LER-1978-033, Forwards LER 78-033/03X-1 |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2371978033R00 - NRC Website |
|
text
...-
CommonweA Edison
- 1.
Dresden Nuclea.,wer Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 E COPY
R~G-U-LAIOJ~Y-D_Q_GKEJ_El_LI~~--
December 12, 1978 BBS LTR #78-1594 James ~. Keppler, Regional Director Directorate of Regulatory Operations - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 Reportable.Occurrence "Update Report" /178-033/03X-1, Docket #050-237 is hereby submitted to your office to supplement Licensee Event Report 78-033/03L-0 concerning the overspeed and subsequent trip of the Unit 2 Diesel Generator.
It addresses the final corrective actions taken to prevent recurrence and: a change in classification.of..Items 18 and 19 on the Licensee Event Report form.
This event was reported to you under Dresden Nuclear Power Station Technical Specifications 6.6.B.2.(c),
observed inadequacies in the implementation of administrative or procedural controls which threaten to cause a reduction of degree of redundance provided in reactor protection systems or engineered safety feature systems.
BBS/deb Enclosure cc:
Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC
~
,_,..,....... (h-'*C:0...
0-'-"4'-.T"..
~
- -., **,<*.*>"A..-.......-...==
.-J-1;/,"1,,">~*..L--.......... *,4
- ~-:.-£.:;:~:.. -:::.-.,;;:*:-.-.:; -..:: *>:-: *....,::;-
~-
-***""T.. -..-*
__ -.;..,1:::.-.--- -
J*.J?aC r:ur11*.i :.;t>U
... ~r-77*:
~..... ';'
CONTROL BLOCK:
e LICENSEE,EVENT REPORT UPiiiE REPORT PR8POUS REPORT DATE 6-21-78 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
~
I 1 IL ID IR Is I 2 10)1 o Io I - Io Io I 01 o jo I-I 01 o!G)I 41 ll ll ll 1101 I 10 7
S 9
LICENS!:E CODE 14 15 LICENSE NUMoER 25 26 LICENSE TYPE JO 57 CAT 58 -------
CON'T [TI2J 7
8
~;:~~~ L!:J© I o I 5 I o 1.0 I o I 2 I 3 I 7 101 o I 5 I 2 I 2 I 7 I 8 I© 11 I 2 l 1
- I 2 I 7 I 8 I G) 60 Gl DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
/While U-2 was locked in refuel during an outage, a test was performed on U-2 D/G Q((IJ I to measure its overshoot and overspeed setpoint.
The diesel tripped four times during!
~
I startup due to overspeed.
Since the unit was not at power, this event has little [Q))J I safety significance.
Similar events had occurred on U2/3 D/G (LER#77-024/01X-l, [QJ]J I 77-025/031-0 & 78-021/031-0, Docket #050-237).
However, this is the first time this
~
I event occurred on this diesel unit.
CQ:ill 7
8 9...
SYST:OM
CAUSE
CAUSE CODE CODE SUBCODE 0."Il IE IE I@ w@ LLJ@ I 8
9 10 11 12 13 SEQUENTIAL
@ LER/RO CVENT YE->.R REPORT NO.
REPORT I 7 I 8 j l==J I 01 31 31 NUMBER 21 22 23 24 26 COMPONENT CODE zl zl zl zl zl zl8 18 OCCURRENCE CODE I/I I o I 3 I 27 28 29 COMP.
SUBCODE LU@
19 REPORT TYPE
~'
30 VALVE SUBCODE w@
20 REVISION NO.
l=:J LJJ 31 32 80 ACTION FUTURE EF~ECT SHUTDOWN r:;:;..
ATTACHMENT NPRD-4 TAKEr*
ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM ~us.
PRIME COMP.
SUPPLIER CO~IPONENT MANUFACTURER LLJ@LJJ@
LJ.J@.UJ I ol ol ol ol.L!J@
WC§ 33 34 35 36 3 7 40 41 42 LAJ@
IE[ l I 6 I ol@
CAUSE DESCRIPTIO~J AND CORRECTIVE ACTIONS @
43 44 47 CI:::[§] j*Gov. speed was found* set too high.
Further test revealed over speed trip wouJd occur ITfil i:due to overshoot if speed was set above 63 Hz.
