ML16342D261

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Insp Repts 50-275/96-02 & 50-323/96-02 on 960121-0302. Violations Noted.Major Areas Inspected:Operation Safety Verification,Maint Observations,Surveillance Observations, Onsite Engineering & Plant Support Activities
ML16342D261
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 04/09/1996
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D260 List:
References
50-275-96-02, 50-275-96-2, 50-323-96-02, 50-323-96-2, NUDOCS 9604160043
Download: ML16342D261 (50)


See also: IR 05000275/1996002

Text

ENCLOSURE

2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-275/96-02

50-323/96-02

Licenses:

DPR-80

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room

1451

P.O.

Box 770000

San Francisco,

California

Facility Name:

Diablo Canyon Nuclear

Power Plant,

Units

1

and

2

Inspection At:

Diablo Canyon ~ite,

San Luis Obispo County. California

Inspection

Conducted:

January

21 through March 2,

1996

Inspectors:

M. D. Tschiltz, Senior Resident

Inspector

S.

A. Boynton,

Resident

Inspector

D.

E. Corporandy,

Project

Inspector

C. J,

Paulk,

Reactor

Inspector

D.

G. Acker, Senior Project Inspector

Approved:

her"

H

Wong,

Re ctor ProJects

Branc

Date

Ins ection

Summar

Areas

Ins ected

Units

1

and

2

Routine,

announced

inspection of operational

safety verification, maintenance

observations,

surveillance observations,

onsite engineering,

plant support activities, followup.operations,

followup

engineering,

in office review of licensee

event reports

(LERs),

and review of

the Upd'ated

Final Safety Analjsis Report .gFSAR).

Results

Units

1

and

2

~Qeratinna:

~

The licensee's

procedure for performing monthly channel

checks of the

incore thermocouple

instruments

did not ensure

the Technical

Specification

(TS) surveillance

requirement

was met.

As

a result,

the

licensee

failed to identify an inoperable

incore thermocouple

instrument

on Unit 2.

A violation was identified (Section 2.1).

9604l60043 9604l0

PDR

ADOCK 05000275

6

PDR

-2-

Operations

responded

promptly and effectively in response

to

a steam

leak

on cold reheat drain piping that necessitated

an unanticipated

reduction of reactor

power to perform repair of a cracked

weld

(Section 2.4).

Operators

failed to identify the potential for spread of contamination

during

a surveillance test of

a containment

spray

pump when leakage

from

the pump's

mechanical

seal

sprayed

outside of the posted

surface

contamination

area

(Section

4. 1).

An operator failed to properly perform

a system

alignment verification

for the performance of TS required surveillance testing.

A noncited

violation was identified (Section 4.2).

Maintenance:

Maintenance

personnel

failed to address

a potential seismically

induced

system interaction

when

a storage

cabinet

was allowed to be placed in

close proximity to safety-related

conduit associated

with the Unit 2

diesel

generators

(Section 2.2).

The licensee's

configuration control

program

and engineering

system

walkdowns failed to identify the installation of improperly sized motor

bearing oilers

on several

safety-related

pumps

(Section 2.3).

The replacement

of Safety Injection (SI)

Pump 2-2 was thoroughly planned

and well coordinated,

enabling

the work to be completed within the

allowed 72-hour action statement.

8riefings conducted

For the test were

informative and personnel

performing testing

were knowledgeable

of their

assigned

duties

(Section 4.3).

En ineerin

The thermography

program

implemented

by predictive maintenance

was

effective in identifying a problem with a containment

fan cooler motor

controller prior to actual failure (Section

3. 1).

The licensee

failed to take timely and appropriate

licensing actions to

pursue

extension of the

TS allowed outage

time for SI

Pump 2-2

replacement,

after noting

a decrease

in pump performance

during

surveillance

testing

and concluding that

LOKTITE had not been applied to

the shaft locknuts

(Section 4.3).

~

Engineering

investigative actions

taken

in response

to concerns

regarding centrifugal

charging

(CC)

pump operability failed to fully

consider

the

impact of closing the recirculation isolation valves

on

accident

analyses.

As

a result,

the failure to take

prompt

and

comprehensive

corrective actions,

a violation was identified

(Section

5. 1).

'

~

Periodic fire brigade proficiency training was not completed

as

required.

and resulted

in unqualified personnel

being assigned

as fire

brigade

members.

A violation was identified {Section 6.2).

~

A number of minor radiological controls deficiencies

were noted,

indicating

a decline in radiological

housekeeping

practices

and worker

awareness

of radiological

hazards

and controls

(Section 6.3).

Summar

of Ins ection Findin s:

~

Violation 323/9602-01

was

opened

(Section 2.1).

Violation 275/9602-02;

323/9602-02

was

opened

(Section

5. 1).

~

Violation 275/9602-03;

323/9602-03

was

opened

(Section 6.2).

~

A noncited violation was identified (Section 4.2).

~

Violation 275/95015-01

was closed

{Section 7.1).

Inspection

Followup Item 275/9334-01

was closed

(Section 8.1).

~

Unresolved

Item 50-275/95014-04

was closed

(Section 8.2).

LERs 275/95-009,

Revision 0; 275/95-012,

Revision 0;

and 275/95-017

Revision

0 were closed

(Section 9).

Attachments:

~

Persons

Contacted

and Exit Meeting

~

List of Acronyms

DETAILS

1

PLANT STATUS

Unit

1

At the beginning of this inspection period, Unit

1 was in Mode

1 at

100 percent

power.

On February

17 operators

reduced

power when

a moisture.

separator

reheater

stop valve failed to reopen during

a surveillance test.

The stop valve

was

reopened within an hour and the unit was returned

to

100 percent

power.

On February

21 power was

reduced

to approximately

10 percent

to allow for a weld repair of a cold reheat drain line.

The unit

returned

to

100 percent

power

on February

22

and remained

there

through the

end of the inspection period.

Unit

2

At the beginning of this inspection period, Unit

2 was

in Mode

1 at

100 percent

power.

The unit remained

at

100 percent

power throughout

the

inspection period.

Between

February

22-24,

the licensee

replaced

SI

Pump 2-2

based

upon

pump performance

concerns

identified during the

pump's routine

surveillance test

(Section 4.3).

2

OPERATIONAL SAFETY VERIFICATION

(71707)

The inspectors

performed this inspection

to ensure

that the licensee

operated

the facility safely

and in conformance with license

and regulatory

requirements.

The methods

used to perform this inspection

included direct

observation of activities

and equipment,

observation of control

room

operations,

tours of the facility, interviews

and discussions

with licensee

personnel,

independent

verification of safety

system status

and

TS limiting

conditions for operation, verification of corrective actions,

and review of

facility records.

The Senior Resident

Inspector

conducted

a review of recent

INPO evaluations

during this inspection period.

2.,1

Incore Thermocou le Channel

Checks'n

February

13 the inspector identified

a discrepancy

between

the incore

thermocouple

readings

on postaccident

monitoring system

(PAMS) Train

A and

Train

8 on Unit 2.

Specifically.

the average

core temperature

on the

PAMS

Train

8 display

was approximately

20'F higher than that

on the Train

A

display.

