ML17138A456

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IE Insp Repts 50-387/78-15 & 50-388/78-13 on 780821-0921. Noncompliance Noted:Failure to Qualify Welders & Failure to Use Specified Curing Compound for Spray Pond
ML17138A456
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 10/17/1978
From: Gallo R, Mcgaughy R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17138A455 List:
References
50-387-78-15, 50-388-78-13, NUDOCS 7812110291
Download: ML17138A456 (16)


See also: IR 05000387/1978015

Text

U.S.

NUCLEAR REGULATORY COMMISSION

OFFICE

OF INSPECTION

ANO ENFORCEMENT

Region I

5 .5~

5

-388/78-13

License

No.CPPR-101

CPPR-102 Prior ity

Licensee:

Penns

lvania

P wer and Li ht

Com an

Category

A

2 North Ninth Street

Allentown

Penns

lvania

18101

Facility Name:

Sus

uehanna

Steam Electric Station, Units

1

and

2

Inspection at:

Berwick, Pennsylvania

Inspection conducted: August 21-September

21,

1978

Inspector

. al

.

M. Gallo,

'i

nt Reactor

Inspector

date

signed

date

signed

date signed

y/

R.

W. McGaughy,

ef

Projects

Section,

dat

si

ned

s gned

Reactor Construction

and Engineering Support

Branch

Ins ection

Summar

Ins ections

on Au ust 21-Se

tember

21

1978

Re ort Nos.

50-387 78-15 and 50-388 78-13

Approved by:

Unit

1

and

Common, Areas

Ins ected:

Routine inspection

by the resident inspector of work

activities relative to: installation

and welding of reactor coolant pressure

boundary

and

other piping; installation of reactor

vessel

internals;

storage of reactor

vessel

8 inter

nals;

site calibration control; and Spray

Pond concrete

placements.

The inspector also

performed plant tours

and revierled licensee

action

on previously identified items.

The

inspection involved 87 inspector-hours

by the

NRC resident inspector.

Results:

Of the six areas

inspected,

no items of noncompliance

were identified in four

..

areas;

two apparent

items of noncompliance

were identified in two areas.

(Infraction-fai 1

ure to qualify welders for the welding process

in use-Paragraph

7.c.(2); Infraction- fail-

ure to use specified curing compound for Spray Pond-Paragraph

9.b.)

Unit 2 Areas

Ins ected:

Routine inspection

by the resident. inspector of work activities re

lative to: installation

and welding of reactor coolant pressure

boundary piping; handling

d storage of reactor, vessel

internals;Rand

storage of reactor vessel.

The inspector al-

performed plant tours

and reviewed licensee

action

on previously identified items.

The

nspection

involved 28 inspector-hours

by the

NRC resident inspector.

Results:

No items of noncompliance

were identified.

1Feg>on

1

Form 12

(Rev. April 77)

DETAILS

Persons

Contacted

Penns

lvania Power and Li ht

Com an

L.

R.

E.

J.

H.

R.

A.

Ballard, Site

QAE

Beckley, Site

QAE

Carroll,, Site

QAE

Green,

Resident

NQA 1/2/3/4/5

Harris, Protect Construction

Manager

Prego, Site

QAE

R. Sabol,

Manager,

Nuclear Quality Assurance

Bechtel

Cor oration

Y.

M.

J.

P.

D.

K.

R.

M.

G.

H.

J.

J.

A.

R.

H.

K.

E.

J.

J.

H.

J.

A.

Ananda, Civil QAE

K. Boone,

Lead. Welding Engineer

A. Dahnert,

QC Engineer-Piping

R. Delorme, Welding Engineer

Dharia, Subcontracts

Engineer

Durland,

QC Engineer-Welding

Drake, Superintendent-Night Shift

A. Drucker, Electrican

QAE 2/3/4/5

Gelinas,

QC Lead Engineer Piping/Mechanical

Goodvin,

QC Engineer-Civil

Hoagland,

Construction Assistant

Khandar,

Mechanical

OAE

Kontura, Mechanical

QAE

Lamb,

QC Assistant

Lead Engineer-Welding

Lilligh, Project

QAE 1/3/5

Stout, Assistant Project Field Quality Control Engineer 2/5

Strzelecki,

QC Lead Engineer Instrumentation

Van Omen, Subcontractor Administrator

5

Vidunas,

QC Lead Engineer Receiving

Oman,. Field Engineer Storage

and Maintenance

O'ullivan, Assistant Project Field Engineer

3

Spielhagen,

Project Field Engineer

2

General Electric, Com an

Nuclear Ener

Division

NED

E.

