ML17055D960

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Insp Repts 50-220/88-07 & 50-410/88-06 on 880229-0304 & 0321-25.No Violations Identified.Major Areas Inspected: Refueling Outage Activities,Plant Maint Mods,Plant Surveillances for Unit 1 & Action on Previous Insp Finding
ML17055D960
Person / Time
Site: Nine Mile Point  
Issue date: 06/14/1988
From: Blumberg N, Gallo R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17055D959 List:
References
50-220-88-07, 50-220-88-7, 50-410-88-06, 50-410-88-6, NUDOCS 8806280204
Download: ML17055D960 (74)


See also: IR 05000220/1988007

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

50-220/88-07

Report Nos.

50-410/88-06

50-220

Docket Nos.

50-410

DPR-63

License

Nos.

NPP-69

Licensee:

Nia ara

Mohawk Power

Cor oration

a

n ie

oa

racuse,

ew

or

13212

Facility Name:

Nine Mile Point

(NMP) Units

1 and

2

Inspection At:

Oswe

o and Syracuse,

New York

Inspection

Conducted:

February

29 - March 4,

1988 and March 21-25,

1988

Inspectors:

M. Dev, Reactor

Engineer

R. Temps,

Operations

Engineer

W. Oliveira, Reactor

Engineer

L. Prividy, Reactor

Engineer

T. Rebelowski,

Senior Reactor

Engineer

G. Napuda,

Senior Reactor

Engineer

Reviewed by:

Approved by:

orman

.

um e

,

se

Operational

Prog

ams Section

OB, Divisi

Reactor Safety - Team Leader

o er

.

a

o,

se

Operations

Branch

Division of Reactor Safety

a e

a

e

F

Ins ection

Summary:

Ins ections

on February

29 - March 4,

1988 and

arc

(Com ine

ns

ec

son

e or

os.

-

-

an

Ar eas

Ins ected:

Inspection of refueling'outage activities which i,ncluded

p an

masn

enance modifications,

and plant surveillances for Unit ); licensee

action

on

a previous inspection finding for Unit 1; observation of a

100% load

rejection startup test for Unit 2; and the procurement

program emphasizing

the

purchase

and dedication of commercial

grade

items for both Units

1 and 2.

>>0~280-04

880m>S

PDR

ADOCK 05000220

8

PDR

Results:

Ho violations were identified.

Overall, activities for both units

were being performed in accordance

with established

procedures

and. personnel

were observed

to be conscientious

and knowledgeable.

The dedication of

commercial

grade

items by the licensee

engineering staff for safety related

use

in, both units was technically

sound

and well documented.

Management

support,

support services

and

gA Department

performance

was

improved and effective at

both units.

At Unit

1 design/modification,

maintenance

work, and plant

surveillances

were technically. sound

and done adequately.

Unit 2 power

ascension

testing

was performed in a controlled manner.

Minor concerns

were identified with respect

to need for improvement in clarity

of design controls

and modification, installation

and maintenance

procedures;

adequacy of control of measuring

and test equipment;

number of persons

in the

Unit 2 control

room during tests;

lack of documentation

of dedications

of

commercial

grade

items

by contractors;

and,

the

need for improvements

in

housekeeping.

0

DETAILS

Persons

Contacted

Nia ara'ohawk

Power Cor oration

NMPC

- Nine Mile Point Unit

1

NMP-1

  • S
  • S

~K.

T.

p.

M.

p.

C.

p.

D.

D.

W.

R.

D.

  • C

p.

  • 7

eJ

J.

"R

  • T

G

AJ

R.

AP

  • J

T

  • K

Agarwal,

Lead Site Licensing Engineer

Aldrich, Technical Assistant

Beckham,

Manager Quality Assurance

Dahlberg, Site Superintendent,

Main'tenance

Egan, Unit

1 Licensing Engineer

Fabin, Quality Assurance

Lead Engineer

Felise,

Site Maintenance

Superintendent

Finnerty, Assistant

Manager,

Nuclear Design

El

Fischer, Electrical Maintenance

Supervisor

Francisco,

Licensing Engineer

Goodney,

Project Engineer

Jakubowski, Electrical

Engineer

James,

Supervisor,

IKC

Klosowski, Manager,

Nuclear Design

Lempges,

Vice President,

Nuclear Generation

Longo, Mechanical

Maintenance

Supervisor

Lundeen, Modification Coordinator

Mangan,

Senior Vice President

Massaferro,

Asst. Supervisor of Technical

Supp

Perkins,

General

Superintendent

Perry,

Vice President,

Quality Assurance

Raby, Site Engineer

Randau,

Operations

Superintendent

Roman, Station Superintendent

Snyder,

Site Engineer

Spadafore,

Technical

Services

Superintendent

Tessier,

Planning Supervisor

Volza, Radiation Protection

Manager

Wi1 1 i s,

General

Superintendent

Wood, Generation Specialist-Training

Zollitsch, Superintendent,

Nuclear Training

ectrical

ort

New York State

Public Service

Commission

NYSPSC

Eddy, Site Representative

United States

Nuclear

Re ulator

Commission

US

NRC

AW

  • R.

"K.

AJ

  • R.
  • W.

Cook, Senior Resident

Inspector

Gallo, Chief, Operations

Branch,

DRS

Hook, Senior Operations

Engineer,

NRR

Johnson,

Chief, Project Section

2C,

DRP

Laura,

Reactor

Engineer

Schmidt,

Resident

Inspector

Indicates

those

persons

attended

the exit meeting on'arch

25,

1988.

The inspectors

also contacted

other administrative

and technical

personnel

during this inspection'.

2.0

General

.2. 1

Objective

and

Sco

e of Ins ection

The objective of this inspection

was to evaluate

the licensee's

program for controlling Unit

1 outage activities.

Particular

emphasis

was placed

on the licensee's

systems for completion

and

closeout including formal corrective actions of activities to assure

plant readiness

for restart.

Also addressed

were engineering/

technical

evaluations (i.e. dedication)

conducted

under the auspices

of 10 CFR 21 to enable

items purchased

for Units

1 and

2 as

"commercial

grade" to be used in safety related applications.

Specific inspection activities in a given functional activity area

are

discussed

in the details of this report:

corrective

and preventive maintenance;

modifications;

plant surveillances;

commercial

grade

procurement;

Units

1 and

2

corrective action overview;

technical

support services;

power ascension

testing (Unit 2);

and

licensee

action

on previous inspection findings

Since

some outage activities were still in progress

during the inspection,

it was not possible

to confirm final closeout of each

outage activity.

However, the status of items within the work control

system

was determined

so as to assure

each

had progressed

properly through the

system

and

appropriate

tracking mechanisms

and procedures

would ensure

proper

closeout prior to plant restart.

2.2

Summar

of Conclusions

and Findin

s

Trained

and qualified maintenance

personnel

comply with a well documented

and administratively controlled maintenance

program.

One concern

observed is the cumbersome

process

of initiating an urgent maintenance

task.

Management is taking corrective action

and expects

to resolve this

problem before

the Unit 2 outage

scheduled

for the fall 1988.

(paragraph

3.3.1).

Design/modification work by engineering

personnel

was found to be

technically

sound.

Generally, modification installation procedures

were

adequate,

and in one instance,

concerns

expressed

by the

NRC will result

in the licensee

re-evaluating their classification of work involving

relocation of poison tank level

and high temperature

alarms

as non-safety

related

even

though those

alarms

serve to alert operations

personnel

of

impending degradation

of a safety function (paragraph

4.4.2).

Installation procedures

provided step-by-step

instructions to the workers.

However, minor problems exist in that

some procedures

are subject to

interpretation

and, therefore,

more prone to causing errors (paragraph

4.3).

A concern

was brought to the licensee's

attention that the non-inclusion

of piping centerline

location tolerances

on installation drawings/

procedures

resulted

in the need for a Reactor Building Closed

Loop Cooling

Piping stress

analysis

to be reconfirmed prior to the conduct of

hydrostatic tests

(paragraph

4.3.2).

It was noted that Kaowool/Flameastic,

identified as non-safety related

sealing material,

was used in safety-related

penetrations

for fire and

pressure

barriers.

Though the sealing material

met the three

hour fire

barrier

requirements,

the licensee initiated

an

NCR to evaluate

the

pressure

retaining capability of Kaowool/Flameastic

(paragraph

4.6.2).

Refueling outage

survei llances

were conducted

in accordance

with

procedures

which were technically adequate.

One area that poses

a

potential for future problems is the manner

in which measuring

and test

equipment is controlled

and their usage

logged (paragraph

5.6)

Additional management

attention is needed

in this area.

The dedication

by licensee

engineering

of items purchased

as commercial

grade for safety related

use in Units I and

2 was technically

sound

and

well documented.

Such dedications

done

by contractors

were minimally

adequate

(paragraph

6.3).

The licensee's

corrective action program

appears

capable of resolving these

concerns.

The corrective action program

and the performance of the guality

Assurance

Department at both units was found to be more effective than

observed

during previous

outage

inspections.

Management

support

was

evident

and self imposed completion dates for identified corrective

actions

were conservative.

This area

was noted to have

improved

significantly since

NRC inspections

performed in 1987 (paragraph

7.2).