The inspector discussed

the temperature

variation with the

engineering

supervisor

responsible

fo~

the incore temperature

monitoring

system

and requested

them to evaluate its impact

on the system's operability.

As

a result.

engineering

determined

that the

PAMS Train

B temperature

indications

were erroneous

and operations

declared

the

PAMS Train

B display

inoperable.

Train

A of the incore thermocouple

PANS continued

to provide

a

sufficient number of operable

thermocouples

to meet

TS requi.ements.

TS require that the incore thermocouples

be calibrated

on

a refueling

frequency

and that

a channel

check

be performed monthly when the unit is

operating

in Hodes

1,

2, or 3.

The inspector

reviewed

the work orders,

documenting

the latest calibrations

performed,

on Trains

A and

B to meet

TS

surveillance

requirements.

The work orders

were complete

and

no abnormal

results

were noted.

The inspector

also reviewed

Procedure

STP I-10,

Revision

25A, "Routine Monthly Checks

Required

By Licenses."

Procedure

STP I-10 is utilized by the licensee

to satisfy the

TS requirement

to perform monthly cha"-"el checks of the incore thermocouples.

Step

11.s. of

Attachment

11.

1 to Procedure

STP I-10 directs operators

to perform

a channel

check of the incore thermocouples

and verify at least four thermocouples

operable

per core quadrant.

The procedure

stipulates

that the indications

may

be read locally (at the

PANS panel) or through

a graphical

interface

on the

plant process

computer

(PPC).

With no other specific guidance

provided for

determining

the acceptability of the thermocouple

indications,

the inspector

questioned

several

control operators

on

how they would evaluate

Step ll.s.

The inspector

determined that,

in general,

operators

would rely upon the

incore thermocouple

map provided

by the

PPC

and not visually observe

the local

indications.

The inspector considered

this to be

a contributing factor in the

operators'ailure

to identify the inoperable

PANS Train

B display.

Concerned with the acceptability of using the

PPC to fulfill the

TS required

channel

check of the incore thermocouples,

the inspector discussed

this

practice with the system engineer,

the operations director,

and the

surveillance

engineering

group.

The operations director

and the surveillance

engineering

group responsible

for the maintenance

and performance of

Procedure

STP

1-10 agreed that

use of the

PPC alone would not adequately

verify operability of the incore thermocouple

accident monitoring instruments.

The operations director initiated

an action request

(AR) for engineering

to

evaluate this issue

and directed

the on-shift operators

to perform

a partial

STP I-ID to verify the operability of the local

PANS displays.

The results of

the partial surveillance

were satisfactory.

The inspector

noted that the incore thermocouple

accident monitoring

instruments

would be relied

upon

by operators

during

an accident

to evaluate

the core cooling critical safety function criteria.

A potential

consequence

of,inadequate

surveillances

of these

instruments

is erroneous

core temperatur%~

indication that could adversely

impact the operators'bility

to effectively

implement the emergency

operating

procedures.

The inspector

concluded that

Procedure

STP I-10,

as written, would not necessarily verify operability of

the incore thermocouples

in that it did not specifically require operators

to

observe

the local indications.

The failure of Procedure

STP

1-10 to

adequately

evaluate

the operability of the

PANS incore thermocouples

is

a

violation of TS 6.8.

1 (Violation 323/9602-01).

2.2

Unit

2 Diesel

Generator Air Exhaust

Room Material Stora

e

On February

1. during

a plant tour of the Unit 2 turbine building, in the

diesel

generator

exhaust

room.

the inspector identified

a potential

seismically

induced

system interaction

(SISI) when

he noted that

a large,

unrestrained

storage

container

had

been

placed

in close proximity to safety-

related electrical

conduit.

The inspector raised

the concern of potential

seismic interactions

between

the container

and the conduit with the

responsible

maintenance

supervisor.

The supervisor

agreed

that the placement

of the container

was inappropriate

and the container

was

moved to

a new

location

and secured.

The inspector discussed

his concerns

with the system engineer

responsible

for

implementation of the SISI program. ~- system engineer, determined that the

conduit was

an SISI "target" in that it contained vital circuits for the

operation of Emergency

Diesel

Generator

(EDG) 2-3.

SISI "targets"

are defined

in Procedure

AD4. 103,

Rev.

1B, "SISI Review of Housekeeping Activities," as

those

components

required for safe

shutdown of the plant or for accident

mitigation.

The system engineer

evaluated

the potential

SISI

and determined

that it was unlikely the container could have

damaged

the conduit in

a seismic

event.

Conclusion:

The inspector

concluded that the maintenance

supervisor failed to

identify the potential

SISI created

by the placement of the storage

container

and,

thus,

the appropriate

evaluation

had not been

performed

by engineering

services.

Similar concerns

had previously

been identified by the inspector

and communicated

to the licensee

for ongoing work in this

same

area.

The

actions

taken to resolve

the issue

had not been effective.

The inspector

considered

these

problems

as

a weakness

in the implementation of the SISI

program during maintenance activities.

2.3

Com onent Coolin

Water

CCW

Pum

Motor Bearin

Oilers

On January

31, during

a plant tour in the Unit

1 auxiliary building, the

inspector

noted that the size of the motor bearing oilers installed

on

CCW

Pump

1-2 were smaller

than that

on the other

CCW pump motors for Unit 1.

The

inspector contacted

the

CCW system engineer

to ascertain

the reason

for the

difference

and to determine if the oiler's smaller capacity could affect the

operability of the

pump.

In response

to the inspector's

concerns,

the

system

engineer

performed

a prompt operability assessment

(POA) of

CCW

Pump

1-2

and

reviewed

the work order history for the

pump motor.

The system engineer

determined

thaWthe instalgod oilers did not meet'esign

requirements;

'however, their smaller'capYc'ity did not affect the operability of the

pump.

The licensee's

review of the maintenance

history on the

pump motor could not

identify a definitive cause for the installation of improperly sized bearing

oilers.

In addition to evaluating

the

impact of the smaller bearing oilers

on

CCW

Pump 1-2,

the licensee visually inspected

the other

CCW pumps

on Units

1

and

2.

The licensee

identified that

an improperly sized bearing oiler had

~iso been installed

o,i

CCW

Pump 2-1.

The inspector

followed up this finding

by visually inspecting all safety-related

pumps

and motors

in the auxiliary

building and identified another

improperly sized oiler on the outboard

motor

bearing of auxiliary feedwater

(AFW)

Pump 2-3.

The inspector

noted that

an

AR

had

been initiated by the licensee

for improper sizing of the motor-bearing

oilers

on

AFW Pump,2-3

and containment

spray

(CS)

Pump 1-2.

The

AR for the

CS

pump included

a

POA justifying the pump's operability.

Although

a formal

POA

was not performed for AFW Pump 2-3, the

AR provided technical justification

for the acceptability of the smaller sized oiler.

The licensee

determined

that the incorrect oiler was installed

due to an error in tne replacement

parts evaluation

(RPE) associated

with the

AFW pump motors.

The licensee

has

revised

the

RPE to reflect the proper oiler size required for the

AFW pump

motors.

The licensee

has also initiated actions

to replace

the incorrect

oilers

on all four pumps.

Conclusion:

The inspector

concluded that the installation of improperly sized

bearing oilers

on the

above

pumps did not impact the pumps'bility to perform

their safety function.