T.

R.

A. Gustafson,

Site Manager

2

M. LeVasseur,

QC Representative

2/5

M. Pulsifier, Mechanical

Engineer

Installation

and Service

En ineerin

IPSE -Reactor Internals

F. Forsythe,

Si te Manager

D. Hess,

QC Engineer

T. Sartain,

Welding Engineer

Dick Cor oration

J. Borst,

FQC Manager

R. Hudak,

QC Inspector

Peabod

Testin

Com an

M. Whalen,

NDE Supervisor

l.

/ denotes

those present at Exit Interview August 25,

1978

2.

/ denotes

those present at Exit Interview September

1,

1978

3.

/ denotes

those present at Exit Interview September

8,

1978

4.

/ denotes

those present at Exit Interview September

15,

1978

5;

/ denotes

those, present at'xit Interview September

21, 1978',

The inspector also interviewed other

PPSL employees

as well as

employees of Bechtel,

Dick Corporation,

Peabody Testing

Company,

and General Electric Company.

Plant Tour

The inspector

observed

work activities in-progress,

completed

work

and plant status

in several

areas of'he plant during general

inspection of'he plant.

The inspector

examined

work for any

obvious defects or noncompliance

with- regulatory requirements or

license conditions. Particular note was taken of presence

of

quality control inspectors

and quality control evidence

such

as

inspection records,

material identification, nonconforming material

identification, housekeeping

and equipment preservation.

The

inspector

interviewed craft. personnel,

supervision,

and quality

inspection

personnel,

as

such personnel

were available in the work

areas.

No items of noncompliance

were identified.

3.

Licensee Action on Previous

Ins ection Findin

s

(Cl'osed)

Unresolved

Item (387(388(78-02-02):

Improved maintenance

of items released

from the warehouse

but not yet installed.

The licensee

had initiated Deficiency Report

No.

0085 to document

specific conditions previously observed

by

NRC inspectors.

Valves HBB-BF-15703R and GBB-'T-F010A and

B were observed with end

caps in place.

Final inspection of these

valves for internal

cleanliness

is done prior. to closure in accordance

with QCI

P 1.10

Revision II.

The response

to Deficiency Report 0085 states

that the corrective

action regarding this, matter included meetings with craft and

supervision

to emphasize

the importance of maintaining

and re-

placing end caps,

assignment of craft personnel

to replace

end caps

at the end of each shift, and

a daily survey

by Field Engineering

prior to the start of the day shift to verify that end caps

are

replaced

and to identify discrepant conditions.

The inspector

verified by discussions

with assigned

individuals that Field

Engineering

personnel

are conducting the required surveys that

QC

personnel

are monitoring this activity. Field Engineering

and

QC

personnel

stated that their surveys

included observation of the

condition of all safety related

equipment in temporary or in-place

storage.

Nonconforming conditions noted are processed

in accor-

dance with Project Special

Provisions

Notice SF/PSP

8G-6.1

Revision

0 or field inspection

procedure

G-3 as appropriate.

The inspector

reviewed the following additional

documentation

regarding this

matter:

Nonconformance

Report

No.

2953

In Process

Rework Notice Nos.

2540,

2543,

2544,

2545

PPSL: letter to. Bechtel

PLB-8575

Bechtel letter to PP8L

BLP 9374

QCIR 73.0-M 204-HBB-116-1

(1)

QCIR 49.0-M 204-GBB-115-1

(2)

The inspector

had no fur ther questions

on this matter at this time.

4.

Reactor Coolant Pressure

Boundar

and Safet

Related

Pi in

Weldin

)

The following listed activities were examined

and verified that

they were being pei formed in accordance

with the

ASME Section III

and IX codes,

PSAR Appendix D, the Bechtel guality Assurance

Manual

Section III, Site Specification

M 204,

and drawings

M-198 and

M-

199.

W~iN

-U i

Fitup, alignment

and welding of joint GBC-101-1

FW 14.

Welding of joint HRC-'2-4

FW

16.

Welding of joint SP-DCA-M 78-35-BW 8 R-2.

-Unit 2

Welding of joint DLA-201-1

FW 3.

