ML17037C136

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Letter Advising That the Power Level of 1850 Mw(T) Was Achieved and Testing Was Performed During the Week of December 5, 1971 and That Comprehensive Reports Are in Preparation and Will Be Available for Review
ML17037C136
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 12/15/1971
From: Schneider F
Niagara Mohawk Power Corp
To: Morris P
US Atomic Energy Commission (AEC)
References
Download: ML17037C136 (6)


Text

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NIAGARA MOHAWK POWER CORPORATION

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MOHAWK 300 E'RIK BOULEVARDWEST SYRACUSE, H.Y. l3ROR QSgga4%$

F9e A December 15, 1971 Dr. Peter A. Morris, Director Division of Reactor Licensing United States Atomic Energy Commission Washington, D. C.

20545

Dear Dr. Morris:

Re:

Provisional Operating License DPR-17 Docket No. 50-220 In our petition for escalation of licensed power to 1850 MW(t) from 1538 MW(t) for Nine Mile,Point Nuclear Station, Unit No.

1 reactor, we described certain tests that would be performed when that power level was reached.

That level was achieved and testing performed during the week of December 5,

1971.

These tests, both static and dynamic in nature, correspond to the listing in Technical Supplement to Petition to Increase Power,Section II, page 33 and demonstrate reactor response and analysis of core operating parameters for several types of perturbations imposed in the system.

1. LPRM 'Calibration The LPRM instrumentation was calibrated to read the average heat flux of the four corner, rods surrounding each detector at the eleva-tion of the detector.

Individual TIP traces were used to calculate required'power-distribution information.

The correct LPRM reading for the existing reactor conditions were determined and the LPRM amplifiers adjusted accordingly.

"2. Core'Performance'Evaluation The principal core parameters of peak heat flux and Minimum Critical Heat Flux Ratio (MCHFR) were determined for several radial locations.

The peak heat flux was found to occur in fuel adjoining LPRM location 04-25, at a value of approximately 94 watts/cm4.

The total peaking factor cal'culated was approximately 2.3, well below the allowable of 3.08.

In addition, the Core Minimum Critical Heat Flux Ratio was found to occur at the location of the peak heat flux.

This was approximately two feet above core bottom with a value of 3.33.

This is above the minimum allowable MCHFR of 1.9 for the full recirc-ulation flow condition.

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Dr. Peter A. Morris, Director Division of Reactor Licensing December 15, 1971 3.

APRM Calibration The Average Power Range Monitors (APRM) were calibrated several times during the pesting period.

The core thermal power was calculated from detailed heat balances of the reactor and associated systems.

Following past practices, APRM's were adjusted to read 100~a with core thermal power between 1538 Ml((t) and 1850 Mif(t).

4.

Power Calibration 'of'Rods During the power ascension to the full design rating, various plant data was collected for the withdrawal of several control rod."

notches.

Changes in the measured parameters were as expected.

S.

Flux Res onse to.'Rods Control rod 10-31 was withdrawn from position 18 to 20 and the response of LPRM 12-33C was recorded.

The local neutron flux initially decreased as the rod was inserted to unlatch the collect fingers and then increased as the rod was withdrawn.

The response of neutron flux, reactor water level and reactor pressure was well-damped with little or no overshoot from their final value at equilibrium.

6. Pressure 'Regulator'Test The performance of the pressure regulation system was demonstrat-ed using both the Electrical Pressure Regulator (EPR) and the Mechanical Pressure Regulator (MPR) as follows:

a.

nominal plus/minus 10 psi set point changes with the turbine control valves providing pressure regulation.

b.

nominal plus/minus 10 psi set point changes with the turbine by-pass valves providing pressure regulation.

c.

demonstration of pressure regulator takeover by both the EPR and MPR.

For all tests, the response of steam flow, reactor pressure, reactor power and reactor water level was well damped showing no significant oscillatory behavior.

7.

By-ass Valve Test The by-pass valve test consisted of opening and closing one by-pass valve to demonstrate the capability of the pressure regulator to minimize reactor'pressure disturbances caused by changes in reactor steam flow.

By-pass valve ¹12 I was opened in approximately 11.S sec-onds using the by-pass valve functional test switch.

The valve remained opened for approximately 65 seconds and then closed.

The response of principal parameters was well-damped and exhibited no major oscillatory behavior.

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Dr. Peter A. Morris, Director Division of Reactor Licensing December 1S, 1971 8.

Feedwater Pum Test Reactor water level was first decreased then increased by approximately 6 inch increments with successive adjustments to the feedwater controller.

Reactor power response in both cases was strongly damped during the subcooling changes produced by the level setpoint changes.

In addition, the feedwater control system was very stable as the feedwater, vessel level response was well-damped.

9.

Recirculation Flow Control The master recirculation speed controller was adjusted to give plus/minus 10~~ flow changes.

During the core flow reduction, core flow rate decreased at an average rate of 6~~ per minute.

Reactor power and pressure decreased with little or no over shoot prior to settling at their respective final equilibrium value.

During core flow increases, core flow rate increased at a faster rate but the system response again well-damped with little or no over shoot.

Response

of the various systems and reactor are at least as good as anticipated and project the ability of the plant to handle transients of greater magnitude.

Therefore, to minimize the detrimental effect of major transient testing on the fuel, we will defer the following tests until just prior to the next time the vessel head is removed, April 1972.

'1.

Maximum Recirculation Flow Changes 2.

Five Recirculation Pump Trip 3.

Turbine Trip This is being done in the spirit of and conformity to recent changes in 10 CFR 20, whereby, we should hold off-gas releases to as 'low a prac-tical value while at the same time assuring the public a dependable source of power.

During the interim period, auto-start recorders will be installed to obtain data necessary to prove-out the above tests should an inadvertent trip of the turbine take place.

Comprehensive reports of the test.performed during the week of December S,

1971 are in preparation and will be available for review.

Very truly yours, F. J Schneider Vice President - Operations

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