ML16341F996

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Insp Repts 50-275/91-02 & 50-323/91-02 on 910211-15.No Violations Noted.Major Areas Inspected:Radiation Protection Measures & Previously Identified Items
ML16341F996
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 03/04/1991
From: Peranich M, Tenbrook W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341F997 List:
References
50-275-91-02, 50-275-91-2, 50-323-91-02, 50-323-91-2, NUDOCS 9103200056
Download: ML16341F996 (16)


See also: IR 05000275/1991002

Text

U.

S;

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos.

50-275/91-02

and 50-323l91-02

License

Nos.

DPR-80 and

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon

Power Plant, Units 1 and

2

Inspection at:

Diablo Canyon Site,

Seven miles north of Avila Beach,

California

Inspection

conducted:

February 11-15,

1991

Inspected

by:

E7l~~-.'-/~FP /P'Y~'i.i~'(

r'-'..

enBrook,

adi ati on Spec> al > st

Approved by:

1/i<~'.~-'~~ l~'~ ~<~

ar

.

eran>c,

et> ng

se

Reactor Radiological Protection

Branch

Date

Soigne

ate

sgne

~Summer:

Areas Ins ected:

Routine unannounced

inspection covering follow-up of open

>tems

an

o servation of radiation protection

measures

during the Unit One

refueling outage.

Inspection procedures

92701,

83726

and 83729 were

addressed.

Results:

Strengths

were noted in the quality assurance

department

plan for

surveiTlance of radiation protection activities during the outage,

which had

identified

a potential violation.

The

ALARA program

had been effective in

achieving the licensee's

collective exposure

goals during the early stages

of

the outage

and

ALARA was well-implemented in work areas.

Radiation protection

technicians

provided thorough coverage of general

areas

and specific jobs.

Weaknesses

were observed

in the personal

conduct of steam generator

maintenance

workers

and training and familiarity problems during staging of

wash-down

equipment at steam generator four, which contributed to exceeding

the job dose estimate.

Dose rate survey data

from steam generators

varied

significantly due to the instrumentation

and techniques

employed.

The

ventilation balance

in the residual

heat removal

pump

room 1-2 caused

minor

contamination

spread.

No violations were identified.

910320005k

950304

PDR

ADOCK 05000275

0

PDR

0

DETAILS

Pers'ons

Contacted

Licensee

Per sonnel

=

M. Angus, Assistant Plant Manager,

Technical

Services

J.

Boots,

Chemistry, Manager

D. Cosgrove,

equality Control Specialist

W. Crockett,

Instrumentation

and Control Manager

R. Flohaug,

Senior equality Assurance

Supervisor

B. Giffin, Assistant Plant Manager,

Maintenance

R. Gray, Radiation Protection

Manager

J. Griffin, Senior Regulatory Compliance

Engineer

J.

Hays, Radiation Protection General

Foreman

J.

Knemeyer,

Senior Chemical

Engineer

R.

Kohout,

Emergency

and Safety Services

Manager

J. Mellinger, Senior Planner

D.

Miklush, Assistant Plant Manager,

Operations

B. Nanninga,

Senior

Mechanical

Maintenance

Engineer

D. Oatley, Assistant Plant Manager,

Support Services

W.

Rapp,

Onsite Safety

Review Group Chairman

J.

Shoulders, Onsite'roject

Engineer

M. Stabler,

equality Control Inspector

D. Taggart, Director, equality Assurance

D. Unger,

Chemical

Engineer

A. Young, Senior equality Assurance

Supervisor

NRC

P.

Galon,

Inspector

K. Johnston,

Resident

Inspector

P. Narbut, Senior Resident

Inspector

B. Olson, Project Inspector

The listed individuals attended

the exit meeting held February

15,

1991.

In addition, di'scussions

were held with other members of the licensee's

staff and contractor personnel.

Follow-u

of 0 en Items (92701)

0 en Item 50-275/88-33-01

(OPEN)

This item concerned

an NRC/licensee

antercompar>son

o

,e-

actlvaty in liquid waste.

Inspection

Report 50-

275/90-25 reported that the subject intercomparison

did not agree,

and

documented

a followup inspection at the licensee's

offsite laboratory.

The report concluded that the licensee's

sampling

and measurement

techniques

were fundamentally

sound.

However, differences

remained

in

sample splitting and preservation

techniques

that could affect the

measurements.

To resolve

these

concerns,

representatives

from the chemistry department

and the licensee's offsite laboratory met with the inspector

and

developed

an experiment to independently verify both the licensee

and

NRC

analyses

of a waste

sample.

A sample of processed'aste

receiver liquid

waste

was obtained

and filtered to remove

any fine particulate iron that

could contribute to a nonhomogeneous

split.

