ML17157A048

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Insp Repts 50-387/90-05 & 50-388/90-05 on 900203-09.No Violations Noted.Major Areas Inspected:Review of Licensee Actions in Response to 900203 Loss of Shutdown Cooling at Unit 1
ML17157A048
Person / Time
Site: Susquehanna  
Issue date: 02/23/1990
From: Anderson C, Barber G, Cheung L, Stair J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17157A047 List:
References
50-387-90-05, 50-387-90-5, 50-388-90-05, 50-388-90-5, NUDOCS 9003070295
Download: ML17157A048 (14)


See also: IR 05000387/1990005

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

Report Nos.

50-387/90-05

50-388/90-05

Docket Nos.

50-387

50-388

License

Nos.

NPF-14

NPF-22

Licensee:

Penns

lvania Power

& Li ht

Com an

2 North Ninth Street

Allentown

Penns

lvania

18101

Facility Name:,Sus

uehanna

Steam Electric Station

Units

1 and

2

Inspection At:

Al 1 entown

Penn s

1 vani a

Inspection

Conducted:

Februar

3-9

1990

Inspectors:

Leonard

Cheung,

Senior

R

tor Engineer

Plant

Systems

Section,

ngineering

Branch, Divisions of Reactor Safety

da

e

G.

. Barber,

Senior

ide t Inspector,

SSES

dat

J.

R.

S ai,

R

s ent Ins

S

ES

dat

Approved by:

C. J.

nderson,

Chief, Plant Systems

Section,

Engineering

Branch,

DRS

date

Ins ection Summa:

Ins ection

on Februar

3-9

1990

Ins ection

Re ort Nos.

50-387/90-05

and 50-388/90-05

Areas Ins ected:

A special

inspection

was conducted

to review licensee

actions

in response

to a loss of shutdown cooling event which occurred

on

February

3,

1990.

Results:

An Alert was declared

on February

3,

1990 due to

a loss of shutdown

cooling (SDC) for Unit

1 with the reactor coolant temperature

exceeding

200

degrees

F.

The loss of SDC was caused

by a failure of the "B" RPS bus

due to

a

ground fault i.n one of the circuit breakers.

The reactor coolant temperature

was stabilized at approximately

250 degrees

F and

SDC was returned to 'service

about

5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> later.

Onsite

and offsite emergency

response

organizations

were

activated in accordance

with the emergency

plans.

The licensee

actions

were

appropriate

and directed

toward plant safety.

Implementation of the emergency

plan onsite

was well coordinated

and effective.

900307(Qp~~ ygpp~(

PDR

ADOCK 0~0003~7

P11C

The root cause of the circuit breaker failure was promptly identified.

A design

modification of the Unit

1

RPS

power distribution panels

to deal with the root

cause

was completed before the conclusion of this inspection.

The licensee

made

an identical modification to the Unit 2

RPS

power distribution panels.

The Unit 2 modification was completed

on February

11,

1990.

The inspector

determined that the licensee's

corrective actions

were adequate.

No violations

were identified.

TABLE OF CONTENTS

~Pa

e

1.0

Introduction

2.0

Background

.

3.0

Sequence

of Events

.

0

~

~

~

1

4.0

Emergency

Plan Implementation

5.0

Reactor Protection

System

(RPS)

Power

Supply Electri

Design

.

5. 1

RPS

Power Distribution

5.2

RPS

Bus "8" Hardware Configurations

.

5.3

Previous

RPS Circuit Breaker Failures

5.4

RPS

Power

Supply Modifications

6.0

Findings

and Conclusions

cal

.

2

3

.

3

.

3

4

~

~

~

5

~

.

6

~

~

~

7.0

Exit Meeting

.

Appendix

1

Persons

Contacted

.

Figure

1, Circuit Breaker

CBSB Mounting Configuration

.

.

7

.

8

.

