ML17059B385

From kanterella
Jump to navigation Jump to search
Forwards Insp Rept 50-220/96-16 & 50-410/96-16 on 961028-1101,1118-22 & 1217-19.Violations Being Considered for Escalated EA IAW NUREG-1600
ML17059B385
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 12/31/1996
From: Wiggins J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Sylvia B
NIAGARA MOHAWK POWER CORP.
Shared Package
ML17059B387 List:
References
RTR-NUREG-1600 EA-96-494, NUDOCS 9701060254
Download: ML17059B385 (8)


See also: IR 05000220/1996016

Text

December

31,

1996

EA No.96-494

Mr. B. Ralph Sylvia

Executive Vice President Generation Business

Group and Chief Nuclear Officer

Niagara Mohawk Power Corporation

Nuclear Learning Center

450 Lake Road

Oswego, New York 13126

SUBJECT:

NINE MILE POINT ENGINEERING INSPECTION 96-16

Dear Mr. Sylvia:

This letter refers to the engineering inspection conducted from October 28, 1996, to

November 1, 1996, and November 18- 22, 1996, at Nine Mile Point Units

1 and 2. The

purpose of the inspection was to determine whether activities authorized by the license

were conducted

safely, and in accordance with NRC requirements.

At the

November 22, 1996, exit meeting, the findings were discussed with Messrs.

R. Abbott and

C. Terry and other members of your staff. Additional findings were also discussed with

Mr. D. Baker of your staff in two telephone

calls on December 5, 1996, and

December 20, 1996.

The inspection was directed toward areas important to public health and safety.

The areas

examined during this inspection included:

1) your corrective actions in response to the

identification of inoperability of redundant control room chillers on August 14, 1996; 2)

your corrective actions following the failure of RCIC turbine lube oil cooler pressure

control

valve (2ICS" PCV115) in January 1991; 3) a plant design change (SC2-0077-93) to

ascertain whether the design and implementation met the regulatory requirements;

and 4)

to evaluate for closure of two previously identified inspection items.

Based on the results of this inspection, the inspector identified several apparent violations.

The NRC considers these issues to be significant and to reflect numerous examples of

weak technical performance

and failures to assure quality in engineering activities.

These

violations involved:

1) making design change

in the reactor core isolation cooling (RCIC)

system without performing a safety evaluation in accordance

with 10 CFR 50.59; 2) two

examples of failure to identify and correct deficient conditions promptly

as required by 10 CFR 50, Appendix B, Criterion XVI, Corrective Action; 3) three examples of failure to meet

the requirements of 10 CFR 50, Appendix B, Criterion III, Design Control; 4) two examples

of failure to meet Nine Mile 2 Technical Specifications requirements;

and 5) failure to

update the Final Safety Analysis Report (FSAR), following the design change of the RCIC

turbine lube oil cooler pressure

control valve from a self-contained downstream

sensing

pressure control valve to an electro-hydraulic control valve, to assure that the information

included in the FSAR contains the latest material developed,

as required by 10 CFR 50. 71 (e).

9'70iOb0254 96i23i

PDR

ADQCK 05000220

8

PDR

DECI

Mr. B. Ralph Sylvia

2

The violations involving multi-examples are explained as follows:

Two examples of failure to identify and correct deficient conditions promptly:

1) the RCIC

turbine lube oil cooler pressure control valve was inoperable for more than five years; and

2) the incorrect condenser water low flow setpoints for the control room chillers, which

existed from 1988 until August 1996, were not identified and corrected although

a control

room chiller was tripped three times due to low flow in September

1995.

Three examples of failure to meet the requirements of 10 CFR 50, Appendix B, Criterion III,

Design Control:

1) the June 15, 1992, calculation that was used as the basis for two

operability determinations was incorrect and had not been independently

reviewed, use of

this incorrect calculation resulted in a wrong conclusion being drawn for the operability

determination;

2) the 1988 setpoint calculation for the control room chiller condenser

water low flow trip, and the 1992 review of the adequacy of this setpoint calculation failed

to include the effect of pressure

and flow transients

in the service water system, resulting

in an incorrect setpoint being implemented;

and 3) the calculation in a recent design

change used an incorrect downstream

pressure for the pressure

control valve, resulting in a

wrong size of a restricting orifice in the RCIC system; this wrong orifice size could cause

a) the RCIC turbine lube oil cooler and its associated

piping to operate beyond their design

pressure;

and b) continuous opening of relief valve during RCIC operation.