Housekeeping

appeared

to be improved to a great extent.

However,

instances

of inadequate

practices

such

as

no dust covers for uncovered

,

manways

indicated

a need for continued

management

attention to this area

(paragraph

4.8).

Support services

were found to be timely, generally complete

and

on

a

continuing

improvement trend (paragraph 8.2).

Power 'ascension

testing at Unit 2 was conducted

in a controlled and

expeditious

manner.

Minor deficiencies

noted were

an excess

number

observers

present

in the control

room during the tests

and the tardiness

of post trip data analysis

review (paragraph

9,.3).

P

Overall, activities were being

per formed in accordance

with established

procedures

and personnel

were observed

to be conscientious

and

knowledgeable.

3.

Corrective

and Preventive

Maintenance

Unit

1

62700

3.1

~Sco

e

Forty five (45) corrective maintenance

and six preventive maintenance

activities conducted

during this outage

were selected

from the

1988

Refueling Outage Baseline

Plan for review by the inspectors prior to

the inspection.

During the inspection

seven corrective maintenance

(CN) activities

and three preventive maintenance

(PM) activities were

observed

being performed.

3.2

Details of the Review

The inspectors initially reviewed the status of the selected

CNs and

PMs with the Planning Supervisor.

Twenty five (25)

CMs and

PNs in

various

stages

of completion were reviewed

by the inspectors for

administrative control, technical

content,

reporting of results

and

data,

and quality assurance

and control

(QA/QC) coverage

as required

by Administrative Procedure

(AP) 5.0 for

CMs and

AP 8. 1 for PNs

as

listed in Attachment

A.

Active CMs and

PNs are

updated

twice

a day

and the inspectors

were given

a copy of the daily Work Tracking

System report to follow the progress of the

CMs and

PMs.

Personnel

involved in the performance

of CMs and

PMs were interviewed to

determine their ability to conduct

an effective maintenance

program.

The results of the inspection

are discussed

in paragraph

3.3.

3.3

~indin<is

3.3. 1

Corrective Maintenance

Work Request

(WR) 140143 requested

that Diesel Generator

(DG)

103 Engine temperature

switches

be recalibrated

in

accordance

with procedure

Nl-IP-92.2.

During the test for

closing the switch, the inspectar

asked

the instrument

and

control

( I&C) technicians

what reference

they used for

determining the acceptance

cri.teria.

They referred to

a

controlled vendor manual for the acceptance

criteria and

the inspector verified that the acceptance

criteria written

in the procedure

agreed with the vendor manual.

WR 132815

was prepared

to investigate

and repair or replace

the leaking packing of Liquid Poison

Pump

No.

11.

The

mechanics

using

a controlled vendor manual,

noted that

corrective maintenance

also included removal

and inspection

of the pistons

and cylinders.

Oifficulty in removing the

pistons

caused

the mechanics

to seek advice

from super-

vision.

The mechanics

acted conservatively

by seeking

advice

and assistance

from their supervision

when

conditions required.

WR 132024's

scope

included overhaul

and inspection of the

OG

103 Cooling Water

Pump flanged discharge

check valve in

accordance

with generic

procedure

Nl-NMP-GEN-241.

The

procedure

simply stated that the overhauled

valve was to be

returned

and bolted to the pipe.

On his

own initiative,

the mechanic

searched

the controlled vendor manual for the

torque values required to bolt the valve to the pipe,

and

used

a calibrated torque wrench to bolt the valve to the

pipe.

QC was notified though the procedure

did not require

QC's presence.

This was another

case of maintenance

workers being conservative

in performing their job.

WR 134000 requested

that the coupling nut and screw to

(hydra'ulic control unit)

HCU 126 valve

be retorqued.

Review of the maintenance

records for the all 258

HCU

valves that were overhauled

during this outage did not

include objective quality evidence that

HCU 126 valve

coupling nut and

screw were torqued.

The mechanics

were

observed

by the inspector retorquing the coupling nut and

screw in accordance

with the

WR and the

QC inspector

verifying that the work was performed with a calibrated

torque wrench

and that the results

were recorded.

Review of the

CM work request

packages

indicate compliance

to AP 5.0.

Two packages

however required explanation of

some of the information in the packages.

In one case

a

memorandum

in

WR 139722 for the Core Spray discharge

valve

motor breaker authorized

an "identical relay" replacement.

A QC Inspection

Report

(QCIR) no.

1-88-0421

questioned

whether the relay from a non-safety related

(NSR) breaker

could be

an identical relay replacement

for the damaged

relay in

a safety related

(SR) breaker just because

they

had the

same

code

number.

QA engineering

explained that

the relays

were identical in every way 'though the

corrective action response

did not clearly state this fact.

In another

case,

WR 106336 included'several

material

issue

forms,

(Form no.

005833 for safety related

valve

stem that

was returned to stores,

and

Form 006291 for a non-safety

related

stem

used in

a safety related valve) ~,A'written

explanation,

"Determination of Appendix

B Requirements"

Determination

No. 86-1025,

was provided to the inspector

who verified that the determination

was processed

in

accordance

with AP5.0.

The inspector

observed

an urgent

WR 139964 being processed

to start work on the

NO.

11 Reactor Building Closed

Loop

Cooling

Pump motor.

It took several

hours to process

the

urgent

WR with the present

Work Control Center

(group).

The Site Maintenance

Superintendent

and the inspector

discussed

the time consuming effort to initiate

a

WR.-

The

Site Mechanical

Maintenance

Superintendent

is on

a task

force to address

this concern

and

a contractor

has

been

selected

to assist

him.

An Administrative Procedure

(AP)

is under preparation

and the licensee

expects

to implement

changes

to the Work Control Center

group in time for the

Nine Mile 2 outage'cheduled

for this fall.

Preventive

Maintenance

Preventive

Maintenance

on

DG 103 was observed

being

performed in accordance

PM procedure

Nl-MPM-DG-R852.

This

PM was being conducted

by a vendor representative

and

supported

by licensee

mechanics.

It is the licensee's

policy to request

vendor representatives

by name to perform

this outage

PM.

A QA engineer

was also conducting

a

surveillance of the

PM activity.

During the check of

piston

and

head clearances

(paragraph

7.4.4 of the

PM

procedure),

the inspectors

noted that all the cylinder and

piston clearances

were checked.

Review of paragraph

7.4.4

indicated only one piston

and

head clearance

check was

required.

Likewise in the subsequent

check of a section of

the camshaft,

the entire camshaft

was checked.

The vendor

representative

told the inspectors

that it is standard

practice to perform these

checks

as observed.

This fact

was later confirmed by the Maintenance

Supervisor

and

he

agreed

to revi se the p'aragraphs

in question.

PM procedure

Nl-EPM-SB-W265 was

used to perform the

125,VDC

Weekly Pilot Valve surveillance

(Nl-ESP-SB-W276).

The

electrician

performing the

PM procedure

was observed

to be

very deliberate

and careful in performing the different

checks.

He also

reminded the lead electrician that the

Emergency

Eye Wash Station did not have

any water,

although

this

same fact was noted

a day earlier by an

NRC inspector

and was brought to the attention of the licensee

and later

corrected.

An outage

PM for the removal,

overhaul

and inspection of

Main Steam Electromatic Relief Valves

and Associated Pilot

Valves was observed.

A special

boring machine. was

used to

cut the seal

weld in Electromatic Relief Valve 01-112 in

'ccordance

with paragraph

7.4.3 of

PM procedure

Nl-MPM-C22.

This work was done

under strict ALARA

requirements

including the use of respirators.

Outage

PM of the 4. 16KV Breaker for Auxiliary Feeder

17B

R1031

was performed in accordance

with

PM procedure

Nl-EPM-GEN-R150 and the controlled vendor manual.

The

inspectors

noted that Mark Up 19545

had

been

performed

by

Operations

personnel

to set isolation boundaries

for the

job,

and that the electrician verified that the panel

was

blue tagged

out befo're the breaker

was

removed

from the

panel.

The inspector

observed

the breaker

being cleaned,

lubricated,

pre-tested,

reinstalled into the panel,

and

readied for post maintenance

testing

(PMT) by Operations.

The electricians

were careful

in the use of cleaning

solvent

and aware of the ventilation requirements.

They

were also careful

in performing the pre-test

and assuring

the breaker

was ready for PMT.

3.4

Conclusions

Individual performances

of the trained

and qualified mechanics

and

technicians

reflected

an attitude to do

a quality job

conscientiously.

Procedures

were followed, administratively

controlled

and adequate

QA/QC coverage

was provided.

The process

to

initiate a co'rrective maintenance

work request is time consuming.

The licensee

recognizes

this fact and the Site Mechanical

Maintenance

Superintendent

has

been

tasked to take the necessary

actions to

provide

a more efficient work control

system for the Nine Mile Unit 2

outage

scheduled

for the fall.

4.0

Modifications Pro

ram

37700

37702

4.1

~Sco

e

The inspector

reviewed the following modifications that were in

various stages

of completion:

Modification

Modification

Oescri tion

85-48

86-66

Replace

Reactor Building Closed

Loop

Cooling Heat Exchangers

ATWS Liquid Poison

System

10

83-83

80-72

86-25

85-92

84-92

4.2

Details of the Review

Replace

Feedwater

Check Valves

ATWS Alternate

Rod Injection

.