The inspector

noted that the

POAs for the

CCW pump

motors

and the

CS

pump were technically sound.

However,

the inspector

considered

the, multiple examples

and failure of system engineers

to note these

problems during system

walkdowns to be indicative of a weakness

in the

licensee's

configuration controls during plant maintenance.

2.4

Control

Room Observations

On February

21 the inspector

observed

the conduct of operations

in the control

room during

a reduction

in power of Unit 1.

The reduction of reactor

power

was required to establish

conditions to perform

a weld repair of a cracked

weld on

a cold reheat

steam line drain connection.

Prior to reducing reactor

power,

a preevolution briefing was conducted.

The inspector

noted that the

appropriate

procedures

were referred to and followed, where applicable,

and

that the briefing covered

the important aspects

of the evolution

and the

applicable precautions.

During shift turnover,

the inspector

observed

the communications

and briefings

of the control

room operators

for the oncoming shift.

The inspector

noted

that the information pertinent

to the evolution was

communicated

during the

shift turnover.

As the reduction in power continued,

the inspector

observed

that the control operator

was attentive

and responsive

to plant parameters

and

conditions.

The inspector

noted that the axial flux diIference

(AFD) limits figure posted

on the control

panel

had expired three day&earlier.

The issued-for-use

interval of 30 days

had bee"

exceeded

without the figure having

been

rever'fied

as current.

The inspector

discussed

the deficiency with the

control operator,

who initiated actions

to obtain

a verified copy of the

figure.

The inspector later determined that the

AFD limits figure had not

been revised

since

the figure was previously issued

and that the

issued-for-use

figure was the latest revision.

Conclusion:

During the reduction of reactor

power levEl, operators

referred

to and followed applicable

procedures.

Crew briefings observed

by the

inspector

covered

the important aspects

of the evolution

and the applicable

precautions.

The failure of the control operators

to verify that control

panel

posted

are maintained current for a period of over

3 days is indicative

of inadequate

tracking of issued-for-use

procedures.

3

PLANT NAINTENANCE

(62703)

During the inspection

period the inspectors

observed

and reviewed selected

documentation

associated

with the maintenance

and problem investigation

activities, listed below, to verify compliance with regulatory requirements,

compliance with administrative

and maintenance

procedures,

required quality

assurance

department

involvement,

proper

use of safety tags,

proper equipment

alignment

and

use of jumpers,

personnel

qualifications,

and proper retesting.

Specifically,

the inspector

reviewed

the work documentation

or witnessed

portions of the following maintenance

activities:

Unit

1

~

Troubleshooting

and repair of containment

fan cooler Unit (CFCU)

1-4

motor controller

~

CCW System Backflush

Unit

2

~

Troubleshoot

and repair

(Pressure

Control Valve)

PCV-21 I/P controller

(10 percent

atmospheric

steam

dump)

~

Replace

PCV-106 regulator (air supply to

EDG 2-3 air start motors)

~

Sl

Pump 2-2 replacement

Selected

observations

from the activities witnessed

are discussed

below.

3. 1

Troubleshootin

and

Re air of Cablin

in CFCU Breaker Cubicle

On February

27

and

28 the inspector

observed

maintenance

personnel

perform

troubleshooting

and repair of cabling inside the breaker cubicle for CFCU 1-4.

This maintenance

was beirjq performed

based

upon periodic thermal

imaging data

collected

by predictive maintenance.

Thermographic

imaging of the breaker

cubicle

had identified

an elevated

temperature

on several

cables.

The inspector

reviewed the associated

work package

and referenced

procedures

and discussed

the

scope of troubleshooting with the maintenance

technicians.

The inspector

noted that the technicians

were knowledgeable

on the breaker

design

and function.

and their approach

to the troubleshooting

was methodical.

The troubleshooting

resulted

in the identification and replacement

of several

degraded

cables.

Postmaintenance

testing verified that the elevated

temperatures

had

been corrected.

Conclusion - The inspector

concluded

that the maintenance

on the

CFCU 1-4

breaker cubicle

was performed

in accordance

with applicable

procedures

and

was

effective in identifying the root cause of the elevated

temperatures

and

resolving the deficiency.

The inspector

also noted that the thermography

program

implemented

by predictive maintenance

was effective in identifying the

problem before

a failure occurred.

3.2

OEG-2-PCV-106

Re lacement

On February

15 the inspector

observed

portions of the work to replace

EDG 2-3

air start motor air supply pressure

reducing Valve DEG-2-PCV-106.

When the

inspector arrived at the work site,

the valve

had already

been

removed

from

the system

and the workers

had

taped foreign material

exclusion postings

over

the

open piping.

The inspector

reviewed

the work package

and noted that,

although the valve had

been

removed

from the system,

two of the prerequisites

for the work had not

been initialed as being completed

in the controlling work document.

The

specific prerequisites

that

had not been initialed as complete

were the

verification of the subclearance

and hanging of the red tag

and the

foreman

reporting

on the clearance.

Prior to leaving the work site the maintenance

mechanic

hung the red tag required

by the subclearance.

When questioned

by

the inspector,

the mechanic

indicated that the

foreman

had reported

on the

clearance

prior to the start of the work although

the step

had not been

initialed.

The inspector later verified that the foreman

had,

in fact,

reported

on the clearance prior to the removal of the valve.

The inspector

reviewed

the licensee's

work order procedures

and did not find

any specific requirement

to complete

work order prerequisites

prior to

commencing

work.

The inspector

discussed

the observations

with the director

of mechanical

maintenance

who indicated that

he did not believe the failure to

complete

work order prerequisites

was

a violation of procedures;

however, it

was management's

expectations

that, prior to commencing

work. prerequisites

would be completed.

Conclusion - The inspector

agreed with the licensee's

conclusion that, during

the replacement

of"'DEG-2-PCV-'106,

the ma5etenance

workers performing the work

failed to meet

management

expectations

for completion of work order

prerequisites.

4

SURVEILLANCE OBSERVATIONS

(61726)

Selected

surveillance

tests

required

to be performed

by the

TS were reviewed

on

a sampling basis

to verify that:

(1) the surveillance

tests

were correctly

included

on the facility schedule;

(2)

a technically adequate

procedure

existed for performance of the surveillance tests;

(3) the surveillance tests

had

been

performed at

a frequency specified

in the

TS:

and

(4) test results

satisfied

acceptance

criteria or were properly dispositioned.

-10-

Specifically, portions of the following surveillances

were observed

by the

inspector during this inspection period:

Unit

1

STP P-CSP-11,

Revision 0, Routine Surveillance

Test of Containment

Spray

Pump

1-1

STP P-1282,

Revision

6, Routine Surveillance

Test of Diesel

Fuel Oil

Transfer

Pump 0-2

STP P-3RV1,

Revision 9, Exercising

10 percent

Atmospheric

Dump Valves

PCV-19,

20,

21,

22

STP I-111A, Revision

5, Functional

Test of Steam Generator

Blowdown

Sample Effluent Liquid Monitor RM-19

Unit

2

~

STP P-SIP-22,

Revision

7, Routine Surveillance

Test of Safety Injection

Pump 2-2

~

STP M-16D, Revision

13A, Operation of Train

B Slave Relay K608 (Safety

Injection)

4.1

Containment

S ra

Pum

Performance

Test

On February

I the inspector

observed

portions of STP P-CSP-11,

Revision 0,

"Routine Surveillance

Test of Containment

Spray

Pump 1-1."

