ML17174A998

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Safety Insp Repts 50-237/91-32 & 50-249/91-35 on 911028-1112.Violation Noted.Major Areas Inspected:Review of Events Surrounding Failure of CP Valve 3-1601-24 & General Review of Leak Rate Test
ML17174A998
Person / Time
Site: Dresden  
Issue date: 11/27/1991
From: Lougheed V, Nejfelt G, Phillips M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17174A997 List:
References
50-237-91-32, 50-249-91-35, NUDOCS 9112030126
Download: ML17174A998 (11)


See also: IR 05000237/1991032

Text

U.S. NuCLEAR REGULATORY COMMISSION

REGION III

Reports No.

50-237/91032 (DRS); 50.-249/91035 (DRS)

Docket Nos. 50-237; 50-249

Licenses No. DPR-19; DPR-25

EA-91-164

Licensee: Commonwealth Edison Company

Opus West III

1400 Opus Place

. Downers Grove, IL

60515

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Inspection At:

Dresden Site, Morris, IL

Inspection Co~ducted: October 28 through November 12, 1991

Inspectors:

v. P. Lough9,ed

Approved By:

Inspection Summary

Section

Date '

.

11/2.t..:/91

Oat~

7

Date

Inspection on October 28 through November 12. 1991

(Reports No. 50-237/91032(DRS); 50-249/91035(DRS))

_

Areas Inspected:

This.was a special announced safety inspection

by regional based inspectors to review the events surrounding the

failure of containment purge valve 3-1601-24.

A general review

of the local leak rate test program was also performed.

Inspection module 61720 was used during this inspection.

Results:

The inspection resulted in one apparent violation

against Technical Specification 3.7.D which requires that

containment isolation valves be operable during periods of power

operation..

Du~ing the last operating cycle, valve 3~1601-24 was

inoperable because, when the valve operator was fully closed, the

valve disk was partially open.

This apparent violation is

9112030126 911127

PDR

ADOCK 05000237

G

PDR

described in section 3 of the report.

The report also discusses

an unresolved item relating to an apparent 50.59 violation where

a required Technical Specification update had not been made

(paragraph 4.A).

A licensee strength was identified in the

conduct and attitudes of the test personnel, which ~esulted in

improvements in the overall test program.

2

REPORT DETAILS

1.

Persons Contacted

Commonwealth Edison

L. Gerner, Technical Superintendent

J. Kotowski, Production Superintendent

J. Gates, Assistant Technical Staff Supervisor

K. Peterman, Regulatory Assurance Supervisor

M. Andjelic, Local Leak Rate Test Coordinator

D. Booth, Master Electrician

B. Col.ebank, Post-Maintenance Testing Coordinator

R. Geier, Master Maintenance Mechanic

J. Harrington, Nuclear Quality Programs Maintenance

Group Leader

M. Horbaczewski, Inservice Testing Group Leader

M. Korchynsky, Unit 3 Operating Engineer

D. Legler, Site Engineer *

D. Lowenstein, Regulatory Assurance Analyst

R. Stachniak, Performance Improvement Supervisor

D.

VeriPelt~*Assistant Maintenance Supervisor

G. Whitman, Inservice Inspection Coordinator*

K. Yates, Onsite Nuclear Safety Administrator

U.S. NRC

W. Rogers, Senior Resident Inspector

D. Liao, Reactor Engineer

All of the above 'were present at the exit held November 12,

1991, with the exception of Mr. Horbaczewski.

The inspectors also interviewed other licensee employees

during the course of the inspection.

2.

Licensee Action on Previous Inspection Findings

A.

B.

(Closed) Unresolved Item 237/90017-05 "Components not

in LLRT [Local Leak Rate TestJ Program":

This item was

addressed ih Inspection Reports No. 50-237/90006(DRS);

No. 50-249/90005(DRS) and a non-cited violation was

issued.

Based on the evaluation and resolution

contained in that report, this item is considered

closed.

(Closed) Unresolved Item 237/90027-09 "Adequacy of

Post-Maintenance.Testing in Regard to Failure of Torus

Purge Valve During an ILRT [Integrated Leak Rate

TestJ":

This unresolved item was resolved through

3

I

issuance of a violation.

See following _item for

closure.

c.

(Closed) Violation 237 /91006-01 "Inadeauate Post-

Maintenance Testing Resulting in Lack of Containment

Integrity for an Entire Cycle":

This violation, along

with a proposed civil penalty, was issued in

April 1991.

The licensee acknowledged the validity of

the violation and paid the civil penalty.

Their

response to the violation was acceptable~ Therefore,

this item is considered closed.

D.

