ML17191A598

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Insp Repts 50-237/98-07 & 50-249/97-07 on 980212-0305. Violations Noted.Major Areas Inspected:M&Te Calibration Control Program & Issues Related to Dresden Station Response to Hypothetical Failure of Dresden Dam
ML17191A598
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 04/14/1998
From: Jeffrey Jacobson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17191A594 List:
References
50-237-98-07, 50-237-98-7, 50-249-97-07, 50-249-97-7, NUDOCS 9804170103
Download: ML17191A598 (12)


See also: IR 05000237/1998007

Text

U.S. NUCLEAR REGULATORY COMMISSION

Docket Nos:.

License Nos:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspector:

Approved by:

9804170103 980414

PDR

ADOCK 05000237

G

PDR

REGION Ill

50-237; 50-249

DPR-19; DPR-25

50-237/98007(DRS}, 50-249/98007(DRS)

Commonwealth Edison Company

Dresden Generating Station, Units 2 and 3

6500 North Dresden Road

Morris, IL 60450-9765

February 12 through March 5, 1998

Gerard F. O'Dwyer, Reactor Inspector

John Jacobson, Chief

Lead Engineering Branch

Division of Reactor Safety

EXECUTIVE SUMMARY

Dresden Generating Station, Units 2 and 3

NRC Inspection Report 50-237/98007(DRS); 50-249/98007(DRS)

An announced regional initiative inspection that reviewed portions of the M& TE calibration

control program and issues related to Dresden Station's response to a hypothetical failure of

the Dresden Dam.

Overall the inspection concluded that the M& TE calibration control program was

effective. M& TE storage controls were adequate and plant temperature instrumentation

was properly calibrated. One violation of NRC requirements was identified.

(Section M 1.1, VIO 50-2371249-98007-01 (DRS))

Various scenarios were identified concerning dam failure both with and without a LOCA,

as described in the UFSAR, which the station may not be able to accommodate.

(Section E3)

2

M1.1

a.

Report Details

II. Maintenance

Measuring and Test Equipment (M&TEl Control Program

Inspection Scope (IP 61725)

The inspector reviewed portions of the M& TE control program, M& TE calibration

re90rds, Technical SpeCifications and M&TE vendor information.

b.

Observations and Findings

The inspector reviewed selected Problem Identification Fc;>rm (PIF) packages related to

the M&TE program.initiated during 1997 and 1998 and found the PIFs appropriately

initiated and dispositioned.

Temperature-initiated safety-related automatic actions were actuated by temperature

switches that were calibrated appropriately to the necessary accuracy to meet the

TS requirements. The control room operators indicated that safety-related manual

. actions (e.g., Emergency Operating Procedure actions) were taken based on the

outputs of annunciators and computer alarms which were also calibrated with

appropriate accuracy.

The M& TE storage controls were found to be adequate. The storage requirements for

the M&TE were very broad, e.g., the vendor-recommended storage range for a Gordon

model 5060 meter was from -40°F to 140°F with no restriction on humidity. The

temperature in the M&TE storage areas was controlled between 60 and 90°F by normal

ventilation.

Calibration lab personnel were required to be trained on the procedures that were used

to calibrate the M& TE. The training records indicated that the calibration lab personnel

had the appropriate training.

Technical Specification 6.8.A.1 required the implementation of certain Regulatory

Guides and American National Standards Institute (ANSI) standards including ANSI

N45.2.9-1974, "Requirements for Collection, Storage, and Maintenance of Quality

Assurance Records for Nuclear Power Plants." Appendix A of ANSI N45.2.9-1974

required that M& TE calibration records be retained as quality records for five years.