Motor Generator

Set Test Blocks

Replace

125

V dc Station Batteries

Motor Generator

Set Reliability

None of the above modifications

had

been

completed.

The inspector

conducted

reviews

and

had specific observations

concerning

each of

these modifications

as follows:

Conducted

system/equipment

walkdowns were conducted

in the field to

confirm as-built information per installation drawings.

Verified that installed conditions conformed to modification

specifications

and drawings.

Observed

ongoing installation work, inspection

and testing.

Reviewed portions of the work that were already completed.

Verified that engineering

work was technically

sound.'erified

that the level

and type of verification of quality was

adequate

for the selected

work.

Determined

proper classification of work according to ASME,

IEEE

and

EQ requirements.

Verified that field changes

were disposit,ioned properly.

Verified that personnel

were being trained

as appropriate

In addition to checking the above

items

on each of the selected

modifications, certain modifications were checked for the following:

That installation

and inspection

procedures

were adequate

That onsite

and offsite review committees

performed

their review responsibilities

concerning the modifications.

That there

was proper level of QA/QC involvement in inspection

activities

and problems.

Specific inspection findings and pertinent inspector observations

concerning

each of the selected

modifications are discussed

below.

~

~

4.3

Reactor Buildin

Closed

Loo

Coolin

RBCLC

Heat

Exchan er

Re lacement

4.3.1

~Sco

e

The original

RBCLC heat exchangers

developed

through wall

leaks in the tube sheet to shell welds due to the

metallurgical differences

between

the silicon bronze

tube

sheet

and the carbon steel

shell.

Supporting straps

were

installed

as

a temporary modification to preclude

catastrophic

failure of the welds.

Modification No. 85-48

was undertaken

to install three

.new heat exchangers

with

stainless

steel

tube sheets

and carbon steel

shells,

thus

eliminating the material incompatibility problem.

Part of

this modification also included the replacement

of service

water and

RBCLC system piping between

the heat exchangers

and their respective

system isolation valves.

The heat

exchangers

were purchased

to

ASME Section VIII requirements

and meet the seismic

requirements

of the original plant

design.

The inspector

noted that the licensee's

Site

Operational

Review Committee

(SORC) conducted

a proper

safety evaluation of this modification.

The heat exchangers

are being replaced

in accordance

with

the rules of ASME Section

XI 1983 Edition including Summer

1983 Addenda.

Only one heat exchanger

is being replaced at

'ny one time and installation work is being performed

by

Chicago Bridge and Iron (CBI).

At the time of the

inspection ¹12 heat

exchanger

had just been replaced,

hydrostatically tested

and placed into service.

The

original ¹11 heat exchanger

was still in- service

and the

replacement

¹13 heat exchanger

was being erected into

position.

4.3.2

~Findin

s

The inspector

reviewed the procedure that was

used to

perform the hydrostatic test of the

new ¹12 heat

exchanger,

after it was installed.

The hydrostatic test

on both the

.tube

and shellsides

were performed satisfactorily.

However, the inspector

noted that

a retest

was required

on

the shell

side

(RBCLC portion) due to

a deficiency noted

by

gC concerning

the improper range of the test

gage

used

during the original test.

An in-depth discussion

on

deficiencies

noted

and corrective actions

implemented

by

the licensee is included in Section 8.0 of this report.

12

In reviewing the installation drawings

and the actual

installation of heat exchanger

¹12, the inspector

noted

that the licensee

took particular care in properly

anchoring

the heat exchanger.

Anchor bolts were specified

to be torqued where designated

and minimum anchor

embedment

was specified to ensure as-built anchor depths

were met.

The south

end heat exchanger

support

was properly detailed

with four slotted holes to permit heat

exchanger

thermal

expansion.

The inspector

made

a specific check of the four

connections

at these slotted holes to ensure that thermal

expansion

movement

was afforded.

The inspector determined

that the

hex nuts threaded

to the anchor bolts were not

torqued which is correct for this application.

They were

properly locked in place 'such that the heat exchanger

support

was free to move in the slotted holes.

The

connections

were satisfactory.

The inspector

reviewed the as-built location for the ¹12

exchanger

and noted that several

piping centerline

locations

were greater

than

one inch from that specified

on the installation drawings.

For example,

pipe support

drawing B-70-SR-23 specifies

the

20 inch

RBCLC piping

horizontal centerline

dimension to be 3'-0" above the

298'-0" floor elevation.

The as-built centerline

dimension

was 2'-10~" above

the 298'-0" floor elevation.

The

inspector discussed

this with the site

and mechanical

'ngineers

and noted that piping centerline tolerances

were

not included in the installation specifications

or

drawings.

Consequently

piping stress

analyses will have to

be confirmed after final as-built dimensions

are obtained.

The inspector

confirmed that the licensee

intended to

perform this analysis

as part of a calculation

package

to

be completed

in conjunction with the final design

stage

verification of this modification.

This analysis will

include final as-built dimensions for both piping and

piping supports.

The mechanical

engineer

noted that the

analysis

intended for use utilizes

a piping system

model

which includes all

3 heat

exchangers.

The inspector stated

that this stress

analysis

needed

to be done

as

soon

as

possible after heat exchanger .replacement

to ensure that

operability is not in question after heat exchanger/piping

hydrostatic testing.

This item will be classified

as

unresolved

(SO-220/88-07-01)

pending satisfactory

completion of this

RBCLC heat exchanger/piping

stress

analysis.

1

13

4. 4

ATWS

Li uid Poison

S stem

4.4.1

~Sco

e

The licensee

committed to complete Liquid Poison

System

( LPS) modifications prior to startup

from the

1988 outage

in order to comply with ATWS Rule

10 CFR 50.62.

This rule

states

that each

BWR shall

have

a

LPS with a minimum flow

capacity

and boron content equivalent 'to those of a

reference

plant.

To comply with these

requirements

the

licensee

planned certain

changes

to the existing

LPS.

This

work was defined

as Modification No. 86-66.

The major

change

involves the concentration

of Boron-10 which is

being increased

in the

sodium pentaborate

solution by

employing

an enriched

Boron-10 solution in the

LPS storage

tank.

Also, instrumentation

and other changes

are being

made

as follows:

(1) pressure

and flow instruments

are

being installed

on the

LPS test line; (2)

a flow deflector

is being

added to the

LPS test tank discharge

line;

and (3)

the

LPS storage

tank level switch (IL01) is being

relocated.

At the time of the inspection this work was

just being started.

The installation is to be performed

by

CBI personnel

for the mechanical

portion while NMPC

personnel

will perform the electrical

and

IKC work.

4.4.2

~Findin

s

The inspector

noted that the

SORC

had reviewed this

modification.

In this regard the inspector

observed that

the

SORC review annotated

the

SORC modificagion

review form that

no Technical Specification'(TS)

changes

were involved with this modification.

This was determined to be

an administrative/non-technical

error since both

SORC and the licensee's

Safety

Review

Board

had reviewed

a proposed

TS change

which had

been

recently submitted to the

NRC.

The inspector

reviewed the installation procedures

intended

to accomplish

the work.

The mechanical

work to be

performed

by CBI was defined step-by-step

on

a traveler

with specific, self-contained

instructions

on who performed

or inspected

the work and what procedures

were to be used.

The electrical

and

IEC work to be performed

by

NMPC

personnel

was defined step-by-step

in an installation plan

which contained

more general

instructions

compared

to the

CBI traveler.

For example,

the

new setpoint

fo'b the

LPS

tank low level alarm was not contained within t'e

installation plan.

Rather,

the plan referenced

an

interoffice memo (087547) for this information.

This

memo

14

in turn was superseded

by another

memo (888085) which

contained

the correct setpoint information.

Also, several

editorial errors existed in the installation plan.

These

observations

caused

concern that the installation plans

developed

by

NMPC engineering

personnel

for this work were

not carefully controlled;

were subject to more were subject

to more interpretation,

and possibly more prone to error.

The inspector discussed

this general

observation with the

licensee's

modification coordinator

who felt that the

NMPC engineering

personnel

were making

improvements

in

installation plans

by closer coordination

between project

and site engineers.

He noted that even though project

engineer

were not directly located at the site, they were

interfacing with the site engineers

via telephone

and

visiting the site when necessary

to resolve

problems.

The

inspector

suggested

that locating project engineers

permanently at the site would strengthen

this interface.

During the review of the installation procedures

the

inspector further noted that portions of the work were

classified

as safety related while other portions were

classified

as non-safety related.

In particular,

the

electrical

and

I8C work concerning relocation of the poison

tank level

and high temperature

alarms

was classified

as

non-safety related.

The inspector

questioned

the

licensee's

basis for classifying this work as non-safety

related

in view of the following:

(a)

The alarms

serve to alert reactor operators

of

impending degradation

of a safety function.

(b)

The level alarm device is mentioned

in the

TS Bases

section.

(c)

The alarms

are classified

as safety related at Unit P2.

The inspector discussed

this matter with the Assistant

Supervisor

of Technical

Support

and requested

that the

-licensee

review their position concerning

the

classification of this work.

