ML17059C112

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Insp Rept 50-220/98-11 on 980404-0609.Violations Noted.Major Areas Inspected:Review of Licensee Activities in Response to Failure to Properly Restore Safety Sys to Operable Condition & Resultant Degradation of Primary Containment Integrity
ML17059C112
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 06/26/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17059C110 List:
References
50-220-98-11, NUDOCS 9807070062
Download: ML17059C112 (20)


See also: IR 05000220/1998011

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket/Report No.:

50-220/98 5Q

License No.:

DPR-63

Licensee:

Niagara Mohawk Power Corporation

P. O. Box 63

Lycomiin, NY 13093

Facility:

Nine Mile Point, Unit 1

Location:

Scriba, New York

Dates:

April4- June 9, 1998

Inspectors:

Approved by:

B. S. Norris, Senior Resident Inspector

T. A. Beltz, Resident Inspector

R. A. Skokowski, Resident Inspector

W. A. Cook, Project Engineer

Lawrence T. Doerflein, Chief

Projects Branch

1

Division of Reactor Projects

9807070062

980626

PDR

ADOCK 05000220

8

PDR

EXECUTIVE SUMMARY

Nine Mile Point Unit 1

50-220/98-1

1

April 4 - June 9, 1998

This NRC special inspection report includes the results of independent inspection and a

review of licensee activities in response to the failure to properly restore

a safety system to

,an operable condition and the resultant degradation of primary containment integrity for

3.5 days.

PLANT OPERATIONS

A Unit 1 reactor operator failed to follow the operating procedure for restoration of the

containment spray system to its standby configuration resulting in the system being in a

degraded condition for 3.5 days.

This was a violation of Technical Specification 6.8.1,

involving the failure to implement procedures,

as written.

(VIO 50-220/98-11-01)

Between April 7 and 11, over sixty control panel walkdowns were unsuccessful

in

identifying this containment spray system mis-positioned valve.

This was a significant

operations staff oversight and indicative of a lack of attentiveness

to safety system

configuration.

In contrast, the in-plant operator's identification of the breaker open/closed

indicating lights deficiency demonstrated

good attention to detail, proper awareness

of

plant conditions, and prompt and appropriate response to a deficient condition.

The licensee's immediate action to conduct control panel system line-up verifications

without referring to the system operating procedures was a poorly founded decision based

upon the control room operators not having identified the flow control valve out-of-position

for 3.5 days by relying on unaided memory of proper systems'onfiguration.

The identification of FCV 80-118 as a primary containment isolation valve by the systems

engineer was good, but the oversight by the operations staff of this valve's primary

containment isolation function reflects poorly on their systems knowledge and sensitivity

to containment integrity monitoring. The failure to maintain primary containment integrity

for 3.5 days was a violation of the Unit 1 Technical Specification 3.3.0.

{VIO50-220/98-

1 1-02)

TABLE OF CONTENTS

EXECUTIVE SUMMARY

TABLE OF CONTENTS

~

III

I. OPERATIONS........... ~........ ~... ~..................

~ ~...

1

01

Conduct of Operations ....

'

~

1

01.1

Failure to Follow the Operating Procedure Resulted in the Unit 1

Containment Spray System Being Degraded

..

1

01.2

FCV 80-118 Primary Containment Isolation Function ...........

3

08

Miscellaneous Operations Issues ....................

~

~

~

~

~

~ 5

08.1

(Closed)

LER 50-220/98-04:

Containment Isolation Valve Left

Open in Violation of Technical Specifications Due to Personnel

Error 5

V. MANAGEMENTMEETINGS...

X1

Exit Meeting Summary

.

~ ..

~

~

~

~

5"

~

~

~

~

~

~

~ 5

ATTACHMENT

Attachment

1 - Partial List of NMPC Persons Contacted

- Inspection Procedures

Used

- Items Opened, Closed, and Updated

- List of Acronyms Used

REPORT DETAILS

Nine Mile Point Unit 1

50-220/98-1 1

April 4 - June 9, 1998

I. OPERATIONS

01

Conduct of Operations

01.1

Failure to Follow the 0 eratin

Procedure

Resulted in the Unit 1 Containment

S

ra

S stem Bein

De raded

a.

Ins ection Sco

e

71707'n

April 7, 1998, while operating at full power, the Unit 1 reactor operator (RO)

responsible for restoring the containment spray (CS) system to the standby

condition failed to close the remote manual test return valve.