The diesel surv. pr.cc. calls for
!:III] la setting of 61 Hz at end of test.
Reason for high settings could not be found.
To [JJJ] I prevent recurrence the overspeed trip setpoint was raised and a caution was added to
[}]}] I the surveillance procedure.
8 9
FACILITY STATUS
% POWER OTHER STATUS GTIJ l!!J@ l.9..1 0 I QJ@.._I __
N_A ___
~
8 9
10 12 11 44 ACTIVITY CONTENT A~OUNT OF ACTIVITY @
RELEASED OF RELEASE GJil W@ Li.1§1 NA 0
9
. 10 11 44 PERSONNEL EXPOSURES
~
METHOD OF DISCOVERY UJ01 45 46 AS 80 DISCOVERY DESCRIPTION Overshoot and Overspeed Setpoint Test!
80 LOCATION OF RELEASE@
NA 80 NUf*11BER Q, TYPE DESCRIPTION~
[Q:2) lo IO loj(0~@)L-~~~~-N=A'--~~~~~~~~~~~~~~~~~~--'
8 9
11 12 13 80 PERSONNEL INJURIES
~
NUMSER DESCRIPTION6 GE] I 0 I 0 I 0 I@
NA 8
9 11 12 80 LOSS OF OR DAMAGE TO FACILITY t43'i TYPE
DESCRIPTION
':::;J [iliJ W@.
NA 8
9 10 BO PUOLICITY r.;:\\.
ISSUEDQ DESCRIPTION~
NRC USE ONLY ITliJ Wei
[ I I I I I I I I I I IJ ~
7. " 8 9
~10~-~-----------l.liA------~---------~--J68 69
- ~~:?.~}_:~-'... ~:~if\\QE:~~~RER *-**_J_o_e_Ch_a_n_* _____
80*;;;
PHONE:--.,..--'4'""2:.:lo..*---------. -'~.~~~~
ATTACHMENT TO LICENSEE EVENT REPORT78-033/03X~l COMHONWEALTH EDISON COMPANY (CWE)
DRESDEN UNI'F-2 (ILDRS-2)
DOCKET ti 050-237 While Unit 2 was locked in refuel during an outage, a test was performed by electrical maintenance to measure the overshooting and overspeed setpoint of Unit 2 diesel generator.
The diesel tripped four times on overspeed during start up.
Since Unit 2 was in refuel, this event is of little safety significance.
Western Engine representative was called in immediately to investigate this event.
He found the governor speed setting was too high.
The setting was lowered and the diesel was started with no problem.
The governor speed should have been set at 61 Hertz (915 rpm) at the conclusion of the last surveillance test of the diesel according to the diesel surveillance procedure.
- It is. possible that the operato~ set the speed too high at that time or someone actuated the governor switch sometime prior to starting the diesel for surveillance.
On June 15, 1978, another Western Engine representative was called in to further investigate the problem.
It was found that if the governor speed was set at 61 Hertz (915 rpm), the overshoot was to 980 rpm, and at the maximum setting which is 64 Hertz (960 rpm) the overshoot was about 1050 rpm.
At a speed setting of 62.5 Hz (940 rpm), the overshooting was to about 1020 rpm.
Since the overspeed trip setpoint of this diesel was tested to be 1030 rpm, any speed setting above 63 Hertz would result in overspeed due to the overshooting. *since the maximum range of the frequency meter in the Control Room is 62 Hertz, it is very unlikely that the operator would set the speed above 62 Hertz.
The exact reason for the high speed setting cannot be determined at this time.
All operators were instructed not to set the speed above 61 Hertz.
Measurements of overshooting and overspeed setpaint have been performed on the other two diesel generators and resulted. in similar values.
Therefore any corrective measures to be done on Unit 2 diesel were
. also applied to the other_ two diesel gerier-~tors; *:,' :*
To prevent recurrence; the overspeed tri~ setpoint was raised to 1035 rpm on all diesels as suggested by manufacturer.
A caution was also added to the surveillance proceduJ'.'.e to make the operator aware of this failure pos-sibility.
In order to prevent the speed switches being actuated inadvertently, the switches will be covered by plastic boxes.
,~i~~)~F,.
...... **. :~*.~~;~,;.:._*::*.*.-*.. r~_;_.._ -.YT:.. ~*~~
~ * *.-*.. *.... -,....
