ML16343A266

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Insp Repts 50-275/94-24 & 50-323/94-24 on 940901-1015. Violations Noted.Major Areas Inspected:Response to Events, Operational Safety Verification,Plant Maint,Surveillance Observations,Plant Support Activities & Onsite Engineering
ML16343A266
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 11/18/1994
From: Kirsch D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342C746 List:
References
50-275-94-24, 50-323-94-24, NUDOCS 9411280044
Download: ML16343A266 (48)


See also: IR 05000275/1994024

Text

APPENDIX B

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-275/94-24

50-323/94-24

Licenses:

DPR-80

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room

1451

P.O.

Box 770000

San Francisco,

California

Facility Name:

Diablo Canyon Nuclear

Power Plant,

Units

1

and

2

Inspection At:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

September

1 through October

15,

1994

Inspectors:

M. Tschiltz, Resident

Inspector

D. Corporandy,

Project Inspector

P. Goldberg,

Reactor

Inspector

C. Paulk,

Reactor

Inspector

L. Ellershaw,

Reactor

Inspector

B. McNeill, Reactor

Inspector

R. Pate,

Reactor

Inspector

Approved:

D, Ki sc

,

C ie

,

eactor

Prospects

rane

Ins ection

Summar

Date

Areas

Ins ected

Units

1 and

2

Routine

announced

inspection of onsite

response

to events,

operational

safety verification, plant maintenance,

surveillance

observations,

plant support activities, onsite engineering,

followup maintenance,

and onsite

and in-office review of licensee

event

reports

(LERs).

Results

Units

1

and

2

~0erati one:

Strength:

~

Refueling evolutions

were conducted

in

a precise

manner.

Problems

which

arose during fuel handling evolutions were resolved conservatively,

with

appropriate

regard for safety.

9411280044

941118

PDR'DOCK 05000275

6

PDR

Weakness:

~

A less

than

adequate

questioning attitude,

regarding

fDG configuration

and test requirements,

resulted

in attempting to test

EDG 2-1 with a

grounding device installed.

Strength:

~

The licensee's

investigation of MSSV and

PRV setpoint inaccuracies

showed significant effort and resources

had

been dedicated

to resolution

of this issue.

Although no specific solution to the problem

had

been

developed to date,

licensee efforts involved with the evaluation of

relief valve setpoint drift are viewed

as proactive

and thorough.

Maintenance:

Strength:

~

The high level of preplanning

and coordination of work and testing

significantly reduced

the duration of the higher risk evolutions during

the outage.

Weakness:

~

During Refueling Outage

2R6 there

were several

examples of deficiencies

in the method of controlling work and managing

equipment configuration.

Although, singularly, these specific instances

were not of great

significance,

when considered

in total there

was

an apparent

weakness

in

system configuration control.

This resulted

in several

instances

of

premature

authorization of work and testing

and inadequate

clearance

boundaries.

~PP

1

Strength:

~

Radiation

exposure

was significantly reduced

from Refueling Outage

1R6.

Although dose rates

were,

in general,

lower in Unit 2 containment,

as

compared to Unit 1, outage preplanning

and incorporation of lessons

learned

from Refueling Outage

1R6 appeared

to be significant

contributors in the reduction of personnel

exposure.

Summar

of Ins ection Findin s:

~

Violation 275/94-24-01

was identified (Section

2. 1).

~

Noncited Violation 323/94-24-01

was identified (Section 2.2),

1

I

1

F

0

~

Noncited Violation 323/94-24-02

was identified (Section

4. 1).

~

LERs 50-275/93-003,

Revision

1; 275/94-016,

Revision 0; 323/94-002,

Revision 0; 323/94-003,

Revision 0; 323/94-004,

Revision 0;

and 323/94-

005, Revision 0,

were closed

(Section 8).

~

LERs 50-275/94-009,

Revision 0,

and 50-275;323/94-003

were reviewed

and

remain

open pending completion of additional

inspection

(Section 9).

Attachments:

~

Attachment

1 Persons

Contacted

and Exit Heeting

~

Attachment

2 Acronyms

DETAILS

1

PLANT STATUS

(71707)

1.1

Unit

1

Unit

1 operated

at

100 percent

power during the entire inspection period.

1.2

Unit 2

Unit 2 operated

at

100 percent until September

21,

1994,

when the unit power

was reduced to maintain plant temperature

as the core reached

the end of life.

On September

24,

1994, Unit 2 was separated

from the grid and shutdown for

Refueling Outage

2R6.

Unit 2 remained

shut

down for the remainder of the

inspection period.

2

OPERATIONAL SAFETY VERIFICATION

(71707)

2.1

ESF

S stem Walkdown

During this inspection period,

the inspectors

performed

a safety

system

verification inspection.

This involved

a detailed inspection of a sample of

the accessible

portions of the instrument alternating current

(AC) system.

The inspectors utilized Operating

Procedure

(OP) J-10: II, "Instrument

AC

System

Alignment Verification," Revision ll, as guidance for the

verification of the system configuration.

The purpose of OP J-10: II is to

verify normal

alignment

and operation of the instrument

AC system.

The inspectors

found two breakers

which were improperly labelled in

Attachment 9. 1 to the procedure.

The first breaker

was labelled

as

"PY-11A

Normal Supply Breaker

11N."

In accordance

with the alignment procedure,

the

breaker

should

have

been labeled

11AN.

The second

breaker

was labeled

as

"PY-

13A Normal Supply Breaker

13N."

In accordance

with the alignment procedure,

the breaker

should

have

been labeled

13AN.

The inspectors

also noted that the

white "power available" indicating light for Panel

PY-11A was not illuminated

as required

by the checklist.

Additionally, the inspectors

observed

that

there

was inconsistency

in the positioning of the spare

breakers

in that

some

were being maintained

in the open position

and others

were closed.

The

inspectors

informed the senior operator

who accompanied

them on

a portion of

the verification of these discrepancies.

During the inspection of the instrument

AC system,

the inspectors

found that

Breaker

11-18 in Panel

PY-11 was

opened without having

an active clearance

request.

This

w'as not in accordance

with Attachment 9. 1 of Procedure

OP J-

10: II, which required all individual load breakers

to be closed

and

any open

breakers

to be tagged

by an active Clearance

Request.

The inspectors

ensured

that the senior operator

was

aware of this discrepancy.

The senior operator

investigated

the required position of Panel

PY-11-18

and determined that the

breaker

should

have

been closed.

Operations

then closed the breaker

and

rt

reperformed

the alignment verification checklist

and found no other anomalies.

The inspectors

also noted that

OP H-5: II, "Control

Room Ventilation System

Alignment Verification," Revision 8, Attachment 9.2,

"Alignment Verification

Checklist," also required

Breaker

PY-11-18 to be closed.

The inspectors

found, in Attachment 9.2 to Procedure

OP H-5: II, that the load was the backup

power supply to the Unit 2 Train A logic and that the breaker

should

have

been

closed.

The inspectors

also found that Section

8. 1 of Procedure

OP H-5: II required

that the completed checklist

be routed to the Shift Technical Advisor,

and

that the completed checklist

be in the control

room file until superseded.