The test is

performed

on

a quarterly frequency to verify continued operability of the

pump.

The inspector

attended

the preevolution briefing and observed

operator

actions

in the containment

spray

pump room.

The inspector

noted that the

briefing appropriately

emphasized

the precautions

and limitations of the

surveillance

and that the procedure

was performed

in

a controlled,

formal

manner.

Duri.ng operation of the

pump,

the inspector

observed

leakage

from the outboard

mechanical

seal

of the

pump at approximately

150 drop's/min.

Noting that the

surveillance

acceptance

criteria for seal

leakage

was

no leakage

or minor

dripping,

the inspector questioned

the operators

on the acceptability of the

observed

leakage.

The operators

and the shift supervisor

agreed

that the

leakage

was greater

than anticipated;

however.

they considered

that the

leakage

would not affect the operability of the

pump

as it did not exceed

the

test's criteria for unacceptable

leakage (i.e.,

steady

stream or spraying).

The inspector discussed

the seal

leakage with the containment

spray

system

engineer.

The system engineer

explained that during previous surveillance

tests of CS

Pump

1-1 the outboard

seal

leakage

had

been

observed

at varying

levels

and that

he believed

the leakage

observed

on Fobruary

1 was not

indicative of a significant seal

degradation.

-11-

Following completion of the, test,

the inspector

observed

that water

had

sprayed

outside

the posted

surface

contamination

area

(SCA) around

the pump's

outboard

seal

area,

and informed the operators.

In response,

the operators

requested

a radiation protection technician

to survey the area.

The results

of the survey identified no spread of contamination

outside of the

SCA.

Conclusion - The inspector

concluded

that the surveillance test

was well

controlled

and that both operations

and engineering

appropriately evaluated

the impact of the observed

seal

leakage

on the operability of the

pump.

However, operators

failed to take action to address

th~ potential

spread of

contamination

from the seal

leakage until prompted

by the inspector.

4.2

Diesel

Fuel Oil Transfer

Pum

Surveillance

Test

On February

6 the inspector

observed

portions of STP P-1282,

Revision 5,

"Routine Surveillance

Test of Diesel

Fuel Oil Transfer

Pump 0-2."

The test is

performed

on

a quarterly frequency

to verify the operability of the

pump per

TS 4.0.5.

During the verification of the

system electrical

lineup, prior to starting

the

pump,

the inspector

noted that the operator failed to perform all of the

required actions of Step

12 '.2 prior to proceeding

to the next steps

Step

12.2.2 requires

that the transfer switch in loadcenter

IH is in the

"Unit 1" position with Breaker

52-1H-65 closed.

During the performance of

this step,

the operator failed to verify the position of Breaker 52-1H-65.

After checking that the step

had

been completed,

and prior to performing the

next step,

the inspector questioned

the operator whether

he

had verified the

breaker position.

The operator

indicated that

he

had not and returned

to the

switchboard

and verified that the breaker

was in the required position

as

required

by the step.

The inspector

observed

the remainder of the test

and noted that the

pump

operated within the limits specified

in the surveillance

procedure

and that

there

were

no leaks during

pump operation

on the portion of the system located

within in the vault.

Conclusion:

The failure to>>.perform the, required actions of a surveillance

test constitutes

a violation of minor significance.

This violation is being

treated

as

a noncited violation, consistent

with Section

IV of the

NRC

Enforcement Policy.

4.3

Sl

Pum

2-2 Surveillance

Test

4.3.1

Licensing Actions in Preparation

for SI

Pump Testing

Background:

Sl

Pump 2-2 was replaced

in March

1995 after the

pump failed to

develop required differential pressure

during surveillance testing.

Prior to

conducting

the test,

the licensee

submitted contingency

License

Amendment

and

Notice of Enforcement Discretion

(NOED) requests

to increase

the allowed

outage

time

(AOT) for the

pump from 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to

7 days for pump replacement.

-12-

The

pump was replaced

in accordance

with 10 CFR 50.59,

tested,

and returned

to

an operable

status

in less

than

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

Since

the

pump was returned

to an

operable

status within the allowed outage

time there

was

no need for NRC

approval of the contingent

requests

and the licensee later formally withdrew

them.

In Hay

1995 the licensee

determined

that the replacement

Sl

pump did not have

documentation

that

LOKTITE had

been applied to the shaft locknuts during

assembly.

The licensee

determined

that the absence

of LOKTITE made

the

locknuts susceptible

to loosening.

This was the

same

mechanism for

degradation

that

was determined

to have

caused

the decrease

in pump

performance of the previously installed

pump.

The licensee

performed

an

operability evaluation

(OE) which provided the basis for concluding that the

pump was operable

and instituted

more restrictive performance criteria during

periodic

pump tests.

During the performance of the quarterly

pump test

in August

1995,

a slamming

noise

was noted

on the

pump start

as well as

a slight decrease

in differential

pressure.

At that point the cause of the noise

was indeterminate;

however, it

was believed

to have

been

caused

by

a water

hammer,

due to

a void in the

piping or check valve slam.

A week later the

pump

was tested

again with

a

slight decease

in performance,

although

no slamming noise

was noted.

The

pump

was tested

again

in November with a continued

decrease

in differential

pressure

and the slamming noise.

The

pump was placed

on

an "alert" status

in

accordance

with the compensatory

measures

established

by the

OE.

Placing

the

pump on "alert," required

pump performance

testing every

6 weeks

as

opposed

to

the normal quarterly frequency.

In January

1996 the

pump was tested with no

change

in differential pressure

and

no slamming noise.

On February

15,

1996,

6 days prior to the next scheduled

performance

of the

pump test,

the licensee

submitted

a license

amendment

request

(LAR) to the

NRC

requesting

an increase

in the allowed outage

time from 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to

7 days for

pump replacement.

On February

22 the licensee

provided the

NRC

a draft

version of

a contingent

HOED request

to allow the continued operation of

Unit

2 with one train of SI system

inoperable for up to

7 days,

4 days longer

than allowed by TS.

Preliminary discussions

regarding

the basis for the

request

between

.the

NRC and the licensee

revealed

that the licensee

had

known

of the pump's

degraded

condition

and the potential

need for an extension of

the

AOT for pump replacement

since

Hay 1995.

Consequently,

sufficient time

nad

been available for the licensee

to process

and gain

NRC approval of an

LAR

to increase

the

pump

AOT.

Therefore.

the condition that resulted

in the

need

for an

NOED was considered

to have

been avoidable.

Following the discussion

with the

NRC the licensee

decided

not to pursue

formal submittal of the

NOED

request.

4.3.2

SI

Pump Testing Resulting

in

Pump Replacement

On February

22 the inspector

observed

the performance of STP P-SIP-22,

Revision

7, "Routine Surveillance

Test of Safety Injection

oump 2-2."

-13-

In preparation

for the

pump test

the licensee

installed acoustic

emission

monitoring equipment

on several

locations

on the

pump

and adjacent piping.

A

temporary procedure

was

issued

to record investigative data concurrent with

the start of the

pump.