- -
- -'"" *-** -~..-**:::-~~~~-~~~:':*=:.:"_":-~~~;;*:*:'*-~.:-. ~:-:.~~.,..*:~-~ ~:~.. --- "::,*-~*
":~~~-~*:*-~;. ~...,.,..... i..~~~ ~<~f. -~::*j... *."':~ '
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000249/LER-1978-001, /03L-0 for Dresden 3 Regarding the Discovery IRM Nos. 15 and 16 to Trip at 109% | /03L-0 for Dresden 3 Regarding the Discovery IRM Nos. 15 and 16 to Trip at 109% | | | 05000237/LER-1978-002-01, /01T-0:on 780105,during Normal operation,locked- Open Suction Valve to Standby Liquid Injection Pumps Were Found Closed.Cause Unknown.Monthly Verification Has Been Added to Surveillance DOS 1100-1 | /01T-0:on 780105,during Normal operation,locked- Open Suction Valve to Standby Liquid Injection Pumps Were Found Closed.Cause Unknown.Monthly Verification Has Been Added to Surveillance DOS 1100-1 | | | 05000249/LER-1978-002, /03L-0 for Dresden 3 Regarding the Failure of MO-3-1501-5C to Reopen While Performing DOS 1500-1. the Motor Oper. Suction Valve to C LPCI Pp. Closed But Could Not Be Reopened from Control Room | /03L-0 for Dresden 3 Regarding the Failure of MO-3-1501-5C to Reopen While Performing DOS 1500-1. the Motor Oper. Suction Valve to C LPCI Pp. Closed But Could Not Be Reopened from Control Room | | | 05000249/LER-1978-003, /01T-0 for Dresden 3 Regarding Discovery of Containment Valve Leakages in Excess of Technical Specification 4.7.A Limits | /01T-0 for Dresden 3 Regarding Discovery of Containment Valve Leakages in Excess of Technical Specification 4.7.A Limits | | | 05000237/LER-1978-003, /03L-0 for Dresden, Unit 2 Re Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems | /03L-0 for Dresden, Unit 2 Re Inadequacies in the Implementation of Administrative or Procedural Controls Which Threaten to Cause Reduction of Degree of Redundancy Provided in Reactor Protection Systems | | | 05000237/LER-1978-004-01, T-0 for Dresden, Unit 2 Re Improper 125V DC Cable Separation | T-0 for Dresden, Unit 2 Re Improper 125V DC Cable Separation | | | 05000249/LER-1978-005, /03L-0 for Dresden 3 Regarding the Discovery of a Pin Hole Leak in Minimum Flow Line from 3B Reactor Feedwater Pump Line 3-3205B-6 | /03L-0 for Dresden 3 Regarding the Discovery of a Pin Hole Leak in Minimum Flow Line from 3B Reactor Feedwater Pump Line 3-3205B-6 | | | 05000237/LER-1978-005, /03L-0 for Dresden Unit 2 Regarding the Receipt of a Torus High/Low Level Alarm as a Result of Torus Level Transmitter Instrument Drift | /03L-0 for Dresden Unit 2 Regarding the Receipt of a Torus High/Low Level Alarm as a Result of Torus Level Transmitter Instrument Drift | | | 05000249/LER-1978-006, /03L-0 for Dresden 3 Regarding the Discovery of Vacuum Breaker 1601-32F Binding | /03L-0 for Dresden 3 Regarding the Discovery of Vacuum Breaker 1601-32F Binding | | | 05000010/LER-1978-007, Cancelled | Cancelled | | | 05000249/LER-1978-007, /03L-0 for Dresden 3 Regarding Dis 2300-6 HPCI Area Temperature SW 2371 a Tripped at 284.3 Degrees Fahrenheit | /03L-0 for Dresden 3 Regarding Dis 2300-6 HPCI Area Temperature SW 2371 a Tripped at 284.3 Degrees Fahrenheit | | | 05000249/LER-1978-009-01, /01X-1 on 780320:Cracks Found on end-to-pipe Weld on CRD Return Line.Caused by Intermittent to Low Cooling Water Flow Leaving the CRD Nozzle.Pipe Was Removed & Replaced. (Encl to 7809180035) | /01X-1 on 780320:Cracks Found on end-to-pipe Weld on CRD Return Line.Caused by Intermittent to Low Cooling Water Flow Leaving the CRD Nozzle.Pipe Was Removed & Replaced. (Encl to 7809180035) | | | 05000010/LER-1978-009, Cancelled | Cancelled | | | 05000249/LER-1978-009, /01T-0 for Dresden 3 Regarding an Ultrasonic Inspection of the Safe End-To-Pipe Weld on the CRD Return Line Revealed Indications Which Suggested Cracking | /01T-0 for Dresden 3 Regarding an Ultrasonic Inspection of the Safe End-To-Pipe Weld on the CRD Return Line Revealed Indications Which Suggested Cracking | | | 05000237/LER-1978-009, /01T-0 for Dresden Unit 2 Regarding an Occurrence of a Conductivity Transient Due to Condensate Demineralizer Resin Introduction Into the Rx Vessel | /01T-0 for Dresden Unit 2 Regarding an Occurrence of a Conductivity Transient Due to Condensate Demineralizer Resin Introduction Into the Rx Vessel | | | 05000249/LER-1978-010, /01T-0 for Dresden 3 Regarding Discovery of 6 Hydraulic Snubbers Nos. 18, 19, 20, and 33 in Unit 3 Drywell and Nos. 1 and 3 in Isolation Condenser Pipeway with Less than Required Amount of Fluid | /01T-0 for Dresden 3 Regarding Discovery of 6 Hydraulic Snubbers Nos. 18, 19, 20, and 33 in Unit 3 Drywell and Nos. 1 and 3 in Isolation Condenser Pipeway with Less than Required Amount of Fluid | | | 05000249/LER-1978-011, /01T-0 for Dresden 3 Regarding Cracks Identified in Cladding of CRD Nozzle Inner Radius and Vessel Wall Beneath Nozzle | /01T-0 for Dresden 3 Regarding Cracks Identified in Cladding of CRD Nozzle Inner Radius and Vessel Wall Beneath Nozzle | | | 05000249/LER-1978-012, /01T-0 for Dresden 3 Regarding Disclosure of One Apparent Crack-Like Indication on the 330 Degrees Feedwater Sparger Along with Several Indications on the CRD Nozzle Thermal Sleeve Retainer | /01T-0 for Dresden 3 Regarding Disclosure of One Apparent Crack-Like Indication on the 330 Degrees Feedwater Sparger Along with Several Indications on the CRD Nozzle Thermal Sleeve Retainer | | | 05000249/LER-1978-013, /01T-0 for Dresden 3 Regarding Setpoints Being Set High by 10% During the Quarterly Scheduled Calibration Dis 1700-1 | /01T-0 for Dresden 3 Regarding Setpoints Being Set High by 10% During the Quarterly Scheduled Calibration Dis 1700-1 | | | 05000249/LER-1978-014, /01T-0 for Dresden 3 Regarding 24/48 Vdc Battery Failure to Pass the Refueling Outage Discharge Test | /01T-0 for Dresden 3 Regarding 24/48 Vdc Battery Failure to Pass the Refueling Outage Discharge Test | | | 05000249/LER-1978-015, /03L-0 for Dresden 3 Regarding Discovery of One Snubber in Drywell to Be Functionally Inoperable by Bench Test During Inspection to Check 10% of All Hydraulic Snubbers During Refueling | /03L-0 for Dresden 3 Regarding Discovery of One Snubber in Drywell to Be Functionally Inoperable by Bench Test During Inspection to Check 10% of All Hydraulic Snubbers During Refueling | | | 05000237/LER-1978-015-03, /03X-1 on 770402:CRD L-5 Uncoupled & Overtraveled When W/Drawn to Pos 48.Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Procedure Rev & QA Coverage Improved to Prevent Future CRD Uncouplings | /03X-1 on 770402:CRD L-5 Uncoupled & Overtraveled When W/Drawn to Pos 48.Caused by Unlatched Inner Filter & Abnormally Long Uncoupling Rod.Procedure Rev & QA Coverage Improved to Prevent Future CRD Uncouplings | | | 05000249/LER-1978-016, /03L-0 for Dresden 3 Regarding Leakage Through Standby Liquid Control Check Valve 3-1101-15 Exceeding the T.S.4.7.A Limit for Single Valve Leakage of 29.38 Scfh | /03L-0 for Dresden 3 Regarding Leakage Through Standby Liquid Control Check Valve 3-1101-15 