The inspector

noted that dual

classifications

of work'ithin a given .modification could

create

confusion in developing installation plans

and

further exacerbate

the concern

noted above.

In discussing

this concern with the Modification Coordinator,

the

inspector

was advised that only a very small percentage

of

modifications

had dual classification of work.

In

conclusion

the licensee's

Assistant Supervisor of Technical

Support agreed

to reeva'luate their position

and to do

a

determination

of 10 CFR 50, Appendix

B quality requirements

concerning

the poison tank level

and high temperature

.alarm

work prior to its completion.

15

4.5

Feedwater

Check Valve

Re lacement

4.5.1

~Sco

e

Extensive

maintenance

had been required during previous

refueling outages

in order to pass

required leak rate

testing for the feedwater

check valves (¹31-01

and 31-02).

As

a result, Modification No. 83-83 was undertaken

to

repl'ace

these

valves.

At the time of this inspection cuts

had

been

made

on both feedwater lines to remove the

original valves.

Workers were machining the piping in the

MSIV Room to produce

the correct

end preparation

and match

it to the

new valve

end connection.

The

new valves were

located in a staging

area

near

the

MSIV Room where their

end connections

were being prepared

for welding.

The

installation work was being performed

by CBI.

4.5.2

~Findin

s

The up-front engineering

design work appeared

to be

technically

sound

as evidenced

by the inspector's

review of

the various documentation

in the conceptual

engineering

package.

Included in this package

was the "Verification of

Acceptability" report for the replacement valves'his

report is

a requirement of Subarticle

IWA-72220 of the

ASME

Code,

Section XI.

In this report the licensee

considered

the Anchor/Darling tilting disk check valves

as suitable

- replacement

valves with a high degree of reliability due to

the following factors:

(a)

The valves

are of

a current design

and were designed,

fabricated

and tested

in accordance

with the

ASME

Code,

Section III, Class l.

(b)

The valve assemblies

are designed

and

have

been

analyzed for a potential

seismic event.

(c)

The valves are

more compact,

weigh less

and easier

to

maintain than the original valves.

(d)

The valves

have

one main bonnet

seal

as

opposed

to two

seals

in the original valves which in turn provides

less

chance for leakage.

The inspector discussed

with the site engineer

the work

status

and other aspects

of the work not,yet accompl'ished.

A joint walkdown of the work area

in the

MSIV Room and

nearby staging

area

was conducted.

The inspector

had the

following observations:

1

16

(a)

The working copy of the

CBI traveler document

was

located at the entrance

to the

MSIV Room.

This

traveler

was very detailed in its definition of the

work including appropriate

procedures

to perform the

work, steps for in-process

inspection,

and hold points

at appropriate

steps.

(b)

The end of the traveler did not include instructions

for retest.

The site engineer

informed the inspector

that

he was in the preliminary stages

of developing

a

test procedure for the hydrostatic test.

The

new

valves,

piping and welds would be tested

separately

from the reactor

vessel

since the modified piping

sections

were isolable.

No,. unacceptable

conditions were noted.

4.6

ATWS - Alternate

Rod Injection

Modification 80-72

4.6.1

~Sco

e

10 CFR 50.62,

paragraph (c)(3), requires that each 'Boiling

Water Reactor incorporate

an alternate

rod injection (ARI)

system to reduce

the risk of anticipated transients

without scram

(ATWS).

The purpose of this modification was

to attain

a functionally redundant

method of rod injection

via addition of two one-i.nch

OC solenoid valves 'in series

in Control

Rod Scram Air Header

system.

The automatic

signals to initiate the ARI function come from high reactor

vessel

pressure

or low low reactor vessel

water level.

Following any of these'initiation

signals

the

scram air

header

valves will open to reduce air pressure

in the

header allowing individual scram inlet valves

and

scram

discharge

valves to open.

The control rod drive units then

i,nsert the control blades

to shut

down the reactor.

The

set point for ARI initiation is chosen

such that

a normal

scram should already

have

been initiated by the above

mentioned reactor

vessel

pressure

and level parameters.

4.6.2

~Findin

The inspector

reviewed the modification package

80-72 and

associated

maintenance

work request

which incorporated

the

installation of two one-inch Valcor dc solenoid valves

and

associated

instrumentation

and controls.

The licensee

safety evaluation

acknowledged that although

the ARI system

is not safety-related,

its implementation is carried out in

a manner that the existing protection

system

meets all

applicable safety requirements.

Accordingly, power supply

17

for logic and control was obtained from RPS power source,

and two Class

1E fuses

were installed for isolation.to

assure

no degradation

of the existing scram system.

All

installation including non-Class

1E components

and wirimg

added to control

room panel

were installed in a manner to

meet the physical separation'criterion

of IEEE Standard

= 384-1977.

The licensee

has also evaluated the structura1

integrity of the ~lectrical cabinets,

pa'nels

and supports

interfacing

ATMS related

equipment

and devices,

and found

...them to be adequate.

Also, procurement

and installation of

<he solenoid valves met the .environmental qualifization

requirements for the electrical

equipment.

Procurement

and

insta1lation of .associated

piping systems.

adhered to ANSI

Power Piping Code B31.1,

1980 edition through the Minter

1982 addenda.

The licensee

analyzed<he

stresses

im the

piping due to'additional of new valve and the.,result

was

acceptable.

'The installation work was done in accordance

with approved

procedures ky a qualified contractor.

Prior to the award

.of the installation contract the licensee

evaluated. the

contractor's qualification and determined that the

,contractor

met

10 CFR 50 Appendix

B and ANSI N45.2 quality

assurance

requirements.

Review of the installation work

package

indicated that adequate

training and indoctrination

were provided to the individuals performing quality control

., activities..

gA/gC hold and witness steps

were also found

to have

been observed

and properly documented.

Duriag Me review. ot the installation package

some

deficiencies of an administrative

nature

were identified by

the

NRC inspector,

and the licensee

corrected

them

promptly.

In another instance, it was found that four

safety-related

penetrations

were sealed with non-safety

related

Kaowool/Flameastic material to provide three

hours

fire and pressure

barriers.

The penetratioms. are I-1483

and I-1244, constituting control

room pressure

boundaries;

.and'3D-F3 and 12B-E1, constituting part of the secondary

containment boundary.,

The licensee initiated a

nonconformance

report (NCR) and is .currently evaluating the

pressure

retaining capability. of the installed non-safety

related

Kaowool/Flameastic

sealing material.

In addition,

<o prevent possible recurrence,

the licensee

Kaowool/

Flameastic

from the. stock and discontinuing its use.

The inspector physically verified the completed

installation work of the Valcor solenoid valves in the

reactor building,

and electrical

and instrument

and contr~i

devices installation in the control

room and the turbine

18

building.

The installations

were found to have

been

performed in accordance

with the requirements

established

in the installation documentation.

4.7

MG Set Test Blocks

Modification No. 86-25

and

MG Set Reliabilit

Modification No. 84-42

4.7.1

~Sco

e

Motor Generator

(MG) Set Test Blocks installation

was

necessitated

as corrective action to the Licensee

Event

Report 86-015,

"Reactor

Scram

and Reactor Building

Emergency Ventilation Initiation."

On May 30,

1986, during

refueling,

Nine Mile Point Unit

1 experienced

a reactor

scram

and reactor building emergency ventilation initiation.

The event

was presumably

caused

by inadvertent lifting of

neutral wire leads

on the output protective relay circuit

'during

a surveillance

test

on

MG set

162 output

voltmeter.

To preclude this event from recurring the

licensee

redesigned

the control circuitry, including

installing two new test blocks in each pro'tective relaying

cabinet of MG Sets

131,

141,

162

167 and

172.

In addition,

fuses

were also installed in the

MG Sets

synchronizing

circuits for -circuit isolations.

4.7.2

The

MG Sets

are connected

to 115

kV system

and any voltage

swing in the

system could constitute

loss of an

MG and

possible plant shutdown.

The

MG Set Reliability per

Modification No. 84-42 was implemented

to avoid this risk.

Accordingly,

each

MG set control circuitry was modified by:

( 1) replacing transfer relays

(83

& 83A) by hermetically

sealed

relays;

(2) installing potentiometers

with numerical

settings;

and, (3) adding alarm contacts for loss of dc

control

(MG Set

162,

167 and

172 only).

~Findin

s

The licensee's

safety evaluation

had determined that

MG

Sets Test Block, Modification No. 86-25 did not constitute

a safety-related

modification..

However,

MG Sets

162 and

172 and related control circuitries were associated

with

the reactor protection

system

(RPS),

and

as

such

10 CFR 50

Appendix

B was

imposed

on installation of isolation fuses

between

MG Sets

162 and

172 and their synchronizing

circuits.

General

Electric Test Blocks Type PK-2, Gould

Shawmut

6 Amp fuses

Type

OT6 and wiring for connection

were

procured

and installed

as

a safety-related

portion of this

modification.

The installation

was conducted

in accordance

with approved

procedures

by qualified individuals.

The

0

0

19

predetermined

witness/holdpoints

were observed

by the

gC

personnel

and quality workmanship

was supported

by adequate

documentation.

A plant tour was conducted

by the

NRC

inspector to verify physical configuration of the. devices

installed.

The modification, was found acceptable.