When the inspectors

requested

a copy of the checklist from the Shift Technical

Advisor, the checklist

was not found in the control

room.

Further

investigation

by the licensee

regarding

the completed checklist failed to

identify its location.

The licensee

reperformed

the checklist

and

has filed

it in the control

room.

Additionally, the licensee verified that copies of

other procedures

were being maintained

as required in the control

room.

Safet

Si nificance

Technical Specification (TS) 3.7.5. 1 requires

at least

two separate

trains of the control

room ventilation system

be operable

in all

modes.

Each unit has

a train of control

room ventilation.

Each of the trains

consists of two subtrains

made

up of a supply fan,

a condenser,

a compressor,

a booster fan,

a pressurization

fan

and heater,

and respective

dampers.

The

subtrains

for each unit share

a

common high efficiency particulate air filter

and charcoal

adsorber

component.

Each of the subtrains

has

both

a normal

and

backup

source of 120 volt instrument

AC.

Breaker

PY-11-18 supplies

the backup

power to Transfer Switch

EJPA, which feeds

the Unit 2 Train

A logic circuits,

Specific loads include:

control

room ventilation intake radiation monitors,

control

room ventilation damper indications,

and nonvital exhaust

Fans

E-35

and

E-36 permissive control circuits.

Normal system operation aligns

one

subtrain

per unit for operation.

The loss of the normal

120 volt instrument

AC power to Unit 2 Train A would result in a radiation monitor failure alarm

on the main annunciator.

If the

120 volt instrument

AC power was aligned to

the backup

power source with the Breaker

PY-11-18 open,

as

was found, the

power would not be restored.

If the problem was not readily apparent,

the

operator could realign to the other unit subtrain

and investigate

in

accordance

with annunciator

response

requirements.

Without 120 volt

instrument

AC, 480 volt equipment

would remain operational

and control

room

ventilation dampers

would fail as-is.

A total loss of a train (i.e., both

unit subtrains)

would result in entry into

a 7-day Action Statement.

If an

event were to have occurred with this alignment,

Emergency Operating

Procedure

(EOP)

E-0 required that operators

check control

room ventilation for

proper alignment following a reactor trip or safety injection and prompts

selection of another

subtrain if the in-service train has failed,

In the

situation where'll control

room heating, ventilation,

and air conditioning is

lost, operators

would have in excess

of

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to reestablish

control

room

ventilation flow without exceeding

control

room temperature limits.

Conclusion

The failure to maintain the breaker closed

as required

by

Procedures

OP H-5: II and

OP J-10: II was

a violation of TS 6.8. 1, which states,

in part, that written procedures

be established,

implemented,

and maintained

covering applicable

procedures

recommended

in Appendix

A of Regulatory

Guide 1.33, Revision

2, dated

February

1978.

Appendix A of Regulatory

Guide 1.33,

Revision 2,

recommends

procedures

covering surveillance testing;

preventive maintenance;

and startup,

operation,

and

shutdown of safety-related

systems.

Contrary to this requirement

implemented

by OPs H-5: II and J-10: II,

on September

22,

1994,

Breaker PY-ll-l8 was noted to be open without having

an

active clearance

request.

This is

a Severity Level

IV violation (275/94-24-01).

2.2

Clearance

of Both Centrifu al

Char in

Pum

s In Mode

4

During the performance of OP L-5, Revision

17, "Plant Cooldown from Minimum

Load to Cold Shutdown,"

both centrifugal charging

(CC)

pumps were cleared

while the plant

was in Mode 4.

TS 3.5.3,

applicable to Mode 4, requires that,

as

a minimum,

one emergency

core cooling system

subsystem

which includes at

least

one

CC pump

be operable.

However, while in Mode 4, both

CC pumps were

inoperable for

a period of approximately

67 minutes.

CC

Pump 2-1 was cleared

during the performance of OP L-5, Step 6.2. 17.

CC

Pump 2-2 was cleared

at the

same time in anticipation of the

TS requirement to disable

an additional

charging

pump when in Mode

5 prior to decreasing

below 161.9'F.

The shift

foreman authorized

the clearance

which removed

both

CC pumps from service.

Prior to providing the clearance

tags to the operators,

the shift foreman

recognized that

TS prohibited clearing both

CC pumps in Mode 4, but failed to

communicate this to the operators

and mistakenly authorized

hanging the tags

for both

CC pumps.

Since the hanging of the tags is controlled

by

OP L-5,

there

was not

a related

clearance

request;

therefore,

Attachment 9.5 of OP L-5

was

used to document

the hanging of the tags in accordance

with the proced'ure.

When hanging the tags,

on the control board,

the attachment

specified

clearance

of CC

Pump 2-1 or

CC

Pump 2-2.

Consequently,

the procedure

did not

have

a provision for the operators

to hang tags

on both pumps.

Additionally,

when hanging the tags

on the power supply breaker,

the procedure similarly

specified: clearance

of the breaker for CC

Pump 2-1 or

CC

Pump 2-2 but did not

have

a provision for disabling both.

In each of these situations,

the

operators

hanging the tags

made unauthorized

changes

to the procedure

by

changing the "or" to "and" and adding signature

blocks for the performer

and

independent verification of the tags.

Approximately 67 minutes after the

CC

Pump 2-2 was declared

inoperable,

the shift foreman,

when observing the

control boards,

noted that both

CC pumps

had

been cleared in contrary to the

TS requirement for Mode 4.

The shift foreman immediately restored

CC

Pump 2-2

to service.

i

Safet

Si nificance

The clearing of both

CC pumps

when in Mode

4 resulted

in

the inadvertent 'entry into TS 3.5.3, Action Statement

a.,

which required at

least

one emergency

core cooling system

subsystem

be restored

to operable

status within the next hour or be in Cold Shutdown within the next

20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />.

Since the plant was

shutdown

and in the process

of cooling down to

a cold

shutdown condition,

and since

CC

Pump 2-2 was returned to service after

0-

l 'I

t

0

removing both

CC pumps for period of slightly greater

than

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, the safety

significance of this event is minimal.

Conclusion

The inadvertent entry into TS 3.5.3 resulted

from inadequate

consideration of TS requirements

for Hode 4.

The improper authorization of a

clearance for both

CC pumps,

combined with the unauthorized

changes

made to

Attachment 9.5 of OP L-5, resulted

in simultaneously clearing both

CC pumps.

The clearance

of both

CC pumps

was not in accordance

with the requirements

of

Attachment 9.5 of OP L-5,

This is

a violation of TS 6.8. 1., which states,

in

part, that written procedures

be established,

implemented,

and maintained

covering applicable

procedures

recommended

in Appendix A of Regulatory

Guide 1.33,

Revision 2, dated

February

1978.

Appendix A of Regulatory

Guide 1.33,

Revision 2,

recommends

procedures

covering surveillance testing;

preventive maintenance;

and startup,

operation,

and shutdown of safety.-related

systems.

Contrary to this requirement,

on September

24,

1994,

both

CC pumps

were cleared while in Hode 4.

