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Category:Code Relief or Alternative
MONTHYEARML23354A0032024-01-19019 January 2024 Authorization and Safety Evaluation for Alternative Request Associated with Successive Inspections for Generic Letter 88-01 / BWRVIP-75-A Augmented Examinations ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML21280A0782021-10-27027 October 2021 Proposed Alternative to Use of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code Case N-893 (Epids L-2020-LLR-0147 and L-2020-LLR-0148) ML21230A2062021-09-0303 September 2021 Proposed Alternative to Use ASME OM Code Case OMN-28 ML21216A2202021-08-0505 August 2021 Proposed Alternative to Eliminate Certain Documentation Requirements for Pressure Retaining Bolting ML20322A0092020-12-10010 December 2020 Issuance of Alternative Requests 41-VRR-8 and 41-VRR-7 Regarding Certain Inservice Testing Program Requirements for Safety Relief Valves ML20280A7572020-11-0505 November 2020 Revised Safety Evaluation of Relief Requests GVRR-8, 11 PRR-1, 90 PRR-1, and 47 VRR-2 Regarding the Fourth 10-Year Interval of the Inservice Testing Program (EPID L-2018-LLR-0384 Through EPID L-2018-LLR-0387) ML20269A2002020-09-30030 September 2020 Request to Use a Provision of Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI (EPID L2020-LLR-0117 ML20252A1352020-09-0404 September 2020 Relief Request I4R-24 Associated with Residual Heat Removal Heat Exchanger Category C-A and C-B Examinations ML20188A2642020-07-0606 July 2020 Clinton Power Station, R.E. Ginna Station, Limerick Station, Nine Mile Point Station & Peach Bottom Station - Proposed Alternative to Utilize Code Case OMN-26 - Response to Request for Additional Information ML20113F0412020-04-30030 April 2020 Proposed Alternative to the Submittal Schedule for Certain Reports (COVID-19) ML20099D9552020-04-17017 April 2020 Request to Use Provisions in the 2013 Edition of the ASME Boiler and Pressure Vessel Code for Performing Non-Destructive Examinations ML20093M8202020-04-0303 April 2020 Exemption from Select Requirements of 10 CFR Part 26 (EPID L-2020-LLR-0014 (COVID-19)) ML20090A6522020-03-31031 March 2020 Verbal Authorization of Relief Request GVRR-9 ML20089A0072020-03-31031 March 2020 Verbal Authorization by the Office of Nuclear Reactor Regulation for Relief Request I4R-23 ML20089A0082020-03-29029 March 2020 Relief Request GVRR-9 Associated with Pandemic Related Issues - Inservice Testing Interval Extension for Motor Operated Valves ML20088B0222020-03-28028 March 2020 Relief Request I4R-23 Associated with Pandemic Related Issues - Examination of Containment Surfaces Requiring Augmented Examination (Category E-C) RS-20-020, Relief Request for Alternative Frequency to Supplemental Indication Requirements of 10 CFR 50.55a(b)(3)(xi)2020-02-28028 February 2020 Relief Request for Alternative Frequency to Supplemental Indication Requirements of 10 CFR 50.55a(b)(3)(xi) ML19228A1952019-10-28028 October 2019 Safety Evaluation of Relief Requests GVRR-8, 11-PRR-1 and 47-VRR-2 Fourth 10-Year Interval of the Inservice Inspection Program EPID L-2018-LLR-0384, EPID L-2018-LLR-0385, EPID L-2018-LLR-0386, and ML19269C5342019-09-27027 September 2019 Proposed Alternative to Use Encoded Phased Array Ultrasonic Examination Techniques ML19161A2572019-06-0404 June 2019 BWR Fleet Msv/Srv - Testing Frequency Relief Request NRC Pre-Application Meeting June 4, 2019 ML19098A0342019-04-30030 April 2019 Units 1 and 2; Limerick, Units 1 and 2; Peach Bottom, Units 2 and 3, and Quad Cities, Units 1 and 2 - Revision to Approved Alternative to Use BWR Vessel and Internal Proj Guidelins ML19099A2632019-04-22022 April 2019 Issuance of Relief Request 14R-08, Revision 1, Regarding Pressure Testing of Containment Atmospheric Control Penetration Piping ML19099A3072019-04-16016 April 2019 Issuance of Relief Request 14R-18 Associated with Inaccessible Supports for the Fourth 10-Year Inservice Inspection Interval Pipping ML19009A0022019-03-0505 March 2019 Issuance of Relief Request IR4-17, Revision 1, Reactor Pressure Vessel Nozzle Repair in Lieu of Specific ASME Code Requirements JAFP-19-0023, Relief Request Associated with the Use of Encoded Phased Array Ultrasonic Examination Techniques in Lieu of Radiography for Ferritic and Austenitic Piping Welds2019-02-15015 February 2019 Relief Request Associated with the Use of Encoded Phased Array Ultrasonic Examination Techniques in Lieu of Radiography for Ferritic and Austenitic