4.8

125

V dc

As discussed

earlier,

since

MG Sets

162 and

172 were

associated

with the

RPS,

the licensee

treated

the modifi-

cation of

MG set reliability as safety-related

and the

modification of MG Set

162 was completed

as

such.

The

modification of MG set

172 will be completed later.

The

inspector verified that procurement

and installation of the

replacement

relays,

potentiometers

and the alarm contacts

met the licensee's

quality assurance

requirements.

Installation

was performed in accordance

with approved

installation procedure

by qualified personnel.

gC has

provided adequate

coverage

to witness

and observation

holdpoints of the installation activities.

The inspector

conducted

a plant walkdown and verified the physical

configuration of the installed devices for MG Set

162.

A

portion of post-modification functional test of

MG Set

162

was also witnessed

by the inspector.

The test

was

performed

by qualified personnel,

and the test objectives,

as delineated

in the test procedure,

N1-POT-249A

(Attachment 1), were accom'pli shed satisfactorily.

Station Batter

Re lacement

Modification No. 85-92

4 '.1

4.8.2

~Sco

e

The purpose of this modification is to replace

both

channels

( 11 and

12) of the

125

V dc station batteries,

install recorders

in the battery

room to monitor floor

vibration,

and provide adequate

ventilation to maintain

proper temperature

in the battery

rooms.

~Findin

s

The licensee

determined that the existing

125

V dc

batteries

are approaching

end of their service lives.

Evaluation

suggested

that

an inadequate

equalizing

charge

had reduced

the battery performance.

In- addition,

the

licensee

suspected

that the floor vibration, caused

by

MG

set operation,

has contributed to sedimentation

and

contamination

in the cell fluids.

The inspectqr discussed

with the cognizant engineer

the replacement

of the station

batteries.

A preliminary calculation

had

been

performed

which determined that the replacement

battery with 59

cells,

instead of 60 cells, would allow for equalization at

or below 137.5 volts as required.

.The licensee

also

20

performed

a calculation for battery cable sizing.

Accordingly,

new cable

has

been installed to meet the

current carrying capacity

and voltage drops.

However,

the

new battery

was not installed.

The inspector

conducted

a

plant walkdown and verified the

125

V d c battery

conditions

and the installation'f new cables.

No

installation deficiencies

were identified.

Subsequent

to

the in'spection,

the licensee

informed

NRC Region I that the

installation of a

new 125 d.c. station battery

has

been

satisfactorily

completed.

4.9

Observation of Work Practices/Housekee

in

During walkdowns of some of the areas

in the Reactor

Building

associated

with the

above modifications,

the inspector

noted several

instances

of inadequate

work practices.

In the MSIV Room items were dismantled

from an outboard

MSIV's

operator.

These

items were tied off and

hung from a permanently

installed pipe line above the operator.

The inspector

noted

that

such items temporarily dismantled

could be supported

from

permanent

structure

and not from lines

such

as conduit or

piping.

At the

LPS storage

tank, several'tems

were noted

as follows:

(a) 'he

top manway cover

was

removed with no dust cover

installed.

(b)

On the tank exterior,

an electrical

connector at the bottom

was coated with boron concentrate.

(c)

The tank exterior contained

an approximate 4-inch diameter

chunk of putty (Duckseal) material

which gave the appear-

ance of a tank patch.

Although each of these

items were either corrected or being appro-

priately addressed

by the licensee

at the

end of the inspection,

the

inspector

noted that these

examples

indicate general

housekeeping

is

an area that can

be improved.

4. 10 Conclusions

Although some minor problems

were noted,

no violations were observed

and modification implementation

appears

to be generally satisfactory.

,However,

the licensee did agree to do

a determination of 10CFR50,

Appendix

8 quality requirements

concerning

the poison tank level

and

high temperature

alarm work prior to its completion.

Inspector

observations

indicated that there

was

need for improvement in the

development of installation plans

by

NMPC engineering

personnel.

21

Generally

examples

where

improvement could be realized would be

developing

more detailed installation plans

and having project

engineers

more familiar.with site activities.

Specific examples

include:

( 1)

RBCLC piping stress

analysis

reconfirmation is required prior to

the conduct of hydrostatic tests.

(2)

Kaowoll/Flameastic

appears

to be

an inadequate

containment

penetration

sealing barrier.

The licensee

must evaluate its

pressure

retaining capability.

5.

Plant Surveillances

Unit

1

61700

5.1

~Sco

e

n

The inspector

observed

outage

surveillances

in the following areas

including testing,

fuel movement,

examination of licensee's

surveillance

program for Hydraulic Control

Rods, control of spent

fuel pool material control

and determine, adequacy

of management

involvement

and supervision of ongoing activities.

The observed

outage

surveillances

and testing

were conducted

over the period of

this, inspections

Individual areas

are discussed. in each paragraph's

findings.

5.2

Inservice

Ins ection

H drostatic Test Procedure

~Sco

e

Observations

were

made of the conduct of "ISI Procedure

No.

Nl-ISI-Hyd. 44.2: Control

Rod Drive Scram

Dump Volume."

The

frequency of this test'is

once every

10 years.

~Fi ndi n

The inspector

reviewed test

and test

changes

to the procedure

and

one

concern

on test pressure

was resolved.

Observations

of the test

and

technicians activities

on job site prior to and during the

preparations

were as follows:

Test

Gauge

was properly calibrated.

Test

hoses

were acceptable.

The weld joints that were inspected

were properly prepared.

Test water source

was of proper quality.

Test boundaries

were verified on

a sampling basis

and found

correct by inspector.

22

The test procedure

choice of valve to be used for filling

system

and pressure

application point could not be used

due to

pipe interference.

A substitute

entrance

point was, documented

and approved

in a test change.

The filling of the

system

was not completed at the time of conclusion

of the inspectors

observation.

The Engineering

Group did not

physically verify their choice of hydro fill connection

which could

not be

used

due to a pipe interference.

However, technicians

were

knowledgeable

and did document

ongoing prerequistes

on

an official

field test procedure.

The test results

were satisfactory

and met

acceptance

criteria.

5.3

Instrumentation

Surveillance

5.3. 1 Reactor Protection

S stem

RPS

~Pur ose

The inspector witnessed

the

RPS transmitter calibration

Procedure

No. N1-ISP-C-RPS-XMIR.

The Rosemont transmitter

Analog Trip System is

a surveillance

required

by Niagara

Hohawk

plant nuclear specification.

~Findin

s

The calibration surveillance is performed

once

per operating

cycle, covering the operating

range of Transmitter

No. 36-04

C

Low Low Reactor

Level..

The as

found and adjusted calibration

were performed

and verified.

Return to service

was verified.

No deficiencies

were noted.

5.3.2

Leaka

e Test

Containment

Boundar

~Pur ose

The inspector verified the containment

boundary of the Core

Spray Valves80-114

and 80-115 which drain the

Core Spray

Header.

~Findin

s

The inspector

observed

the leak rate monitor being

used during

the leak rate test.

The instrument's

flow meter

and pressure

gauge

were properly calibrated

and the "Daily Check of the

Leakage Test"

had

been

performed.

The inspector verified the

boundaries

and vent valves'n addition, prior to the test,

23

the closure of the boundary valves

was witnessed

from the

control

room.

The licensee

maintained test pressure

for greater

than fifteen minutes

and

a leak rate of 3.0

SCFH was

'

established.

This valve is part of 'the data for the

summation

to determine total containment

leak rate.

No deficiencies

were

observed

during the test.

Test Procedure

No. Nl-IP-25 L.L. R;

Monitor Daily Check and Nl-ISP-C-25.2 Checklist data

sheet

were

used in the performance

of this test.

No deficiencies

were

identified.

5.4

Surveillance

and Observation of Fuel

Floor Activities

5.4. 1

Movement of Ei ht Fuel Assemblies

The licensee

had placed 'the

new fuel in dry storage

to

examine

the channel

to fuel assembly

tolerance.

The

purchased

clips that join channel

and fuel assembly

were

found to protrude into areas that would cause

interferences

during fuel loadings.

New clips were put in place

and fuel

was

moved from dry to wet storage

in the spent fuel pool.

The inspector

observed

the movement of eight fuel

assemblies

from the dry storage

racks to the spent fuel

pool.

Operators

were knowledgeable,

reactor analysts

were

tracking fuel movement,

communications

were established

'ith the control

room, proper logs were maintained to

verify fuel positions in the pool,

and material control. in

areas

of concern

were established.

The inspectors

observation of fuel movement

noted that the operations

department

had controlled procedures

that documented

placement of moved fuel.

No deficiencies

were identified.

5.4.2.

Surveillance Testin

of Hi

h Densit

Fuel

Rack

Neutron Attenuator

A review of available surveillance testing

procedures

indicated that Procedure

Nl-FHP-36 was not in the

licensee's

biannual

review schedule.

Discussions with

.the licensee

ascertained

that the procedure

"High

Density Racks

Boron Surveillance

Program"

was to be

modified and

had not been

completed at the previous

outage.

The schedule

to conduct procedures

Nl-FHP-36 was to be at

the first and

second refueling outages.

.The

new high

density

spent fuel racks were installed in 1985 and the

initial test

was performed in 1986.