Since the violation is of very low 'safety

significance

and since the inspectors

are satisfied with the

adequacy of the

corrective actions,

in accordance

with Section VII.B.(2) of the Enforcement

Policy, this violation was not cited (323/94-24-01).

3

PLANT HAINTENANCE

(62703)

During the inspection period,

the inspector

observed

and reviewed selected

documentation

associated

with the maintenance

and problem investigation

activities listed below to verify compliance with regulatory requirements,

administrative

and maintenance

procedures,

required quality assurance/quality

control department

involvement, proper

use of safety tags,

proper equipment

alignment

and

use of jumpers,

personnel

qualifications,

and proper retesting.

Specifically, the inspector

witnessed

portions of the following maintenance

activities:

Unit

1

Relief Valve CVCS-1-8116

Replacement

~

CC

Pump 1-2 Gear Oil Cooler Inspection

Unit 2

~

Resistance

Temperature

Detector

(RTD) Bypass Hanifold Elimination

~

Fuel

Bundle Visual Examinations

~

Core Offload and Reload

~

Inverter IY-22 Installation

3. 1

RTD

B

ass Manifold Elimination

The inspector

observed

welding being performed

by a licensee

vendor in

conjunction with the

RTD modification on two occasions:

gas tungsten

arc

welding on Joint

FWI-FH207 and shielded

metal

arc welding on Joint FW4-FH207.

The inspector

reviewed

and verified that the weld procedure

specifications

(WPSs)

were properly qualified in accordance

with the

ASHE

Code.

During each of the observations,

the inspector verified that the welder

used

the proper

WPS

and that the heat

numbers of the welding material

in the

welder's

possession

were the

same

as that which were identified and documented

on the welder's

weld rod requisition slip.

During the gas tungsten

arc

welding process,

the inspector verified that the argon

gas flow rate

was set

in accordance

with the

WPS.

Additionally, the inspector

observed

the vendor

quality control inspector

measure

both the interpass

temperature

and the

amperage.

The measured

values

were within the established

limits specified

by

the

WPS.

During observation of the shielded

metal

arc welding on Joint

FW4-FH207, the

inspector

noted that the coated electrodes

(Type E-316L) were properly stored

in heated

electrode

caddies.

This particular weld joint required the initial

passes

to be performed

using the gas tungsten

arc welding process

and the

remaining

passes

to be performed using the shielded

metal

arc welding process.

The gas tungsten

arc welding had

been

completed

and the inspector

observed

the

welder begin the shielded

metal

arc welding.

The welder

had already set the

amperage

and voltage

on the power source.

However, after striking an arc

on

the component

and depositing slightly less

than

a 1/2-inch bead,

the welder

determined that

a higher amperage

was needed.

The welder stopped welding,

reset

the power source to

a higher amperage,

and ground out the weld metal

he

had just deposited.

The inspector questioned

the welder regarding his use of

the actual

component rather than

a "strike" plate to determine if he

had

sufficient amperage.

The welder stated that

he often used

a file or chipping

hammer

as

a "strike" plate,

but since the gas tungsten

arc welding and the

shielded

metal

arc welding

WPSs

had virtually the

same

amperage

parameters

(for the size electrode

being used),

and since the power source

had

been set

up by the previous welder

and verified by

a quality control inspector,

he

concluded it was not necessary.

The welder did obtain

an available

mockup of

the component to verify that his

new amperage

setting

was sufficient prior to

resuming welding on the actual

component.

While it did not appear that the

WPS

had

been violated, the inspector

considered

the

use of an actual

component,

rather than

a "strike" plate, to

determine if sufficient amperage

existed,

to have

been

an example of poor

practice.

The inspector discussed

this observation with licensee

and vendor

management.

It was determined that there

was

no prohibition regarding this

practice,

and eRisting general

welding procedures

did not address

the subject.

In any event,

licensee

and vendor management

personnel

acknowledged

and

understood

the concern.

The vendor quality assurance

site manager

immediately

discussed

this concern with the vendor welders

and conducted

a documented

"tailboard" (training session).

The session

used

a training document that

clearly described

the checking of welding parameters

prior to welding on

production parts or equipment.

The methodology consisted

of welding on

a

stainless

steel test piece to verify proper operation of the welding equipment

and the use of a calibrated

amperage

probe to check

amperage

and voltage prior

to production work.

It was also stressed

that the preset

welding parameters

are to be rechecked

any time welding variables

are

changed

and that these

activities will be monitored to assure

compliance.

Conclusion

The inspector considered

that the licensee's

corrective actions

were sufficient to address

the identified welding technique

concerns.

3.2

Inverter IY-22 Installation

The inspector

observed

selected

cable pulls which were part of Design

Change

Package

(DCP) DC2-E-48283.

Cables

211D,

211N,

G35POOA,

G35POOB,

and

G35POOC

were pulled from Cable Tray

RPAC through Conduits

K458H and

K7661 to

Panel

IY-22.

The inspector verified that the configuration

and mounting

detail

were properly implemented

by the licensee.

Also, the inspector

observed that cable pull techniques

(e.g.,

minimum bend radius,

no nicks,

cuts,

or scratches)

were proper

and that the quality control inspector

completed all required quality control hold point inspections.

Conclusion

The observed

cable pulls for the selected

cables

were

made in

accordance

with the work order.

3.3

Confi uration

Mana ement Durin

Refuelin

Outa

e

2R6

During Refueling Outage

2R6, there

were

a number of problems involving the

control of work.

These

problems

occurred

as

a result of the licensee's

failure to adequately

consider the effects of existing plant conditions

on

changes

in work activity schedules,

the licensee's

haste to accomplish

work,

and inadequate

communications.

3.3. 1

Auxiliary Feedwater

(AFW) Discharge

Check Valve (AFW-2-380) Bonnet

Removal

Work was authorized

on Valve AFW-2-380 which involved disassembly

of the

valve.

Valve AFW-2-380 is not isolable

from Steam Generator

(SG) 2-4.

Containment closure

was in effect at the time the work was being performed,

since core alterations

were in progress.

Work on Valve AFW-2-380 was within

the boundaries

set for containment closure,

since the secondary

side of SG 2-4

was

open to containment

atmosphere.

Valve AFW-2-380 work was originally

scheduled

to commence after the completion of core off-load; however,

changes

in the outage

schedule

resulted

in disassembly

of the valve during core

alterations.

During removal of Valve AFW-2-380, bonnet water was observed

to

be leaking from the body-to-bonnet

connection.

When the mechanic

working on

the valve noted the water,

work on the valve was stopped

and the body-to-

bonnet joint was tightened.

The licensee's

investigation revealed that the

work on Valve AFW-2-380 had improperly occurred during core alterations.

-10-

Safet

Si nificance

Containment

closure

was not violated when Valve AFW-2-380

was partially disassembled

since the feed line was full of water; therefore,

the loosening of the valve bonnet did not provide

a direct path from the

containment

atmosphere

to the outside

atmosphere.

~Summar

Work controls were inadequate

in that they did not prevent work

within the boundaries

established

for containment closure.