The

pump start

was initiated by energizing

the Train

B

slave relay at the solid state protection

system

safeguard

test cabinet.

Initiating the

pump start with the test signal

also started

the following

pumps:

CC

Pump 2-2, Residual

Heat

Removal

(RHR)

Pump 2-1,

CCW

Pump 2-2.

The

inspector

was in the

pump

room for the test

and hea"d

a loud slamming noise

concurrent with the stuart of the

pump.

The licensee's

evaluation of the acoustic

emission

data

indicated that the

noise

emanated

from SI

Pump 2-2.

The

pump performance

data did not

show any

further degradation

in pump performance

since

the previous surveillance test;

however,

since

the

slamming noise

was determined

to have

come

from the

pump,

the licensee

declared

the

pump inoperable

and

commenced

replacement

of the

pump.

It should

be noted that the licensee

considered

that there

was

a

potential for the

slamming noise to have

been

caused

by

a water

hammer

from

the start of the

RHR pump;

however,

there

were insufficient accelerometers

installed

on the suction of SI

Pump 2-2 to provide the data

necessary

to

further investigate

the issue.

4.3.3

Postmaintenance

Testing Following SI

Pump Replacement

Following replacement

of the

SI

pump,

the inspector

attended

the preevolution

briefing and observed

the test of the replacement

pump.

The replacement

pump

was instrumented

to monitor for any unusual

noises

during the test.

The

pump

was started

manually from the control

room and developed

a differential

pressure

greater

than the minimum required

by TS and within the acceptable

band of the surveillance.

There

was

no slamming noise

noted during the

pump

start or at any other time during

che testing.

4.3.4

Conclusion

The replacement

and testing of Sl

Pump 2-2 was well coordinated,

and,

as

a

result,

was accomplished

in

a timely manner within the allowed 72-hour action

statement.

Briefings conducted for the test

were thorough.

The testing

observed 4y the inspector

was well organized

and the personnel

involved were~

knowledgeable of their assigned

duties.

Following'he licensee's

conclusion

that

LOKTITE had not been

used during

pump assembly

and the decrease

in pump

performance,

the licensee failed to take appropriate

licensing actions

to

pursue

extension of the

TS allowed outage

time for pump replacement

as

opposed

to reliance

upon

an

NOED request.

The

LAR submitted

on February

15,

1996, did

not allow sufficient time for public comment

and

NRC review prior to the

scheduled

performance

of the surveillance test.

4.4

Exercisin

10 Percent

Atmos heric Steam

Dum

Valves

On February

6 the inspector

observed

portions of STP V-3R1, Exercising

10 percent

Atmospheric

Dump Valves

PCV 19,

20,

21,

22, which accomplished

the

quarterly inservice

atmospheric

steam

dump valve stroke timing pursuant

to the

S

-14-

requirements

of TS 4.0.5.

The measured

stroke testing of PCV-19 was within

the acceptance

limits of the procedure.

The inspector

noted that the first

stroke of the valve in the test direction

was recorded

as the official test

and that the appropriate

TS action statement

was entered

during the

performance of the test.

During the testing,

the inspector

noted that the cover to mechanical

panel,

PM-308, which contains

the solenoid valves

and control air lines that supply

the

PCV-19 actuator,

was not securelg&astened.

Closer inspection

revealed

that

a number of the clips that hold the panel

cover in place

had not been

tightened.

The inspector questioned

the operator

about

the condition of the

panel.

The operator

opened

the panel

and noted approximately

1/2 to

1 inch of

standing water in the bottom of the panel.

The operator

then

opened

Panel

PM-309 for PCV-20

and noted approximately

1/8 inch of water in the

bottom of the panel.

The inspector

noted that there

were drains installed in

each of the panels

but the installation did not allow all of the water to

drain from the panels.

The operator wrote

an

AR to document

the standing

water found in the panels'he

response

to the

AR concluded that the water

intrusion did not effect the safe operation of the solenoid

valves

and exposed

terminal

boards

mounted

in the panel.

Conclusion:

The inspector

noted that the test

was performed per the procedure

and that the valve operated within the acceptable

limits of the surveillance.

The water in the panels

did not appear to have

any current

impact

on valve

operability;

however, failing to secure

the panel

cover clips

on

safety-related

panels

exposed

to the weather

was judged to be

a poor work

practice.

5

ONSITE ENGINEERING

(37551)

5. 1

Investi ation of

CC

Pum

Surveillance Testin

5. 1.1

Background

On September

15,

1994,

the licensee

discovered

that closing the

CC pumps

common recirculation flow path isolation valves

(CVCS-8105 or 8106) during

periodic

pump performance~tests

potentially impacted

the oPerability of both

'harging

pumps.

The concern identified that closing the recirculation valves,,

secured

the minimum flow re"uired for internal cooling of the

pump to prevent'

overheating.

5.1.2

Licensee

Investigation

and Corrective Actions

Following identification of the concern,

the licensee's

regulatory compliance

organization

was consulted

to determine

the reportability of the condition.

Since

the

impact of clos~no

the valves during testing

had not been fully

evaluated,

no reportability determination

was

made at that time; however,

a

nonconformance

report

(NCR) was initiated

on September

24,

1994.

-15-

The

NCR documented

that the closure of the

CC

pump recirculation valves during

periodic

pump testing

was inconsistent with the licensee's

response

to

NRC

Bulletin 80-18,

"maintenance

of Adequate

Minimum Flow Thru Centrifugal

Charging

Pumps

Following Secondary

Side High Energy Line Rupture."

The

NRC

bulletin identified the potential for CC

pump failure due to loss of

recirculation flow under accident conditions

where reactor coolant

system

pressure

remained

at or near the

CC

pump shut-off head.

The licensee's

initial investigation of the issue

focused principally upon the

impact of the

loss of recirculation

on the cooling of the

pumps.

The licensee

responded

to

the concern

by revising the surveillance

procedure

to c'lose

a manual

isolation

valve that secured

the recirculation flow 'only for the

pump being tested.

After revision of the surveillance

the technical

review group

(TRG) did not

close

the

NCR and did not hold any meetings

to discuss

the issue for a period

of approximately

6 months.

Closing

CC

pump recirculation isolation valves during testing

increases

the

charging injection flow rate.

The

TRG failed to evaluate

the

impact of the

increased

charging injection flow on the accident

analyses until January

19,

1996,

when concerns

were raised

to the

TRG by

a system engineer.

On February

1,

1996.

the licensee

determined

that closure of recirculation

flow path Valves 8105

and

8106 for testing placed

the emergency

core cooling

system

in an unanalyzed

condition.

Following the determination

the licensee

made

1-hour nonemergency

report to the

NRC that both units

had

been previously

placed

in an unanalyzed

condition during

CC

pump surveillance testing.

From September

1994 to February

1996 the investigative actions

taken in

response

to concerns

regarding

CC

pump operability failed to consider the

impact of closing the recirculation isolation valves

on the accident

analyses.

Significant conditions that are adverse

to quality are required to be

investigated

and corrected

in

a timely manner.

The actions initiated by the

licensee

following identification of concerns

with

CC

pump surveillance

testing

were not considered

to have

been either prompt or comprehensive.