(Closed) Systematic Evaluation Program Topics VI-4;

VI-6 "Installation of Proper Leak Rate Test Taps on the

Reactor Building Closed Cooling Water-System":

The

inspectors reviewed theinethodology Used by the

licensee to perform local leak rate testing of both the

supply and return on the reactor building closed

cooling water system.

The inspectors were satisfied

that the licensee was testing these penetrations in

accordance with the requirements of Appendix J.

This

item is considered closed.

E.

(Open) Systematic Evaluation* Program Topic VI-4.

"Leakage Conditions Under Which the Remote Manual

Isolation Valves on LPCI [Low Pressure Core Injection]

and Core Spray Systems Should be Isolated Are

Incorporated Into the Emergency Procedures":

At the

time of the inspection,** these conditions were not

covered in any emergency procedures, to the best of the

licensee's knowledge.

The licensee was unable to discern who had immediate

responsibility for closure of this item.

Therefore,

this item will remain open.

3.

Review of Events Surrounding the Failure of Unit 3

Containment Purge Valve 3-1601-24

A.

Sequence of Events

On December 25, 1989, a local leak rate test was

performed on penetration X-125, the Drywell/Torus Vent,

with successful results (8.49 standard cubic feet per

hour (scfh)).

This penetration was comprised of inside

containment valves 3-1601-23 and 3-1601-62, and outside

~alves 3-1601-24, 3-1601-60, 3-1601-61, and 3-1~01-63.

On January 27, 1990, a work request was generated to

repair the operator on valve 3-1601-24, an 18-inch*

butterfly valve, due to failure of Dresden Technical

Surveillance (DTS) 1600-27 "Fail-Safe Air Test~" The

4

maintenance performed involved replacement of the valve

operator piston rod.

A post-maintenance local leak

rate test was neither specified nor performed.

Maintenance was completed on February 3, 1990.

The following day (February 4, 199-0) an integrated leak

rate test was performed.

The* integrated test was

acceptable in the as-left condition, with a final

leakage rate of 1.02 wt%/day as compared to the

allowable of 1.2 wt%/day).

Unit 3 was returned to power on February 11, 1990.

At

this time known leakage from all local leakage source~

was 485.43 scfh.

Technical specification allowable

leakage was 488.452 scfh.

Approximately 19 months later, on September 9,* 1991,

Unit 3 shut down for .its next refueling outage.

A

local leak rate test was performed on penetration X-125

on September 16, 1991.

The* penetration could not be

pressurized.

On September 20, 1991 the licensee

identified that the leakage was through outboard

isolation valve 3-1601-24.

Investigation, by the

licensee, into the cause of the failure

determined

that, as part of the maintenance performed during the

previous cycle~ a new piston rod had been iristalled.

This piston rod increased the valye actuator stroke by

approximately one-eighth of an inch which resulted in

the valve disk rotating past the fully closed position

to where it was partially reopened.

The valve position

had been incorrect over the entire previous operating

cycle.

After making this determination, the licensee

immediately notified the NRC under the requirements of

10 CFR 50. 72 (b) (2) (iii).

B..

Regulatory Requirements

Drywell purge valve 3-1601-24, a containment isolation

valve, is addressed in Technical Specification

Table 3.7.1.

Technical Specification Limiting

Condition for Operation 3.7.D required that, during

power operation, all isolation valves listed in

Table 3.7.1 were to be operable.

If a containment

isolation valve was not operable, then the unit was

either to be shutdown, or the redundant isolation

valves in the line were to be isolated, with their

positions recorded daily.

Valve 3-1601-24 could not be

considered operable during the previous reactor power

operating cycle, because with the operator in the fully

closed position, the valve disk was partially open.

Because the licensee did not recognize that the valve*

was inoperable, the limiting conditions for operation,

5

c.

specified in Technical Specification 3.7.D,*were not

met.

This is an apparent violation of Technical

Specification 3. 7. D (249/91035-01 (DRS)) .*

Ro.ot Cause

The root cause was characterized by the licensee, ;in

Licensee Event Report (LER) 50-249/91-009, Revision o,

a?"*** inadequate controls were provided with the work

package ..** "

The inspectors concluded that the use of

informal communication methods, due to inadequate

procedures, contributed to the inadequate post-

maintenance testing.

A local leak rate test was not specified as a required

post-maintenance test*. following the val v.e operator

maintenance.

The maintenance workers did not convey*

back to the work analyst that they had installed a new

piston rod, nor did the work analyst inform the

technical staff of.the known scope of the repair.

The

technical staff considered a local leak rate test

following maintenance unnecessary, if the work

performed was on only the valve operator, and not on

the valve seating surface.

As this was their

understanding of the maintenance being performed on

valve 3-1601-24, they did not require a local leak rate

test.