9

DETAILS

1 '

Introduction

During

a plant startup

on February

3,

1990 at 5:53 p.m.,

the licensee

declared

an Alert condition due to a loss of shutdown cooling

(SDC) with

the reactor coolant temperature

exceeding

200 degrees

F.

The loss of SDC

was caused

by the inability to restore

power to

a Reactor Protection

System

(RPS)

bus after it was deenergized

for surveillance testing.

Alternate

cooling was established

which stabilized the reactor coolant temperature

at approximately

250 degrees

F.

Shutdown cooling was reestablished

and

the core

was cooled to below 200 degrees

F by 12: 15 a.m.,

February

4,

1990,

The Alert was terminated at 12:25 a.m.,

February

4,

1990.

No radioactivity

was released offsite during the event.

'he

cause of the event

was

a ground fault on the "B" RPS bus.

An insulator

for one of the circuit breakers

on the

bus was found to be damaged,

which

provided

a shorting path to ground.

The licensee

evaluated

the

damaged

insulator

and determined that

a modification to the breaker

design

was

necessary.

Unit 2 scrammed

on February

6 due to an unrelated

problem.

A new type of distribution breaker

was installed in both of the Susquehanna

units prior to their startup.

~Back round

The Unit

1 reactor

had been previously

shutdown

on February

1,

1990 when

an electro-hydraulic control

(EHC) system leak was discovered

on the Unit

1

main turbine

number

4 control valve.

A power reduction

began at 8:55 a.m.,

February

1,

1990, to repair the leak.

The shutdown

was performed in a

controlled manner

by manually inserting individual control rods prior to

a manual reactor scram at

17 percent

power at 1:50 p.m.

Cold Shutdown

was

entered at 2:40 a.m.

on February 2,

1990.

It was necessary

to cooldown

below hot shutdown conditions,

since the

EHC leak could not be isolated

from the turbine bypass

system

and control of these

valves is needed for

decay heat

removal

in hot shutdown.

The licensee

was making preparations

to startup

from this short duration outage

when the loss of shutdown

cooling occurred.

3.0

Se uence of Events

During

a plant startup

on February

3,

1990 at 5:53 p.m., the licensee

declared

an alert condition due to a loss of shutdown cooling with reactor

temperatures

exceeding

200 degrees

F.

Prior to the loss of shutdown

cooling, the operators

were establishing

the conditions necessary

to test

the backup

power supplies for the "A" and "B" Reactor Protection

System

(RPS)

busses.

The licensee

expected certain

system isolations to occur as

a result of deenergizing

the "B" RPS bus,

such as,

Reactor Water Cleanup

(RWCU) and Residual

Heat

Removal

in the

SDC mode.

They prepared for the

isolations

and manually initiated the Standby

Gas Treatment

System

(SGTS).

One reactor recirculation

pump was started prior to the start of the

surveillance.

I

When the normal

power supply to the "B" RPS bus

was deenergized

for the

surveillance,

the backup

power supply circuit breakers

could not be closed

to reenergize

the bus.

The normal

and backup

supply breakers

were then

manually closed in sequence

but subsequently

tripped.

The deenergized

"B" RPS bus caused

a number of programmed isolations to occur,

including

the

shutdown cooling (SDC)

system

and the reactor water cleanup

system

(RWCU).

The reactor coolant

began to heatup without the

SDC in operation.

The licensee

declared

an alert when the reactor coolant temperature

exceeded

200 degrees

F.

The loss of SDC procedure directed

the operators

to open

Safety Relief Valves (SRVs),

as

needed,

with the reactor coolant temperature

above

212 degrees

F.

Three

SRVs were opened.

The open

SRVs along with

the inflow from the control

rod drive system

in the feed

and bleed

mode,

were found to be sufficient to stabilize the reactor coolant temperature

at approximately

250 degrees

F.

Shutdown cooling was reestablished

at

11:02 p.m.

and the reactor coolant temperature

was below 200 degrees

F by

12:15 a.m.,

February 4,

1990.