5. 1.3

Conclusion

10

CFR gart 50, Appendix B, Criterion XVI "Corrective Action,",requires that

measures

shall

be established

to assure

tkht conditions

adverse

'to quality.A

such

as failures, deficie",-ies,

and deviations

are promptly identified and

corrected.

The licensee's

failure to fully consider

the effect of closing the

CC

pump recirculation valves

on accident

analyses

for over

1 year after the

initial concerns with the test

were identified is

a violation of

10 CFR Part 50, Appendix B. Criterion XVI, Corrective Action (Violation 275/9602-02,

323/9602-02).

-16-

6

PLANT SUPPORT

ACTIVITIES

(71750)

The inspectors

evaluated

plant support activities

based

on observation of work

activities,

review of records,

and facility tours.

The inspectors

noted the

following during these evaluations.

6. 1

Re air of Fire

Pum

0-1 Dischar

e Isolation Valve

On February

7 licensee

mechanical

maintenance

personnel

overhauled

the

discharge

isolation valve to fire Pump 0-1.

The clearance

associated

with the

maintenance

required that several fire water hose reel stations

be isolated

in

the Unit

1 Fuel Handling Building.

The inspector discussed

with the licensee

the compensatory

actions

implemented

to ensure

adequate

fire fighting

capability was maintained

in the fuel handling building.

The inspector also

toured the fuel handling building with a fire brigade

member to walk down the

temporary fire hoses

that

had 'been

staged for providing water to the isolated

hose reel stations.

The inspector

noted that the fire brigade

member

was

knowledgeable

on the actions

they would take in the event of

a fire in the

affected

areas.

The inspector

concluded that the licensee

had adequately

assessed

the

impact

of the maintenance

on the in-plant fire protection

system

and

had

implemented

appropriate

compensatory

measures.

Following completion of the work the

inspector

observed

portions of the surveillance

on firewater

Pump 0-1

performed in accordance

with STP P-13A,

Rev.

15

XPR, "Fire Pumps

Performance

Test."

6.2

Failure to Meet Fire Bri ade Trainin

Re uirements

6.2.1

Background

On January

19 the licensee

noted in AR A0391417 that there

were several

members of the fire brigade

whose qualifications

had lapsed

because

they had

not completed all of the requalification requirements.

Further investigation

by tne inspector

revealed

that

as of January

19, greater

'..')an

70 percent of

the personnel

listed

as qualified fire brigade

members

did not have current

qualifications.

In order

to,.be able to meet

minimum fire brigade

manning

requi'rements

Ne licensee

administered

challenge

exams

to personnel

whose

qualifications

had lapsed.

Prior to January

19,

1996,

the licensee

had utilized

a computer bulletin board

to list all qualified fire brigade

members;

however,

as fire brigade

member

training lapsed,

the bulletin board

had not been properly updated.

Since the

shift watchlists,

which designate fire brigade

members,

had

been written

utilizing the bulletin board.

personnel

whose training

had lapsed

had

been

assigned

to the fire brigade.

-17-

6.2.2

Review of Fire Brigade Training

The inspector

reviewed

the qualification matrix previously used

by the

licensee

to track fire brigade training

and noted that in January

1996,

the

fire brigade qualifications for 79 of the

97 personnel,

listed

as being

qualified fire brigade

members,

had lapsed.

The majority of the individuals

had not received

the required biennial portable fire extinguisher training

since July 1993.

In addition,

the inspector

noted that other fire brigade

members'raining

had lapsed

in other areas,

including techniques

for

suppression

of electrical

and radiological fires.

The inspector

reviewed

the shift watchlists for December

29,

1995, for the

7 p.m.

to

7 a.m.

watches.

The review found that none of. the personnel

listed

as fire brigade

members

had current fire brigade qualifications.

6.2.3

Fire Brigade Training and Manning Requirements

TS 6.8.1 requires that written procedures

shall

be established,

implemented,

and maintained that cover the implementation of the fire protection

program.

Fire Brigade training is

a part of the fire protection

program.

Diablo Canyon

Procedure

Tgl.DC12, Revision

1, "Fire Brigade Training," details

the training

requirements

for fire brigade

members.

Section 5.3.3.c.3

requires that fire

brigade continuing training include

a biennial

review of the subject matter

contained

in the initial fire brigade

member

and leader training courses

in

each of the subject

areas

specified

in UFSAR Appendix 9.5H.

The classroom

instruction program described

in the

UFSAR requires

instruction in the proper

use of fire fighting equipment

and the correct

method for fighting various

types of fires.

Fire brigade

manning requirements

are detailed

in OP1.DC12,

Revision

2,

"Conduct of Routine Operations."

OPI.DC12 Section

5.9 requires that

a site

fire brigade of at least five members

shall

be maintained onsite at all times.

6.2.4

Previous

NRC Findings in the Area of Fire Brigade Training

NRC Inspection

Report 50-275/95-09;

50-323/95-09,

issued

on July 7,

1995,

contained

a Notice of Violation (275/950)-02)

that cited

a Severity Level=,IV

violation regarding

the licensee's

failu're to ensure that all members of the

fire brigade participated

in required quarterly fire drills.

Following

receipt of the violation, the licensee initiated

an

NCR on the missed fire

drills.

The inspector discussed

the

scope of the

NCR with the individual

assigned

as the chairman of the

TRG responsible

for investigation of the

NCR.

The individual indicated that although

the

TRG had questioned

whether there

were problems

in other areas

of fire brigade training,

no in-depth review had

been

performed.

Although the initial problem with fire brigade

member qualification was

identified by the licensee,

the issue

is considered

to

be more than

a minor

violation for several

reasons.

0

-18-

Corrective actions initiated in response

to Violation 275/9509-02 failed

to identify fire brigade

member qualification deficiencies.

~

The errors resulted

in

a significant number of personnel

being routinely

assigned

to the fire brigade without having completed

the required

training.

~

The situation existed over

a period of several

months.

6.2.5

Conclusion

The failure to complete proficiency training required

by Tgl.DC12 and the

UFSAR for individuals assigned

to the fire brigade is

a violation of TS 6.8.1,

which requires

that written procedures

sha'll

be established,

implemented,

and

maintained that cover the implementation of the fire protection

program

(Violation 275/9602-03,323/9602-03).

6.3

Radiolo ical

Work Practices

within the Radiolo icall

Controlled

A~rea

RCA

6.3. I

Observations

and Findings

The inspector

performed

several

tours of the

RCA to assess

the effectiveness

of the licensee's

radiological controls.

As

a result,

several

deficiencies

in

radiological

work practices

were identified.

During

a to<<r of the

RCA on

February

5,

1996,

the inspector

noted

poor housekeeping

practices

associated

with ongoing work in the hot shop

SCAs located

in the fuel handling

building (FHB).

The inspector

noted the following deficiencies

which

increased

the potential for the spread of contamination

outside of the

SCAs:

Items were laid across

SCA boundaries.

Tools

and trash

were

on the floor of the

SCA.

Used protective clothing was laying on the floor.

A hose

crossed

the

SCA boundary without being taped

down.

The radiological posting at the entrance

to the

SCA was down.

.Based

upon:.these

observations,

the inspector questioned

whether it would be

prudent to perform

a survey of the area

to verify that there

was

no spread of

contamination.