The licen~ee identified, in their licensee event

report, two other Unit 2 valves which had not had local

leak rate test performed following operator

maintenance.

These were the reactor head cooling check

valve, 2-2.05-27, and a torus/drywell purge outboard

isolation valve, 2-1601-63.

The inspectors concluded

that a common cause, contributing to the failure to

perform post-maintenance local leak rate tests on these

valves, was that these were unanticipated maintenance

activities which came up during the last two weeks of

the outage.

The group responsible for performing local

leak rate tests did not have the opportunity to

determine the scope of the. maintenance and to identify

to the work analysts that local leak rate tests were

required, due to the informal methods of communication

being used.

During the past two and a half years,. the Quality

Assurance organization (QA), in their audits and

surveillances, neither considered whether appropriate

post-maintenance tests were specified nor if the work

analyst had suff i.cient information to determine what

the appropriate post-maintenance tests should have

been.

Rather, QA only verified that the testing that

6

D.,

was specified was that which was performed.

Consequently, QA did not provide a comprehensive

oversight of the post-maintenance testing program.

  • corrective Actions

As part of their response to the event, the licensee

immediately initiated a comprehensive audit to ensure

that all containment isol_ation valves on the operating

Unit 2 had local leak rate tests administered following .

maintenance.

Additionally, those corrective actions

being implemented due to the failure of the inner

flange on Unit 2 torus purge valve, such as the .

. .

development and distribution of color coded drawings

showing the containment boundaries and isolation

valves, were reviewed and expanded.

Finally the lead

engineer for the local leak rate test program was

designated to review, on a. daily basis, all work

requests being performed.

However, the inspectors

identified that all of these corrective actions were

being done informally rather than through formal .

procedures.

For example, the initiative to perform the

daily reviews, discussed above, was specified by a

maintenance memorandum.

In the long term, the licensee committed to implement

further corrective actions, including:* (1) performanqe

of a comprehensive review on Unit 3 to ensure no local

leak rate tests -were omitted during the current outage

prior to Unit 3 startup; (2) development of a matrix

identifying all components having local leak rate. test,

inservice test, or other mandatory post-maintenance

testing requirements; (3) training, both initial and

requalification, of staff and operators concerning

local leak rate testing requirements; (4) formalization

of post-maintenance testing requirements into a

procedure; *and (5) evaluation of approaches used by

other Commonwealth Edison nuclear stations to ensure

that appropriate post-maintenance testing requirements

are included in work packages.

  • The inspectors had no concerns with the proposed

long-term corrective actions.

4.

Review of Local Leak Rate Test Program

A.

Procedural Review

The licensee controlled the local leak rate test

program through Dresden Administrative Procedure (DAP)

14-05, "Leak Rate Testing Program", Revision 5.

Local

leak rate testing of individual Type B and C components

.J

7

was done in accordance with the following Dresden

Technical Surveillances:

1).

(DTS) 1600-1, Revision 14 (primary containment

valves);

2)

DTS 1600-2, Revision 6 (Bellows); DTS 1600-4,

Revision 9 (Electrical Penetrations);

3)

DTS 1600-14, Revision 9 (Personnel Access Lock);

4)

DTS 1600-15, Revision 8 (Double Gasketed Seals);

and

5)

DTS 0250-01, Revision 9, and DTS 0250--03,

Revision 3, (Main Steam Isolation Valves Dry and

Wet Tests)~

The inspectors reviewed these procedures against the

requirements of Appendix J, and the licensee's *

Technical Specifications.

The inspectors found that the procedures met all

Appendix J testing requ_irements, however, two concerns

were identified.

The first* involved the licensee's use

of long lengths of tubing to pressurize penetrations.

This was done to reduce the accumulated dose to the

staff performing the tests.

The inspectors discussed

with the licensee the potential.for a pressure drop

through the tubing, as well as the methodology used by

other sites to prevent this problem.

The licensee

committed to resolving this .concern.

The second

concern related to those tests performed against

reactor water head pressure.

The licensee committed to

  • review the procedures for performing tests against a

water head, to ensure that these tests would be

  • performed against the correct test pressure.

.

.

.

B.

Technical Specificat-ion/A'ppendix J Disagreement

The inspectprs identified that the licensee had changed

their airlock test methodology because of a 1982 NRR

Safety Evaluation Report which found that the

licensee's previous method of testing the airlocks did

not meet Appendix J requirements.

When the licensee

revised.the airlock test to be consistent with Appendix

J requirements, they failed to amend their Technical

Specifications. As of November 1991, the Technical

Specifications still. specified that the airlock be

tested at 10 psig with an acceptance criteria of

0.0375 La.

The licensee was performing airlock testing

at Pa, 48 psig, with an acceptance criteria of 0.05La.