The Alert was terminated at 12:25 a.m.

No

radioactivity was released offsite during the event

and

no personal

contamination

occurred.

4.0

Emer enc

Plan

Im lementation

At 5:25 p.m., the operations staff recognized that

an Alert condition would

be reached

following the loss of the "B" RPS

bus

and the inability to restore

shutdown cooling prior to reaching

200 degrees

F in the reactor coolant

system.

Callout for Technical

Support Center

(TSC) manning

commenced prior

to reaching

the Alert condition.

The Alert condition was correctly classified

and declared

at 5:53 p.m.

Accountability was initiated immediately following

the event declaration

and was completed within 29 minutes.

Notification

of the Alert was transmitted to the State

and County emergency

response

organizations

at 5:56 p.m.

and to the

NRC at 6:00 p.m.

At 6:30 p.m.

the

NRC Senior Resident

Inspector

was notified.

The

TSC was fully manned

and

activated at 6:45 p.m.

Assumption of command

and control by the

TSC occurred

at 7:30 p.m.

The Media Operations

Center

(MOC) was

manned at 7:25 p.m.

Operators

exhibited familiarity with the Abnormal Operating

Procedure

used

to provide

an alternate

method of Decay Heat

Removal during the loss of

shutdown cooling (SDC) and with the

Emergency

Plan

Implementing Procedures

used during the event.

The reactor coolant temperature

was stabilized at

approximately

250 degrees

F at about 8:00 p.m.

and maintained there until

SDC was restored

at 11:02 p.m.

Control of the plant was maintained at all

times throughout the event.

The Reactor Coolant temperature

was reduced

below 200 degrees

F at 12: 15 a.m.

on February

4,

and the Alert was terminated

at 12:25 a.m.

Overall

implementation of the emergency

plan onsite

was well coordinated

and effective.

However,

a few areas

where

improvements

could be

made

were noted with respect

to communications with the

news media during the

event

an'd should

be addressed

by the licensee

in order to preclude

any

future recurrences.

Specifically,

a delay in opening the

MOC exacerbated

the

news media desire for immediate information for ongoing events.

This

occurred

due to difficulty in contacting

the

on duty Public Information

Manager (PIM).

The first media contact

from the

MOC occurred at 7:45 p.m.

Although the licensee

has several

backup

PIMS, they were not immediately

available.

1

~P

imp

The licensee

held

a critique of their emergency

plan implementation

in

order to identify areas of weak performance

or other problems which had

been

encountered

during the emergency.

Their assessment

identified the

problems with communications,,with

the

news

media

and the

need to assure

that

a

PIM is available for press inquiries much earlier during an event.

A task force comprised of senior

management

and

headed

by the chief

executive officer has

been established

to explore various

ways of improving

communications with offsite agencies.

5.0

Reactor Protection

S stem

RPS

Power

Su

1

Electrical

Desi

n

5.1

RPS

Power Distribution

RPS bus "B" ( 120V AC single phase)

gets its power supply from 2 sources:

1) the normal

power supply from the

RPS

M-G set

"B" and 2) the alternate

power supply from MCC 18261 through

a step

down transformer.

A selector

switch located

on the main control board allows the operator

to select

the

power supply from either

one of these

power sources

through

2 contactors.

The

RPS

bus "B" power distribution is housed

in cabinet

1Y201B which contains

7 circuit breakers,

CB2B through

CB8B.

Circuit breaker

CB8B provides

control

power to the reactor trip system,

the nuclear

steam

supply shutoff

system

(NS4)

and

scram discharge

volume panel

"B".

When the incident

happened

on February

3,

1990, Unit

1 was in Condition

4 (cold shutdown).

The

RHR system

was in the shutdown cooling mode.

The

RHR inboard containment

isolation valve HV1515009

and outboard containment isolation valve HV151F008

were

open to provide the

shutdown cooling suction path.