Piping Welds ML18274A0152018-10-0101 October 2018 Relief Request 14R-OB, Revision 1, Associated with Pressure Testing of Containment Atmospheric Control Penetration Piping ML18165A0022018-06-11011 June 2018 Relief Request 14R-18 Associated with Inaccessible Emergency Service Water and Residual Heat Removal Service Water Pump Supports JAFP-18-0053, Proposed Alternative to Utilize Code Cases N-878 and N-8802018-05-30030 May 2018 Proposed Alternative to Utilize Code Cases N-878 and N-880 JAFP-18-0052, Proposed Alternative to Utilize Code Case N-8792018-05-30030 May 2018 Proposed Alternative to Utilize Code Case N-879 ML18129A3312018-05-0404 May 2018 Proposed Relief Request Associated with Reactor Pressure Vessel Nozzle Repairs ML17208A0902017-08-14014 August 2017 Relief Request I4R-17 Associated with the Alternate Repair of a 2-Inch Instrument Line Nozzle at Penetration N-16D on the Reactor Pressure Vessel ML17170A0132017-06-26026 June 2017 Proposed Alternative to Eliminate Examination of Threads in Reactor Pressure Vessel Flange (CAC Nos. MF8712-MF8729 and MF9548) ML17137A3072017-05-17017 May 2017 Verbal Authorization by the Office of Nuclear Reactor Regulation for Relief Request I4R-17 ML17004A0632017-02-0707 February 2017 Proposed Alternative Request GVRR-8 Inservice Testing Program Third 10-Year Interval ML16344A3242016-12-29029 December 2016 Safety Evaluation of Relief Request I4R-01 for the Fourth 10-Year Interval of the Inservice Inspection Program for Limerick Generating Station, Units 1 and 2 ML16301A4012016-11-21021 November 2016 Safety Evaluation of Relief Requests I4R-02 and I4R-10 for the Fourth 10-Year Interval of the Inservice Inspection Program for Limerick Generating Station, Units 1 and 2 ML16230A2372016-09-0606 September 2016 Fleet Request for Proposed Alternative to Use ASME Code Case N-513-4 (CAC Nos. MF7301-MF7322) ML12121A6372012-05-10010 May 2012 Request to Use Code Case N-789 ML0930803822009-11-17017 November 2009 Evaluation of Relief Requests Associated with the Third Inservice Testing Interval (TAC ME0742 - ME0751) ML0809803112008-04-30030 April 2008 Relief Request to Use Boiling Water Reactor Vessel & Internals Project Guidelines.. ML0312601152003-06-23023 June 2003 Relief Request Review, American Society of Mechanical Engineers Boiler and Pressure Vessel Code-Relief for Qualification Requirements for Dissimilar Metal Piping Welds ML0311300292003-05-0505 May 2003 Relief from Requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI, Concerning Check Valve Inservice Testing Program, MB4804 & MB4805 ML0306204912003-03-0303 March 2003 Relief, American Society of Mechanical Engineers Boiler and Pressure Vessel Code - Relief for Risk-Informed Inservice Inspection of Piping, MB4633 and MB4634 ML0208701612002-05-0202 May 2002 Evaluation of Relief Requests RR-05, RR-07, RR-12, Tables RR-12-5 and RR-12-9 and RR-13, Tables RR-13-8 (TAC Nos. MB1018 and MB1019) ML0210607752002-05-0202 May 2002 Evaluation of Relief Request RR-12, Table RR-12-6, Rotation of Snubbers and Relief Valves (TAC Nos. MB1018 and MB1019) ML0208604792002-03-15015 March 2002 Request for Relief, Alternative to ASME Boiler & Pressure Vessel Code Section XI Requirements for Class 1 & 2 Piping ML0201501402002-02-14014 February 2002 Evaluation of Relief Request RR-12, Table RR-12-7, Underwater Welding (Tac Nos. MB1018 and MB1019) ML0202502652002-02-14014 February 2002 Evaluation of Relief Request RR-04 - ASME Class 1, 2, 3 Snubbers Visual Examination and Functional Testing (TAC Nos. MB1018 and MB1019) 2024-01-19
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Temporary Verbal Authorization Project Manager: V.Sreenivas VERBAL AUTHORIZATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION FOR RELIEF REQUEST I4R-17 ALTERNATE REPAIR OF INSTRUMENT NOZZLE N-16D ON THE REACTOR VESSEL LIMERICK GENERATING STATION UNIT 2 EXELON GENERATION COMPANY DOCKET NO. 50-353 May 17, 2017 Technical Evaluation read by David Alley, Chief of the Component Performance, Non-Destructive Examination, and Testing Branch, Office of Nuclear Reactor Regulation By letter dated May 15, 2017 (Agencywide Documents Access and Management System Accession No. ML17135A423), with a supplement dated May 16, 2017 (ADAMS Accession No. ML17137A068), Exelon Generation Company, LLC (the licensee) requested relief from certain requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code (ASME Code),Section XI, at the Limerick Generating Station, Unit 2.