Iron particles

were visible

on the filter.

The filtered liquid was acidified and two aliquots were

preserved for the licensee

and

NRC as "control" samples

to provide the

baseline result of Fe-55 activity in the sample.

A portion of the

remaining liquid was placed in a volumetric flask, spiked with a NRC-

supplied

Fe-55 concentrate

solution,

and diluted to the mark with sample

liquid.

The spiked liquid was split between the licensee

and

NRC and

preserved

as "treatment"

samples.

The inspector

was the only party aware

of the amount of Fe-55

added. 'ach laboratory's

measurement

of the

"control" and "treatment"

samples,

and the difference

between

the

measurements

as

compared with the

known spike, will be evaluated to

determine

the accuracy of both licensee

and

NRC measurements.

The

results will be evaluated

during

a subsequent

inspection.

~

0 en Item 50-275/90-03-02

(Closed):

This item concerned

the logging of

qua i y con ro

c ec

s

or a

p a- eta counters

on control charts

per

regulatory guide 4. 15, "equality Assurance for Radiological Monitoring-

Effluent Streams

and the Environment."

Control charts of source

and

background

checks

were specified in revisions to chemical'nalysis

procedures

CAP B-15, "Operation of the Liquid Scintillation Counter...,"

and

CAP 8-16, "Proportional Counter."

The charts

were maintained in the

laboratories.

The inspector

had no"further concerns

in this matter.

0 en Item 50-275/90-20-02

(0 en):

This item concerned

high levels of Fe-

in

iqui

ra waste,

w ic

caused

the licensee

to exceed their

corporate curie release

goal during the previous year.

Inspection report

50-275/90-25,

and the licensee's

own intercomparison

studies with other

offsite laboratories,

concluded that the licensee's

measurements

of Fe-55

in releases

were generally

sound,

despite

the analytical

concerns

addressed

above.-

The inspector

concluded that measurement

inaccuracy did

not account for the high measured

Fe-55 levels.

The licensee

had been aggressively

reducing the size of micron filters

throughout the plant, both in response

to the high levels of Fe-55

and to

reduce overall effluent levels

and radiation

dose rates

due to

particulate target material in the reactor coolant system.

Chief among

the staged

decreases

in filter size were the letdown filters, spent fuel

pool filters and liquid radwaste

treatment

system filters.

Host of these

filters were

one micron or less,

absolute.

The following total quarterly

curies of Fe-55

had been released

to date:

First quarter,

1990:

9.3E-1

Ci

Second quarter,

1990:

4: 5E-1 Ci

Third quarter,

1990:

'.7E-2

Ci

Fourth quarter,

1990:.

l. 5E-1 Ci

The data

show

a reduction of one order of magnitude of total Fe-55

released

per quarter.

The licensee

suspected

that levels of iron would

3.

be affected

by forced oxygenation of the reactor coolant system prior to

the Unit One refueling outage

and unplanned trips of Unit Two during the

first quarter

of 1991.

This item will be evaluated after data for the

first quarter

o'f 1991 are available.

Occu ational

Ex osure Durin

Outa

es

Contamination Control

Surve

s and

Qnltorl n

Radiation Morker Trainin

-

The inspector

reviewed lesson

plan series

GRPA 400; for generic radiation

protection training,

and

GRPO 650I, for site specific radiation

protection procedures.

The inspector

observed that the materials

thoroughly discussed

external

exposure,

including the federal

guidance

for emergency

exposure

levels in excess

of the limits of 10 CFR 20 'and

discussion of the recent risk data

from the 'Biological Effects of

Ionizing Radiation

Committee Report V.

The inspector did not note

a discussion of the conduct of radiation

workers in the breaching of contaminated

systems

or containers

of

radioactive material, or in the movement of such material.

The inspector

inquired whether

such

a discussion

was considered

by training in light of

a March 1990 incident where

I8C contractors

moved contaminated

equipment

to a sea-train without informing radiation protection,

leading to

personnel

contaminations

and contamination of the sea-train.

The licensee

provided the inspector with Action Request

A0184275,

documenting the licensee's

corrective actions for the incident.

The

action request

documented tailboard meetings with I8C contractors to

discuss

the incident, but the issue

had not been considered

appropriate

for general

discussion.

The licensee

stated that general

employee

traini ng discussed

radiation work permit requirements,

and radiation, work

permits, in turn, discussed

specific requirements

for radiation

protection coverage

during the breaching of systems.

Also, the inspector

learned that lesson

GRPD 650I-7,

"Radwaste Minimization," contained

a

discussion of tool control per.administrative

procedure

0-55, including

the requirement for radiation protection approval of tool storage

locations.

The inspector

concluded that general

employee training and the specific

requirements

of radiation work permits provided adequate

instructions for

workers per 10 CFR 19.12.