Additionally, when

the work on the valve was rescheduled,

inadequate

consideration

was given to

the requirements

for the conditions which were required for the work.

This

problem has

been appropriately

documented

by the licensee

in an Action

Request.

3.3.2

Removal of Hain Steam Safety Valves

(HSSVs)

Following cooldown to Mode 5, the removal of the

HSSVs

was authorized.

The

clearances

issued for the work were administrative

in nature

and required only

that the plant

be in Mode 5.

Although the Shift Foreman,

who authorized

the

clearances,

discussed

the

need to vent the

SGs, prior to removal of the

HSSVs,

with the Mechanical

Maintenance

Foreman,

the

need for venting

was not included

in the turnover to the night-shift Mechanical

Maintenance

Foreman.

Instructions for coordinating with Operations

to verify the

SGs were vented,

prior to HSSV removal,

were only included

on two of the six subclearances.

When the Mechanical

Maintenance

Foreman

reviewed the packages,

the special

instructions

on two of the six subclearances

were not considered.

Residual

heat in the

SGs resulted

in the production of steam,

and removal of the

HSSVs

was

commenced without the

SGs being adequately

vented.

During

a walkdown of

the area,

the licensee

observed that removal of the

HSSVs

had

commenced

without the

SGs being vented

and expressed

this concern to the mechanics.

At

this point mechanics

were cleared

from the area

and the

SGs were vented

by

opening

steam

dumps.

Safet

Si nificance

Mechanical

maintenance

personnel

were authorized to

remove the

HSSVs without adequate

consideration for the steam pressure

in the

SGs.

~Summar

Adequate control of WSSV removal

was not maintained.

WSSV removal

was authorized without ensuring the proper conditions

were established

for the

work.

This problem has

been

documented

by the licensee

in an Action Request

and the licensee

problem resolution

process will follow corrective actions.

3.3.3

Emergency Diesel

Generator

(EDG) 2-1 Testing with Grounding Device

Installed

~Back round

During postmaintenance

testing of EDG 2-1, the

EDG was started

twice with a grounding device installed

on the

EDG output breaker.

Both times

EDG 2-1 tripped

on differential current

across

the output breaker.

The

differential current trip compares

the current flow coming into the

EDG output

breaker

and the current flow going out of,the breaker

and shuts

down the

EDG

at approximately

17

amps differential.

The grounding device which was

installed

on the

EDG output breaker provided

a current path to ground at the

4

I~

-11-

breaker.

Following the second

attempt to start the

EDG, it was determined

that the grounding device

was the source of the problem.

The grounding device

was

removed

and

an inspection of the control circuitry was performed.

The

inspection did not reveal

any damage

as

a result of leaving the grounding

device installed during testing.

Safet

Si nificance

EDG 2-1 was not considered

operable

during this testing.

Therefore,

problems

associated

with testing did not adversely affect the

operability of electrical

power sources

required

by plant TS.

~Summar

Although it was

known prior to commencing

EDG 2-1 testing that the

grounding device

was installed in the output breaker,

the effect of the device

remaining installed during testing

was not thoroughly understood

by the

personnel

involved with the testing.

Controls established

to ensure that

EDG 2-1 was ready for testing were inadequate

in that they did not preclude

the performance of testing with the grounding device installed.

The testing

was not properly controlled in that the initial

EDG trip during testing

was

not thoroughly investigated prior to continuing with the testing.

The

licensee

has

documented this problem in a nonconformance

report.

3.3.4

Insufficient Clearance

Established for Installation of Drain Adapter

Work involving the installation of a drain adapter

on the containment 'closed

drain piping system

was not adequately

isolated

from other

connected

systems.

As

a result,

an evolution being performed,

which created

increased

backpressure

in the reactor coolant drain tank,

caused

a radioactive spill

inside containment

from the drain adapter of approximately

100 gallons.

The

licensee's

investigation revealed that, in addition to inadequate

controls

being established

for the work, the system

had

been

breached prior to purging

the volatile gases

in the reactor coolant drain tank.

Safet

Si nificance

Failure to establish

adequate

boundaries for the breach

of a radioactive

system created

the potential for personnel

injury, the spread

of radioactive contamination,

and equipment

damage.

~Summar

The clear ance

used for the installation of the drain adapter

was

inadequate

in that it did not adequately

isolate the portion of the system

being breached for the work and

no other controls were in effect which would

have precluded

other system interactions

from affecting the work area.

Overall Conclusion

The problems described

in Sections

3.3. 1 through 3.3.4 are

of concern to the

NRC because

the contributing causes

include inadequate

communications,

a perceived

need for haste

in accomplishing

outage

work,

and

an inadequate

consideration

of existing plant conditions

on work schedule

changes.

The controls which ensure that proper conditions

are establi,shed

for

work and testing

were not adequate

in these

circumstances

to preclude

foreseeable

problems

from occurring.

None of these specific examples,

when

considered

separately,

resulted

in situations of significant safety concern.

However,

since these

same controls were used during the outage for work on

safety-related

systems,

the

NRC was concerned

about the number of these

-12-

problems which occurred during Refueling Outage

2R6

and their potential for

recurrence

in circumstances

of increased

safety significance.

4

SURVEILLANCE OBSERVATIONS

(61726)

Selected

surveillance tests

required to be performed

by the

TS were reviewed

on

a sampling basis

to verify that:

(1) the surveillance tests

were correctly

included

on the facility schedule;

(2)

a technically adequate

procedure

existed for performance of the surveillance tests;

(3) the surveillance tests

had

been

performed at

a frequency specified in the TS;

and

(4) test results

satisfied

acceptance

criteria or were properly dispositioned.

Specifically, portions of the following surveillances

were observed

by the

inspector during this inspection period:

Unit

1

~

Surveillance

Test Procedure

(STP) I-lA, Revision 47, Routine Shift

Checks

Required

by Licenses

Unit 2

~

STP M-12A21, Revision 2, Station Battery

121 Performance

Test

~

STP 1-72B, Revision

11, Seismic Trip Channel

Calibration

~

STP V-15, Revision 4,

ECCS Flow Balance Test

~

STP P-3A, Revision

12,

Performance

Test of Residual

Heat

Removal

(RHR)

Pumps

4. 1

STP

P-3A

Performance

Test of RHR

Pum

s

The

STP P-3A test provides data for determining

RHR pump performance

under

conditions of pump recirculation to maximum flow.

While observing

the

performance of the test,

the inspector

noted that the licensee

personnel

involved with the surveillance

were recording the

pump recirculation data in

accordance

with Step 12.7.6 with Valve RHR-2-8809B in the

open position.

During the portion of the test where

RHR

Pump 2-2 is aligned to run

on

recirculation,

Valve RHR-2-8809B is required to be closed

by Step 12.2.6.

The

inspector questioned

the system engineer

regarding the reason

Valve RHR-2-

8809B was

open since the procedure

required it to be shut.

The system

engineer

reviewed the procedure

and remarked that the valve should

be closed.

The system engineer

then notified the operator performing the test that the

valve should be'losed.

