ML17187B216
| ML17187B216 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 12/05/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML17187B214 | List: |
| References | |
| 50-249-97-27, NUDOCS 9712160289 | |
| Download: ML17187B216 (5) | |
See also: IR 05000249/1997027
Text
U.S. NUCLEAR REGULATORY COMMISSION
Docket No.:
License No.:
Report No.:
Licensee:
Facility:
Location:
Dates:
Inspector:
Approved by:
9712160289 971205
ADOCK 05000249
Q *
REGION Ill
50-249
50-249/97027 (DRS)
Commonwealth Edison Company
Dresden Generating Station, Unit 3
6500 North Dresden Road
Morris, IL 60450
November 5 - 19, 1997
D. E. Jones, Reactor Inspector
J. A. Gavula, Chief
Engineering Specialists Branch 1
Division of Reactor Safety
EXECUTIVE SUMMARY
Dresden Nuclear Power Plant, Unit 3
NRC Inspection Report 50-249/97027(DRS)
This inspection included a review of the implementation of the inservice inspection program for
the Unit 3 refueling outage 14.
Maintenance:
In general, the licensee's inservice inspection program implementation met ASME,
Section XI requirements (Section M3).
A violation was cited for inability to retrieve the radiographic record of a Unit 3 pipe weld
(Section M3).
Report Details
II. Maintenance
M3
Maintenance Procedures and Documentation
M3.1
lnservice Inspection <ISi) Examination Documentation
a.
Inspection Scope (73753. 73755)
The inspector reviewed inservice examination reports and ISi personnel certifications for
examinations recorded in "Dresdefl Station D3R14 Refueling Outage lnservice
Inspection Summary Report." The examination reports reviewed included the following:
Liquid penetrant examination
Report # 0064
Report # 0067
Report # 0070
Ultrasonic examination
Report # 0057
Report # 0060
Report# 0061
Magnetic particle examination
Report # 0009
Report # 0007
Report # 0010
Radiographic examination
Report # Conam 2200
Report# Conam 2214
Report# Conam 2221
b.
Observations and Findings
Personnel certification records met ASME Code requirements for the selected
examinations completed in refueling outage D3R14. The examination records were
complete with the appropriate calibration records and required examination data. For
the selected examinations reviewed from the summary reports, the inspector identified
no deviations from ASME Code requirements, e~pt as discussed below.
The inspector identified that the radiographic film of the examination of Unit 3 high
pressure coolant injection turbine drain pot return line extension pipe replacement weld
(work request 950065745, minor plant change E12-3-95-246), could not be retrieved by
the licensee. The licensee subsequently issued problem identification form 01997-
08032 to address this issue. The licensee's inability retrieve the radiographic record of
the Unit 3 HPCI pipe weld {FW-3) is considered a violation of 10 CFR 50, Appendix B,
Criterion XVII, "Quality Assurance Records," {VIO 50-249/97027-01{DRS)).
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c.
Conclusions
The inspectors determined that ASME Code requirements had been met for select
examinations completed in the refueling outage D3R14. However, the inspector
identified that the radiographic record of the Unit 3 pipe weld could not be retrieved.
M7
Quality Assurance in Maintenance Activities
M7.1
ISi Program Implementation
a.
Inspection Scope (73051)
The inspector reviewed the licensee's ISi program plan, "Dresdan Station 3rd Interval
lnservice Inspection Plan," effective March 1, 1992 through and including February 28,
2002.
b.
Observations and Findings
The plan represented the third ten-year interval of the ISi program for Dresden Station
Units 2 and 3. The licensee had procured the services of an Authorized Nuclear
lnservice Inspector (ANll) from Hartford Steam Boiler Inspection and Insurance Co. of
Hartford, Connecticut. The ANll reviewed procedures, personnel qualifications,
instrument and material certifications, and examination results. Examinations were
- performed in accordance with the Unit 3 Technical Specifications, the ASME Code,
Section XI, 1989 Edition, and Generic Letter 88-01. The inspector's review indicated
that the ISi program was acceptable.
c.
Conclusions
The licensee's ISi program implementation met ASME Code Section XI, 1989 Edition
requirements.
V. Management Meetings
X1
Exit Meeting Summary
The inspector presented the inspection results to a member of licensee management at
the conclusion of the inspection on November 19, 1997. The licensee acknowledged
the findings presented and did not identify any of the potential report input discussed as
proprietary.
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PARTIAL LIST OF PERSONS CONTACTED.
Commonwealth Edison:
B. Casey, ISi Coordinator
G. Abrell, NRC Coordinator
US NRC:*
K. Riemer, Senior Resident Inspector
B. Dickson, Resident Inspector
Opened
INSPECTION PROCEDURES USED
INSERVICE INSPECTION
INSERVICE INSPECTION-REVIEW OF PROGRAM
INSERVICE INSPECTION-REVIEW OF DATA
ITEMS OPENED, CLOSED or DISCUSSED
VIO 50-249/97027-01
Inability to retrieve the radiographic record of a Unit 3 HPCI pipe
weld.
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