This adverse

condition was not recognized for 3.5 days, even though there were over 60 control

room panel walkdowns conducted by three different operating shift crews.

The inspectors discussed the event with the Unit 1 Operations Manager and the

General Supervisor of Operations

(GSO) and conducted independent interviews with

the responsible

RO and several other ROs and senior reactor operators

(SROs) who

performed the panel walkdowns before the open valve was identified.

In addition,

the inspectors observed management

meetings related to the event, including a

Station Operations Review Committee (SORC) meeting, and reviewed the

associated

operating procedures,

the Unit 1 Technical Specifications (TSs) and

Updated Final Safety 'Analysis Report (UFSAR). The inspectors also conducted

an

independent walkdown of the control room panels to verify that all safety systems

were aligned properly.

b..Observations

and Findin s

On April 7, operators were using the ¹121 CS pump to lower water level in the

torus per NMPC Oper'ating Procedure N1-OP-14, "Containment Spray System."

As

required by the TSs, the appropriate Limiting Condition for Operations (LCOs) were

entered.

After the desired torus level was achieved, the Assistant Station Shift

Supervisor (ASSS) directed the operators to restore the containment spray system

to the standby condition, using Section "G" of N1-OP-14.

The Chief Shift Operator

(CSO) performed the portions of the procedure

in the control room and directed an

in-plant operator to perform those steps outside of the control room.

The inspectors

determined that the CSO was using a controlled'working copy of the procedure and

was using the "place keeping" method, of checking off the steps as they were

1 Topical headings such as 01, MS, etc., are used in accordance with the NRC standardized reactor inspection report outline.

Individual reports are not expected to address

all outline topics.

The NRC inspection manual procedure or temporary instruction

ITI) that was used as inspection guidance is listed for each applicable report section.

completed.

The day-shift crew that started the restoration completed steps G.1.1

through G.2.12.

This crew was then relieved by the night-shift crew.

The night-

shift CSO was tasked with completing the remainder of the restoration; specifically,

steps G.2.13 through G.2.19. At 8:23 pm, the CSO reported that the containment

system restoration was complete, and that the ASSS could exit the applicable TS

LCOs.

However, as discovered on April 11, the CSO failed to perform step G.2.18

which states,

in part, to verify closed valve 80-118, the containment spray test

return to torus flow control valve (FCV). The failure to properly complete step

G.2.18 of procedure N1-OP-14 is a violation of Unit 1 TS, Section 6.8.1, which

requires procedures to be implemented, as written.

(VIO 50-220/98-11-01)

The inspector. determined that for the remainder of the April 7 night shift, and

subsequent

shifts until April 11, the CSO or extra control room operator (CRE)

performed panel walkdowns every two hours, as prescribed by the Operations

Manager.

This expectation

is contained in the Nine Mile Point 0 erations Manual

(common to both units) and the Unit I Reference Manual (predecessor

to the

Operations Manual).

However, the inspector noted that there is no specific

guidance for the panel walkdowns, such as systems'alve

position checklists, to

ensure the standby configuration of each safety system.

Additionally, procedure

N1-ODP-OPS-0101, "Shift Turnover and Brief," requires each oncoming RO and

SRO to walkdown the control room panels prior to assuming the shift. This

requirement, likewise, does not provide specific guidance as to what the turnover

panel walkdown should accomplish.

As a consequence,

over 60 control room panel

walkdowns.were unsuccessful

in identifying the mispositioned FCV 80-118,

At approximately 8:30 am, on April 11, an in-plant operator noted that both the

open (red) and closed (green) indicating lights on the local panel for the FCV 80-118

motor operator breaker were not lit. After replacing the light bulbs, the operator

recognized that FCV 80-118 should be closed and immediately notified the control

room. The SSS directed that the valve be closed and the TS LCOs properly exited

(valve 80-118 was closed before the CS system LCO allowed outage time expired)

~

The SSS initiated Deviation/Event Report (DER) 1-98-0851 to document this event

and to initiate a root cause analysis and identify appropriate corrective actions.

At

that time, the event was determined not reportable to the NRC.

Inspector follow-up identified that a verification checklist previously used at Unit 1,

on a shiftly basis, had been eliminated about three years ago.

The inspectors

learned that the checklist had been removed from N1-ODP-OPS-0101

because

the

control room operators did not see any benefit to the checklist based upon no

valves ever being identified as out-of-position using the checklist.