The inspector verified selected

detailed

drawings, welding

procedure,

base

and filler metal certifications, welder

qualification, quality control documentation,

weld appearance,

welding variables

such

as

gas flow and amperage,

and non-

destructive testi'ng activities

as appropriate.

b.

Non-Destructive Testin -Unit

1

Liquid Penetrant

testing of weld joint Nos.

SP-DCA-M 78-4-FW"8 (c) R-l.

GBB-109-2

FW l-l (Excavation).

GBB-109-2

FW 12 (Excavation).

VNB-B21-2

FW A15.

The inspector verified'surface preparation,

qualification of

examiners,

and testing technique.

No items of noncompliance

were identified.

5.

Reactor Coolant Pressure

Boundar,

and Safet

Related

Pi in

a.

Piping System Activities.

The inspector

examined

work activities for the Main Steam

System- Line

B inside containment- and Main Steam Relief Lines

for Line B.

The inspector verified that the activities

exam-

ined were in accordance

with the

ASME Code Section III, PSAR

Appendix D,

FSAR Sections

5.4.9

and 10.3,

the Bechtel guality

Assurance

Manual Section III, GE Specification

22A 4628,

Bechtel Specifications

M-201, M-204 and drawings

M-199,

VNB

B21-2,

GBC 101-12-1

and GBC-101-30-1.

The inspector observed

handling, installation, protection,

initial alignment,

and identification.

The inspector

reviewed

associated

gC inspection records, verified material certifications,

and reviewed

gC Engineering certification records.

b.

The inspector

examined

two partially completed piping runs

and

verified that they were installed in accordance

with approved

drawings

and specifications.

Piping runs

examined were:

(1)

The 20"

RHR piping. from containment penetration

X-12 to

.pipe spool

DCA-108-1-3.

The inspector verified conformance

to

FSAR Section 5.4.7

and

drawings

DCA-108-1

and M-151.

(2)

The

RHR Service Water System Spray

Pond Network B-l.

The inspector verified conformance with FSAR Section 9.2.6

and

drawings

HRC-2-4, HRC-2-11,

M-80-1 and M-80-2.

No items of noncompliance

were identified.

6.

Reactor

Vessel Installation Units

1

and

2

The inspector

examined protection of the installed reactor vessels

and stored closure heads'for

compliance with site procedures

and

PSAR Appendix

D commitments.

The inspector

reviewed the procedural

requirements for vessel

protection

and verified that required

inspections

and preventive maintenance

were being completed.

The

inspector observed

that openings

were covered

as required,

work

platforms inside the Unit I vessel

were nonflamable

and that Unit I

access

was controlled.

The inspector also observed

the condition

of a selected

closure

head stud hole to verify freedom from rust

and condensation.

Documentation

reviewed

by the inspector included

Field. Inspection

Procedure

6-5, Revision 0.

Project Special

Provisions Notice SF/PSP

G-5.1, Revision 3.

Equipment Maintenance

Requirement

and Record

Form for

Unit

1

and

2 Reactor Vessels

and for Reactor

Vessel

Closure Heads.

No items of noncompl.iance

were identified.

7.

Reactor Vessel

Internals

a.

Protection of Stored

Vessel Internals-Units

1

and

2

The inspector

examined protection of the stored reactor vessel

internals for compliance with site. procedures

and

PSAR Appen-

dix D commitments.

The inspector

reviewed the procedural

require-

ments for internals protection

and verified that required inspec-

tions were being completed.

The inspector

observed

the in-plant

storage of the Unit

1

Steam Dryer and the shroud

head

and separator.

The inspector

also observed

the movement

and subsequent

in-

plant storage of the Unit 2 Steam Dryer and shroud

head

and

separator.

The inspector

noted that

NCR was issued

by guality

Control regarding

the storage 'ondition of these

components.

The. inspector also noted that the equipment maintenance

requirements

and record form for the aforementioned

Unit 2 components

had

not been rewritten to reflect their movement to in-plant

storage.

Documentation

reviewed by the inspector included:

Field Inspection

Procedure

G-5, Revision 0.

Project Special

Provisions Notice SF/PSP

G-5..1, Revision

3.

Equipment Maintenance

Requirements

and Record

Form for

Unit

1 and

2 Steam Dryer and the Shroud

Head

and Separ-

ator.

The inspector stated that the disposition of NCR and the

revised

equipment maintenance

requirements

and record form for

the aforementioned

Unit 2 components

would be examined during

a future inspection.

(388/78-13-01 )

II

b.