Exceeding the T.S.4.7.A Limit for Single Valve Leakage of 29.38 Scfh | | | 05000249/LER-1978-017, /01T-0 for Dresden 3 Regarding an NRC Request That Immediate Action Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction Va | /01T-0 for Dresden 3 Regarding an NRC Request That Immediate Action Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction Valves | | | 05000249/LER-1978-018, /03L-0 for Dresden 3 Regarding the Discovery of U3 Diesel Oil Storage Tank at 9000 Gal. Which Is Below the 10000 Gal. Limit Required by Technical Specification 3.9.c | /03L-0 for Dresden 3 Regarding the Discovery of U3 Diesel Oil Storage Tank at 9000 Gal. Which Is Below the 10000 Gal. Limit Required by Technical Specification 3.9.c | | | 05000249/LER-1978-019, /03L-0 for Dresden 3 Regarding the Discovery of Ps 504C and 504D Found to Trip at 403 PSI and 405 PSI Respectively | /03L-0 for Dresden 3 Regarding the Discovery of Ps 504C and 504D Found to Trip at 403 PSI and 405 PSI Respectively | | | 05000237/LER-1978-020, /03X-01 for Dresden, Unit 1 Re Cause of Failure of the Diesel Generator to Start | /03X-01 for Dresden, Unit 1 Re Cause of Failure of the Diesel Generator to Start | | | 05000249/LER-1978-020, /03L-0 for Dresden 3 Regarding Discovery of Ps 3-203-3C Tripped at 1148 PSI Rx Pressure Incr | /03L-0 for Dresden 3 Regarding Discovery of Ps 3-203-3C Tripped at 1148 PSI Rx Pressure Incr | | | 05000249/LER-1978-022, /03L-0 for Dresden Unit 3 Regarding Discovery of High Flow Isolation Switches DPIS 261-2C, 261-2N, and 261-2S to Trip at Values Exceeding the Technical Specification Limit | /03L-0 for Dresden Unit 3 Regarding Discovery of High Flow Isolation Switches DPIS 261-2C, 261-2N, and 261-2S to Trip at Values Exceeding the Technical Specification Limit | | | 05000249/LER-1978-023, /01T-0 for Dresden Unit 3 Regarding Source Range Monitors 24 and 21 Being Declared Inoperable on 05/20/1978 | /01T-0 for Dresden Unit 3 Regarding Source Range Monitors 24 and 21 Being Declared Inoperable on 05/20/1978 | | | 05000249/LER-1978-024, /03L-0 for Dresden Unit 3 Regarding the Discovery of PS3-263-53A to Trip at 1178 PSI Which Is Above Technical Specifications | /03L-0 for Dresden Unit 3 Regarding the Discovery of PS3-263-53A to Trip at 1178 PSI Which Is Above Technical Specifications | | | 05000237/LER-1978-025-03, Re While Preforming LPCI and Ccsw Surveillance on Unit 3 Prior to Taking the U-3 D/G Out of Service, a Spike Was Found on the Liquid Process Radiation Monitor for the Service Water Discharge | Re While Preforming LPCI and Ccsw Surveillance on Unit 3 Prior to Taking the U-3 D/G Out of Service, a Spike Was Found on the Liquid Process Radiation Monitor for the Service Water Discharge | | | 05000010/LER-1978-025, Cancelled | Cancelled | | | 05000237/LER-1978-025, /03L-0 for Dresden Unit 3 Regarding Discovery of a Spike on the Liquid Process Radiation Monitor for the Service Water Discharge | /03L-0 for Dresden Unit 3 Regarding Discovery of a Spike on the Liquid Process Radiation Monitor for the Service Water Discharge | | | 05000237/LER-1978-026-03, Re While Performing LPCI Both Indicating Lights Went Out and the Motor Stopped | Re While Performing LPCI Both Indicating Lights Went Out and the Motor Stopped | | | 05000237/LER-1978-027, /03L for Dresden, Unit 2 Re a Sample Taken from Radwaste a WST at 1020 After the Tank Was Filled to 88% | /03L for Dresden, Unit 2 Re a Sample Taken from Radwaste a WST at 1020 After the Tank Was Filled to 88% | | | 05000010/LER-1978-028-03, /03L-0:on 780815,weekly Reactor Protection Sys Functional Operability Test Postponed But Not Rescheduled. Caused by Personnel Error.Personnel re-instructed Re Importance of Scheduled Surveillances.