Personnel

performed

a survey of the hot shop

and determined

that there

had

been

no spread of contamination

outside of the

SCAs.

After the

inspector

voiced concerns

over the condition of the

SCAs in the hot shop,

the

licensee

stopped all work in these

areas until conditions

were

improved.

The

actions initiated by the licensee

in response

to the

issues

were aggressive

and

have significantly improved the conditions

in the

FHB hot shop work area,

The inspector considered

these

actions

to be warranted

and prudent

based

upon

the conditions

noted.

0

JP 8

In addition,

the inspector

noted other conditions within the

RCA which raised

concerns

about the implementation of radiological controls.

Observations

included the following:

~

Dry boric acid crystals

in

a walkway which had accumulated

as

a result

of a dripping pipe cap.

This condition was estimated

to have existed

for several

days.

A contamination

survey performed

indicated

the

presence

of contamination

outside of a surface

contamination

area.

~

A radiation

area posting that

had fallen down

ana

was

no longer

effectively posting the area.

~

Hags of used potentially contaminated

protective clothing were setting

in

a puddle of rainwater that crossed

over

an

SCA boundary.

~

Welding lines that were coiled across

the

SCA boundary during the

SIP-2-2 replacement.

6.3.2

Conclusions

The inspector dete rmined that these

issues

were weaknesses

and did not

constitute

a violation.

The observations

have,

however,

furthered

a

continuing concern

about radiological

housekeeping

practices

and worker

awareness

of radiological

hazards

and controls.

It is also noteworthy that

routine supervisor

tours of the

RCA had not identified and corrected

the

problems

noted

by the inspector.

The inspector

concluded that the

observations

were indicative of a decline in performance

in the area of

radiological controls.

7

FOLLOWUP - OPERATIONS

(92901)

7.1

Closed

Violation 50-275 95015-01:

Failure to Ensure

Ade uate

Containment

Closure Durin

Refuelin

0 erations

~

Disconnected

instrument tubing to

RHR Pump 2-1 recirculation flow switch

was noted to be dripping onto the

RHR pump

room floor.

The subject violation occurred during Onit

1 refueling operations

(core"

offload) when the licensee

discovered that

two of the main steam isolation

valves

(NSIVs)

had failed to fully close.

This condition,

in conjunction with

the removal of the

steam generator

secondary

manways,

provided

a direct

pathway

from the containment

atmosphere

to the environment.

The inspector

reviewed

the licensee's

response

to the Notice of Violation,

dated

December

21.

1995,

and

LER 275/95-012,

Revision 0, dated

November

10,

1995.

The inspector also verified the licensee's

installation of gag devices

on the HSIVs prior to the subsequent

core reload.

-20-

The main factor that contributed to the violation was the licensee's

failure

to implement

adequate

corrective actions

from

a similar event that occurred

in

1994.

The licensee

previously identified incomplete closure of the

MSIVs

during

a Unit

2 refueling outage

in October

1994.

As

a result of that event,

the licensee

planned

to revise its operating

procedures

to require

a visual

inspection of the actuator position of the MSIVs.

However, visual observation

of the HSIV actuator position during the subsequent

Unit

1 refueling outage

was not performed until after the core offload.

Licensee corrective actions

included replacement

of the HSIV actuator

pins to reduce frictional bin&~g of

the valves

and the revision of the library clearance

work instruction to

require

the installation of an HSIV gagging device

when the HSIVs are relied

upon to provide containment

closure.

As discussed

above,

the gagging devices

were installed

on Unit

1 prior to core reload.

In their response

to the

Notice of Violation, the licensee

has also committed to replacing

the actuator

pins

on the Unit

2 MSIVs during its next refueling outage,

scheduled

for April

1996.

The inspector verified that the actions described

in the licensee's

response letter of December

21,

1995,

to be reasonable

and

appeared

to address

correction of the circumstances

which contributed

to the violation.

8

FOLLOWUP ENGINEERING

(92903)

8.1

Closed

Ins ection Followu

Item 50-275 9334-01:

Unex lained Difference

Between Calculated

and Actual Estimated Critical Position of Control

Rods

During

a restart

on December

31,

1993, following a trip on December

26,

1993,

the actual critical position of the control

rods

was

79 steps

less

than the

calculated

estimated critical position.

While the difference

between

the

actual

and estimated critical positions

was the largest

experienced

by the

licensee

to that time, it was within TS limits.

The licensee

and Westinghouse

engineers

performed

an investigation of the

large difference

between

actual

and estimated critical posi:ions.

Westinghouse

issued its report

on June

7,

1994.

The inspector

reviewed

the licensee's

and Westinghouse's

evaluations.

The

inspector

found that both concluded that the calculated

value provided

by the

, Westinghouse

APEX code

was in good agreement

with the

3D ANC model.

Westinghouse

concluded that the effects of variations

in boron concentrations,

measured

boron-10 isotopics,

and rod positions, collectively, could have

4dused

the difference

between

the actual

and estimated critical positions.

The inspector

concluded that, while c'riticality occurred

sooner

than expected,

the estimated critical position

was appropriately calculated

and criticality

occurred within the allowable range..

The inspector

also

found that

a

conservative

approach

was taken

by licensee

engineers

to evaluate this issue

and reach

an appropriate

conclusion.

0

-21-

8.2

Closed

Unresolved

Item 50-275 95014-04:

Ade uac

of 230 kilovolt

kv

S stem Corrective Actions

and

0 en

Licensee

Event

Re ort 50-275

95007:

230 kv

S stem Outside

10 CFR Part 50

A

endix A. General

Desi

n

Criteria

17

in Some

Cases

The unresolved

item was

opened

to review the root cause(s)

of the degraded

230 kv source of offsite power to the Diablo site.

Violation 50-275/95014-03

documented initial failure of the licensee

to take corrective actions after

they

became

aware of the degraded

230 kv system.

The inspector

reviewed the

unresolved

item and determined

that it was

now duplicated

by

LER 50-275/95007,

as discussed

below.

Final

NRC review of the acceptability of the licensee's

root cause

and corrective actions for the degraded

230 kv system will be

by

further review of the

LER.

The inspector

reviewed

the operability of the

230 kv and

500 kv sources

of

offsite power during the storm of December

11,

1995.

The inspector determined

that the

500 kilovolt system

remained

operable

throughout

the storm,

and that

the

230 kilovolt system

was properly declared

inoperable

when

two of four

power lines supporting

the system

were lost.

The inspector

noted that the problems with the

230 kv system

were reported

in

LER 50-275/95007,

Revision 0.

This brief LER stated

that

a revision would be

issued

to provide

a root cause

and corrective actions.

The inspector

determined

that

an understanding

of the licensee's

position

on the cause(s)

of

the

LER and their planned corrective actions

would assist

in the review of the

LER.

The licensee

informed the inspector that they planned

to issue

the

revision in the near future.

The inspector deferred

review of the

LER pending

the licensee

planned revision.

9

IN-OFFICE REVIEW OF LICENSEE

EVENT REPORTS

(90712)

The inspectors

performed

a review of the following LERs associated

with

operating

events.

Based

on the information provided in the report,

review of

associated

documents,

and interviews with cognizant

licensee

personnel,

the

inspectors

concluded

that the. licensee

had

met the r porting requirements,

addressed

root causes,

and taken appropriate corrective actions.