As a corrective

action, the GSO re-instituted the use of a checklist at Unit 1. The inspectors

confirmed that a system status checklist was still in use at Unit 2. After using the

new checklist for several weeks, the checklist was revised and incorporated into the

preventive maintenance

program (N1-PM-S5, "Control Room System Lineup

Verification").

Additional corrective actions for this event included a verification, using N1-OP-14,

that the other valves manipulated to lower torus level were in the proper position

and a panel walkdown (without using system operating procedures),

to ensure that

all safety systems were properly aligned in their standby configuration.

No

discrepancies

were identified. The inspectors considered the decision to conduct

the panel walkdowns without referring to the system lineups in the operating

procedures to be a weak corrective action because

of the susceptibility to human

error by verifying the safety system standby line-ups from memory. This

observation was discussed with the GSO and a second panel walkdown was

performed using the applicable operating procedures.

No discrepancies

were

.

identified.

The inspectors conducted

an independent safety system panel

walkdown using the Operational Safety Verification Checklist, developed by the

resident staff, and identified proper systems'onfiguration.

C.

Conclusions

A Unit 1 reactor operator failed to follow the operating procedure for restoration of

the containment spray system to its standby configuration resulting in the system

being in a degraded condition for 3.5 days.

This was a violation of Technical Specification 6.8.1, involving the failure to implement procedures,

as written.

(VIO 50-220/98-1 1-01 )

Between April 7 and 11, over sixty control panel walkdowns were unsuccessful

in

identifying this containment spray system mis-positioned valve.

This was a

significant operations staff oversight and indicative of a lack of attentiveness

to

safety system configuration.

In contrast, the in-plant operator's identification of the

breaker open/closed indicating lights deficiency demonstrated

good attention to

detail, proper awareness

of plant conditions, and prompt and appropriate response

to a deficient condition.

The licensee's

immediate action to conduct control panel system line-up

verifications without referring to the system operating procedures was a poorly

founded decision based upon the control room operators not having identified the

flow control valve out-of-position for 3.5 days by relying on unaided memory of

proper systems'onfiguration.

01.2

FCV 80-118 Primar

Containment Isolation Function

a ~

Ins ection Sco

e

71707

During the licensee's follow-up of the FCV 80-118 mis-position event, they

identified that FCV 80-118 is also a primary containment isolation valve (PCIV). As

such, the DER was revised and a 10 CFR 50.72 notification was made.

The

inspectors reviewed the revised DER, the LIFSAR and TSs, and discussed the issue

with Unit 1 management.

The inspectors also interviewed the SSS who made the

original reportability decision and observed the SORC meeting for the associated

Licensee Event Report (LER).

Observations

and Findin s

The system engineer's involvement in the disposition of DER 1-98-0851 resulted in

the recognition that FCV 80-118 also serves

a primary containment isolation

function. The Unit 1 UFSAR, Table Vl-3b, "Primary Containment Isolation Valves

[for] Lines Entering Free Space of the Containment," lists the normal position of

FCV 80-118 as "Closed."

FCV 80-118 is a remote manual valve and does not have

an automatic containment isolation feature.

Unit 1 TS, Section 1.11.a, defines

primary containment integrity and lists the conditions which must be satisfied.

One

of those conditions is that all non-automatic PCIVs, not required to be open for

routine plant operations, must be maintained closed.

TS Section 3.3.0 requires

primary containment to be maintained when the reactor is critical ~ The failure to

maintain primary containment integrity from April 7 through April 11, 1998, is a

violation of Technical Specifications.

(VIO 50-220/98-11-02)

In-office inspector review of the primary containment integrity TS non-compliance

identified that, although TS defined containment integrity (remote manual valves

closed) was not satisfied, containment integrity was not significantly challenged by

the open FCV 80-118.

The design of the containment spray system, as a closed

loop extension of primary containment and the inability to local leak rate test the

system's PCIVs (pre-Standard

Review Plan facility), necessitated

an NRC approved

exemption from 10 CFR 50, Appendix J, testing requirements.

Specifically, the

automatic operation of the containment spray system under design basis accident

(DBA) conditions ensures the establishment of a water seal between the primary

containment free air space

and the outside environment.

The inspectors determined

that, even under worst case single failure conditions (loss of one emergency diesel

generator and its associated

electrical bus), the water seal is maintained.

