LER-1978-064, Forwards LER 78-064/03L-0 |
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e Commonwealth Edison ! !i Dresden Nuclear Power Station R.R. #1
. Morris, Illinois 60450 Telephone 815/942-2920
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December 21, 1978 BBS LTR #78-1637 James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 Reportable Occurrence Report 1178-064/031-0, Docket #050-237 is hereby submitted to your office in accordance with Dresden Nuclear Power Station Technical Specificaticn 6.6.B.2.(d), abnormal degradation of systems other than those specified in item B.l.e.designed to contain radioactive material resulting from the fission process *.
BBS/deb Enclosure cc: *Director of Inspection & Enforcement *
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Director of Management Information & Program Control File/NRG
- REGULATORY DOCKET FJLE COPY
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LICE~JSE-E EVErJI REPORT CONTROL BLOCK:
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
CON'T ITI:D.
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- ~~~~~ L1J©I ol sl ol ol ol 21 31 1101 11 11 2! 41 71s!G)l11 21 21 11 11 sl© 60 61 DOCKET NUMBER 68 69 EVENT DATE.
74 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
!During routine inspection in the 2/3 Radwaste basement, a leak was found in the
!Im 16" X 6" X 4" eductor on the 2/3 waste collector tank recirculation line (2/3-20150-4")4 [QJI] !Safety significance minimal since all leakage contained in Radwaste floor drain systemJ
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7 8 9 021 7
B SYSTE~1 CODE IM IA I@
9 10
CAUSE
CODE SU9COOE co.*.:PONENT CODE SUBCODE UJ@ LPJ@ 1p1r1 p 1E1x1x1e w 11 12 13 18 HJ SEQUENTIAL OCCUR REi'iCE REFORT V~.LV=
SUBCODE w@
- 20.
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LER*RO c~VEMTYEft.R REPORTNO.
CODE TYPE IV' :i~~~; I 1 I s I I I
. l o I 6 I 4 I I /I I o I 3 J LlJ -
I I 21 22 23 24 26 2 7 28 29 30 31 REVISION NO.
LQJ 32 80 ACTIOIJ FUTURE EFFECT SHUTDOWN
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ATTACHMENT NPRD-4 PRIME C0\\1P.
T,O.KE!-l ACTIO:~
O~JPLANT MET!-iOD HOURS SUBMITTED FORM SUB.
SUPPLIER COMPO.'l!ENT MA;*UFACTURER Ll.J@lLJ@
~@ ~.Io I 01 01 01 W@ Li(§ *LJLJ@
33 34 35 36 37 40 41 42 43 I GI 0 ! 8 I 0 I CAUS:: DESC~IPTIOi\\J AND CORRECTIVE ACTIONS @
44 47
!Probable cause-acid COLrosion of the carbon steel side of weld.
Leak repaired by pad ITIIJ 1welding.
The carbon steel* flange will be replaced with one made of stainless steel,
- I o:JJJ 1which is not susceptible to corrosion from dilute acid.
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FACILITY
METHOD OF
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% PO'NER OTHER STATUS ~ DISCOVERY
.. O.ISCOVERY OESCRl?TION '2V CU}]*. l.]_J@ I 0 I 9 1
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Commonwealth Edison
-=--~V~ATION R~EPORT.
DYR NO.
I STA UNIT YEAR NO.
D-12-2/3 123 PARTl[TITLE OF DEVIATION OCCURRED
2/.3-R..W.* -Wast_e-Gol-lec. -~or-reci-rc-line-leak-------------------- --1T/T4778 __._0_Tff0~
.DATE TIME SYSTEM AFFECTED 2000 PLANT, CONDITIONS TESTING CJ OCT 2/3 Rad Waste MODE N/A PWRfMWT)
N/A
, LOAD(MWE)
N/A YES NO DESCRIPTION OF. EVENT While making routine inspection of pumps in 2/3 RW basement the waste collector recirc line was found to have pinhole leaks on a 3" reducer flange.
DESCRIPTION OF GAUSE Water erosion on the inside of reducer
.. OTHER. APPL I CABLE INFORMATION W.R. No. 9199 was submitted, use of WC pump kept to a minimum and replacement of piping put on priority as soon as feasible.
EQUIPMENT Ll[] YES DR NO.
FAILURE CJ NO NA WR NO.
9199 PART 2 I OP ER AT I NG ENGINEERS COMMENTS Larry Larsen
_ RESPONSIBLE SUPERVISOR All leakage contained within normal plant drain systems.