The license's

vendor

that conducted this test failed to complete or document the

results of his his surveillance test.

The licensee

had initially installed

a surveillance

sample

train that consisted of a poison

assembly that was placed

in the spent fuel pool in an area

where the spent

assemblies

with the highest radioactive levels were to

radiate

samples

of boraflex.

The

sample train is a series

of

. 1 inch thick 2 inch, squares

of boraflex of the

same

material lot that was

used during manufacture

of the racks.

The removal of one

sample of boraflex and the testing of

the

sample for boron depletion

and flexibility is scheduled

for November,

1988.

No deficiencies

were identified.

5.4.3

S ent Fuel

Pool

SFP

- Cleanu

The inspector

observed

the material

stored in the

SFP

that was found in

a disarrayed

manner.

Corrective action

was discussed

with cognizant licensee

personnel.

The

licensee

had recognized after the

1986 outage that

a major

cleanup effort was necessary

to rid the fuel pool of spent

Source

Range Monitors (SRM), Intermediate

The

Range

Monitors (IRM), Low Power

Range monitors

(LPRM) and

numerous

other objects.

Initial review identified unmarked

material

hung

from the side of the fuel pool.

The licensee

has

a material

count list that identifies the material

in

the pool but it does not specify the area

where stored.

The inspector's

discussion with the Reactor Analyst staff,

'indicated that

a contract to cleanup

SFP

had been

completed

early in 1987 but due to the failure of the bridge crane

the contract

was

suspended.

A cleanup restart in early

October,

1988 is scheduled.

The licensee

stated that prior

to cleanup, all future material

placed in SFP will be

properly labeled

as to type, location

and date of

storage'ased

on licensee

committed resources

to cleanup

and

prepare

proper identification procedures,

the inspector

has

no further questions.

5.5

Surveillance of Work Re vest Retest

Re

uirement'he

inspector

observed

retests

of Work Requests

and to verified that

proper tests

vs. Technical Specification, requirements

were identified

on the uncompleted

work requests.

A number of work requests

(WR) were reviewed to determine that the

WR

packages

were complete

and that testing could proceed.

The

MR retest

review of the following WR No.

111271,

133369,

133407,

139662,

25

106344,

131920,

133596,

133595,

133342,

139719,

134178

and

133375

was

performed'he

typical work request

package

included:

Lifted lead

and jumper log identification notices

Repair procedure

Material issue chits

Crimping Tool Calibration Sheets - where applicable

Asbestos

Work

Permits'leanliness

Control

and Verification Sheets

and (}uality

Control Inspection

Reports

All retests

were found satisfactory.

When work requests

of a

greater

degree

of complexity were identified

a detailed

procedure

was required to accomplish acceptable

retests.

The

inspector

had

no other questions.

5.6

Surveillance of the Control

Rod Drive

CRD

H draulic

Control Unit

HCU

Isolation Valves

The plant's

Nuclear

Steam

System Supplier

(NSSS)

issued

Service

Information Letter (SIL) ¹419

on

a

CRD system

problem.

The SIL

discussed

failures in

HCV isolation valves where valve wedge

and

stem

separations

occurred.

as

a result the licensee

undertook

a program to

liquid penetrant

examine 10;.'f the valves,

which include

10 inlet

and

10 outlet valve wedges.

The licensees

liquid penetrant

examination of the

No.

101

and

No.

102

HCU valves

was performed during the

CRD removal for

maintenance.

The results of the examination

were that for the

101 valves,

2 rejections

were identified out of the

10 sample'd

and for the

No.

102 valves,

5 rejections

out of the

10 sampled.

The rejected

wedges

and

stem were replaced.

The licensees

valves,

which are closed only for maintenance,

are installed

with wedges

in

a horizontal position.

Failures would leave the

valve in an as-is position.

At the exit meeting the licensee

stated that

a safety evaluation

for the unlikely event

a wedge failure that could effect

operability would be performed prior to conclusion of the

outage.

The completion of the

HCU inspection

was scheduled

for

the next refueling outage.

During

a subsequent

period after

this inspection

the licensee

replaced all suspect

stems

and

wedges.

Licensee's

action is completed

and the inspector

has

no

further questions

in this area.

. 26

5.7

Low Power

Ran

e Monitor

LPRM

Plun er

Anamo'1

The fuel movement (core vnloading) surveillance

requires. the

replacement

or repositioning of the

LPRN's.

The

LPRN is placed in .the

core

upper grid plate

by the depression

of the top plungers.

Two

LPRN assemblies

experienced

.a pull-out of plunger from these

assemblies.

The licensee

scheduled

seven

replacements

of spent

LPRM's.

Installation calls for the upper spring loaded plunger section <o be

compressed

to locate

the

LPRM into the upper grid plate.,

'On release

of .plunger

a preloading of LPRM occurs ." During the replacement of

the

LRPM's into the vessel

two wf six Westinghouse

WL 24117

LPRM

assemblies

failed when cycled.

Zt was determined that when cyc1ed

the plunger sleeve flare .fails and separates

from the.- assembly.

The inspector

examined

the failed plunger parts and;<he to-be-

installed replacement

GE LPRM,'s.

The sleeve flare on failed

Westinghouse

LPRN's appears

to be

a case of metal rollover.

Additional test calibration by. Westinghouse. indicated that the spring

force from the

sudden

release

at two thirds (2/3).plunger depression

is more than twice the force necessary

to damage or overcome flare

retention in the piston tube.

The licensee's

review of the problem concluded that all newly

installed Westinghouse

LPRN's were

removed from the core due-to %he

potential

interference with the control

rod movement.

The inspector

witnessed

preliminary preparation for the installation of the

new QE

LPRM's.

The cavse of failure appears'.to

be

a Generic

Issue in that

a

similar failure of Westinghouse

had occurred. at. another nuclear

facility. The low power range monitor wnamoly was.competently

reviewed

by the Reactor Analyst staff and a decision .to remove The

new Westinghouse

LPRM'

was conservative.

The replacement

General Electric .LPRM's .have

been insta1led without

incident.

A potential

generic issue-will. be submitted to DQEA for

review.

5.8

Surveillance of Measurement

and Test

E vi

ent

METE)

In the course of observing.a

number. of surveillances,

a variety of

test instruments

were

used to determine

operating

parameters.

To.

determine

status of the

MATE program,

observations

were

made. at <he

combined mechanical

and electrical, tool. rooms and the Instrument and

Control Calibration area.

The licensee

has

a program for the control

and -evaluation of

calibrated

instrumentation.

A calibration frequency'has

been

established

and responsibilities for performance, of calibration is in

place

by the

use of a master test-5chedvle.

Recently <he .MLTE

C

, 27

controls of Units

1 & 2 has

been

combined.

A licensee audit of

equipment identified that approximately

30 instruments

were missing

and

a program to recover

and identify usage

is now underway.

The

M&TE program

has

a number of areas that exhibit

a potential for

future p'roblems.

The usage

log does not clearly define the area or

test that is to be monitored.

In one example,

and

an instrument

drawn out of the tool

room could be out

a equal to the calibration

frequency of the instrument.

The system

employed

by the licensee is

predominately

a manual

system that tends to fall easy

prey to

personnel

mistakes.

Additional management

attention

should

be

expended

to prevent future degradation

in this area.

This area

needs

additional

management

overview, for the calibration

program for

measurements

and testing of instruments.

Additional revision to the

program to eliminate

a number of concerns

in the area of recall of

instruments

and documentation

of usage of instruments

are

needed.

'.9

Conclusion

The inspectors

observations

and review of surveillance

program

indicated that licensee

had

a competent staff that produced

, workable procedures

that were properly implemented.

6.

" Procurement

Unit

1 and

2

35701

38701

36100

6.1

~Sco

e

s

Niagara

Mohawk Power

Company

(NMPC) (juality Assurance

Department

(gA)

had recently issued

two "stop work" orders at the plant

on the

use of

items for safety-related

applications that

had

been

purchased

as

commercihl

grade.

Therefore,

the review of this functional area

focused

on procurements

which primarilyi included

spare

and replace-

ment parts that were purchased

as commercial

grade

and dedicated for

safety related

use under the provisions of 10 CFR 21.

The implemen-

tation of this aspect of the procurement

program was assessed

to

determine if ( 1) evaluations

for. suitability of application were

being conducted;

(2) supporting documentation justified safety-

related applications;

and, (3) acceptance

criteria verified critical

attributes/characteristics.

Additionally, particular attention

was

given to the adequacy

and timeliness of corrective

measures

associ-

ated with the two stop work orders.

The procurement

practices

were

also reviewed for a selected

number (see Attachment A) of items that

were installed during the maintenance

and modification work discussed

in paragraphs

3 and 4.

6.2

~Findin

s

Concerns

about the manner

in which the engineering

evaluations

dedicating

commercial

grade

items for safety-related

use

28

resulted

in

QA issuing Corrective Action Requests

(CAR) during

May,

1987 (see

paragraph

7 for a more detailed discussion

on

corrective actions).

The specific evaluations

involved were

performed

by Stone

and Webster Corporation

(S&W), the architect

engineer

(A/E) for Unit 2.

Previous

CARs had been

issued

by QA

on similar concerns

and then additional

concerns

in the subject

area

were identified.