The operator

then repositioned

Valve RHR-2-8809B to

the closed position.

Review of the master

copy of the procedure

being used

for the test indicated that the operator

had,

in error, initialed for

Valve RHR-2-8809B being in the closed position in Step 12.2.6

when, in fact,

the valve was open.

I

-13-

Safet

Si nificance

The impact of Valve RHR-2-8809B being in the incorrect

position was minimal since,

during the portion of the

pump testing which

measured

recirculation flow, an upstream valve,

RHR-2-HCV-637,

was closed.

As

a result,

the recirculation flow of the

pump would not have

been affected

by

the improper positioning of Valve RHR-2-8809B,

assuming that Valve RHR-2-HCV-

637 did not have significant leakage.

Following completion of the

recirculation flow measurements,

the surveill,ance

procedure

Step

12.9 directs

the opening of RHR-2-8809B.

Therefore, if the licensee

had not identified

that Valve RHR-8809B was in the incorrect position prior to that point in the

procedure,

the improper positioning would have

been self-revealing during the

performance of Step

12.9 and,

as

a result,

would not have

impacted the

remainder of the test.

The licensee

issued

a bulletin to the test

team

and

the operations

department

to correct the cause of the problem.

The bulletin

described

the preferred

methods of self-verification during the performance of

surveillances.

Conclusion

The requirements

of STP

P-3A were not met for the performance

of

RHR

Pump 2-2 recirculation testing in that Valve RHR-2-8809B

was

open

when the

procedure

required it to be closed.

The failure to perform the surveillance

in accordance

with the procedure

is

a violation of TS 6.8. 1', which states,

in

part, that written procedures

shall

be established,

implemented,

and

maintained

covering applicable

procedures

recommended

in Appendix

A of

Regulatory

Guide 1.33,

Revision

2, dated

February

1978.

Appendix A of

Regulatory

Guide 1.33,

Revision

2,

recommends

procedures

covering surveillance

testing; preventive maintenance;

and startup,

operation,

and shutdown of

safety-related

systems.

Contrary to this requirement,

on October ll, 1994,

Valve RHR-2-8809B was not closed during the performance of STP P-3B as

required

by Step 12.2.6.

Since the violation is of very low safety

significance

and since the inspectors

are satisfied with the adequacy of the

corrective actions,

in accordance

with Section VII.B.(1) of the Enforcement

Policy, this violation was not cited (323/9424-02).

5

ONSITE ENGINEERING

(37551)

5.1

Failure of EDG l-l to Stabilize

Between

59 and

61 Hertz

Hz

Within

13 Seconds

On March 29,

1994, with Unit

1 defueled,

during the performance of

Surveillance Test Procedure

(STP)

M-9A, "Emergency Diesel

Engine Generator

Routine Surveillance Test,"

EDG 1-1 failed to meet the acceptance

criteria for

frequency during the simulated

undervoltage start.

The frequency stabilized

at

a value of 60.3

Hz in 15.74 seconds,

which exceeded

the

TS acceptance

criteria of 13 seconds.

At the time, the other two Unit

1 diesel

generators

were out of service for maintenance activities.

Following the failure of

EDG 1-1 to pass

STP M-9A, the licensee parallelled

EDG 1-1 to the

bus

and continued to allow it to run, in order to return it to

operable

status until determination of the cause of the frequency

problem.

The licensee

based

the conclusion of

EDG operability after

a stabilization

time problem on

TS Interpretation

85-02, which assumed

that start

and

0

0

-14-

frequency stabilization

was not required,

since the diesel

generator

was

already parallelled to its bus.

The licensee initially postulated that the most probable

cause of the

frequency stabilization problem was related to electrical

governor

performance.

Core alterations

and movement of irradiated fuel were suspended

as

a precautionary

measure

to allow for the diesel

generator to be taken out

of service for corrective maintenance.

Maintenance

personnel

successfully

adjusted

the governor during the second

adjustment.

On March 30,

1994,

EDG 1-1 was declared

operable after successful

completion of STP H-9A.

The licensee

continued to investigate

the root cause of the failure of EDG 1-1

to achieve rated frequency within TS time limits.

The licensee's

investigation

included talks with the governor manufacturer,

checking of

potentially affected diesel

generator

components,

and

a review of industry

and

Diablo Canyon experience.

Although, at the time of the inspection,

the

licensee

had not conclusively determined

the root cause,

the licensee's

corrective actions

appeared

to be directed

towards identification of the root

cause

and resolution of the problem.

For example,

measures

were being

implemented for all six diesel

generators

to periodically ensure that the

electrical

governor adjustment

locknuts are properly tightened

and that needle

valve "as-found" settings

are trended to determine if drift of the settings

is

a contributing factor.

Conclusion

The licensee's

response

to the

EDG l-l frequency stabilization

problem appeared

to be timely, thorough,

and appropriate to the circumstances.

5.2

Review of DCP M44425

The inspectors verified that the design basis

was not altered without proper

NRC notification and that adequate

postmodification testing

was planned.

In

addition,

the quality of the

DCP, proper reviews,

and design interface

controls were verified.

The following DCP was reviewed with no comments:

DCP H44425,

Revision 3,

"Remove the Narrow Range

RTD Bypass

Piping Network and

Install Thermowells in the Reactor

Coolant

System

Loop Piping with New Fast

Response

RTDs," and associated

Design

Change

Notices

(DCN):

DC2-EM-44425,

Revision 2,

and Field Change

H-18002;

DC2-EP-44425,

Revision

0 and Field

Changes

P-17936,

P-17932,

and P-18013;

DC2-EC-44425,

Revision

1,

and Field

Change

C-01813;

DC2-EP-46280,

Revision

1

and Field Changes

H-17965,

H-17934,

and H-17933;

DC2-EP-46281,

Revision 0,

and Field Change

H-17963;

DC2-EP-46282,

Revision 0; DC2-EP-46283,

Revision 0,

and Field Change

H-17964;

and DC2-SP-

44425,

Revision 0,

and Field Changes

H-17962

and H-18062.

5.3

RTD

B

ass'limination

DCN DC2-EH-44425,

through Revision

2, described

a modification that consisted

of replacing the existing single-element

RTDs with new "fast response"

dual-

element

RTDs.

This included removing the

RTD bypass piping,network and

associated

supports

connected

to the reactor coolant

system at the hot legs,

f'I

4 %. g

gl

'ta.

-15-

cold legs,

and crossover

legs, installation of thermowells to house the

new

RTDs,

and addition of new cabling to connect the

new

RTDs to the plant process

protection

system cabinets.

This

DCN was considered

the principal design

document,

and it addressed

work activities by discipline (i.e., mechanical,

electrical, etc.),

and identified each of the applicable

sub-DCNs.

During this inspection,

the primary in-process

work activity observed

by the

inspector dealt with installation (i.e., machining,

welding,

and

nondestructive

examination)

of thermowells

and caps.

This work had

been

contracted

to Westinghouse

Electric Corporation

and

was being performed

under

DCN DC-2-EP-44425,

Revision 0.