11/24/78
.DATE TYPE OF DEVIATiON EVENT OF POTENTIAL REPORTABLE OCCURRENCE PUBLIC INTEREST TECH SPEC VIOLATION NON-REPORTABLE
- OCCURRENCE ANNUAL REPORTING SAFETY-*
RELATED WR ISSUED D 14 DAY D 10CFR21
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30 DAY NOTI Fl CATIQN D
LXJ 6.6.B.2.(dJ REPORTABLE OCCURRENCE NUMBER ACTION ITEM NO.
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78 -
64 - 03L-0 NA 24-HOUR NRC NOTIFICATION DTPH NA REGION I I I DATE TIME DTGM NA REGION I I I & DOL CATE TIME.
RESPONSIBLE COMPANY OFFICER INFORMED OF IOCFR21 C NDITIONS AND THEIR REPORT TO C
ACCEPTANCE BY STATION AS REQUIRED DATE RESOLUTION APPROVED AND AUTHORIZED FOR DISTRIBUTION D
D YES~
YES D
.No*O NO ~
PROMPT ON-SITE NOTIFICATION A. Roberts Asst. Supt.
Tl TLE.
NA TITLE PROMPT OFF-SITE NOTIFICATION F. Palmer Tl TLE J.
11/28/78.
DATE DATE 11/28/78 DATE 11/28/78
.DATE DATE
.ll/28/}8_
DATE 1500 TIME TIME 4:20
.TIME 4:20 TIME TIME
.. 86-5176 10-77
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| 05000249/LER-1978-001, /03L-0 for Dresden 3 Regarding the Discovery IRM Nos. 15 and 16 to Trip at 109% | /03L-0 for Dresden 3 Regarding the Discovery IRM Nos. 15 and 16 to Trip at 109% | | | 05000237/LER-1978-002-01, /01T-0:on 780105,during Normal operation,locked- Open Suction Valve to Standby Liquid Injection Pumps Were Found Closed.Cause Unknown.Monthly Verification Has Been Added to Surveillance DOS 1100-1 | /01T-0:on 780105,during Normal operation,locked- Open Suction Valve to Standby Liquid Injection Pumps Were Found Closed.Cause Unknown.Monthly Verification Has Been Added to Surveillance DOS 1100-1 | | | 05000249/LER-1978-002, /03L-0 for Dresden 3 Regarding the Failure of MO-3-1501-5C to Reopen While Performing DOS 1500-1. the Motor Oper. Suction Valve to C LPCI Pp. Closed But Could Not Be Reopened from Control Room | /03L-0 for Dresden 3 Regarding the Failure of MO-3-1501-5C to Reopen While Performing DOS 1500-1. the Motor Oper. Suction Valve to C LPCI Pp. Closed But Could Not Be Reopened from Control Room | | | 05000249/LER-1978-003, /01T-0 for Dresden 3 Regarding Discovery of Containment Valve Leakages in Excess of Technical Specification 4.7.A Limits | /01T-0 for Dresden 3 Regarding Discovery of Containment Valve Leakages in Excess of Technical Specification 4.7.A Limits | | | 05000237/LER-1978-003, /03L-0 for Dresden, Unit 2 Re Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems | /03L-0 for Dresden, Unit 2 Re Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems | | | 05000237/LER-1978-004-01, T-0 for Dresden, Unit 2 Re Improper 125V DC Cable Separation | T-0 for Dresden, Unit 2 Re Improper 125V DC Cable Separation | | | 05000249/LER-1978-005, /03L-0 for Dresden 3 Regarding the Discovery of a Pin Hole Leak in Minimum Flow Line from 3B Reactor Feedwater Pump Line 3-3205B-6 | /03L-0 for Dresden 3 Regarding the Discovery of a Pin Hole Leak in Minimum Flow Line from 3B Reactor Feedwater Pump Line 3-3205B-6 | | | 05000237/LER-1978-005, /03L-0 for Dresden Unit 2 Regarding the Receipt of a Torus High/Low Level Alarm as a Result of Torus Level Transmitter Instrument Drift | /03L-0 for Dresden Unit 2 Regarding the Receipt of a Torus High/Low Level Alarm as a Result of Torus Level Transmitter Instrument Drift | | | 05000249/LER-1978-006, /03L-0 for Dresden 3 Regarding the Discovery of Vacuum Breaker 1601-32F Binding | /03L-0 for Dresden 3 Regarding the Discovery of Vacuum Breaker 1601-32F Binding | | | 05000010/LER-1978-007, Cancelled | Cancelled | | | 05000249/LER-1978-007, /03L-0 for Dresden 3 Regarding Dis 2300-6 HPCI Area Temperature SW 2371 a Tripped at 284.3 