ML16342A439

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-275/93-32 & 50-323/93-32
ML16342A439
Person / Time
Site: Diablo Canyon  
Issue date: 02/23/1994
From: Vandenburgh C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Rueger G
PACIFIC GAS & ELECTRIC CO.
References
NUDOCS 9403150454
Download: ML16342A439 (22)


See also: IR 05000275/1993032

Text

5

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION

NBR e 9403 1 50454

DOC ~ DATE ~ 94/02/23

NOTARIZED e

NO

DOCKET

g

ACIL:50-275 Diablo Canyon Nuclear

Power Plant, Unit 1, Pacific

Ga

05000275

50-323 Diablo Canyon Nuclear

Power Plant, Unit 2, Pacific

Ga

05000323

AUTH.NAME

AUTHOR AFFILIATION

VANDENBURGH,C.

Region

5 (Post

820201)

RECIP.NAME

RECIPIENT AFFILIATION

RUEGER,G.M.

Pacific Gas

& Electric Co.

SUBJECT:

Ack receipt of 940204 ltr informing NRC of steps

taken to

correct violations noted in insp repts

50-275/93-32

&

50-323/93-32.

DISTRIBUTION CODE:

IEOlD

COPIES

RECEIVED:LTR

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SIZE:

TITLE: General

(50 Dkt)-Insp Rept/Notice of Violation Response

NOTES:

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NOTE TO ALL'RIDS

RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK.

ROOhk PI-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION

LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES

REQUIRED:

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UNITED STATES

NUCLEAR REGULATORYCOMMISSlON

REG(ON V

1450 MARIALANE

WALNUTCREEK, CAUFOFINIA94596-5368

FEB 2 3

1SS4

Docket Nos'. 50-275

50-323

Pacific

Gas

and Electric Company

Nuclear

Power Generation,

B14A

77 Beale Street,

Room 1451

P.O.

Box 770000

San Francisco,

CA

94177

Attn:

Hr. G. H. Rueger

Senior Vice President

and General

Hanager

Nuclear Power Generation

Gentlemen:

Thank you for your letter of February 4,

1994, in response

to our Notice of

Violation and Inspection

Report

No. 50-275/93-32

and 50-323/93-32,

dated

January

7,

1994,

informing us of the steps

you have taken to correct the items

which we brought to your attention.

Your corrective actions will be verified

during

a future inspection.

Your cooperation with us is appreciated.

Sincerely,

C. A. VanDenburgh

Acting Deputy Director

Division of Reactor Safety

and Projects

CC:

Dr. Richard Ferguson,

Energy Chair, Sierra Club California

Hs.

Nancy Culver,

San Luis Obispo Hothers for Peace

Ns. Jacquelyn

C. Wheeler

Nanaging Editor,

The County Telegram Tribune

Chairman,

San Luis Obispo County Board of Supervisors

Hr. Truman Burns, California Public Utilities Commission

Hr. Robert Kinosian, California Public Utilities Commission

Robert

R. Wellington, Esq.,

Diablo Canyon

Independent

Safety Committee

Nr. Steve

Hsu, Radiologic Health Branch, State

Department

of Health Services

Hr. Peter

H. Kaufman,

Deputy Attorney General,

State of California

Christopher J. Warner,

Esq.,

PG&E

Hr. John Townsend,

Vice President

and Plant Hanager,

Diablo Canyon

94031,50454

940223

PDR

ADOCK 05000275

PDR

0

gpss 2S

19S4

Docket Nos.

50-275

50-323

Pacific Gas

and Electric Company

Nuclear

Power Generation,

B14A

77 Beale Street,

Room 1451

P.O.

Box 770000

San Francisco,

CA

94177

Hr.

G. H. Rueger

Senior

Vice President

and General

Manager

Nuclear

Power Generation

Gentlemen:

Thank you for your letter of February 4,

1994; in response

to our Notice of

Violation and Inspection

Report

No. 50-275/93-32

and 50-323/93-32,

dated

January

7,

1994,

informing us of the steps

you have taken to correct the items

which we brought to your attention.

Your corrective actions will be verified

during

a future inspection.

Your cooper ation with us is appreciated.

Sincerely,

C. A. VanDenburgh

Acting Deputy Director

Division of Reactor Safety

and Projects

CC:

Dr. Richard Ferguson,

Energy Chair, Sierra Club California

Hs.