However, the licensee identified that prior to December 22, 1997, the Master Records

Retention Schedule of General Procedure GP 136, dated September 15, 1995,

"Retention of Company Records," failed to designate M& TE calibration records as

quality assurance (QA) records and the procedure allowed the calibration records to be

disposed after three years. This was a severity level IV violation of TS 6.8.A.1

(VIO 50-237/249-98007-01 (DRS)); however, safety consequences were minimal

because the licensee had not needed to retrieve any calibration records older than three

years. Also, all M&TE was calibrated at least once a year, creating a more recent

3

calibration record so the potential to need an older record was reduced each year. On

January 19, 1998, the Dresden Central File Supervisor approved a change to the

Master Record Retention Schedule to require the M& TE calibration records to be

retained as QA records for at least five years. The M& TE supervisor informed the

inspector that: 1) the Master Schedule was for all Com Ed sites and changes sometimes

required an extensive time to be implemented, therefore the Dresden Nuclear Power

Station Record Retention Schedule had been created; 2) the change still had to be

approved and implemented on the Master Schedule by ComEd corporate personnel;

and 3) while the Master schedule was being corrected, the Dresden schedule had

already been changed to meet the requirements. When responding to the violation, the

licensee should specify when the change to the Master schedule will be implemented.

c.

Conclusions

The M& TE calibra,ion control program was effective in maintaining plant temperature

instrumentation properly calibrated. PIFs related to M& TE were properly dispositioned.

Failure to designate and maintain M&TE calibration records as QA records for five years

was a severity level IV violation of TS 6.8.A.1. (VI~ 50-237/249-98007-01 (DRS))

Ill. Engineering

E3.1

Updated Final Safety Analysis Report (UFSAR) Section 9.2.5.3.2 Review

a.

Inspection Scope OP 37550)

The inspector reviewed section 9.2.5.3.2, "Dam Failure Coincident with a LOCA," of the

UFSAR, Revision 2, docketed letter dated October 16, 1968, from the Atomic Energy

Commission (AEC) staff to Dresden staff amendments 9 and 1 O to the applications for

the operating licenses for Unit 2 & 3, and docketed letter dated March 13, 1998, from

the site vice president to the NRC.

b.

Observations and Findings

The im:;pector noted that Section 9.2.5.3.2 stated that the Dresden Station could be

safely shutdown if there was a catastrophic failure of the Dresden dam coincident with a

design basis loss of coolant accident (LOCA ) in either Unit 2 or Unit 3, without using

. any seismic Class II systems and with a loss of offsite electrical power (LOOP). The.

inspector determined that it could not be demonstrated that Section 9.2.5.3.2 could be

met without using Class II systems for isolation condenser make up and the cognizant

senior design engineer agreed. The inspector also determined that even if the Class II

systems were assumed to be operational, the Containment Cooling Service Water

(CCSW) system would not maintain the required 30 pounds per square inch differential

(psid) greater than the low pressure coolant injection (LPCI) system and Part 100 limits

may be exceeded. The Site Engineering Manager and the licensee's NRC Coordinator

informed the inspector that the Com Ed position was that this capability was not required

by the license or the design basis. However, the inspector noted that by docketed letter,

4

c.

dated October 16, 1968, the Atomic Energy Commission (AEC) staff had requested the

Dresden staff to provide an evaluation to complete the application for the operating

licenses for Units 2 & 3. The AEC required the evaluation to describe the effect of an

earthquake which disabled the dam, all Class II systems, offsite power and caused a

design.basis LOCA in one of the two units. By docketed letter, dated February 28,

1969, Dresden answered, in amendments 9 and 10, to the applications for the operating

licenses for Unit 2 & 3 that the station can safely shutdown after all those coincident.

events. Dresden also placed the. evaluation in the FSAR. By docketed letter, dated

March 31, 1998, the Dresden site vice president stated that a dam failure coincident with

a LOCA was beyond the design basis of the Dresden Station and that clarifications to

the UFSAR would be made through the 10 CFR 50.59 provisions.

Conclusions

It was. not demonstrated that the station could shutdown per the UFSAR statements in

Section 9.2.5.3.2 post dam failure coincident with a LOCA. This will be reviewed as part

of a previously opened unresolved item. (URI 50-237/249-97021-01A (DRS))

E3.2

Review of UFSAR section 9.2.5.3.1. "Dam Failure During N.ormal Plant Operation"

a.

Inspection Scope

The inspector reviewed UFSAR section 9.2.5.3.1, "Dam Failure During Normal Plant

Operation."

b.