All hardware for this job, including welding

materials,

had

been

procured

by the licensee,

who was also responsible for the

performance of all postmodification

and functional testing.

The inspector

reviewed the following WPSs

and procedure qualification

records

(P(Rs) that were applicable to the

RTD modification:

WPS 10800,

Revision 5,

and

P(R 418, Revision 0, for the shielded

metal

arc welding

process;

and

WPS 50800,

Revision 7,

and

P(R 417,

Revision

1, for the gas

tungsten

arc welding process.

These

WPSs

had

been

developed

and qualified for

welding of groove

and fillet welds in stainless

steel

in accordance

with the

1993 Addenda to the

1992 Edition of the

ASME Code.

The inspector verified

that all

ASHE Code required essential

variables for both welding processes

had

been identified, qualified,

and included in the

WPSs.

The inspector also verified that all

ASME Code required tests

and examinations

had

been identified and incorporated into the

RTD design

change.

This

included hydrostatic testing,

visual examination, liquid penetrant

examination,

and radiography.

The hydrostatic testing

and radiography

were

within the licensee's

scope of work, while the visual

and liquid penetrant

examinations

were within the scope of the vendor's contract.

Conclusion

The licensee

and vendor

had properly considered

and accounted for

ASHE Code requirements

regarding welding, testing,

and examination during

development of the

RTD modification project.

With the exception of welding, observation of the work (i.e., machining

and

nondestructive

examination)

was performed

by the inspector during review of

the licensee's

repair

and replacement activities,

which are part of the

ASHE

Code Section

XI in-service inspection

program.

This subject is addressed

in

NRC Inspection

Report 50-275/94-25;

50-323/94-25.

6

FOLLOWUP HAINTENANCE

(92902)

The licensee

has experienced

problems with the pressurizer

backup heater

circuit breakers.

Host of the problems

were related to the breaker failing to

close

as

a result of binding.

In October

1993,

the licensee initially attributed the failure of

Breaker 52-IH-74 to dried lubricant.

As

a result of the licensee's

investigation, it was noted that this particular breaker,

and three other

I

-16-

breakers,

had not been included in the preventive maintenance

program.

The

licensee

then developed

a preventive maintenance

task for these

breakers.

Three of the four breakers

had the preventive maintenance

by September.

1994.

The remaining breaker,

52-1H-74,

which was the first to fail, was scheduled

for, but had not undergone,

preventive maintenance.

On September

6,

1994,

Breaker

52-1H-74 failed to actuate.

The electrical

craft initially identified the cause

to be excessive dirt buildup on the

operating

mechanism

because

of the lubricant.

An electrical craft supervisor,

however,

noticed

a difference

between

the failed breaker

and

a spare

breaker.

The difference

was that the tab of the close latch release

lever was not bent

at

a 45 degree

angle

on the failed breaker.

As a result of the lever not

being bent,

the coil was required to move further to allow the breaker to

close.

This extra

movement required extra time, giving the appearance

of

sluggish operation,

which initially was thought

by the licensee

to be

as

a

result of a sticking mechanism.

The licensee

bent the tab of the close latch

release

lever to approximately

45 degrees

and tested

the breaker

satisfactorily.

Conclusion

The licensee

planned to either revise

Procedure

HP E-64.4,

"Maintenance of FPE Type

FPS2 Circuit Breakers,"

to include

a check for the

angle of the latch release

lever, or replace

the breakers

with a different

design.

These

actions

appeared

to appropriately

address

correction of the

problem.

7

PLANT SUPPORT ACTIVITIES

(71750)

7. 1

Ph sical Securit

Observations

7. 1. 1

General

Integrity of Protected

Area

(PA) Barriers

The inspector

performed

a walkdown of the

PA perimeter

boundary.

The fence

support

members,

fabric,

and barbed wire were examined.

No damage

or

degradation

was found.

The inspector verified that the size of all openings

were well within the acceptable criteria and there

were

no signs of erosion at

the base of the fence.

The fence

was generally taut

and the bottom bar or

wire prevented

the fabric from being lifted.

The inspector

attempted

to lift

the bottom of the fence in several

places.

In the area

where the fence

was

the most loose,"it could only be raised

1 -

2 inches.

The maximum allowable

is

6 inches.

Conclusion

The

PA barrier

was determined

to be generally in good condition

and in compliance with the licensee's

Security Plan.

7. 1.2

Maintenance of Isolation Zones

Around

PA Barriers

During the walkdown of the

PA perimeter fence,

the isolation zones

around the

PA barriers

were found to be free of objects, clearly marked,

and of

sufficient size to permit clear observation

and assessment

of any unauthorized

activity by the security force members.

-17-

Conclusion

The isolation zones

are being maintained

in accordance

with

licensee

procedures.

7. 1.3

PA Personnel

and

Package

Access

The inspector

reviewed the

PA personnel

and package

access

process,

including

the explosive detector,

metal detector,

and x-ray machine,

with a Security

Shift Supervisor.

The operation of each device

and the expected

actions

and

responses

by the security officers observing or operating

the equipment

were

discussed.

The inspector

observed

the operation of the search tt ain for

approximately I/2 hour during the period day shift was reporting to work.

The

responses

to the explosive detector

alarms,

metal detector

alarms,

and

unidentifiable objects

passing

through the x-ray machine

were observed.

The

resulting pat-down

searches

or package

inspections

appeared

to be adequate

to

identify any unauthorized

materials,

The security officers issuing the

picture badges

were careful to check that the badges

issued

were for the

individuals pictured

on the badges.

Conclusion

The access

to the

PA for personnel

and packages

was being

adequately

controlled in accordance

with licensee

procedures.

7. 1.4

Protected

Area Vehicle Access

The inspector

observed

the entry of a vehicle into the

PA.

The vehicle

was

searched

by

a security officer.

The search

included the cab,

engine

compartment,

undercarriage,

cargo area,

and tool boxes.

No unauthorized

material

was found.

However, the officer did identify two objects that were

initially omitted from the materials verification form, but were subsequently

allowed into the

PA after the driver of the vehicle completed

the required

documentation.

The inspector

examined

several

parked vehicles inside the

PA.

All but one

were licensee

owned vehicles.

The inspector verified that the ignition keys

had

been

removed

and the doors locked

on the licensee's

vehicles

and that,

in

addition, the steering

had

been disabled

on the nonlicensee

vehicle.

Conclusion

The access

to the

PA for vehicles

was being adequately

controlled

in accordance

with licensee

procedures.

7. 1.5

Physical

Security

Power Supply

The inspector

reviewed the records for the tests of the physical security

secondary

power supply.

Diablo Canyon Nuclear

Power Plant tests

the secondary

power supply once

each quarter.

The inspector verified from the records that

the security die'sel

generator

picked

up the loads in less

than the minimum

time allowed when the normal

power supply was interrupted.

Conclusion

Inspected

elements

of testing the physical security secondary

power supply were in accordance

with licensee

procedures.

-18-

7.2

Emer enc

Pre aredness

7.2. 1

Emergency

Preparedness

Exercises

and Drills

During review of the records for exercises

and drills for 1994,

the inspector

verified that the drills and exercises

were being conducted

as required

and

all findings and deficiencies

were tracked

on the Drill Action Item Report.