With FCV

80-118 open, the water seal is degraded

due to the diversion of flow and resultant

lower CS system developed head at the containment spray nozzles.

However, a

single operating CS pump in each loop ensures sufficient system pressure

above

containment accident pressure to provide containment integrity.

The inspectors identified that there was no TS required periodic verification of PCIV

status.

In contrast, the Unit 2 TSs have a monthly surveillance for this specific

purpose.

Following discussions with the GSO, this issue was captured in another

DER (1-98-1033) and forwarded with a recommendation to perform such a

verification at Unit 1. The inspectors consider the absence of such a verification to

be a weakness

in the Unit 1 surveillance program.

Conclusions

The identification of FCV 80-118 as a primary containment isolation valve by the

systems engineer was good, but the oversight by the operations staff of this valve's

primary containment isolation function reflects poorly on their systems knowledge

and sensitivity to containment integrity monitoring. The failure to maintain primary

containment integrity for 3.5 days was a violation of the Unit 1- Technical

Specification 3.'3.0.

(VIO 50-220/98-11-02}

08

Miscellaneous Operations Issues

08.1

Closed

LER 50-220 98-04: Containment Isolation Valve Left 0 en in Violation of

Technical S ecifications Due to Personnel

Error

90712

The events associated with this LER were described in Sections 01.1 and 01.2 of

this inspection report.

The inspectors conducted

an in-office review and verified

that the LER fulfilledthe requirements of 10CfR50.73.

Specifically, the description

and analysis of the event were consistent with the inspectors'nderstanding

of the

event.

The root cause and corrective actions described in the LER were

appropriate.

This LER is closed.

V. MANAGEMENTMEETINGS

X1

Exit Meeting Summary

At periodic intervals, and at the conclusion of the inspection period, meetings were

held with senior station management to discuss the scope and findings of this

inspection.

A preliminary exit meeting was held on May 8, during which the

inspectors initial findings were presented.

On June 10, 1998 the final exit was

held.

NMPC did not dispute any of the findings or conclusions.

Based on the NRC

Region

I review of this report, and discussions with NMPC representatives,

it was

determined that this report does not contain safeguards

or proprietary information.

ATTACHMENT1

PARTIAL LIST OF NMPC PERSONS CONTACTED

R. Abbott

B. Booth

J. Conway

P. Farsaci

T. Gardner

P. Mezzafero

J. Mueller

B. Murtha

B. Ness

R. Sanaker

R. Smith

C. Terry

D. Wolniak

Vice President,

Nuclear Engineering

General Supervisor of Operations, Unit 1

Vice President,

Nuclear Generation

Supervisor of Operations, Unit 1

Chief Shift Operator, Unit 1

Manager, Unit 1 Technical Support

Senior Vice President 5 Chief Nuclear Officer

Manager, Unit 1 Operations (Acting)

Assistant Station Shift Operator, Unit

1

Station Shift Supervisor, Unit 1

Plant Manager,:Unit

1

Vice President, Nuclear Safety Assessment

Bc Support

Manager, Licensing

INSPECTION PROCEDURES USED

IP 71707

IP 90712

Plant Operations

In-Office Review of Written Reports of Nonroutine Events at Power

Reactors

ITEIVIS OPENED

CLOSED AND UPDATED

OPENED

50-220/98-1 1-01

50-220/98-1 1-02

VIO

Failure to follow operating procedure for restoration of

containment spray system

VIO

Failure to maintain primary containment integrity

CLOSED

50-220/98-04

LER

Containment isolation valve left open in violation of TSs

due to personnel error

UPDATED

none

Attachment

1 (cont.)

LIST OF ACRONYMS USED

ASSS

CFR

DER

EA

ECCS

EEI

ESF

GSO

IR

LER

NMPC

NRC

RO

SORC

SRO

SSS

TS

UFSAR

Unit 1

VIO

PCIV

Assistant Station Shift Supervisor

Code of Federal Regulations

Deviation/Event Report

Enforcement Action

Emergency Core Cooling System

Escalated Enforcement Item

Engineered Safeguards

Feature

General Supervisor of, Operations

Inspection Report

Licensee Event Report

Niagara Mohawk Power Corporation

Nuclear Regulatory Commission

Reactor Operator

Station Operating Review Committee

Senior Reactor'perator

Station Shift Supervisor

Technical Specification

Updated Final Safety Analysis Report

Nine Mile Point Unit 1

Violation

Primary Containment Isolation Valve

A-2