Degrees Fahrenheit | /03L-0 for Dresden 3 Regarding Dis 2300-6 HPCI Area Temperature SW 2371 a Tripped at 284.3 Degrees Fahrenheit | | | 05000249/LER-1978-009-01, /01X-1 on 780320:Cracks Found on end-to-pipe Weld on CRD Return Line.Caused by Intermittent to Low Cooling Water Flow Leaving the CRD Nozzle.Pipe Was Removed & Replaced. (Encl to 7809180035) | /01X-1 on 780320:Cracks Found on end-to-pipe Weld on CRD Return Line.Caused by Intermittent to Low Cooling Water Flow Leaving the CRD Nozzle.Pipe Was Removed & Replaced. (Encl to 7809180035) | | | 05000010/LER-1978-009, Cancelled | Cancelled | | | 05000249/LER-1978-009, /01T-0 for Dresden 3 Regarding an Ultrasonic Inspection of the Safe End-To-Pipe Weld on the CRD Return Line Revealed Indications Which Suggested Cracking | /01T-0 for Dresden 3 Regarding an Ultrasonic Inspection of the Safe End-To-Pipe Weld on the CRD Return Line Revealed Indications Which Suggested Cracking | | | 05000237/LER-1978-009, /01T-0 for Dresden Unit 2 Regarding an Occurrence of a Conductivity Transient Due to Condensate Demineralizer Resin Introduction Into the Rx Vessel | /01T-0 for Dresden Unit 2 Regarding an Occurrence of a Conductivity Transient Due to Condensate Demineralizer Resin Introduction Into the Rx Vessel | | | 05000249/LER-1978-010, /01T-0 for Dresden 3 Regarding Discovery of 6 Hydraulic Snubbers Nos. 18, 19, 20, and 33 in Unit 3 Drywell and Nos. 1 and 3 in Isolation Condenser Pipeway with Less than Required Amount of Fluid | /01T-0 for Dresden 3 Regarding Discovery of 6 Hydraulic Snubbers Nos. 18, 19, 20, and 33 in Unit 3 Drywell and Nos. 1 and 3 in Isolation Condenser Pipeway with Less than Required Amount of Fluid | | | 05000249/LER-1978-011, /01T-0 for Dresden 3 Regarding Cracks Identified in Cladding of CRD Nozzle Inner Radius and Vessel Wall Beneath Nozzle | /01T-0 for Dresden 3 Regarding Cracks Identified in Cladding of CRD Nozzle Inner Radius and Vessel Wall Beneath Nozzle | | | 05000249/LER-1978-012, /01T-0 for Dresden 3 Regarding Disclosure of One Apparent Crack-Like Indication on the 330 Degrees Feedwater Sparger Along with Several Indications on the CRD Nozzle Thermal Sleeve Retainer | /01T-0 for Dresden 3 Regarding Disclosure of One Apparent Crack-Like Indication on the 330 Degrees Feedwater Sparger Along with Several Indications on the CRD Nozzle Thermal Sleeve Retainer | | | 05000249/LER-1978-013, /01T-0 for Dresden 3 Regarding Setpoints Being Set High by 10% During the Quarterly Scheduled Calibration Dis 1700-1 | /01T-0 for Dresden 3 Regarding Setpoints Being Set High by 10% During the Quarterly Scheduled Calibration Dis 1700-1 | | | 05000249/LER-1978-014, /01T-0 for Dresden 3 Regarding 24/48 Vdc Battery Failure to Pass the Refueling Outage Discharge Test | /01T-0 for Dresden 3 Regarding 24/48 Vdc Battery Failure to Pass the Refueling Outage Discharge Test | | | 05000249/LER-1978-015, /03L-0 for Dresden 3 Regarding Discovery of One Snubber in Drywell to Be Functionally Inoperable by Bench Test During Inspection to Check 10% of All Hydraulic Snubbers During Refueling | /03L-0 for Dresden 3 Regarding Discovery of One Snubber in Drywell to Be Functionally Inoperable by Bench Test During Inspection to Check 10% of All Hydraulic Snubbers During Refueling | | | 05000237/LER-1978-015-03, /03X-1 on 770402:CRD L-5 Uncoupled & Overtraveled When W/Drawn to Pos 48.Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Procedure Rev & QA Coverage Improved to Prevent Future CRD Uncouplings | /03X-1 on 770402:CRD L-5 Uncoupled & Overtraveled When W/Drawn to Pos 48.Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Procedure Rev & QA Coverage Improved to Prevent Future CRD Uncouplings | | | 05000249/LER-1978-016, /03L-0 for Dresden 3 Regarding Leakage Through Standby Liquid Control Check Valve 3-1101-15 Exceeding the T.S.4.7.A Limit for Single Valve Leakage of 29.38 Scfh | /03L-0 for Dresden 3 Regarding Leakage Through Standby Liquid Control Check Valve 3-1101-15 Exceeding the T.S.4.7.A Limit for Single Valve Leakage of 29.38 Scfh | | | 05000249/LER-1978-017, /01T-0 for Dresden 3 Regarding an NRC Request That Immediate Action Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction Va | /01T-0 for Dresden 3 Regarding an NRC Request That Immediate Action Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction Valves | | | 05000249/LER-1978-018, /03L-0 for Dresden 3 Regarding the Discovery of U3 Diesel Oil Storage Tank at 9000 Gal. Which Is Below the 10000 Gal. Limit Required by Technical Specification 3.9.c | /03L-0 for Dresden 3 Regarding the Discovery of U3 Diesel Oil Storage Tank at 9000 Gal. Which Is Below the 10000 Gal. Limit Required by Technical Specification 3.9.c | | | 05000249/LER-1978-019, /03L-0 for Dresden 3 Regarding the Discovery of Ps 504C and 504D Found to Trip at 403 PSI and 405 PSI Respectively | /03L-0 for Dresden 3 Regarding the Discovery of Ps 504C and 504D Found to Trip at 403 PSI and 405 PSI Respectively | | | 05000237/LER-1978-020, /03X-01 for Dresden, Unit 1 Re Cause of Failure of the Diesel Generator to Start | /03X-01 for Dresden, Unit 1 Re Cause of Failure of the Diesel Generator to Start | | | 05000249/LER-1978-020, /03L-0 for Dresden 3 Regarding Discovery of Ps 3-203-3C Tripped at 1148 PSI Rx Pressure Incr | /03L-0 for Dresden 3 Regarding Discovery of Ps 3-203-3C Tripped at 1148 PSI Rx Pressure Incr | | | 05000249/LER-1978-022, /03L-0 for Dresden Unit 3 Regarding Discovery of High Flow Isolation Switches DPIS 261-2C, 261-2N, and 261-2S to Trip at Values Exceeding the Technical Specification Limit | /03L-0 for Dresden Unit 3 Regarding Discovery of High Flow Isolation Switches DPIS 261-2C, 261-2N, and 261-2S to Trip at Values Exceeding the Technical Specification Limit | | | 05000249/LER-1978-023, /01T-0 for Dresden Unit 3 Regarding Source Range Monitors 24 and 21 Being Declared Inoperable on 05/20/1978 | /01T-0 for Dresden Unit 3 Regarding Source Range Monitors 24 and 21 Being Declared Inoperable on 05/20/1978 | | | 05000249/LER-1978-024, /03L-0 for Dresden Unit 3 Regarding the Discovery of PS3-263-53A to Trip at 1178 PSI Which Is Above Technical Specifications | /03L-0 for Dresden Unit 3 Regarding the Discovery of PS3-263-53A to Trip at 1178 PSI Which Is Above Technical Specifications | | | 05000237/LER-1978-025-03, Re While Preforming LPCI and Ccsw Surveillance on Unit 3 Prior to Taking the U-3 D/G Out of Service, a Spike Was Found on the Liquid Process Radiation Monitor for the Service Water Discharge | Re While Preforming LPCI and Ccsw Surveillance on Unit 3 Prior to Taking the U-3 D/G Out of Service, a Spike Was Found on the Liquid Process Radiation Monitor for the Service Water Discharge | | | 05000010/LER-1978-025, Cancelled | Cancelled | | | 05000237/LER-1978-025, /03L-0 for Dresden Unit 3 Regarding Discovery of a Spike on the Liquid Process Radiation Monitor for the Service Water Discharge | /03L-0 for Dresden Unit 3 Regarding Discovery of a Spike on the Liquid Process Radiation Monitor for the Service Water Discharge | | | 05000237/LER-1978-026-03, Re While Performing LPCI Both Indicating Lights Went Out and the Motor Stopped | Re While Performing LPCI Both Indicating Lights Went Out and the Motor Stopped | | | 05000237/LER-1978-027, /03L for Dresden, Unit 2 Re a Sample Taken from Radwaste a WST at 1020 After the Tank Was Filled to 88% | /03L for Dresden, Unit 2 Re a Sample Taken from Radwaste a WST at 1020 After the Tank Was Filled to 88% | | | 05000010/LER-1978-028-03, /03L-0:on 780815,weekly Reactor Protection Sys Functional Operability Test Postponed But Not Rescheduled. Caused by Personnel Error.Personnel re-instructed Re Importance of Scheduled Surveillances.