Pursuant to 10 CFR 50.55(a)(z)(2), the licensee submitted Relief Request I4R-17 associated with the alternate repair of a 2-inch instrument line nozzle at penetration N-16D on the reactor pressure vessel on the basis that compliance with the specified ASME requirements would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety.
During refueling outage Li2R14, the licensee discovered a leak at the instrument penetration nozzle N-16D as part of the routine system leakage test. The licensee proposed to repair the subject nozzle using a half-nozzle repair method based on applicable requirements of the ASME Code,Section XI. The licensee proposed to remove a portion of the existing nozzle penetration, install a new reinforcement pad onto the existing weld pad, weld a new nozzle to the new weld pad, weld a reducing insert to the new nozzle, and weld the existing piping to the reducing insert.
The licensee asked relief from various requirements of ASME Code,Section XI, such as flaw removal or reduction in flaw size, flaw characterization, post-weld heat treatment, and ambient temperature temper bead welding technique.
The NRC staff finds that the repaired nozzle is acceptable for fuel cycle 15 based on the licensees flaw evaluation, design analysis, and corrosion evaluation. The flaw evaluation showed that a postulated flaw in the existing Alloy 82/182 weld will not affect the reactor vessel base metal significantly during fuel cycle 15. The design analysis showed that the nozzle will not eject from the reactor vessel shell during fuel cycle 15. The corrosion evaluation showed that the reactor vessel base metal will not be significantly affected by general corrosion, crevice corrosion and galvanic corrosion during fuel cycle 15. The NRC staff further finds that the licensee satisfied the extent-of-condition inspection and that loose parts will not be a safety concern.
The NRC staff finds the hardship justification is acceptable because performing the repair in accordance with the ASME Code,Section XI would result in significant increase in radiological exposure.
The NRC staff finds that the licensee's proposed repair of Nozzle N-16D provides reasonable assurance of structural integrity and leak tightness for fuel cycle 15.
Temporary Verbal Authorization Project Manager: V.Sreenivas Authorization read by Rick Ennis, Acting Chief of the Plant Licensing Branch I, Office of Nuclear Reactor Regulation As Acting Chief of the Plant Licensing Branch I, Office of Nuclear Reactor Regulation, I concur with the Component Performance, Non-Destructive Examination, and Testing Branchs determinations.
The NRC staff concludes that the proposed alternative provides reasonable assurance of structural integrity and leak tightness of the instrument line nozzle at penetration N-16D on the reactor vessel. The NRC determines that complying with the ASME Code requirement would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety. Accordingly, the NRC staff concludes that the licensee has adequately addressed all of the regulatory requirements set forth in 10 CFR 50.55a(z)(2). Therefore, as of May 17, 2017, the NRC staff authorizes the use of relief request I4R-17 for fuel cycle 15, which is scheduled to end in the spring of 2019, at Limerick Generating Station Unit 2.
All other requirements of ASME Code,Section XI, for which relief was not specifically requested and authorized by the NRC staff remain applicable, including the third party review by the Authorized Nuclear In-service Inspector.
This verbal authorization does not preclude the NRC staff from asking additional clarification questions regarding Relief Request I4R-17, while preparing the subsequent written safety evaluation.