(Encl to 7809260056) | /03L-0:on 780815,weekly Reactor Protection Sys Functional Operability Test Postponed But Not Rescheduled. Caused by Personnel Error.Personnel re-instructed Re Importance of Scheduled Surveillances.(Encl to 7809260056) | | | 05000249/LER-1978-028-03, Re While Performing Surv. Dis 250-1, MSL Hi Flow Isolation Sw. Dpis 3-261-2c Tripped at 117 Psid | Re While Performing Surv. Dis 250-1, MSL Hi Flow Isolation Sw. Dpis 3-261-2c Tripped at 117 Psid | | | 05000237/LER-1978-028, /01X-1 for Dresden, Units 2 and 3 Re NRC Request for Immediate Actions to Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suct | /01X-1 for Dresden, Units 2 and 3 Re NRC Request for Immediate Actions to Be Taken to Mitigate the Potential for a Spurious Closure of a Recirculation Loop Suction Valve with a LOCA Occurring Between the Loop Discharge and Suction Valves | | | 05000010/LER-1978-028, Forwards LER 78-028/03L-0 | Forwards LER 78-028/03L-0 | | | 05000237/LER-1978-029-03, Re Safety Implications Were Minimal Because 1 or More Operable APRMs Per Channel Remained Available as Required by TS 3.2 | Re Safety Implications Were Minimal Because 1 or More Operable APRMs Per Channel Remained Available as Required by TS 3.2 | | | 05000237/LER-1978-030-01, /01X-1 on 780428:During Unit 2 Startup Opers, a LPCI & Core Spray Subsys Were Inadvertantly Rendered Inoper Because Personnel Had Closed LPCI Pump & Discharge Valves on Unit 2 Vice 3.(Encl to 7809180320) | /01X-1 on 780428:During Unit 2 Startup Opers, a LPCI & Core Spray Subsys Were Inadvertantly Rendered Inoper Because Personnel Had Closed LPCI Pump & Discharge Valves on Unit 2 Vice 3.(Encl to 7809180320) | | | 05000237/LER-1978-030, Forwards LER 78-030/01X-1 | Forwards LER 78-030/01X-1 | | | 05000237/LER-1978-031, /03L-0 for Dresden, Unit 2 Re PS-2-1430-1466C Failed to Operate | /03L-0 for Dresden, Unit 2 Re PS-2-1430-1466C Failed to Operate | | | 05000249/LER-1978-032-03, /03L on 780817:room Cooler Fans Failed to Start When Pumps 3B & 3C started.4KV Switchgear 33 & 34 Auxiliary Contacts Were Found Dirty.(Encl to 7809220129) | /03L on 780817:room Cooler Fans Failed to Start When Pumps 3B & 3C started.4KV Switchgear 33 & 34 Auxiliary Contacts Were Found Dirty.(Encl to 7809220129) | | | 05000249/LER-1978-032, Forwards LER 78-032/03L | Forwards LER 78-032/03L | | | 05000237/LER-1978-032, /03L-0 for Dresden, Unit 2 Re During Steady State Operation, Torus to Drywell Vacuum Breaker 2-1601-33E & F Were Found Inoperable During Routine Operability Surveillance | /03L-0 for Dresden, Unit 2 Re During Steady State Operation, Torus to Drywell Vacuum Breaker 2-1601-33E & F Were Found Inoperable During Routine Operability Surveillance | | | 05000010/LER-1978-033, Cancelled | Cancelled | | | 05000237/LER-1978-033, Forwards LER 78-033/03X-1 | Forwards LER 78-033/03X-1 | | | 05000237/LER-1978-033-03, /03X-1 on 780522:during Test Performed on U-2 D/G to Measure Overshoot & Overspeed Setpoint,The Diesel Tripped 4 Times Due to Overspeed Caused by Governor Speed Set Too High | /03X-1 on 780522:during Test Performed on U-2 D/G to Measure Overshoot & Overspeed Setpoint,The Diesel Tripped 4 Times Due to Overspeed Caused by Governor Speed Set Too High | |
|