Handlin

of Internals-Units

1

and

2

The inspector

observed,. lifting and handling of the Unit 2

Steam

Dryer

and the shroud

head

and separator

from temporary

storage silos to in-plant storage.

The inspector also observed

the installation

into the reactor pressure

vessel of the

Unit

1 shroud.

The inspector verified that the lifting and

handling were consistent with established

requirements, lifting

equipment

was

as specified

and testing

completed prior to

lifting, and placement

and installation

were in conformance

with requirements.

Documentation

reviewed

by the inspector

included:

GE I8SE Procedures

160 A71211 Revision 0,

160 A71210 Revision 1,

160 A81201 Revision l.

Bechtel

FCI-M-156, Revision

1 for dynamicload testing of

crane.

No items of noncompliance

were identified.

c ~

Installation of Internals-Unit

1

(1)

The inspector

observed

completed

work and work in progress

relative to the installation, of'elected reactor internals

components.

Items inspected

included:

jet pump

beam

bolt tensioning,. jet pump head

beam bolt-tack welds,

and

jet pump riser to brace

arm welds.

Except

as noted in

Paragraph

(2) below the inspector

determined that work

procedures

were being followed; installation

was in

accordance

with specifications

and

gC inspection activ-

ities were in accordance

with established

procedures.

The

inspector

reviewed selected

documents relative to this

work including:

FSAR Section

3.2

GE drawings

197F 633, Revision 8;

117C 4354, Revision

8

GE Specification

22A 4273 Revision

2

GE I8SE Jet

Pump Installation Travelers

11T

GE IPSE Jet

Pump

Head Bolt Tensioning Special

Beam

Process

Control Sheets

No. 115-15.

GE IPSE Jet

Pump

Beam Bolt Tack Weld Joint Process

Control Sheets

11J-21

Except as noted below,

no items of noncompliance

were identified.

(2)

The inspector

examined the completed jet pump riser to

jet pump brace

arm welds for jet pumps A,B,C,D,F,G, and

H.

The welds examined

met the requirements

of the following

General Electric Drawings:

GE Drawing 117C 4354 Revision 8.

GE Drawing 197R 633 Revision

8

The welds required

by these

drawings are partial penetration

single bevel flush contour groove welds.

The inspector

also

reviewed records relative to these

welds.

The records

included jet pump installation travelers,

joint process

control sheets,

visual

and liauid penetrant

examination. results,

material certifications for weld

electrode, certificationof conformance for base material,

welder qualification records,

and welder mock-up test

records.

Documents

examined were:

Jet

Pump Installation Traveler llT

Joint Process

Control Sheets

11J-12

and

13 for Jet

Pumps

A, B,

C,

D, F,

G, and H-includes record of

visual

and

PT examination

Material Certification for Weld Filler Metal-Heat

No.

C3548

R308L

GE Cerfiticates of Conformance

for Riser Brace

Arm

and Jet

Pump Risers

PgC Nos.-SJ

3371,

01249,

01237

Record of Welder Performance

Test in Accordance with

Welder gualification ISE-Wg-31.

10

Record of Mock-up Testing in Accordance with Mock-up

Test ll NU-3

GE

IPSE Weld and

NDE Information Spread

Sheet

160-

77E-D155 Revision

5

Detail

Weld Procedure

ISE-DWP-3004 Revision

1

Welder Qualification ISE-WQ-32 Revision 0-A

Welder Qualification

ISE-WQ-31. Revision 0-A

During this review the inspector

noted that Detail Welding

Procedure

ISE-DWP-3004,

a

Gas Tungsten

Arc Welding

(GTAW)

Process,. is specified for the jet pump riser to brace

arm

weld by GE Weld identification diagram 160-77E-0154.

This

GE Weld identification diagram requires

Welder

Qualification ISE-WQ-31 for this weld.

However, Detail

Welding Procedure

ISE-DWP-3004 requires

Welder Qualifi-

cation

ISE-WQ-32.

ISE-WQ-31 specifies

the use of a

consumablc insert,

where

as

ISE-WQ-32 does not.

, Welders

who had welded the jet pump

riser to jet pump brace

arm,

a weld with no consumable

insert or other backing,

were qualified only in accord-

ance with ISE-WQ-31.

The

ASME Boiler and Pressure

Vessel

Code Section IX, 1974 Edition, QW-356.1 lists

QW 404.22

as

an essential

variable for the performance qualification

of Gas Tungsten

Arc Welding.