Conclusion

The emergency

preparedness

drills and exercises

were being

performed at the required periodicity,

and the findings

and deficiencies

were

being tracked

in accordance

with the

Emergency

Plan.

7.2.2

Emergency

Response

Facilities

The inspector toured the Technical

Support Center with one of the

Emergency

Planning Coordinators

and verified the facility was readily available for

emergency

operations.

The emergency

procedures

were available

and were being

maintained.

There were

some

spaces

that were being used for normal

operations,

but these

areas

would be promptly vacated

to make

them usable for

emergency

operations.

The inspector verified that the telephones

were

operational

by selecting

and testing several

at random.

Conclusion

The Technical

Support Center

was readily available

and maintained

for emergency

operations.

8

IN-OFFICE REVIEW OF LERs

(90712)

The inspectors

performed review of the following LERs associated

with

operating events.

Based

on the information provided in the report,

review of

associated

documents,

and interviews with cognizant licensee

personnel,

the

inspectors

concluded that the licensee

had met the reporting requirements,

had

addressed

root causes,

and

had taken appropriate corrective actions.

The

following LERs are closed:

275/93-003,

Revision

1

Low Temperature

Overpressure

Protection Setpoint

Analysis Nonconservatism

Due to Miscommunication

275/94-016,

Revision

0

Diesel

Generator

Started

as

Designed

Upon De-

energization of Startup

Bus

Due to Offsite

Wildfire

323/94-002,

Revision

0

TS 3.0.4 Not Met Following Inadequate

In-Service

Testing

323/94-003,

Revision

0

Auxiliary Building Ventilation System Outside of

Design Basis

Due to Previous

Nonconservative

ASTM Testing

C, ),

-19-

323/94-004,

Revision

0

Partial

Phase

A Containment

Isolations

Due to

Safeguards

Output Driver Card Failure

323/94-005,

Revision

0

Fuel

Handling Building Ventilation System

Outside of Design Basis

Due to Previous

Nonconservative

ASTN Testing

9

ONSITE LER REVIEW

(92700)

9. 1

0 en

LER 275 94-009

Revision 0:

TS 3.4.2.2

Not Met Durin

Pressurizer

Code Safet

Valve Surveillance Testin

Unit

1

LER 94-009,

Revision 0, identified that the three Unit

1 pressurizer

safety valves were set-pressure

tested

at the Westinghouse

Service Center test

facility in Harch

1994.

The as-found setpoints of all three valves were found

outside the

TS tolerance of 2485 psig, plus or minus

1 percent.

These valves

were reset to the correct set pressure

prior to being reinstalled.

The

LER

which reported

the failure of the valves to liftwithin the required

band

stated that the root cause of the valves

being outside of the

TS tolerance

had

not yet been determined.

However,

NRC review of this issue

revealed that

PGEE

had performed

an extensive

safety valve test

program

and

was in the process

of

evaluating the results of the program.

The Diablo Canyon pressurizer

safety valves are Crosby Valve and

Gage .Company,

size

6M6, Model HP-BP-86, valves

and were installed

on loop seals

on both

Units

1 and 2.

The Diablo Canyon

TS and the

ASNE Code required that the

pressurizer

safety valves

be periodically tested to verify the setpoint to be

2485 psig, plus or minus

1 percent.

A review of the periodic test results for

the as-found setpoint data indicated the valves failed to meet the setpoint

tolerance

on numerous

occasions.

The inspectors

reviewed

Document

BL1-996C, "Diablo Canyon Pressurizer

Safety

Valve Test

Program Results."

The test

program started

in 1990

and included

dimensional verification of valve tolerances

and design

and fabrication of a

prototype valve.

The prototype valve

and standard

safety valve were tested

under the

same conditions

and results

compared.

The initial tests

performed

were

steam tests without

a loop seal.

The results of the steam tests for both

the prototype valve

and the standard

valve indicated that the setpoint varied

a great

deal

depending

on

how much seat

leakage existed prior to opening.

The

report concluded that steam testing

was inappropriate for the valve, since the

valve leaked during steam testing

and the setpoint could not be accurately

determined.

The second

series of tests

were performed with a loop seal

in

place.

The loop seal

temperature

and ambient temperature

were closely

maintained to the actual conditions at the plant.

A number of setpoint tests

were performed

bn the standard

and the prototype valves.

The repeatability of

the setpoint of the standard

valve was plus or minus 0.9 percent

(22 psi).

The repeatability of the setpoint of the prototype valve was plus or minus

0.4 percent

(11 psi).

I

k

-20-

The pressurizer

safety valve test

program report

had

a number of

recommendations.

Among the recommendations

were,

having the licensee

prepare

an exemption request

which would allow testing of the pressurizer

safety

valves with a loop seal

in place instead of testing directly on steam,

modifying the six pressurizer

safety valves to match the prototype valve

configuration,

and revising appropriate test procedures

to specify testing the

valves

on

a loop seal

instead of directly on steam.

The inspectors

reviewed mechanical

maintenance

Procedure

HP H-7.36, Revision

14, "Pressurizer

Safety Valve Lift Point Setting Using Steam."

The procedure

contained

a detailed discussion

on

how the setpoint

should

be determined.

The

procedure

included the requirement to use

a loop seal

and

an environmental

chamber with temperature

requirements

specified for the loop seal,

valve inlet

flange,

body,

and bonnet.

The procedure

included the

ramp rate for the

pressure

increase

during the test.

The inspectors

concluded that the

procedure

had excellent detail

and

was very clear.

The inspectors

noted that

all of the recommendations

for the test

program were incorporated.

Nonconformance

Report

DC1-89-TN-N099, Revision 3, dated January

1,

1994,

was

initiated in 1989

and remains

open.

The nonconformance

report documented

the

concern that the

TS setpoint tolerance of plus or minus

1 percent for the

pressurizer

safety valves could not

be maintained

at Diablo Canyon.

The

report documented

the history of the valve failures since

1989

and the

corrective actions to attempt to solve the setpoint drift problems.

The inspectors

reviewed Calculation

N-126, dated April 22,

1994,

"Overpressure

Analysis for Unit

1

1R6 as found pressurizer

safety valve setpoints."

This

calculation

was performed to show that the Unit

1 pressurizer

safety valves

were capable of providing adequate

overpressure

protection for the reactor

coolant

system with the as-found setpoints.

The analysis

showed that the

reactor coolant

system pressure

was lower that

110 percent of its design

pressure.

The calculation

concluded that there

was sufficient overpressure

protection with the as-found setpoints.

The inspectors

considered

that the

calculation

was adequate.

Conclusion

Overall, the inspectors

concluded that the Diablo Canyon personnel

were being proactive in the manner in which they were researching

the safety

valve setpoint drift problem.

This

LER remains

open pending completion of the

corrective actions.