The final corrective actions to address

all of the

QA concerns

were basically to ( 1) have the station

Material

Management

group identify instances

of commercial grade-

items, used in safety-related

systems;

(2) determine that

adequate

documentation

of the engineering

evaluation which-

dedicated

the items for safety-related

use existed;

and, (3)

implement appropriate corrective actions

as

needed

(e.g. re-

dedication,

replacement,

Technical Specification

considerations).

Periodic

QA Surveillances

were initiated to

monitor these corrective actions.

When

one of these

survei llances identified the use of a non-dedicated

commercial

grade

item in a safety related

system the subject

stop work

orders

were issued.

Two of the additional controls

added to

existing corrective actions

were placing all commercial

grade

items

on

a "hold" status

in the warehouses

and the

need for

Quality Control

(QC) to verify that

an adequate

engineering

evaluation

was available prior to the release

of such

items for

safety-related

work.

A validation of the acceptability of issued

and in-stock

commercial

grade

items for safety-related

use at Unit

1 had

been

previously conducted for NMPC in 1985 by a contracted

agent.

Therefore

the current reviews,

mandated

by the corrective

actions

imposed,

would involve only those

procurements

since

that time.

The reviews at Unit 2 included

any and all

procurements.

Engineering staff of NMPC are conducting the

review of dedication

records at Unit

1 while

S&W has

been

contracted to do this review at Unit 2.

Numbers of engineering

evaluations

dedicating

commercial

grade

items for safety-related

application

deemed

acceptable

by

NMPC and

S&W engineers

were

reviewed during this inspection

to verify their adequacy.

The main warehouse

and storage

areas

were toured to verify that

commercial

grade

items were indeed placed

in

a hold status.

The

racks,

cabinets,

etc. containing these

items were prominently

identified by tape,

rope

and signs.

The Purchase

Orders

(PO), Material Issue Slips, dedication

packages

and other pertinent records

were reviewed for selected

commercial

grade

items that were installed during the mainte-

nance

and modification work discussed

in paragraphs

3 and

4 of

this report.

29

6.3

Conclusions

The documented

engineering

evaluations

performed

by NMPC.engineering

staff were thorough

and well written.

Critical attributes

and

characteristics

were identified and appropriate

examinations

and

tests

were specified for acceptance

of commercial

grade

items to be

used in safety-related

applications for both the re-dedications

done

at Unit

1 and the maintenance/modification

work.

An example

was the

engineering

evaluation

where material

composition

and harness

were

correctly considered

to be critical attributes/characteristics

of

emergency

diesel

generator

rocker assembly parts'imensions

and

surface finish should

have

been

i'ncluded in the list of attributes

to be verified during the dedication

process

even though defects of

this type would be identified during installation of the parts.

Also, subsequent

to this inspection

a former review of commercial

grave electrical

items dedicated for safety related

use

was conducted

and is discussed

in combined Inspection

Report 50-220/88-13

5 50

410/88-11.

No safety significant concerns

were identified but

examples

of improvements

to these evaluations

were discussed

with

NMPC cognizant

personnel

during the inspection

and

NMPC management

at

the exit interviews.

The engineering

evaluation

done

by

SEW for Unit

2 dedications

were minimally acceptable.

The methods

employed to identify commercial

grade

items

on hold were

adequate

and acceptable.

The requirement for gC to release

commercial

grade

items intended for safety-related

applications

only after

veri'fication of their acceptabil'ity

should prevent the

use of suspect

or unsuitable

items.

However, this

gC assignment

is not of a

permanent

nature

and

no permanent

resolution to prevent recurrence

has yet been defined.

Items installed during the maintenance

and modification work,

reviewed during this inspection,

was purchased

in accordance

with

established

requirements

and appropriate

dedication of commercial

grade

items

was accomplished

as necessary.

Further, it is the intent

of NMPC management

to have all corrective actions for Unit

1

completed

and closed out prior to restart

from the current refueling

outage.

Also, the

NMPC engineering

evaluation discussed

heretofore

indicated that

none of the approximately

60 identified instances

of

suspect

commercial

grade

items installed in safety

systems at Unit 1

resulted

in an unsafe condition or required. the replacement

of an

item.

The four instances

of suspect

items installed in safety

systems

at Unit 2 also did not cause

any safety concerns.

Therefore,

based

on the licensee's

technical

reviews the continued operation of

Unit 2 while the corrective actions

are still ongoing should not

compromise

safety.

t

'

30

7.

Corrective Actions Overview

Units

1 and

2

92720)

7.1

7.2

~Sco

e

The corrective Action Reports

and Nonconformance

Reports associated

with the maintenance

and modification work (see

paragraphs

3,

4 and

5) were evaluated for adequate

technical disposition

and timeliness

of resolutions.

Particular in depth analysis

was performed

on the

Corrective Action Reports

addressing

Commercial

Grade

(see

paragraph

6 and Attachment A) items

and their impact

on overall operations

of

both plants

and the procurement

process.

Conclusions

The resolutions

and disposition of Nonconformance

Reports,

which

deal primarily with hardware deficiencies,

were found to be

technically

sound.

The resolution of concerns

and unacceptability

of the affected

items

was completed prior to their operational

users

Corrective Action Reports

(CAR) were initiated promptly; resolutions

were technically sound;

and, closeouts

were reasonably

timely.

Those

CARs associated

with the commercial

grade

issue

were of long standing

duration.

The closeout of,CARs affecting Unit

1 has

been established

as

a requirement prior to plant re-start

by

NMPC management.

Corrective actions resulting

from especially

the gA Surveillance

effort appear to reverse

negative quality trends prior to development

of major problems.

The effectiveness

of corrective actions in which the guality

Assurance

Department

has

been

involved have

been significantly more

effective during approximately the past year since

a previous

NRC

inspection

performed in 1987.

8.

Su

ort Services

Units

1 and

2

35701

8.1

~Sco

e

The support services

provided to plant operations

were reviewed

with respect

to responsiveness

to plant needs,

attention to

completeness

of the assistance

provided;. and,

the performance of the

verification of quality.

The groups included were Engineering,

Material Management,

Procurement,

Maintenance

and guality Assurance

and their performance

was evaluated

during the review of the

specific functional

areas

discussed

in paragraphs

3, 4,

6 and

7 of

this report.

'

31

8.2

Conclusions

The various groups providing services

to plant operations

provided

timely assistance

when requested

and their effort was generally

found

to be complete

( see

referenced

paragraphs

for details)..

This was

noted to be

a continuing improvement during the past year and

previous outages with the area

most improved being engineering

support.

Also, the effectiveness

of independent

overview by QA/QC

personnel

was similarly found to be significantly improved.

Especially noteworthy was the effectiveness

of the

QA Surveillance

effort.

9.

Power Ascension Testin

- Unit 2

72700

9.1

~Sco

e

The licensee's

power ascension

program includes

a Generator

Load

Rejection Test,

Test

Number N2-SUT-27-6.

The test is performed to

demonstrate

the response

of the reactor

and control

systems to

a load

rejection.

The licensee's

preparation

for the generator

load reject

test requires

a method of simulating

a generator trip at the near

rated

power by opening the electrical line breakers

at the Scriba

Electrical

Load Station.

The review of procedures

and general test

method did not address

an unexpected

anomaly that did occur,

which

included

a trip of the reactor

and automatic actuation of engineered

safeguard

equipment.

9.2

Fi ~di n<i s

The inspector's

observations

prior to witnessing the t;est included

a

.

review of control

room panels,

checkoff of prerequisites

and

precautions

and the test directors briefing of test

team members.

Vendor personnel

were in attendance

and additional

licensed operators

were assigned

to monitor reactor

and secondary

system control panels.

At 11: 17 a.m.

on March 5, the electrical

breakers

were tripped at the

Scriba

Power Station.

Unit 2 was at

100% power and the unit tripped as

expected.

The expected

fast transfer of station

loads did not occur

and

the vital buses

were temporary stripped of loads.

The two operating

main

and booster reactor

feedwater

pumps tripped

and lowered. reactor

water'evels.

The automatic actuation

of the engineered

safeguards

equipment

occurred

when reactor water level

reached

108.8 inches; with the High

Pressure

Core Spray

and Reactor. Coolant Injection pumps aptivated

return the reactor to normal water levels.

Minimum observed

reactor

water

1'evel

recorded

as

97 inches.

Additional equipment 'activated

included the Standby

Gas Treatment

System, ventilation fans,

and

actuation of two (2)

SRV Relief Valves.

An "Unusual

Event" (UE) was

declared at 11:20 a.m.

due to the actuation of the Safeguard

Equipment.

On the re-establishment

of reactor

water the

UE was

terminated at 11:28 a.m.

'

32

9.3

Assessment

of the Event and Licensee

Performance

The inspector

was in the control

room prior to, during and after the

conclusion of the

UE and observed

the following:

The test director (TD) was cognizant of the event.

The various

control panel

operators

updated

the

TD as to system

parameters

at

frequent intervals.

Operators

remained at control panels

and

returned

the plant to normal in a controlled expeditious

manner.

However,

the control

room was occupied

by numerous

observers

that

were not contributing to the test.

Also, the post trip data analysis

was not available in

a timely manner.

