd9wn Hours Hours Generator On-Line Unit Reserve Shutdown Hours Gross Thermal Energy Gen~rated (MWH)
Gross Electrical ~nergy Generated (MWH)
Net Electrical Energy Generated (MWH)
Unit Service Factor Unit Availabi~ ity Factor Unit Capacity Factor (Using MDC Net)
Un.it Capacity Factor {Using PER Net)
- Unit Forced Outag~ Rate This Month 672 664.3 0
660.2 0
1.520, 173
.499,636 476z953.
98.2 98.2 92.1 89.7 1.8 Yr-to-Date 1,416 1,393.6 0
1,374.5 0
3, 113,481 1,023,75.7 975,700 97.1 97.1 89.3 86.9 2.4 Shutdowns Scheduled Over Next 6 ~onths (Ty~e, D~te, ~nd Duration of Each Curou:l.at i.\\!e. **
.84,241 63,680.6 0
61,007.8 o*
. 119,597,951 39,024,325 36,9982600 72.4 72.4 56.8 55.3 15.o.
- 25.
If Shut Down At End Of Report Peri ad? Estimated Date of Sta rt up:_. _N_A ____________ _
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AVERAGE DAILY UNIT POWER LEVEL
\\,~:.. :~.*
MONTH FEBRUARJ, 1981 DAY AVERAGE DAI LY.POWER LEVEL.
2 3
4 5
6 7
8 9
. 10 11
. 12 lJ 14 15
.16 (MWe-Net) 0 0
0 0
0 0
.0 0
0 0
0 0
0
. *t *.
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i.*
.~ :
~
~-
- /. -*
DOCKET NO. 050-010 Ull IT Dresden I.
DATE March 3, 1981 COMPLETED BY D. C. Maxwell TELEPHONE (815) 942-2920 DAY
- AVERAGE DA IL Y PO\\./ER LEVEL (MWe-Net) 17 0
18 0
19 0
20 0
21 0
22 0
23, 0
24 0
25 0
26 0
27 0
28 0
29 30 31
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- e AVERAGE DAILY UNIT POWER LEVEL MONTH FEBRUARY, 1981 08Y 2
3 4
5 6
7 8
9 10 11 12 13 14 15
.16 AVERAGE DAILY POWER LEVEL (MWe-Net) 0 0
0 0
0 0
0 0
0 0
d 0
0 DAY 1/'
18 19 20 21 22 23 24 25 26 27
- 28.
29 30 Jl DOCKET NO. 050-237 UU IT Dresden II.
DATE March 3, 1981 COMPLETED BY D. C. Maxwe 11 TELEPHONE (815) 942-2920 AVERAGE DAILY POWER LEVEL (MWe-Net) 0 0
0 0
0 0
0 0
0 0
0
':'~...............-__.. ***-: *-
-""**--.****""""'~..--..-.;.-.-_......:;...........
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MONTH 08Y 2
3 4
5 6
7 8
9 10 11 12
.13.
14 15 16
\\;-:.~)/)
.. ~
- =.
AVERAGE DAILY UNIT POWER LEVEL FEBRUARY, 1981 AVERAGE DAILY POWER LEVEL DAY.
(MWe-Net) 755 17 792 18 785 19 784
- 20.
751 21 794 22 782 23 763 24
- 777, 25 26 792 27
. 7.87 28
' 797 29 784 30 759 3 l '
787 '
DOCKET NO. 050-249 UUIT.Dresden III DATE March 3, 1981 COMPLETED BY D. C~ Maxwell TELEPHONE
~815) 942-2920 AVERAGE DAILY POWER LEVEL (MWe-Net) 770 790 788
. 777 398 536 169 456 611 666 769 734
~ -'
No.
- DATE.*
- 8 781031 L
1.:.*
F:.Forced,
- . s:. Scheduled*
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT MONTH F~BRUARY, 1981 METHOD OF LICENSEE TYPEl. DURATION REASON2 SHUTTING EVENT SYSTEM COMPONENT s
2 (HOURS)
DOWN.REACTOR3 REPORT 672 c
3 Reason_:
A-Equipment Failure (Explain)
B-Maintenance of Test
. C-Refueling.
D-Regulatory Restriction-E-Operator Training & License F.-Administrative G-OperationalError
. H-Other (Explain)
Examination ii CODE4 CODES I
Method:
1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)
DOCKET NO. 050-010
~~~~~~~~
UNIT NAME Dresden I DATE March 3, 1981 COMPLETED BY D, C, Maxwe 11 TELEPHONE (815) 942-2920 CAUSE & CORRECTIVE ACTION TO PREVENT RECURRENCE n
Refueling and Chemical Cleaning Outage
- 4.
- Exhibit G-lnstructions for.
Preparation of Data Entry Sheets for Lice_nsee Event Report (
) File (NUREG-0161) i,,
- ,..N.O.
...DATE *.
- 1*:
810103 umbers c
.*.**1 *..
F:
Forced Scheduled
. ?,*
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UNIT SHUTDOWNS AND. POWER REDUCTIONS REPORT MONTH FEBRUARY 1 METHOD. OF LICENSEE DURATION REASON2 SHUTTING E~NT (HOURS).