When

RPS

bus "B"

lost power due to

a ground fault in circuit breaker

CBBB, several

of the

isolation valve interlocking relays

(K88 for the inboard valve and K95,

K92 and

K30 for the outboard valve) were deenergized,

causing

the inter-

locking contacts

to close.

The closure of these

contacts

allows the

valves'losing

coils to be energized,

thus closing the inboard

and outboard

isolation valves.

These

valves cannot

be reopened until power is restored

to

RPS

bus "B".

5.2

RPS

Bus "B" Hardware Confi uration

RPS bus "B" power distribution panel

1Y201B, about

3 feet wide and

4 feet

high, is classified

as non-safety related

equipment.

It contains

2

contactors

(K1B and K2B), one 2-pole,

200

amp circuit breaker

(CBlB, for

alternate

power supply),

two 100

amp circuit breakers

(CB2B and CB8B),

one

30

amp circuit breaker

(CB3B) and four 15

amp circuit breakers

(CB4B through

CB7B).

The two contactor s are operated

from the selector

switch in the

control

room to allow selection of the power source either from the "normal"

or the "alternate"

power supply.

The

seven single-pole,

General Electric

type

TEB molded case circuit breakers

were mounted

on

a vertical metal

mounting plate.

Each of the circuit breakers

was supported

by two copper

extension bolts which were also

used for power connections,

one for power-in,

one for power-out.

For circuit breaker

CBBB, which had caused

the ground

fault problem,

the power-in bolt is about 3/8" in diameter

and 5" long

(see

Figure

1 for more detail),

One

end was secured

to the circuit breaker

and the other

end

was connected

to the power-in terminal lug.

The copper

extension bolt passed

through

a hole in the metal mounting plate.

An inner

cylindrical sleeve

about

30 mils thick made of impregnated

paper

separated

the copper extension bolt and the metal

mounting plate.

This sleeve

serves

as

an insulator

between

the power conductor (the bolt) and the metal

panel

which is at ground potential.

An outer sleeve

(the collar), slightly larger

and

much thicker than the inner sleeve,

also

made of impregnated

paper,

was

used for securing

the copper extension bolt.

The bolt was tightened

by lock-nuts,

compressing

the collar against

the metal

mounting plate.

The inner sleeve is brittle.

Damage'r

cracking of the sleeve

could

create

an electrical

path which in turn could cause

the insulation to

deteriorate,

leading to complete insulation failure,

In addition,

the

licensee

discovered that the inner sleeve of CB88 was shorter

than it

should

have

been,

leaving

a small portion of the copper extension bolt not

covered with insulation.

The licensee

determined that the ground fault

was

a result of the copper extension bolt touching the metal

mounting

plate.

The inner

sleeve

removed

from CBBB indicated

excess

damage at one

end of the sleeve.

Part of the bolt was also

damaged

due to electric

arcing.

Excessive

leakage current from the bolt to the metal

panel

caused

the upstream circuit breakers

to trip, resulting in the loss of power to

RPS

bus "B".

5.3

Previous

RPS Circuit Breakers

Failures

The inspector

reviewed three

Licensee

Event Reports

(LERs) of previous

RPS

circuit breaker failures.

One applies

to Unit 1,

two apply to Unit 2.

LER 89-020 reported termination/mounting

problems with RPS circuit breaker

CB8B.

These

problems

caused

numerous

power interruptions

in the "B" RPS

distribution systems

of Unit l.

Each interruption resulted

in the actuation

of several

engineered

safety feature

(ESF)

systems

and components

(initiations of the Standby

Gas Treatment

System,

Control

Room Emergency

Outside Air Supply System,

isolations of HVAC Zones

I and III, Reactor

Water Cleanup

System

and Reactor Recirc

Pump cooling water isolation).

On

July 2,

1989,

the

ESF actuation

signals

occurred

three times,

caused

by

CB8B trips.

This circuit breaker

was subsequently

replaced.

On July 5,

1989,

the short circuit in the mounting stud of CBBB caused

the upstream

Electrical Protection

Assembly to trip, causing

loss of power to the

RPS

"B" bus.