(Encl to 7809260056) | /03L-0:on 780815,weekly Reactor Protection Sys Functional Operability Test Postponed But Not Rescheduled. Caused by Personnel Error.Personnel re-instructed Re Importance of Scheduled Surveillances.(Encl to 7809260056) | | | 05000249/LER-1978-028-03, Re While Performing Surv. Dis 250-1, MSL Hi Flow Isolation Sw. Dpis 3-261-2c Tripped at 117 Psid | Re While Performing Surv. Dis 250-1, MSL Hi Flow Isolation Sw. Dpis 3-261-2c Tripped at 117 Psid | | | 05000237/LER-1978-028, /01X-1 for Dresden, Units 2 and 3 Re NRC Request for Immediate Actions to Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suct | /01X-1 for Dresden, Units 2 and 3 Re NRC Request for Immediate Actions to Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction Valves | | | 05000010/LER-1978-028, Forwards LER 78-028/03L-0 | Forwards LER 78-028/03L-0 | | | 05000237/LER-1978-029-03, Re Safety Implications Were Minimal Because 1 or More Operable APRMs Per Channel Remained Available as Required by TS 3.2 | Re Safety Implications Were Minimal Because 1 or More Operable APRMs Per Channel Remained Available as Required by TS 3.2 | | | 05000237/LER-1978-030-01, /01X-1 on 780428:During Unit 2 Startup Opers, a LPCI & Core Spray Subsys Were Inadvertantly Rendered Inoper Because Personnel Had Closed LPCI Pump & Discharge Valves on Unit 2 Vice 3.(Encl to 7809180320) | /01X-1 on 780428:During Unit 2 Startup Opers, a LPCI & Core Spray Subsys Were Inadvertantly Rendered Inoper Because Personnel Had Closed LPCI Pump & Discharge Valves on Unit 2 Vice 3.(Encl to 7809180320) | | | 05000237/LER-1978-030, Forwards LER 78-030/01X-1 | Forwards LER 78-030/01X-1 | | | 05000237/LER-1978-031, /03L-0 for Dresden, Unit 2 Re PS-2-1430-1466C Failed to Operate | /03L-0 for Dresden, Unit 2 Re PS-2-1430-1466C Failed to Operate | | | 05000249/LER-1978-032-03, /03L on 780817:room Cooler Fans Failed to Start When Pumps 3B & 3C started.4KV Switchgear 33 & 34 Auxiliary Contacts Were Found Dirty.(Encl to 7809220129) | /03L on 780817:room Cooler Fans Failed to Start When Pumps 3B & 3C started.4KV Switchgear 33 & 34 Auxiliary Contacts Were Found Dirty.(Encl to 7809220129) | | | 05000249/LER-1978-032, Forwards LER 78-032/03L | Forwards LER 78-032/03L | | | 05000237/LER-1978-032, /03L-0 for Dresden, Unit 2 Re During Steady State Operation, Torus to Drywell Vacuum Breaker 2-1601-33E & F Were Found Inoperable During Routine Operability Surveillance | /03L-0 for Dresden, Unit 2 Re During Steady State Operation, Torus to Drywell Vacuum Breaker 2-1601-33E & F Were Found Inoperable During Routine Operability Surveillance | | | 05000010/LER-1978-033, Cancelled | Cancelled | | | 05000237/LER-1978-033, Forwards LER 78-033/03X-1 | Forwards LER 78-033/03X-1 | | | 05000237/LER-1978-033-03, /03X-1 on 780522:during Test Performed on U-2 D/G to Measure Overshoot & Overspeed Setpoint,The Diesel Tripped 4 Times Due to Overspeed Caused by Governor Speed Set Too High | /03X-1 on 780522:during Test Performed on U-2 D/G to Measure Overshoot & Overspeed Setpoint,The Diesel Tripped 4 Times Due to Overspeed Caused by Governor Speed Set Too High | |
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