Observations and Findings

The inspector noted that section 9.2.5.3.1 stated that the Dresden station could be

safely shutdown after a dam failure with no LOCA, without using Seismic Class II

systems and with a LOOP. The section discussed only methods of shutdown which

relied on Class II systems that required special lineups to be powered from the

Emergency Diesel Generators. The inspector noted that similar statements were in the

AEC-requested evaluation discussed in section E3.1. The inspector determined that the

Dresden station could not be safely shutdown by only Class I systems under the stated

conditions because all Isolation Condenser Makeup methods used Class II systems and

the containment cooling service water (CCSW) system would not function without

Class II systems. The. licensee stated that this requirement was not part of the design

basis of the Dresden Station and that UFSAR clarifications will be made as discussed in

paragraph E3.1.

Even if the Class II systems were assumed to operate, the Dresden station might still

not be able to shutdown safely after a catastrophic dam failure that lowered the intake

canal water level to the postulated 495' MSL. The inspector was eoncemed that the

Unit 2 & 3 reactor vessels (RV) might not be adequately cooled. Section 9.2.5.3.1

stated that the isolation condensers (IC) would be used to cool the .RVs. All Isolation

Condenser makeup methods used Class II systems; however, the licensee assumed

one would still function. The AEC-requested evaluation stated that there would be nine

5

million gallons available for IC makeup in the Ultimate Heat Sink (UHS) because the

discharge canal level would fall to 498' MSL after a dam failure. The inspector identified

that the discharge canal level would fall to 495' MSL which would result in six million

gallons available in the UHS. Such a significant underestimation of UHS capacity might

invalidate the ability of the Unit 2 & 3 ICs to cool the RV. The licensee stated that this

UFSAR statement will be corrected by a 50.59 UFSAR change.

The UFSAR discussed using the Service Water Pumps (SWPs) if the intake level

dropped to 495 feet MSL after a dam failure. The inspector was concerned because the

Hydraulic Institute Standards, ANSI/HI~ 1994 Edition, Figure 1.66 contained the general

recommendation of a minimum of five feet submergence to prevent excessive vortexing

of a pump with 15,000 gpm rated capacity such as each SW pump. If intake level

dropped to 495 feet, the SWPs would only have 1 foot 2.5 inch submergence. This

might allow enough air-entraining vortexing for the SWPs to lose their prime and to not

function. The licensee was generating calculations to demonstr~te that the Dresden

SWPs will operate adequately with intake at the postulated 495 feet level. If the SWPs

do not function at full capacity, the SWPs might not be able to be used to cool the

reactor building closed cooling water (RBCW) and achieve cold shutdown via the

shutdown cooling heat exchangers as stated in the UFSAR. Also, the inspector

identified that since the SWPs indirectly cooled the reactor recirculation pump (RRP)

seals, the seals may eventually fail if the SWPs are at less than full capacity. *

Additionally, loss of CCSW, as discussed in S~ction E3.3, may impact long term cooling.

of the plant.

c.

Conclusions

It was not demonstrated that Dresden station could be safely shutdown during normal

operation following a dam failure as described in Section 9.2.5.3.1 of the UFSAR, using

seismic Class I systems only. The licensee does not believe that this requirement is

part of the design basis and intends to clarify the UFSAR. However, assuming no

damage to Class II systems, the UHS inventory is less than that assumed in the

evaluation and SWP performance at the 495' MSL has not been evaluated. These

concerns will be reviewed as part of a previously opened unresolved item.

(URI 50-237/249-97021-01 B(DRS))

.

E3.3

Procedural Problems

a.

Inspection scope <IP 37550. 92903)

The inspector reviewed the CCSW suction piping drawings and Procedure

DOA 0010-01, Rev. 7, "Dresden Lock and Dam Failure."

b.