The mounting stud was subsequently

reworked (changed

the orienta-

tion of the insulation sleeve),

LER 85-010 reported that

on February

23,

1985, circuit breaker

CB8B in

Unit 2

RPS

power distribution panel

2Y201B tripped prematurely three times,

each

caused

a reactor "half scram",

main

steam isolation valve logic

"half isolation", auto start of the 'B'tandby

Gas Treatment

System,

isolation of Reactor Water Cleanup

System,

closure of the containment

isolation valves for the Hydrogen-Oxygen Analyzers

and Containment

Radia-

tion Monitors and isolation of cooling water to the Reactor Recirculation

Pumps.

CBBB was subsequently

replaced.

LER 85-018 reported that

on May 29,

1985 circuit breaker

CB8B in 2Y201B

'ripped prematurely twice.

The circuit breaker

was subsequently

replaced.

These

LERs indicated that failures identical to the failure that occurred

on July 5,

1989 in

Unit 1 and similar failures

had occurred to the

RPS

trip logic circuit breakers.

For those

instances,

the licensee

corrected

the problems,

but they did not conduct

a rigorous root cause

analysis of

the failures.

This was

a result of the nonsafety classification of the

RPS

power

supply.

No loss of shutdown cooling occurred

as

a result of

these failures because

the reactor

was operating.

5.4

RPS

Power

Su

1

Modification

Following the February

3,

1990 loss of shutdown cooling incident,

the

licensee

decided to modify the design of the existing

RPS power distribution

panels

(1Y201A and

1Y201B).

On February

6,

1990,

the licensee

issued

Plant

Modification Package

DCP No. 90-2006.

The modification included the

following changes:

1.

Circuit breakers

CB3B through

CB8B, mounting plate

and hardware,

hot

bus

and standoff hardware

(CB2B is mounted separately

on

a non-metal

plate,

not affected)

were

removed

from panel

1Y201B.

2.

The above circuit breakers

were to be replaced with GE type

TEY

breakers,

mounted

on

a

GE 3-phase distribution panel

(P/N AEF31125B).

Only one

phase

was used.

3.

The

new panel

was to be mounted inside

1Y201B.

4.

The

same

changes

apply to panel

1Y201A, except the circuit breakers

to be replaced

were

CB2A through

CB7A.

(CB8A is mounted separately

on

a non-metal plate,

not affected).

5.

The modification was completely within panels

1Y201A and

1Y201B,

between existing circuit breaker

CBlA (for 1Y201A),

CB1B (for 1Y201B)

and existing load conductors.

The system logic was unchanged.

The above modification for Unit

1 was completed

on February 9,

1990.

In

order to shorten

the time during which power from the

RPS distribution

panel

was unavailable,

the licensee

installed

a temporary panel

which con-

tained

6 circuit breakers with current rating corresponding

to the

6

circuit breakers

to be replaced.

The

RPS power supply was transferred

to

the temporary

panel while the circuit breaker

replacements

were taking place.

The power supply transfer

was accomplished

through manipulation of the two

Electrical Protection Assemblies

upstream of the

RPS distribution panel.

A procedure

(TP-158-013,

dated

February

2,

1990) entitled "Installation

and

Removal of Temporary

Power to

RPS Panels

Loads

1Y201A and

1Y2018 for

Performance

of Modification Work" had

been

developed

by the licensee

to

cover the power transfer activities, including circuit breaker testing.

The licensee

stated that the

RPS

power distribution panels for Unit 2 would

also

be modified.

The

same modification package

and the

same

procedure

for temporary

power transfer applied to Unit 2.

At the conclusion of this

inspection,

the modification work for Unit 2 had not been started.

However,

following the inspection

the inspector

was informed that the modifications

for both panels

(2Y201A, 2Y2018) were completed

on Sunday,

February

11,

1990.