9.2

0 en

LER 275 323 94-003

Revision 0:

TS 3.7. 1. 1 Not Het Durin

HSSV

Surveillance Testin

Units

1

and

2

LER 94-003,

Revision 0, identified that

on February

9,

1994, for

Unit

1

and

on Harch 5,

1994, for Unit 2, while performing setpoint testing

on

the

HSSVs,

TS 3.7. 1. 1 was not met.

Thirteen Unit

1 valves

and

15 Unit 2

valves did not meet the

TS setpoint tolerance of plus or minus

1 percent.

For

Unit 1:

one valve was

between

1 - 3 percent

low; five valves were between 1

3 percent high; five valves

were greater

than

3 percent

high with a maximum of

9 percent;

and two valves did not lift due to the test equipment

load cell

-21-

limitations.

For Unit 2:

one valve was between

1

3 percent

low; one valve

was

between

1

3 percent high;

seven

valves

were between

1 - 3 percent high;

and six valves were greater

than

3 percent high.

The highest

was

approximately

9 percent

above the setpoint.

Additional testing

was conducted

and adjustments

made

as necessary

until all of the valves lifted within TS

tolerances.

The

LER stated that the root cause

and corrective actions for the

HSSVs being out of TS tolerance

had not been determined.

The root cause

and

corrective actions

would be included in a supplemental

LER.

The

20 Unit

1 valves

were sent off-site to the Westinghouse

Western Test

Center

and tested

on steam.

The

20 Unit 2 valves

were tested

in place using

the Trevitest lift assist

device.

The Trevitest lift assist

device allowed

the valve to be tested

in place

by using system pressure

and the additional

,force of the assist

device to lift the valve stem.

The set pressure

was

calculated

by knowing the

mean seat

area of the valve.

For both Units

1 and

2

valve tests,

the licensee

stated that the vendor

had provided

a

new mean seat

area

since the area previously used

was not accurate.

In addition,

the

licensee

stated that the

20 Unit 2 valves would all

be tested

on steam during

the Unit

2 outage this year.

The inspectors

reviewed Calculation N-110, Revision 0, "Overpressure

Study for

unit

1

1R6 As Found

HSSV Setpoints."

The calculation

was performed to

determine if the capability of the

HSSVs with the Unit

1 as-found setpoints

would provide overpressure

protection for the

SGs.

The calculation

assumed

that the two valves which did not open

due to the limitations of the test

equipment

were unavailable.

The calculation concluded that the peak

SG

secondary

side pressures

were lower than

110 percent of the design pressure;

therefore,

the

HSSVs with the as-found setpoints

would have provided adequate

overpressure

protection.

The inspectors

considered

the calculation to be

adequate.

Nonconformance

Report DC1-89-TN-N098, Revision 00, dated April 28,

1994,

"Hain

Steam Safety Valve Lift Point," was initiated in 1989

and remains

open.

This

nonconformance

report documented

the history of the valve failures since

1989

and the corrective actions to attempt to solve the setpoint drift.

The

licensee

stated that the Unit 2 HSSV tests,

which will be performed during

Refueling Outage

2R6,

may be included in this nonconformance

report.

The licensee

stated that Diablo Canyon

had completed

a test

program for the

HSSVs in August

1994.

They stated that the test

program consisted

of setting

the valves

on steam

and then setting

them using the

AVK lift assist

device.

The purpose of the test

program

was to determine

the

mean seat

area of the

valve that would be used with the lift device which would correlate with the

set pressures

determined

during steam testing.

The licensee

stated

they had

performed

a large

number of tests

both

on steam

and then using the

AVK

equipment.

Three valves set at three different set pressures

were used for

the tests.

The inspectors

requested

a copy of the test procedure

used for

this series of tests.

However, the licensee

stated

they had not used

a test

procedure.

The licensee

stated that the test results

were preliminary since

the testing

was concluded

August 26,

1994.

The inspectors

did not review any

P

-22-

of the test data.

The licensee

stated that the preliminary test results

indicate that the correlation

between

steam testing

and the lift assist

device

testing

was very close

and setpoint

spread

was within plus or minus

1 percent.

Conclusion

An NRC review of the final report of the set pressure

correlation

tests

should

be performed prior to closing this

LER.

,,II

1

PERSONS

CONTACTED

1.1

Licensee

Personnel

ATTACHMENT 1

G.

H.

Gen

  • W. H.
  • R.

PE

T.

LE

J.

S.

J.

R.

D.

H.

S.

G.

  • W. G.
  • S.

R.

  • B. W.

J. J.

C.

R.

J.

A.

  • K. A.

M.

E.

  • D. B.

S.

R.

P.

G.

  • D. A.

B. T.

E.

V.

R.

H.

D.

B.

Rueger,

Senior Vice President

and General

Manager,

Nuclear

Power

eration

Business

Unit

Fujimoto, Vice President

and Plant Manager,

Diablo Canyon Operations

Powers,

Manager,

Nuclear guality Services

Grebel,

Supervisor,

Regulatory Compliance

Bard, Director, Mechanical

Maintenance

Becker, Shift Supervisor,

Operations

Behnke,

Senior Engineer,

Regulatory Compliance

Chesnut,

Supervisor,

Reactor

Engineering

Crockett,

Manager,

Technical

and Support Services

Fridley, Director, Operations

Giffin, Manager,

Maintenance

Services

Griffin, Group Leader,

Onsite Engineering

Groff, Director, Plant Engineering

Hays, Director, Onsite guality Control

Hubbard,

Engineer,

Regulatory

Compliance

Leppke, Assistant

Manager,

Technical

Services

Miklush, Manager,

Operations

Services

Ortore, Director, Electrical Maintenance

Sarafian,

Senior Engineer,

Nuclear guality Services

Taggart, Director, Onsite guality Assurance

Hansen-Harris,

Watch

Commander,

Security

Waage,

Supervisor,

Emergency

Planning

Horris, Coordinator,

Emergency

Planning

Harsh,

Coordinator,

Emergency

Planning

1.2

NRC Personnel

  • H. Tschiltz, Resident

Inspector

  • Denotes -those attending

the exit meeting

on October

18,

1994.

In addition to the personnel

listed above,

the inspectors

contacted

other

personnel

during this inspection period.

2

EXIT MEETING

An exit meeting

was conducted

on October

18,

1994.

During this meeting,

the

resident

inspector

reviewed the scope

and findings of the report.

The

licensee

acknowledged

the inspection findings documented

in this report.

The

licensee

did not identify as proprietary

any information provided to, or

reviewed by, the inspectors.

'V

r

ATTACHNENT 2

ACRONYNS

AC

AFW

ASNE

ASTM

CC

CVCS

DCN

DCP

EDG

LER

MSSV

OP

PA

PQR

RHR

RTD

SG

STP

TS

WPS

alternating current

auxiliary feedwater

American Society of Mechanical

Engineers

American Society for Testing

and Materials

centrifugal

charging

(high head injection)

chemical

and volume control

system

design

change notice

design

change

package

emergency

diesel

generator

licensee

event report

main steam safety valve

operating

procedure

protected

area

procedure qualification records

residual

heat

removal

resistance

temperature

detector

steam generator

surveillance test procedure

Technical Specification

weld procedure specifications