Observations and Findings

The UFSAR stated that a CCSW pump would be put in-service after a LOCA coincident

with a dam failure that lowered the intake water level to 495 feet MSL. The bottom of

6

the CCSW suction line was at 498 feet MSL, so the suction piping would drain and

  • approximately 200 feet of horizontal piping for each pump would fill with air. The

UFSAR stated that the CCSW intake bay would be sealed and the water level raised so

that the CCSW intakes would be covered and the CCSW pumps 6ould provide water for

containment cooling. However, the inspector identified that there were no high-point

vent valves to vent the air that would be trapped inside the piping when water level was

restored. With the water level restored, the trapped air volume would prevent CCSW

pump operatiqn. Previous to December 1997, Procedure DOA 0010-01, Revision 7,

"Dresden Lock and Dam Failure," did not have provisions for venting the trapped air.

The licensee revised Procedure DOA 0010-01 to cut holes in the top of the CCSW

suction piping in the CCSW bay to vent the air. Since the holes would be at 500' MSL,

the inspector was concerned that the CCSW bay water level might not be able to be.

restored high enough to prevent excessive air-entraining vortexing through the holes

which may prevent the CCSW pumps from pumping adequate water.

The UFSAR stated that the CCSW intake bay would be sealed by installing stoplogs

across the two openings to the bay. The licensee did not quantify the maximum leakage

expected. The inspector was concerned that the stoplogs would leak excessively,

further reducing the CCSW capacity. Evaluatior) of CCSW pump performance with vent

holes cut in the suction piping and the stoplogs in place is considered an unresolved

item. (URI 50-237/249-98007-02(DRS))

c.

Conclusions

Prior to December 1997, Procedure DOA 0010-01 would not have supported CCSW

pump operation after a dam failure as stated in the UFSAR. Furthermore, adequate

pump performance with suction piping vents and intake bay stoplogs has not been

demonstrated.

E3.4

Other UFSAR Discrepancies

a.

Inspection scope OP 37550. 92903)

The inspector reviewed UFSAR section 9.2.5.3.1, "Dam Failure During Normal

Operations," PIF D1998-00455, "Suction of Unit 2 & 3 Diesel-Driven Fire Pump

Uncovered Following Dam Failure," and interviewed the Diesel Fire Pump (DFP)

System Engineer.

b.

Observations and Findings

The UFSAR stated that the DFP's suction was at 492', the DFP took suction from the

CCSW bay and the DFP would operate after a dam failure lowered CCSW bay level to

  • 495' MSL. However; the inspector identified that-the suction could not be at 492'

because the CCSW bay floor elevation was at 493' 8" MSL. PIF D1998-00455 was

initiated which stated that the vendor-recommended minimum intake water level was

498' 10." Engineering personnel stated that the CCSW bay level.would not be restored

7

c.

until two hours after a dam failure. The inspector was concerned because even if bay

level was restored, the DFP would be competing with the CCSW pumps for water if the

DFP was needed. The docketed letter dated March 31, 1998, from the site vice

president stated that the license did not require the DFP to function after a dam failure.

The licensee stated the DFP suction level specified in the UFSAR will be corrected by

the UFSAR 50.59 change process. The NRC will review the safety evaluation for this

change. (IFI 50-237/249-98007-03(DRS))

Conclusions

The DFP intake water level post dam failure may not be adequate to support DFP

operation. The acceptability of a two hour delay and reduced performance for the DFP

after a dam failure will be reviewed when the 50.59 evaluation is made available.

E3.5

Canal Pikes

a.

Inspection Scope (IP 37550)

The inspector performed a walkdown of some of the canals and reviewed portions of the

safety evaluation of Hydrology SEP topics 11.3.C, SafetY Related Water Supply (Ultimate

Heat Sink) contained in docketed letter dated June 21, 1982.

b.

Observations and Findings

A dike is located at the south side of the hot canal to the Dresden lake near the

intersection of Collins and Dresden roads. All the canal dikes were seismic Class II and

assumed to fail after an earthquake strong enough to destroy the dam. It appeared that

the failure of this dike might lower intake level to below 495' MSL. This failure did not

appear to have been analyzed in the safety evaluation of Hydrology SEP topics 11.3.C,

Safety Related Water Supply (Ultimate Heat Sink). Review of the potential for dike

failure to lower the intake level below the assumed 495' MSL is considered an

unresolved item. (URI 50-237/249-98007-04(DRS))

c.