Observation of Steam Generator

Oecontamination

The inspector

observed

the decontamination

of unit one steam generator

channel

heads.

Four technicians

were assigned

at each of the two steam

generator

access

control points;

one maintained radio contact

and video

surveillance of the work crew,

one was stationed

on the clean area of the

step-off pad,

another at the labyrinth entrance

and

a fourth technician

accompanying

the crew.

The responsible

radiation protection engineer

was

continuously involved as the job progressed.

Protective

equipment,

including air-fed suits

and hoods,

was properly

donned.

However, while contract workers waited to don protective

equipment,

the inspector

observed

some

examples of poor conduct.

A

con'tract worker sportively shoved another worker aga'inst the bioshield

wall repeatedly.

Since the shoved worker did not wear their protective

clothing in a manner consistent with procedure i.e.,

hood undone,

the

worker's o'uterclothing contacted

the shoved

wor ker's

neck and chin.

The

responsible

radiation protection technician

and the contractor area

coordinator were immediately informed.

No personnel

contamination

resulted

from the conduct

and the inspector did not observe

widespread

instances

of poor conduct in controlled areas.

The inspector

observed

two delays during the steam generator

bowl

decontamination.

Morkers at steam generators

one

and two were

hampered

by radio transmission difficulties.

Morkers at steam generators

three

and four appeared

to misplace or misassemble

components for the bowl

wash-down, resulting in a delay of approximately

one half hour during the

transition from steam generator

three to four.

After obtaining

assistance

from the contractor's

area coordinator,

the bowl wash-down

equipment

was readied

and work commenced.

These

delays contributed to

the crews exceeding

the estimated

2.5 person-rem for the job, accruing

4.3 person-rem.

The inspector

reviewed survey data obtained before

and after the steam

generator

bowl decontamination.

Since the decontamination

was intended

to remove radioactive particles emitting high beta

dose rates,

the

inspector did not expect

a reduction in gamma

dose rate.

The inspector

noted that tubesheet

and divider plate post-decontamination

dose rates

on

steam generator l-l and 1-2 ranged

30-50K higher than pre-decontamination

dose rates.

The inspector investigated

these differences

and found that

compensated

geiger-meuller detectors

were used for the post-

decontamination

survey

as

opposed to the preferred ion chamber

instruments

used for the pre-decontamination

survey.

Geiger-Meuller

instruments

were substituted

due to maintenance

problems with the ion

chamber

instruments.

Data obtained for all four steam generators

suggested

a less

severe

variation overall, particularly since the

same type of instrument

was

used for each

survey of steam generators

three

and four.

However,

a +/-

33/o variation remained.

Since the four steam generator

average

dose rate

increased

after decontamination,

and the average

was

used to calculate

stay times for steam generator

work, the inspector

concluded that the

post-decontamination

survey conservatively predicted

personnel

exposure.

However,

the variation of survey techniques,

and the resulting variation

in dose rate averages,

could affect evaluations

of radiation field

control methods.

The conduct of steam generator

maintenance

workers

and their performance

during staging of wash-down

equipment at steam generator

four

suggested'raining

weaknesses.

Dose rate survey data in steam generators

varied

significantly due to the instrumentation

and techniques

employed,

but

personnel

were adequately

protected.

Ho violations of radiation

protection requirements

were observed.

5

Removal of Residual

Heat Removal

Pum

1-2 Im eller

The inspector

observed

the "removal of the residual'heat

removal

system

pump 1-2 impeller in preparation

to remoVe the

pump motor for

maintenance.

The impeller removal

was covered

by two radiation

protection technicians,

one inside the contaminated

area

and one at the

step-off pad for support.

The

pump motor was hoi'sted to place the shaft

in a vertical position, approximately

two meters within the boundaries

of

contaminated

area

and high radiation area.

A high-efficiency particulate

air filter (HEPA) unit took suction across

the impeller,

away from the

step-off pads.

A breathing-zone air sample was'in-progress

and workers

=

in the contaminated

area

wore respirators

as

a precaution during work

with the highly contaminated

impeller'uring

the removal of the impeller, the inspector

and the radiation

protection technician at the step-off pad noted that the ventilation

system

was creating positive pressure within the room.

A rush of air

occurred

each time the door

was opened.

The technician

began

a large

.area contamination

survey of the step-off pad and entrance

stairway,

and

initiated an air sample

on the stairway.

Direct frisk of the area wipes

measured

two hundred net counts per minute.

The radiation protection

foreman

was informed and the step-off pad/surface

contamination

boundary

was

moved to the entrance

to the room.

Shortly after, the impeller was

removed

from the shaft

and stored in the

contaminated

area.