QW-404.22 states,

"The

omission or. addition of preplaced

consumable

inserts.

Qualification in a singled-welded butt joint, with or

without consumable

inserts, qualifies for fillet welds

and single-welded butt joints with backing."

The failure to qualify welders for the welding process

used is'contrary. to the requirements

of 10 CFR 50,

'Appendix B, Criterion IX.

(387/78-15-01)

By letter. dated 'August 31,

1978,

to the Bechtel Field

'onstruction

Manager,

the

GE Installation

and Service

Engineering Site Manager stated that the brace

arm to

riser welds are considered

to be sound

and will perform

their intended fuction based

upon:

(1) Welder quali-

fication on

a brace

arm mock-up

(11

MU-3) prior to

welding the brace;

(2) inspection of the sectioned

mock-

up -indicated that deposited

welds were sound

and

had full

penetration;

(3) the'welders

were qualified to a proce-

dure similar to the one required;

(4) welders'erform-

ance

on these

and other welds

has

been excellent;

(5) the welds

had liquid dye penetrant

examination

(PT)

of the root and final pass

and were found acceptable.

The inspector

examined

the sectioned

mock-up and noted

that in addition to the requirements

of the procedure

used

in the production welding, one weld pass

had

been

made from

the opposite side of the weld.

It did appear that adequate

penetration

to meet the requirements

of the design weld

had

been achieved.

8.

Control of Measurin

and Test

E ui ment

The inspector

examined Bechtel's

program

and activities relative to

the control of measuring

and test equipment.

The inspector verified

that these activities were in accordance

with commitments

in the

PSAR Appendix D; Field Inspection

Procedure

G-4, Revision 6; Project

Special

Provisions Notice SF/PSP

G-4.1, Revision 2.

The inspector

examined the following relative to the above:

Measuring

and Equipment List, gC-G-4-1

Calibration Record

Card File

Out of Calibration Notices for CT 676 and

CT 538

Instrument Calibration Instruction 5, Revision

2

Calibration Test Report for CT 1243

No items of noncompliance

were identified.

9.

S ra

Pond Concrete

Work

a.

Concrete Activities

The inspector

examined

concrete

work activities in progress

for Spray

Pond placement

S-60.

The inspector verified, except

as noted in b. below, that these activities were in accordance

with commitments in the

PSAR Appendix D;

FSAR Section 9.2.7;

Bechtel Specification

C-36 and Dick Corporation Procedures.

12

The inspector

examined

the following activities relative to

the above:

placement

preparation,

delivery and placement,

wire mesh installation,

and curing.

Documents

reviewed

by the

inspector included:

Bechtel

Drawings

C-65 and C-66

Dick Drawings

SK 1-2

Concrete

mix test results truck 15 ticket 52322

Dick gC in process

records

including Pre-placement,

Placement,

Concrete

Placement

Release,

Concrete

Testing Record,

and Concrete

Curing Record.

Except as noted below,

no items of noncompliance

were identified.

C~id

d

During the inspection,

on September.6

and 7, 1978, of the

concrete acti vities in a.

above the inspector noted that the

contractor,

Dick Corporation,

was using

a c~ring compound

identified as

Horn Clear Seal

150.

The inspector

determined

that this product was

a Type

1 curing compound in accordance

with ASTM Specification

C309.

However,

Bechtel specification

C-36 Paragraph

7.4.9 (b) states

"Liquid membrane

curing com-

pound shall

be Type

2 in accordance

with ASTM C309-58."

On September

13,

1978,

Bechtel

approved Supplier Deviation

Disposition Request

No.

034 permitting the

use of the Type

1

curing compound.

On September

21,

1978,

the inspector

examined

40 completed

concrete

slabs

on the Spray

Pond. slopes.

Of these

40,

8 were

observed

to have

one or two hairline cracks of varying length.

Representatives

of the licensee

stated that the Spray

Pond

cracks

had

been noted previously and would be documented

and

dispositioned.

The inspector stated that the failure to use

the curing compound required

by Specification

C-36 was contrary

to the requirements

of 10 CFR 50, Appendix B, Criterion V.

(387/78-15-02;

388/78-13-02)

d

13

10.

Exit Interviews

At periodic, intervals.- during the course of this inspection,

meetings

were held with facil.ity management

('ates

and attendees

are denoted

in Detail 1) to discuss

inspection

scope

and findings.