8

c.

The licensee had prepared a Technical Specification

update; however, it had never

been submitted to the

Commission.

This concern is being tracked as an

Unresolved Item (237/91032-03(DRS); 249/91035-03(DRS)),

pending further review of the circumstances surrounding

the licensee's failure to amend the technical

specifications at the time of changing its testing

requirements.

Review of Testing Results

The inspectors reviewed the results of the as-found

local leak rate tests for the 1991 Unit 3 refueling.

The inspectors noted that, besides the X-125

penetration discussed above, the licensee had a number

of other penetrations which also could not be

pressurized.

One of these was the single valve pathway

on the high pressure coolant injection (HPCI) turbine

exhaust.

As a res.ult of this one valves' failure,

the

containment exceeded both the 0.6La maximum pathway

leakage requirement and the 0.75 minimum pathway

leakage requirement.

The licensee considered the large

number of failed valves to be unusual and not in

keeping with normal site practices.

D.

Bellows

Because of a problem identified concerning the *adequacy

of Type B testing of bellows seal penetrations at

Quad Cities, the licensee recognized that the local

leak rate test results on Dresden Unit 3 might be

non-conservative.

The licensee performed tests on all

the Unit 3 bellows with both air and helium.

Only one

penetration showed signs of excessive leakage (main

steam line A) and was replaced during the outage.

The

licensee planned to submit a temporary waiver of

compliance on the bellows to NRR prior to unit startup,

explaining their intended course of action.

Additionally, the licensee committed to perform an

integrated leak rate test every refueling outage, on

both units, until either the bellows had been replaced

with testable bellows, or such testing was no longer

necessary.

E.

Licensee Self-Initiated Study of Containment Isolation

Valves

The licensee initiated a study of all containment

isolation valves on.Dresden in the 1989-1990 time

period.

The licensee has committed to submitting the

results of this study as a revision to the Updated

Safety Analysis Report (USAR) *Table 5.2.2.5 (i.e., the

9

table would be updated to show which valves arid

penetrations required Type B or c testing).

Several

penetrations were added to the local leak rate testing

program as a result of the study.

However, the study

also identified some penetrations where all the

containment boundaries were not be"ing properly tested

(e.g., the inboard flanges on the drywell and torus

purge valves) ..

At the time of the inspection, the

licensee stated that the study was on hold, awaiting a

meeting to be held.between the licensee and NRR.

The

date for that meeting had not been set.

5.

Unresolved Items

Unresolved items were matters about which more information

is required in order to ascertain whether they are

acceptable items*, items of noncompliance, or deviations.

An

. unresolved item disclosed during the inspection is discussed

in paragraph 4.B.

6.

Exit Interview

The inspectors met with licensee representatives (denoted in

paragraph 1) throughout the inspection.

An exit meeting was

held prior to leaving the site on November 12, 1991.

During

the exit, the inspectors summarized the scope and apparent

findings of the inspection.

The inspectors also *discussed

the likely informational content of the inspection report

with regards to documents or processes reviewed by the

inspectors during the inspection.

The licensee did not

identify any such d_ocuments or processes as proprietary*.

10

Commonwealth Edison Company *

2

test was not performed following the maintenance.

The failure to

prescribe and perform a local leak rate test as part of the post-

maintenance testing was partially due to the use of informal

communication between the maintenance groups and the local leak

rat.e test group as to when these tests were required. *

Accordingly, no Notice of Vio.lation is presently being issued for

this inspection finding.

Please be advised that the number and

characterization of apparent violations described in the enclosed

inspection report may change as a result of further NRC review.

You will be advised by separate correspondence of the results of

our deliberations on this matter.

No response regarding the

apparent violation is required at this time.

We do request; however, that you respond within 60 days of the

date of this letter to the unresolved item identified in the

attached inspection report.

Your response should include the

date when you expect to submit the Technical Specification

amendment.

In accordance with 10 CFR 2.790 of the Commission's regulations,

a copy of this letter and the enclosures will be placed in the

NRC Public Document Room.*

The responses directed by this letter are not subject to the

_clearance procedures of the Office of Management and Budget as

  • required by the Paperwork Reduction Act of 1980, PL 96-511.

We will gladly discuss any questions you have concerning this

inspection.

Enclosure:

Inspection Reports

  • No. 50-237/91032(DRS);

No. 50-249/91035(DRS)

See Attached Distribution

Sincerely,

Hubert J. Miller, Director

Division of Reactor Safety

RIII

RIII

RIII

RIII

--~-----SEE PREVIOUS PAGE----------------------

Loughe~g

Nejfelt

Phillips Wright

11/ /13i\\ .

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