The inspector

reviewed the modification package

and the procedure for

temporary

power transfer.

No deficiencies

were identified.

5.5

Ph sical Observation

of Unit

1

RPS

Power

Su

l

Modification

The inspector physically observed

the existing circuit breakers

and the

mounting hardware

before they were replaced,

and the

new circuit breakers

in Unit

1 after they were installed.

The inspector

observed

that the

mounting configuration of the

new circuit breakers

are substantially

different from the old ones.

The inspector determined that the

new

installation eliminates

the short circuit problem observed

in the old

circuit breakers.

The inspector also observed

the process

for the

RPS power supply to be

transferred

from the

RPS

bus "A" power distribution panel

to the temporary

panel,

including splicing of the affected cables.

No deficiencies

were identified.

6.0

Findin

s and Conclusions

The Senior Resident

Inspector

was contacted

at

home

and arrived onsite at

7:00 p.m.,

February

3,

1990.

The operators

completed actions

per procedure

ON-149-001,

Loss of RHR shutdown cooling mode

and continuously monitored

cooling effectiveness

to ensure

adequate

core cooling.

Other activities

were observed

throughout

the event.

It was noted that the licensee's

actions

were appropriate

and directed

toward plant safety.

The licensee

promptly recognized

that

an Alert condition would soon

be

reached

and

made the correct classification

and declaration.

In addition,

appropriate

emergency

response

organizations

were notified in a timely

manner.

The operators

were familiar with and properly followed the proce-

dures required for the event.

As a result, plant conditions were stabilized

in

a timely manner

pending recovery

from the event.

Overall implementation

of the emergency

plan onsite

was well coordinated

and effective,

and the

licensee's

handling of the event

was commendable.

10

Due to problemMs experienced

during the event,

the licensee

is taking

steps

to explore ways to improve communications with the

news media

and

local

emergency

response

organizations.

These

are

good initiatives

by the licensee

to ensure

timely and accurate

information is provided

to the public.

Following the loss of shutdown cooling,

the licensee

promptly determined

the cause

of the problem

and quickly initiated corrective actions to restore

the

shutdown cooling capability.

The root cause of the circuit breaker

failure was subsequently

identified.

A design modification of the Unit

1

RPS

power distribution panels

to deal with the root cause

was completed

before the conclusion of this inspection.

An identical modification was

made to the Unit 2

RPS power distribution panels.

The inspector

was informed

that the Unit 2 modification was completed

on February ll, 1990.

These

modifications should eliminate repeat

problems

in the future (identical or

similar circuit breaker failures occurred

in 1985 for Unit 2,

and in 1989

for Unit 1).

The inspector determined that the licensee's

corrective

actions for this event were adequate.

The licensee

completed

the review of their safety-related

equipment list

about

a week following conclusion of this inspection.

The licensee deter-

mined that

GE circuit breakers with similar mounting configurations

are

not used

in any safety-related

systems

in Susquehanna

Unit

1 or 2.

~Ei

M

At the conclusion of the inspection

on February

9,

1990,

the inspectors

met with the licensee

representatives

denoted

in Appendix

1.

The

inspectors

summarized

the

scope

and results of the inspection at that

time.

At no time during this inspection

was written material

given to the

licensee.

APPENDIX

1

Persons

Contacted

1.0

Penns

lvania

Power

& Li ht

Com an

J. Blakeslee,

Assistant

Supt. of Plants

R. Bogar, Electrical

Maintenance

Supervisor

AD Dominguey, Operation,

Senior Results

Engineer

D.

McGann,

Compliance

Engineer

  • D. Roth, Senior Compliance

Engineer

  • P.

Rusanowsky,

Compliance

Engineer

  • E. Stanley,

Supt. of Plants

2.0

Commonwealth of Penns

lvania

DER/BRP

  • S. Maingi, Nuclear Engineer
  • D. Ney, Nuclear Engineer
  • Denotes

those

personnel

present at the exit meeting

on February

9,

1990.

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