The

followigg LERs were closed:

tl

9. 1

Closed

LER 275 95-09

Revision 0:

Turbine

and Reactor Trip Due to

Failure of Auto Stop Oil Pilot Valve Seat Material.

This event

was discussed

in Inspection

Report 50-275/95-14.

No new issues

were revealed

by the

LER.

9.2

Closed

LER 275 95-012.

Revision 0:

Technical Specification 3.9.4,

Requirement

for Containment

Closure During Refueling Not Met as

a Result of

Inadequate

Evaluation.

This event is discussed

in Section

7. 1.

9.3

~Closed

LER 275 95-17.

Revision 0:

Manual Reactor Trip Due to Heavy

Debris Loading to Traveling Screens.

This event

was discussed

in

NRC

Inspection

Report 50-275/95-18.

No new issues

were revealed

by the

LER.

-22-

9.4

Closed

LER 275 95-15

Revision 0:

Manual Reactor Trip Oue to Loss of

Feedwater

Oue to Design Deficiency.

This event

was discussed

in Inspection

Report 50-275/95-16.

No new issues

were revealed

by the

LER.

10

REVIEW OF

FSAR

COMMITMENTS

A recent discovery of a licensee

operating their facility in

a manner contrary

to the

UFSAR description highlighted the

need for a special

focused

review

that compares

plant practices,

proces~res,

and/or parameters

to the

UFSAR

description.

During

a portion of the inspection period (February

1 through

March 2,

1996),

the inspectors

reviewed the applicable

sections of the

UFSAR

that related to the inspection

areas

discussed

in, this report.

-The following

inconsistency

was noted

between

the wording of the

UFSAR and the plant

practices,

procedures,

and/or parameters

observed

by the inspectors.

10. 1

UFSAR Radionuclide

Source

Term

During

a review of the licensee's

UFSAR, the inspector identified an apparent

discrepancy

in the assumptions

utilized to determine

the plant's radionuclide

source

term.

Specifically, the

UFSAR assumed

the plant would operate

on

a

12-month cycle at

a capacity factor of 80 percent.

Currently, Diablo Canyon

Units

1 and

2 are operating

on

an

18-month cycle

and

have historically

exceeded

an

80 percent capacity factor.

In response

to the inspector's

concerns,

the licensee

reviewed their source

term analyses

and determined

that calculations

had

been

performed for various

operating cycle lengths,

including

18 months,

and that the

12-month operating

cycle effectively bounds

the source

term.

Similarly, capacity factor

differences

did not affect the source

term calculation.

The inspector

reviewed the analyses

and

had discussions

with licensee

and

NRC personnel

to

confirm the licensee's

conclusion that the calculations

for the

12-month cycle

with an

80 percent capacity factor were bounding

and reasonable.

The licensee

has

issued

an

NCR to clarify the

FSAR.

I ~

ATTACHMENT 1

PERSONS

CONTACTED

Licensee

Personnel

G.

H. Rueger.

Senior Vice President

and General

Manager,

Nuclear

Power

Generation

Business

Unit

W.

H. Fujimoto, Vice President

and Plant Manager,

Diablo Canyon Operations

L.

F.

Womack,

Vice President,

Nuclear Technical

Services

  • S.

D. Allen, Supervisor,

Balance of Plant Engineering

M. J.

Angus,

Manager,

Regulatory

and Design Services,

  • T. R. Baldwin, Senior Engineer,

Nuclear

Steam

Supply System

(NSSS)

Engineering

J.

R. Becker, Director, Operations

D.

H. Behnke,

Senior Engineer,

Regulatory Services

E.

Chaloupka,

Engineer,

Surveillance

Engineering

  • D. K. Cosgrove,

Supervisor,

Safety

and Fire Protection

  • W. G. Crockett.

Manager,

equality Services

H.

E. Craig, Shift Foreman,

Operations

  • R. N. Curb,

Hanager.

Outage

Services

J

~

S. Ellis, Instructor,

NPG Training

  • T. F. Fetterman,

Director, Electrical

and Instrumentation

and Control

Systems

Engineering

J.

  • N
  • W.
  • T
  • C
  • L
  • C
  • R
  • J

H

C

R

  • R

H.

A.

L.

R.

A.

D.

A.

A.

Galle,

Engineer,

NSSS Engineering

Gaudiuso,

Supervisor,

Procedure

Services

Team

Ginter,

Engineer,

NSSS Engineering

Grebel, Director, Regulatory

Support

Groff, Director,

Secondary

Systems

Engineering

Hagen, Director, Safety,

Health

and

Emergency

Services

Harbor,

Engineer,

Regulatory

Support

Harris. Director. Materials Services

Hays, Acting Manager,

Operations

Services

Hinds. Director. equality Control

Hug, Supervisor.

Emergency

Planning

Johnson,

Fire Marshall.

Emergency

Services

Johnson,

Supervisor.

Regulatory Services

Hagruder,

Shift Supervisor,

Operations

  • D. B. Hiklush, Manager,

Engineering

Services

  • J. E.:Holden,

Manager,

Maintenance

Services

  • E: P. Nelson,

Supervisor,

Materials Services

p

  • D
  • L
  • R

H

  • H
  • D
  • D

R

  • J

Nugent,

Senior

En..',neer,

Regulatory

Support

Oatley, Director, Hecnanical

Maintenance

Parker,

Engineer.

Nuclear Safety Engineering

Powers,

Acting Plant Manager,

Diablo Canyon Operations

Phillips. Director. Technical

Maintenance

Somerville.

Senior Engineer,

Radiation Protection

Taggart. Director. Nuclear Safety Engineering

dosburg.

Director.

NSSS Engineering

Waltos, Director, Balance of Plant Engineering

Young. Director, equality Assurance

1.2

NRC Personnel

  • M. Tschiltz, Senior Resident

Inspector

  • J. Sloan,

Senior Resident

Inspector,

San Onofre Nuclear Generating

Station

  • Oenotes

those

attending

the exit meeting

on March 6,

1996.

2

EXIT MEETING

An exit meeting

was conducted

on March 6,

1996.

Ouring this meeting,

the

inspectors

reviewed the scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed

by

the inspectors.

0

ATTACHMENT 2

ACRONYHS

AFO

AFW

AOT

AR

CCW

CFCU

CS

EDG

FHB

LAR

LER

HSIV

NCR

NOED

NSSS

OE

PANS

PCV

PDR

POA

PPC

RHR

RPE

SCA

SI

SISI

STP

TRG

TS

UFSAR

axial flux difference

auxiliary feedwater

allowed outage

time

action request

component cooling water

containment

fan cooler

containment

spray

emergency

diesel

generator

fuel handling building

license

amendment

request

licensee

event report

main steam isolation valve

nonconformance

report

notice of enforcement discretion

nuclear

steam

supply system

operability evaluation

post accident monitoring system

pressure

control valve

public document

room

prompt operability assessment

plant process

computer

residual

heat

removal

repair parts evaluation

surface

contamination

area

safety injection

seismically

induced

system interaction

surveillance test

procedure

technical

review group

Technical

Specification

Updated

Final Safety Analysis Report

O.