Two examples of Technical Specifications violations:

1) From June 1989, till

August 14, 1996, both control room chiller subsystems

were inoperable in that the chiller

trip setting for the condenser water low flow trip was too high (250 gpm).

During a

postulated design basis accident when the diesel generators

start, the service water

pressure transient could cause both chillers to trip. This is in violation of Nine Mile Point

Unit 2 Technical Specifications, Section 3.7.3, which requires two independent

control

room chiller subsystems

to be operable when the plant is in operation modes

1, 2, 3 and

when irradiated fuel is being handled in the reactor building and during core alterations and

operations with a potential for draining the reactor vessel and uncovering irradiated fuel.

2) Nine Mile Point Unit 2 Technical Specifications, Section 3.7.4 requires that the RCIC

system shall be operable when the reactor steam dome pressure

is greater than 150 psig;

however, there was no valid operability determination to demonstrate that the RCIC system

was operable between January 26, 1991, and September

1996, when the RCIC turbine

lube oil cooler pressure

control valve 2ICS"PCV115 was in the failed open position.

The above apparent violations are being considered for escalated

enforcement action in

accordance with the "General Statement of Policy and Procedure for NRC Enforcement

Action" (Enforcement Policy), NUREG 1600.

A predecisional enforcement conference to

discuss the apparent violation will be scheduled

soon.

The decision to hold a predecisional

enforcement conference

does not mean that the NRC has determined that violations have

occurred or that enforcement action will be taken.

The conference

is being held to obtain

information to enable the NRC to make an enforcement decision, such as a common

understanding

of the facts, root causes,

missed opportunities to identify the apparent

violations sooner, corrective actions, significance of the issues,

and the need for

0

Mr. B. Ralph Sylvia

3

lasting and effective corrective action.

ln addition, this is an opportunity for you to point

out any errors in our inspection report and for you to provide any information concerning

your perspectives

on:

(1) the severity of the violations, (2) the application of the factors

that the NRC considers when it determines the amount of a civil penalty that may be

assessed

in accordance

with Section VI.B.2 of the Enforcement Policy, and (3) any other

application of the Enforcement Policy to this case, including the exercise of discretion in

accordance

with Section Vll.

You will be advised by separate

correspondence

of the results of our deliberations on these

matters.

No response

regarding the apparent violation is required at this time.

ln accordance

with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure,

and your response

will be placed in the NRC Public Document Room (PDR).

Sincerely,

ORIGINAL SIGNED BY:

A. Randolph Blough for

James T. Wiggins, Director

Division of Reactor Safety

Attachment:

As stated

Docket Nos.

50-220, 50-410

cc w/encl:

R. Abbott, Vice President & General Manager - Nuclear

C. Terry, Vice President- Safety Assessment

and Support

M. McCormick, Vice President - Nuclear Engineering

N. Rademacher,

Unit 1 Plant Manager

J. Conway, Unit 2 Plant Manager

D. Wolniak, Manager, Licensing

J. Warden, New York Consumer Protection Branch

G. Wilson, Senior Attorney

M. Wetterhahn, Winston and Strawn

J. Rettberg, New York State Electric and Gas Corporation

Director, Electric Division, Department of Public Service, State of New York

C. Donaldson,

Esquire, Assistant Attorney General, New York Department of Law

J. Vinquist, MATS, Inc.

P. Eddy, Power Division, Department of Public Service, State of New York

F. Valentino, President,

New York State Energy Research

and Development Authority

J. Spath, Program Director, New York State Energy Research

and Development Authority

0

Mr. B. Ralph Sylvia

~

~

D. Screnci, PAO

Region

I Docket Room (with concurrences)

Nuclear Safety Information Center (NSIC)

PUBLIC

NRC Resident Inspector

J. Wiggins, DRS

L. Cheung,

DRS

W. Ruland, DRS

R. Correia, NRR

R. Frahm, Jr., NRR

DRS File

W. Dean, OEDO

B. Norris - Nine Mile Point

S. Bajwa, NRR

D. Hood, NRR

K. Cotton, NRR

M. Campion,

Rl

Inspection Program Branch (IPAS)

DOCUMENT NAME: A:iNM961616.INS

To receive a copy or this document, indicate in the box: "C"

Copy without attachment/enclosure

E" ~ Copy with attachment/enclosure

'N" ~ No copy

OFFICE

RI/DRS

NAME

LCheung

RI/DRS

< RI/

WRuland

RI/

RI/

DATE

12/27/96

12/

/96

12/

/96

12/

/96

12/

/96

OFFICIAL RECORD

COPY