The Test Director and operators

properly controlled the event.

Procedures

were

used

where required to bring equipment

back

on line.

The critique after the event

added meaningful

information to the

analysis of test results.

The overall licensee

personnel

conduct

during and after the event

was satisfactory.

A detailed

review of the course of the trip including the slow

transfer of electrical

loads is discussed

in

NRC Report

No.

50-410/88-02.

10.

Licensee Action on Previous

Ins ection Findin

s

Unit

1

(Open) Unresolved

Item (50-220/86-07-04):

The'nspec'tor

noted that the

licensee

did not have

a methodology for determining the effect

on ac and

dc emergency

busses

when

new loads are

added to the plant.

Based

on the

finding the licensee

agreed

to the following:

(2)

Revise station

procedure

AP-6.0,

Procedure

for Modification, to

consider

the effect of changing electrical

loads.

4

(3)

Review the effects that the

new safety related electrical

loads

may

have following station blackout'such

as

adequacy of battery life;

adequacy

of the battery charger;

and,

adverse effects

on breaker

relay coordination, if any.

The inspector verified the following licensee corrective actions.

(1)

Revise administrative

procedures

to require the maintaining of an

up-to-date listing of safety related

ac

and dc electrical

loads

and

procedures

for performing load change calculations.

The licensee

had established

extensive

safety related

ac and dc

load profiles; issued

125

v dc one line diagrams,

that did not

previously exist; revised engineering

procedure

NB-130, Design

Input Checklist,'o consider

ac

and dc load changes;

revised

procedure

NEL-021 to include electrical

load and component

J

33

change

sheets;

and,

revised

procedure

NEL-022 to

refer to load calculation procedures.

These

procedures

had not

yet been

approved or issued

and the estimated

issue. date

was

June

30,

1988.

Electrical design guidelines

have

been

issued

for performing interim electrical calculations.

The licensee

revised

procedure

AP-6 several

times

so that it is

now a broad policy procedure

and design checklists

are

now

included in other engineering

procedures.

This was verified

and, therefore,

AP-6 does

not need to refer to load change

considerations.

The licensee

stated that load change calculations

were

based

on the plant worse

case

scenario

which is loss of offsite

power with a concurrent

loss of coolant accident.

A station

blackout is not considered

in the station design basis.

Further,

a station blackout is an

open issue with the

NRC and

the licensee

is waiting for a final

NRC ruling on station

blackouts prior to taking further action.

Based

on the

above

review this item remains

open

pending

subsequent

review by the

NRC to verify that the engineering

pr'ocedures

discussed

above

have

been

approved.

11.

Unresolved

Items

Unresolved

items are matters

about which more information is required to

ascertain

whether they are acceptable

items or violations.

An Unresolved

Item is discussed

in paragraph

4.2;2.

12

Mana ement Meetin

s

The licensee

management

was informed of the

scope

and purpose of this

inspection at entrance

meetings

conducted

on February

29,

1988 and March

21,

1988.

The findings of the inspection

were discussed

with the licensee

representatives

during the course of this inspection.

An exit meeting

was

conducted

on March 25,

1988 at the conclusion of the inspection to provide

the findings of, this inspection to the licensee

management

(see

paragraph

1.0 attendees).

At no time during this inspection

was written material

provided

to the licensee.

The licensee

did not indicate that-any

proprietary information was involved within the

scope of this

inspection.

Attachment

A

Reference

Documents

1.0

2.0

Administrative Procedures

~AP

AP-5.0,

Procedure

for Repair,

Rev.

11

AP-8. 1, Preventive

Maintenance,

Rev.

3

I

Mechanical

Maintenance

Procedures

3.0

Nl-EPM-GEN-R150,

4. 16KV Breaker/Motor Inspection,

Rev.

0

Nl-EPM-SB-W265,

DC Batteries Pilot Cell Test,

Rev.

0

Nl-NMP-GEN-241, Overhaul

and Inspection of Station

Gate,

Globe,

Plub,

Ball and Butterfly Valves

Nl-MPM-C22, Removal,

Overhaul,

and Inspection of Main Stream Electromatic

Relief Valves

and Associated Pilot Valves

Nl-MPN-DG-R852, Emergency Diesel

Generator

Inspection,

Rev.

0

Work Re uests 4.0

132024,

Overhaul

and Inspect

DG Cooling Water

Pump

103 Discharge

Check

Valve

13205,

Overhaul

and Inspect

DG Cooling Water

Pump

102 Discharge

Check

Valve

132815,

Replace

Liquid Poison

Pump Packing

139722,

Replace

Relay

on Core Spray Discharge

Valve Breaker.

134000,

Retorque

Coupling Nut and

Screw

on

HCU 126 Valve

139964,

Check Switch Problem

on

RBCLC. Pump

No.

11

140143,

DG 103 Engine Temperature

Switches

Instrument

and Control Procedures

Nl-IP-92.2, Temperature

Switch,

Rev.

1

Nl-ICP-A-041-001, Instrument Calibration Procedure

for Liquid Poison

System,

Rev.

0

Nl-ESP-Sb-W276,

125

VDC Weekly Pilot Cell Surveillance,

Rev.

0

Nl-ESP-Sb-W276,

125

VDC Weekly. Pilot Cell Surveillance,

Rev.

0

5.0

En ineerin

Documents

NMPC Specification

No.

330M - Installation of Reactor Building Closed

Loop Cooling Heat Exchangers

Nuclear Engineering

and Licensing Procedure,

Design

Verification, Rev.

2

Conceptual

Engineering

Package for Alternate

Rod Injection System,

March 24,

1987

Conceptual

Engineering

Package

for Addition of Motor Generator

Set Test

blocks,

February

27,

1987

E

Attachment

A

6.0

Preliminary Calculation for the Station Battery Cell Reduction,

Calc.

No.

125VDC-MG161-ES

Functional Specification for Motor Generator

Set Reliability,. May 12,

1985

Conceptual

Engineering

Package for Feedwater

Check Valve Replacement,

October 8,

1987

Conceptual

Engineering

Package

for Reactor Building Closed

Loop Cooling

Heat Exchanger

Replacement,

May 28,

1987

Other Reference

Documents

10 CFR 50, Appendix

B

10 CFR 50.59

Quality Control Inspection

Report 1-88-0421,

NSR Relay Replacement

for

SF Breaker

Determination of Appendix

B Requirements,

No. 86-1025,

Determining

When

Valve Stems

Are Safety Related

Safety Evaluation for Addition for Motor Generator

Set Test Blocks,

Rev.

2, September

15,

1987

Safety Evaluation,

Control

Rod Drive/Scram

Dump Volume, February

12,

1981

Pre-Operational

Test Procedure

No.

249A,

MG Sets Reliability -

MG Set

162, January

5,

1988

Project Report for Motor Generator

Set Reliability, March 18,

1985

Project Report for ATWS - Alternate

Rod Injection System,

February

4,

1987

LER 86-15,

Reactor

Scram

and Reactor Building Emergency Ventilaton

Initiation

ualit

Control Ins ection

Re orts

1-88-0014,

Receipt inspection of Heat Exchangers

1-88-0421,

NSR Relay Replacement

for

SF Breaker

Determination of A

endix

B

Re uirements

86-1025,

Determining when valve

stems

are safety related or not

ualit

Assurance

Surveillance

Re orts

88-20131,

88-20168,

88-20123,

88-20120,

88-20114,

88-20113,

88-20104,

88-20090,

88-20029,

. 88-20018,

88-20016,

87-20060,

Welding

QC

CBI Installation work

CBI Fabrication work

CBI Fabrication

work

Heat Exchanger

Replacement

Heat Exchanger

Supports

Heat Exchanger

Replacement

Heat Exchanger

Internals

Grout and Anchor Bolt Installation

Rigging/Lifting of Heat Exchanger

Heat Exchanger

Straps

0

~ Attachment

A

10.

Corrective Actions

Re orts

87.3060,

Commercial

Grade

GE Items

87.30336,

Commercial

Grade Evaluations

87.3037,

Commercial

Grade

Purchase

Orders

87.3038,

Valve Evaluations

87.3039,

Receipt Inspection

88.2008,

Material

Useage

88.2009,

Heat Exchanger

Descrepancies

88.2002,

Grout and Anchor Bolts

SUMMARY OF MAINTENANCE

~Stree

tha

Individual performance

of mechanics

and technicians

reflected

a genuine

desire to do

a quality job.

A mechanic,

for example

researched

the

vendor technical

manual for the torque values for a check valve flanges

on the

DG cooling water

pump.

The generic

procedure

Nl-MMP-GEN-241

simply required

the flange bolts to be tightened.

~Ade uate

Procedures

were adequate

and followed.

Personnel

were adequately

trained

and qualified.

QA/QC coverage

was adequate.

Documented

Work Request

(MR) packages

were adequate.

Weaknesses

Paperwork to initiate

a corrective maintenance

(WR) action is time

consuming.

An urgent work request

(MR 139964) for the Reactor Building

Close

Loop Cooling

Pump

No.

11 motor took several

hours to process.

NM1

mechanical

Maintenance

Superintendent

has

been

assigned

the task to

streamline the'ork control effort.

He will be supported

by

a contractor.

-