DOWN REACTORl REPORT {}.
6.72 2
ried 0 er from 1 80 repor s.
2 Reason:
A"."Equiprnerit Failure (Explain)
B-Maintenance of. Test C-Refueling D-Regulatory Restriction E-Operator Tr.aining & License Examination F-:-Administrative G-Operational Error H;..Other *.*(Explain) 3 1981 SYSTEM COMPONENT CODE4*
CODES Method:
1-Manual*
2-Manual Scram 3-Automatic Scram 4-0ther (Explain)
DOCKET NO.
050-237
~-------~~~~~~
UNIT NAME Dresden II DATE March* 3, 1981 COMPLETED BY D. C, Maxwell TELEPHONE (815) 942~2920 CAUSE & CORRECTIVE ACTION TO PREVENT RECURRENCE Refueling and Turbine Overhaul Outage Exhibit G-lnstructions for Preparation of Data Entry Sheets for Licensee Event Report (
) File
.. (NUREG-0161)
UNIT. SHUTDOWNS AND POWER REDUCTIONS REPORT MONTH _,..,.FE=B=R=U=AR=Y..._, _1-.:9;...;8"""1'-* _
METHOD OF LICENSEE NO~.
DATE*
. TYPEl *DURATION REASON2. SHUTTiNG EVENT SYSTEM COMPONENT (HOURS)*
DOWN REACTORl REPORT {}
CODE4 CODES
-4**
" 810223 F
11:49 A
3
- ' = Numbers ca ried. o~er from 1180 repor1 s.
- 2.
F:
Forced
- .s: *.Scheduled*
Reason:
A-Equipment Failu{e (Explain)
B-Maintenance of Test C-Refueling D-Regulatory Restr:iction E"'."'Operator Training & License Examination F-Administrative G-Operational.Error H-Other (Explain) 3 Method:
1-Manual 2-Manual Scram 3-Automatic Scram 4-0ther (Explain)
DOCKET NO. 050-249'
......;;~-...,.-'-"--=,.,,,...~__,-
UN IT NAME Dresden III 3B DATE March 3, 1981 COMPLETED BY D, C. Maxwe 11
. TELEPHONE (815) 942-2920 CAUSE & CORRECTIVE:
ACTION TO
.PREVENT RECURRENCE Recirc. M.G. Set spiked high caused APRM' s to spike high and resultant scrammed Rx.
4 Exhibit G-Instructio~s for Preparation of Data Entry Sheets for Licensee Event Report (
) File (NUREG-0161)
. l
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- i.
L
. EQUiPMENT NATURE OF MAIUTENANCE Spad~ Accu~ula-Preventive WR ://8584 tors 1*.
DRESDEN* UNIT SAFETY RELATED MAINTENANCE~ FEBRUARY, 1981 LER OR OUTAGE NUMBER CAUSE N/A MALFUNCTION*
\\
. ~
I* r RESULT CORRECTIVF~ACTION N/A
- Rebuilt 4.sp~res *.
NATURE OF HAIUTENANCE
.MSL Area Temp.
Corrective.WE. 1/11317
- Switches
\\. '
- MSL' *chai{fte 1
- A
- corrective WR 1195 38
- Temp.~ Switches 0CRD.E-:9 (18-3_*5)
Preventive *wR 1111104
- CRD 553C.
CRD.1099
.Refuel Grapple.
.Scram* Discharg
- Volume Hy'dro~
laze* Flanges
- Fuel Pool Inne
- * * -Gat:e. Gasket *
- .. B. R~circ. oi:..t-
. let. *safe End Preventive WR. #2759 Preventive WR./16260980 Preventive WR.#11041 Prevel,1tive WR IF'.11217 P*reveritive WR l/11087.
- Preventive WR IH1273
. Reftiel Grapple Corrective WR IH1190 D.iesel Genera-.
Corrective WR 1Hi304
. *. ior DRESDEN UN IT :2.
SAFETY RELATED HAiNTENAHCE -:-- FEBRUARY, 1981 LER*OR OUTAGE NUMBER MAL FUN CT I OH*
CAUSE RESULT CORRECTIVF7ACTION
. 180 *capillary
- Broken~ 16B In-ternal Corrosion Switches Failed Replaced ~witches.
26l.... l8A Bad
- N/A
. N/A
.: ***N/A
- N/A
- . N/A
- : N/A
- . * 'N/A Switch Failed N/A N/A N/A N/A.
N/A N/A N/A Checked & foung* okay -
reinst.alled.
Flushed to observe flow thru ball check v~lve to CRD e~haust port~
Rebuilt per procedure.
Rebuilt per procedure.
Replaced air hose for
- main mast.
Removed & replaced flanges.
Installed new gasket-l f
Ground off PT i11!iication i
off safe end.
wo Wires Shorted on ~utton of Up/
Down Switch Switch Inoperative Repaired short & replaced r Loose Screw On Diff." Lock-Out Relay at 4KV Bus up relay.