Conclusions

The inspector identified a potential for dike failure to lower the intake bay below the

495' MSL. Evaluation of this potential could not be located during the inspection .

8

t

V. Management Meetings

X1

Exit Meeting Summary

The inspector presented the final inspection results to members of licensee management at the

conclusion of the inspection on March 5, 1998. During the meeting, the inspector questioned

licensee personnel as to the potential for proprietary information being included or retained in

the inspection report material as discussed at the exits. No proprietary information was

identified as included or retained.

9

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

G. Abrell, NRC Coordinator, Regulatory Assurance

R. Book, CAP Staff, Quality & Safety Assessment .

A. Casillo, Mechanical Lead (M1), Design Engineering

P. Channel, Control Rod Drive System Engineer, Systems Engineering

M. Crowley, Circulating Water System Engineer, Systems Engineering

G. Feige, M& TE Supervisor

J. Fox, Senior Design Engineer, Design Engineering

R. Freeman, Site Engineering Manager, Dresden

W. Halcott, Auxiliary System Lead, Systems Engineering

J. Kish, CCSW System Engineer, Systems Engineering

K. Peterman, Supervisor, Configuration & Administration Management; DEAG Member

P. Planing, Superintendent, Systems Engineering

W. Poppe, Reactor Recirculation System Engineer; Systems Engineering

B. Shete, Mechanical Engineer, Design Engineering

F. Spangenb.erg, Regulatory Assurance Manager, Dresden

L. Weir, Superintendent, Design Engineering

LIST OF INSPECTION PROCEDURES USED

IP 37550:

Engineering

IP 61725 *

IP 92903

Surveillance Testing and Calibration Control Program

Follow up - Engineering

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-2371249-98007-01 (DRS)

50-237 /249-98007-02(DRS)

50-237 /249-98007-03(DRS)

50-237 /249-98007-04(DRS)

Discussed

50-237/249-97021-01 (DRS)

VIO

Improper M&TE record retention requirements

URI

CCSW Pump Operability, post dam failure

IFI

50.59 to evaluate DFP use during dam failure

URI

Evaluate effect of dike failure on intake bay level

URI

UFSAR Dam Failure Discrepancies

10

ATTN

ANSI

BWR

ccsw

CFR

Com Ed

DAP

DES

DFP

DRP

DRS

E&TS

GL

JSPLTR

LOCA

LOOP

LPCI

LPM

MSL

NEP

NRC

NRR

NTS

PDR

PIF

psid

Q&SA

RBCCW

RG

SEP

SER

SRI

SW

TS.

UFSAR

URI

USQ

VIO

LIST OF ACRONYMS

Attention

American National Standards Institute

Boiling Water Reactor

Containment Cooling Service Water

Code of Federal Regulations

Commonwealth Edison

Dresden Administrative Procedure

Dresden Engineering Surveillance

Diesel Fire Pump

Division of Reactor Projects

Division of Reactor Safety

Engineering and Technical Support

Generic Letter

ComEd (J.S. Perry) Letter

Loss of Coolant Accident

Loss of Offsite Electrical Power

Low Pressure Coolant Injection

Licensing Project Manager .

Mean Sea Level

Nuclear Engineering Procedure

Nuclear Regulatory Commission

Office* of Nuclear Reactor Regulation

Nuclear Tracking System

Public Document Room

Problem Identification Form

pounds per square inch differential

Quality and Safety Assessment

Reactor Building Closed Cooling Water

Regulatory Guide

Systematic Evaluation Program

Safety Evaluation Report

Senior Resident Inspector

Service Water

Technical Specification

Updated Final Safety Analysis Report

Unresolved Item

Unreviewed Safety Question

Violation

11

DOCUMENT

NUMBER

PIF # D1997-08290

PIF # 227A-12-1997-012788

PARTIAL LIST OF DOCUMENTS REVIEWED

REVISION OR

DOCUMENT DESCRIPTION

DATE ISSUED

NRC Concerns About CCSW System

November 25, 1997

Performance After a Dam Failure Coincident With

a LOCA

UFSAR Implied One CCSW Pump Operation

February 25, 1997

After a Dam Failure Coincident With a LOCA

12