Nancy Culver,

San Luis Obispo Mothers for Peace

Hs. Jacquelyn

C. Wheeler

Managing Editor, The County Telegram Tribune

Chairman,

San Luis Obispo County Board of Supervisors

Hr. Truman Burns, California Public Utilities Commission

Mr. Robert Kinosian, California Public Utilities Commission

Robert

R. Wellington, Esq.,

Diablo Canyon

Independent

Safety Committee

Hr. Steve

Hsu, Radiologic Health Branch, State

Department

of Health Services

Hr. Peter

H. Kaufman,

Deputy Attorney General,

State of California

Christopher J.

Warner,

Esq.,

PG&E

Hr. John Townsend,

Vice President

and Plant Manager,

Diablo Canyon

bcc w/copy of letter dated

February 4,

1994:

Docket File

Resident

Inspector

Project Inspector

G.

Cook

K. Perkins

D. Clevenger

bcc w/o copy of letter dated February.4,

1994:

H. Smith

Region V/ann

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Pacific Gas and Electric Company

77 Beale Street, Boom1451

P.O. Box 770000

San Francisco, CA 94177

415/973-4 6S4

Fax 415/973-2313

Gregory M. Rueg~r'

Cp/ly'po

Senior Vice President an4fpg

General Manager

REQ/pN ~

Nuclear Par"r5en~ration

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February 4, 1994

PG&E Letter No. DCL-94-026

U.S. Nuclear Regulatory Commission

ATTN: Document Control Desk

Washington, D.C. 20555

Re:

Docket No. 50-275, OL-DPR-80

Docket No. 50-323, OL-DPR-82

Diablo Canyon Units

1 and 2

Reply to Notice of Violation in NRC inspection

Report Nos. 50-275/93-32 and 50-323/93-32

Gentlemen:

NRC Inspection Report Nos. 50-275/93-32 and 50-323/93-32, dated

January 7, 1994, contained a Notice of Violation that cited one

Severity Level IV violation regarding failure to follow procedure

requirements.

PG&E's response to the Notice of Violation is provided

in the enclosure,

Sincerely,

.Gregory M. Rueger

cc:

IVlary H. Miller

Kenneth E. Perkins

Sheri R. Peterson

Diablo Distribution

Enclosure

DCO-93-PG-N048

11 68S/KWR/2237

PGKE Letter No. DCL-93-026

ENCLOSURE

REPLY TO NOTICE OF VIOLATIONIN

NRC INSPECTION REPORT NOS. 50-275/93-32 AND 50-323-93-32

On January 7, 1994, as part of NRC Inspection Report Nos. 50-275/93-32 and

50-323/93-32, NRC Region V issued a Notice of Violation citing one Severity

Level IV violation for Diablo Canyon Power Plant, Units 1 and 2. The statement

of violation and PG&E's response follow.

STATEMENT OF VIOLATION

"During an NRC inspection conducted from November 4 through December 8, 1993,

a violation of NRC requirements

was identified.

In accordance with the "General

Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2,

Appendix C, the violation is listed below:

Diablo Canyon Technical Specification 6.8.1 states,

in part, that

written

procedures shall be established,

implemented and maintained covering the fire

protection program and the applicable procedures

recommended

in Appendix A

of Regulatory Guide 1.33, Revision 2, dated February 1978.

Appendix A of Regulatory Guide 1.33, Revision 2, recommends

procedures

covering surveillance testing; preventive maintenance;

and startup,

operation, and shutdown of safety-related systems.

1.

Paragraphs

5.3.5 and 5.3.6 of Plant Procedure AP C-3S3, Revision

1, "Dealing with Gage Oscillations During the Performance of ASME

Section Xl Required Pump Tests," require that, ifaveraging is

required when reading a gauge, the remarks section of the

procedure shall be annotated

and an Action Request written.

Contrary to this requirement, on November 10, 1993, the remarks

section of the procedure was not annotated

and an Action Request

was not written when the averaging technique was used during the

performance of a surveillance test on RHR pump 1-1.

2.

Paragraph 4.2.2 of Procedure AP C-151, Revision 7, "Procurement,

Storage and Handling of Hazardous Materials," requires that

flammable liquids be physically separated

from other hazardous

materials.

Contrary to this requirement, on November 18, 1993, corrosive

chemicals were stored adjacent to flammable liquids in the

radiologically controlled area {RCA) flammable liquids locker

'provided for lubricant storage.

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3.

Paragraph 5.2.2 of Plant Procedure AP D-753, Revision 20, "Control

of Plant Lubricants", states that the foreman shall review the

lubricant storage log book weekly.

Contrary to this requirement, the log book for the RCA lubricant

storage area was not reviewed during the second week of November

1993.

4.

Paragra'ph

6.1 of Plant Procedure

OP B-3B:II, Revision 8,

"Accumulators - Alignment Verification Checklist for Plant

Startup," referencing Attachment 9.2, requires that Circuit

Breaker 52-1F-46R be in the closed position.