The workers, technicians

and the inspector performed

a local frisk and passed

through the personnel

contamination monitors

without incident.

Later review of air sample

data revealed

0.01 maximum

permissible concentration

(MPC) airborne activity on the entrance

stairwell

and 0. 11

MPC at the clean area

on the north end of the

room.

Natural airborne activity could have predominated

in these

samples,

as

neither

sample

met the licensee's

0.25

MPC criteria for gamma isotopic

analysis.

The inspector

noted that the design

bases for the auxiliary building

ventilation system,

Final Safety Analysis Report section 9.4. Z. 1, state

that the flow of air is always directed

from areas

of low potential

contamination to areas

of higher potential

contamination.

After

investigating the conditions in the

pump room, the radiation protection

department

informed the inspector that particular areas of the plant

would not exhibit ideal ventilation flow during periods

when ventilation

systems

were affected

by outage

maintenance.

The licensee

stated that

room ventilation balance

would be evaluated prior to reinstallation of

the impeller.

The inspector

concluded that the observed ventilation balance

did not

create

an unanalyzed

condition while the residual

heat

removal

system

was

out of service,

but the flow caused

minor contamination

spread.

No

violations were identified.

ualit

Assurance

The inspector

reviewed the quality assurance

department's

involvement'in

radiation protection activities since the prior inspection.

The quality

surveH lance group

had performed observation of several

radiation

protection activities, including cavity decontamination

and temporary

shielding installation'.

During the inspection,

the radiation protection

manager

informed the

inspector of a quality finding from a February 12,

1991 surveillance of

radiation protection activities in containment.

Morkers had entered

the

reactor coolant

pump 1-3 cubicle via a route that avoided high radiation

areas.

Radiography

was subsequently

initiated near the cubicle 1-3

entrance,

creating

a high radiation area,

so

one worker was forced to

exit to the opposite

side of containment via a catwalk near the steam

generators,

also

a posted

high radiation area.

The surveillant observed

the worker exiting the posted

high radiation area without an alarming

dosimeter or a technician with a dose rate instrument,

a potential

violation of technical specification (TS) 6.12.

Action Request

A0217882

was initiated to track resolution of the observation,

and further

investigation revealed that the worker did not pass

through any area that

actually exceeded

the

100 mR/hr

dose rate. specified in TS 6. 12.

The

inspector

had

no further concerns

and remanded

the matter to the

licensee.

The quality assurance

department

had established

an effective plan for

surveillance of radiation protection activities during the outage.

Kee in

Dose

As

Low As Reasonabl

Achievable

(ALARA)

The inspector

performed

dose rate measurements

in controlled areas

using

ion* chamber instrument

NRC 015844.

Boundary postings

were consistent

with 10 CFR 20.203.

The inspector

observed

thorough radiation protection

technician

coverage of each containment elevation during tours of general

areas.

A checkpoint

was set

up at each elevation

and

no personnel

were

permitted without informing the on-duty technician.

The balance of the

elevation

was covered

by roving technicians

or those

assigned

to

continuous

coverage.

The licensee's

ALARA precautions

in work areas

were strong.

The

inspector

observed

workers staging

equipment in a reactor coolant

pump

bat to sludge-lance

steam generators,

working quickly and efficiently to

minimize exposure.

"Co'1d areas"

and localized radiation areas

were

conspicuously

posted in containment.

Workers were aware of measures

available to minimize exposure.

The licensee's

outage

dose report demonstrated

that the collective

exposure

accrued to date

was tracking with corporate

ALARA goals.

The

licensee

was encouraged

by the performance

to date,

as the

315 person-rem

corporate

goal

was thought to be ambitious,

given the outage

scope.

The

inspector

reviewed collective doses

on individual radiation work permits

and identified few instances

where

doses

had exceeded

those estimated.

Among those permits that

had exceeded their dose estimates,

the steam

generator

bowl decontamination

accounted for over half. the total 3.3

7

person-rem

excess,

followed by the elimination of boron injection tank,

0.87 person-rem

over estimate.

The inspector also examined

steam generator

channel

head average

dose

rate data spanning all four- unit one refueling outages.

The average'data

compared favorably with charts of,channel

head

dose rates at various

plants versus

operating time as presented

in Electric Power

Research

Institute report NP-4505-SR,

"Manual of Recent Techniques for LMR

Radiation Field Control," demonstrating that historically good fuel

integrity and measures

to keep radiation fields ALARA were effective in

reducing

dose.

The inspector

concluded that the licensee's

ALARA program

had been

effective in achieving the licensee's

goals during the early stages

of

the outage.

~Eit H ti

The inspector

met with licensee

management

on February

15,

1991 to

discuss

the scope

and findings of the inspection.

The licensee

acknowledged

the inspector's

observations.