Prevented Shut-Tightened screw.
doWll Relay from Operating & D/G No-Start
DRESDEN* UNIT 2*
SAFETY RELATED HAiNTENANCE.,.: FEBRUARY, 1981
- ~
--r-------------------.,.-------------------r-.---~...... ---~-..:...-,----
- .]
- EQUIPMENT Latch Light on*
Refuel_" Grappl_e NATURE OF
- . _:tor.. *.*. *'
Refuel.*Platform
.**.* Main Winch Mo to Bus Tie.Break-
~r*s.*2a to* 29
- *.HPCI Mo-z...:2301-.
9
(
- Torus Vent
.., ya1v*e -1601-22.
Torus Vent.
- , valve 1601-21 Corrective WR //:11314 Preventive WR //11290 Cor.r*ect i ve WR //3088097 Preventive* WR /Hl328 Preventive WR f/1132J
- 12sv iatteries
- Preventive WR //9051
- . 24/48V.Bat.:..
tedes
- CCSW Vault
<*Drain
- .. ~.*.
Pr even d v.e WR //905 2 Preventive WR #10953
)
LER OR OUTAGE NUHBER Bad Bad MALFUNCTION*
CAUSE N/A N./A Brake Coil N/A Stem & Yoke N/A
.:N/A
. :N/A
- .N/A
.*N/A RESULT N/A N/A Smoking &
Inoperative N/A CORRECTIVr~ACTION Inst*lled new cable~
ested for trip -
- perated normally
- eplaced with coiJ
... 3 grapple.
umpered per procedure.
Valve.Won't Close eplaced stem, yoke, &
N/A N/A
.. N/A N/A N/A limi torque.
ir leakage work to be one ~/work req.#3746
- 1r leakage - work to be one.w/work req.#3745.
erformed battery dis~
barge test.
erf9rmed,battery di~
harge test.
epaired open lead at solenoid.
- ~.
.~ *,. '
.. *.~.
. NATURE OF
- HAlllTENAH_CE Preventive WR #11120 DRESDEN* UNIT 2/3 SAFETY RELATED HAiNTENANCE '"".FEBRUARY, 1981 MALFUNCTIOH*
LER OR OUTAGE NUMBER
- ~
- . CAUSE...
RESULT
.N/A.
N/A
~...
CORRECTIVr~ACTION C
isassembled, fospected, ebuilt per DMP 300-15.
- i f t l
I i*
'~:..
.. :'EQUIPMENT.
Accum. 18-43
. Contr61 *Rod
... **tiri~e.scram
- :* *Pifot: v'aiVes *
. Scram Re~et.
.switch' Af'WS Inst. &.
.Tt-ip Unit
. Calihration NATURE OF MAlllTENAHCE Preventive WR 1!11369 Preventive WR 1Hi288 Preventive WR 1!4722.
- Preventive WR 1!11522
- Pr.eventive WR 1HQ184 DRESDEN* UN IT 3 SAFETY RELATED HAiNTEt~ANCE :-- FEBRUARY, 1981 LER OR OlJTAGE MALFUNCTIOH* *
. NUMBER.
CAUSE RESULT N/A N/A N/A N/A N/A *
. N/A
- N/A N/A
- N/A N/A CORRECTIVF~ACTION Replaced K4 relay.
Replaced accumulator.
Rebuilt 177 accumulator scram pilot solenoid~~
Replaced switch.
f I
l t
l Calibrated per procedure.
1
SUMMARY
OF OPERATING EXPERIENCE UNIT ONE FEBRUARY, 1981 2-1 to 2-28 Unit One was shutdown for the entire month, awaiting license approval for the chemical cleaning.
Major work scheduled to be c~pleted following chemical cleaning is as follows:
HPCI install.ation for ECCS upgrading, equip-
.ment upgrade to IEEE 279, major in-service inspection, and refuel.
- }
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SUMMARY
OF OPERATING EXPERIENCE UNIT TWO FEBRUARY, 1981 2-1 to 2-28 Unit Two was shutdown for the entire
. *r-.***
month for its scheduled refueling and equipment overhaul outage.
Major work inciuded-torus modifications, CRD re-placement, and turbine overhaul. *
' ~.
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'.... ~ _..**
. *~
~:.
SUMMARY
OF OPERATING EXPERIENCE UNIT THREE 2-1 to 2-23 2-23 to 2-28 FEBRUARY, 1981 Unit Three enteredthe month operating.
at a power level of 825 MWe and operated continuously at approximately this level (except for weekend surveillances) until February 23, 1981.
At 0011 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> o~ the 23rd, the 3B Recirc. M.G. Set spiked high and caused the'APRM's.t? trip high, auto-matically scramming the reactor and unit.
The reactor was brought critical on the
.23rd at 0753 hours0.00872 days <br />0.209 hours <br />0.00125 weeks <br />2.865165e-4 months <br />, and the Unit was placed in service at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> and oper~
ated throughout the remainder of the month, reaching a power level of 810.MWe with a capacity factor.of 89.36% and an av.aila-bility of 98.24%.
'** *c,.:
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