Contrary to this requirement, on November 16, 1993, Circuit

Breaker 52-1F-46R was in the open position.

This is a Severity Level IV violation (Supplement 1), applicable to both Units

1

and 2."

REASON FOR THE VIOLATION

PGSE agrees with the violation as stated in the Inspection Report.

PGSE

management

also identified concerns regarding compliance with procedures by plant

personnel.

In response to this concern, management formed a Continuous

Improvement Team on November 30, 1993, to identify the causes of noncompliance

with procedures

and to implement corrective actions to improve procedural

compliance.

The team identified the generic causes of failure to follow procedures

as: inadequate understanding

of management

expectations

regarding adherence to

procedures;

reluctance to use the procedure revision process; overly restrictive

procedure usage requirements;

and personnel error. Although PGSE has not

concluded that current examples of procedural noncompliance constitute a significant

quality problem, PGSE agrees that the aggregate of self-identified procedural

noncompliances

and noncompliances

identified by NRC inspectors require evaluation

and comprehensive

corrective actions.

The actions taken to address the generic

causes

are discussed

below.

The causes of the four specific instances of failure to follow procedures identified in

the Notice of Violation are as follows.

1.

Documentation of gauge oscillations during surveillance testing:

During surveillance testing of residual heat removal (RHR) Pump 1-1, an operator

used the averaging technique as permitted by Administrative Procedure

(AP)

C-3S3, but failed to annotate the remarks section of the test procedure and

initiate an Action Request.

During performance of the test, the operator

questioned the method of reading the oscillating gauge and was referred to the

appropriate procedure AP C-3S3.

The operator read the procedural steps

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associated with how to use the instrument averaging techniques, but failed to

read the remainder of the procedure where the requirement for documentation

was discussed

and, therefore, failed to complete the required documentation.

The cause of this event is personnel error, failure to follow procedure.

2.

Corrosive chemicals stored adjacent to flammable liquids:

While.performing the inspection of the lube oil storage cabinet,

a corrosive liquid,

identified by PGSE personnel to be a partially used container of a two-part,

organic-based

paint package, was found inside the cabinet adjacent to

combustible lube oil. The cause of this event is personnel error in that the

appropriate procedures for storage of hazardous/flammable

materials were not

followed.

I

Log book for the RCA lubricant storage area not reviewed as required:

An upgrade foreman was performing the duties of the normally assigned foreman

during the week of the missed review of the lubricant storage log book.

The

upgrade foreman inadvertently failed to perform the required lubricant storage

cabinet review due to personnel error.

Circuit Breaker 52-1F-46R in the "open" position:

An investigation of the mispositioned breaker determined that the breaker was

verified to be in the correct (closed) position approximately two weeks prior to

the time it was found in the "open" position. A review of clearances

determined

that no activities were performed that could have resulted in the breaker being

mispositioned.

It was noted that a temporary scaffold had been erected adjacent

to the subject breaker.

It was concluded that the most likely cause of the

breaker being mispositioned was isolated personnel error during the construction

activities for which the scaffolding was being used.

CORRECTIVE STEPS TAKENAND RESULTS ACHIEVED

Documentation of gauge oscillations during surveillance testing:

An Action Request was initiated as required by Procedure AP C-3S3.

The RHR Pump 1-1 was operated to investigate the gauge osciltations.

The

gauge was found to oscillate uniformly-around 178 PSID. It was determined that

the oscillations were acceptable for the conditions that existed during the test,

and that proper averaging techniques

were used to record the data.

The

"averaged" value was compared to Section XI trending data for RHR Pump 1-1

differential pressure data and found to be consistent.

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Corrosive chemicals stored adjacent to flammable liquids:

This condition was corrected promptly by removing the corrosive materials from

the lubricant locker as required by Procedure AP C-251, "Procurement,

Storage

and Handling of Hazardous Materials."

3.

Log book for the RCA lubricant storage area not reviewed as required:

This condition was corrected by performing and documenting the weekly log

book review. The general foremen and foremen were counseled

regarding the

requirement for a weekly inspection of the storage areas to satisfy the

requirements of AP D-753, "Control of Plant Lubricants." The weekly log book

review has been performed as required since this event.

4.

Circuit Breaker 52-1F-46R in the "open",position:

Breaker 52-1F-46R was placed in the "closed" position as required by the

alignment verification checklist.

Primary Breaker 52-'I F-46 was also verified to

be in the sealed "off" position as required for accident mitigation. Emergency

procedures were reviewed and determined to provide proper guidance for closing

Breaker 52-1F-46R, if required.

During investigation of this event, it was noted that pre-outage work scaffolding

erection resulted in increased activity in the area that could have resulted in

inadvertent opening of the circuit breaker.

In response to this concern, PGSE

immediately halted all construction work and reviewed, through tailboards with

all personnel involved with field construction activities, the importance of

preventing inadvertent operation of equipment and the need for immediate

notification of the control room whenever plant equipment is disturbed.

CORRECTIVE STEPS THATWILLBE TAKEN TO AVOID FURTHER VIOLATIONS

Documentation of gauge oscillations during surveillance testing:

A shift order was initiated to require that all operating crews review Procedure

AP C-3S3, stressing the importance and requirement to document use of this

procedure.

Procedure AP C-3S3 will be revised to clarify documentation

requirements for use of the "averaging" technique.

2.

Corrosive chemicals stored adjacent to flammable liquids:

Some repetitive discrepancies

have been identified that indicate a problem with

control of lubricants at Diablo Canyon.

After an extensive evaluation by plant

staff and management,

a new procedure, CF5,ID11, "Lubricant Selection,

Storage and Dispensing," was approved on January 3, 1994, which improves

the control and use of lubricants at Diablo Canyon.

The responsibility for storage

of lubricants is being changed from the Mechanical Maintenance Section to the

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Material Services Section.

The satellite lubricant storage locations are being

reduced to facilitate control.

Procedure AP C-251 will be replaced with a new procedure, EV2.ID4-

."Hazardous Materials Management Program," which willinclude tighter controls

on all hazardous

materials.

Training.on the new requirements of Procedures

CF5.ID11 and EV2.ID4 requiring

pre-authorization for the storage of oils outside of the new lube oit storage

facility, the reduction of the satellite storage facilities, and the tighter controls on

hazardous

materials, will help ensure no further violations of the

hazardous/flammable

materials storage requirements.

3.

Log book for the RCA lubricant storage area not reviewed as required:

I

Procedure

CFG.ID11 provides guidance to Material Services personnel to perform

periodic reviews of lubricant storage logs to ensure completeness

and accuracy.

Training of Material Services personnel

on their new responsibilities for lubricant

, control under procedure CF5.ID11 will help ensure no further violations.

4.

Circuit Breaker 52-1F-46R in the "open" position:

Plant operations has initiated a program where sensitive plant areas that are

subjected to heavy construction work are identified by the operations work

planning center.

This list of work areas is delivered to shift supervisors,

and the

operations shift crew makes

a once-a-shift survey of each area, looking for

equipment damage or inadvertent operation due to the construction work in the

area.

This program was implemented via shift orders in December 1993, and

will remain in place until plant management

is confident that the culture

regarding the importance of preventing inadvertent operation of equipment and

the need for immediate notification of the control room whenever plant

equipment is disturbed, has been reinforced.

As indicated above,

a Continuous Improvement Team was initiated to identify

enhancements

that would result in generally improved procedural compliance.

The

Continuous Improvement Team identified that the existing procedure change

process,

consisting of Procedure AD1.ID2, "Review Level "A" Procedure Review,

Approval, Revision Control and Training Notification," does not provide for

expeditious processing of procedure changes at the working level since this

procedure is intended primarily for procedure writers. If a procedure discrepancy was

considered minor, personnel sometimes performed the procedure as it should be

performed, versus the way the procedure was written, since there was a reluctance

to use the existing cumbersome

procedure revision process.

To accommodate

both

procedure writers and field personnel,

Procedure AD1.ID2 will be revised, and a new

procedure developed to allow field personnel

a better understanding

of "intent"

change.

This action is to encourage field personnel to correct procedural flaws using

the on-the-spot-change

(OTSC) process versus a complete procedure document

revision.

The new procedure willprovide guidance to field personnel for processing

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minor procedure changes

(Le., editorial changes).

Procedure AD2.ID1, "Procedure

Use and Adherence," will be rewritten to be more usable for field personnel, to

clarify procedural usage guidelines, and to emphasize

management

expectations

regarding adherence to procedures.

Management expectations regarding procedural

adherence will be clearly communicated

and emphasized to plant personnel.

DATE WHEN FULL COMPLIANCE WILLBE ACHIEVED

PGSE is currently in full compliance.

The Continuous Improvement Team

recommendations to revise procedures AD2.IDI and AD1.ID2 and to develop the

new field guidance procedure should result in improving the procedure change

process in order to facilitate timely procedure revisions, resulting in better procedural

compliance.

The Continuous Improvement Team recommendations

discussed

above

will be completed prior to the start of the Unit 1 sixth refueling outage.

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