ML16341F666

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Insp Repts 50-275/90-05 & 50-323/90-05 on 900128-0310. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items,Lers & Selected Independent Insp Activities
ML16341F666
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 04/04/1990
From: Mendonca M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341F664 List:
References
50-275-90-05, 50-275-90-5, 50-323-90-05, 50-323-90-5, IEB-89-006, IEB-89-6, NUDOCS 9004230585
Download: ML16341F666 (30)


See also: IR 05000275/1990005

Text

U.

S.

NUCLEAR REGULATORY

COMMISSION'EGION

V

Report Nos:

50-275/90-05

and 50-323/90-05

Docket Nos:

50-275

and 50-323

License

Nos:

Licensee:

DPR-80 and

DPR-82

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo'Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

January

28, through March 10,

1990

Inspectors:

P.

P. Narbut, Senior Resident

Inspector

K.

E. Johnston,

Resident

Inspector

Approved by:

en onca,

se

,

eac or

roJec

s

ec

son

~/W4 go

a

e

>gne

Summary:

Ins ection from Januar

28 throu

h March 10

1990

Re ort Nos.

50-275/90-05

an

/

Areas Ins ected:

The inspection

included routine inspections of plant

opera lons,

ma)ntenance

and surveillance activities, follow-up of onsite

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

30702,

30703,

37700,

37702,

40500,

42700,

61726,

62702,

62703,

71707,

92700,

92701,

92703,

92720,

and 93702 were used

as guidance during this inspection.

Safet

Issues

Mana ement

S stem

SIMS) Items:

None.

Results:

General

Conclusions

on Stren th and Weaknesses

Additional

E ui ment Lineu

Problems:

Twice during the inspection period

operators

ma

e sign>>cant

equipment lineup errors which affected the

operation of safety related

equipment

(paragraphs

4e and 4h).

The errors

indicated that operations

management

had not yet been fully successful

in

communicating their expectations

regarding the equipment lineup process

to

operations

personnel.

p0042-"

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cyPO404

PI3R

AG~

'gC

Q

Desi

n Mork Concerns:

In this inspection period there were'wo concerns

on design work.

Paragraph

3c describes

a situation where security personnel

designing modifications to

the intake area security barriers

based

design

assumptions

on inaccurate

information regarding the normal configuration of the auxiliary

saltwater'ystem.

Although this did not result in a violation of the licensee's

security plan, it indicated

a weakness

in the communications

between security,

plant engineering

and operations with respect to security design.

Paragraph

4j discusses

the last minute postponement

of the removal of the Unit 2 Boron

Injection Tank due to design

problems discovered

by both design Engineering

and equality Assurance.

Failure to Reco nize and Elevate

Problems

In September

1989, general

construction personnel,

excavating for a design

modification, unearthed

and gouged safety related auxiliary saltwater

piping

without recognizing the significance of the act and did not notify plant

management

or initiate the required problem reporting process

which resulted

in a violation (paragraph

5a).

Timel

0 erator Action

At the start of the Unit 2 refueling outage,

Operators

on Unit 2 recognized

and took corrective actions'to

address

a rather obscure potential

Residual

Heat Removal

system suction valve isolation problem (paragraph

4).

Good Problem Identification

Although also mentioned

as

a design

w'ork concern,

Engineering

and

gA

identified problems with the Boron Injection Tank removal modification and

took conservative

action to postpone

the design

change.

Si nificant Safet

Matters:

None.

Summar

of Violations and Deviations:

One violation was identified

concerning

a) ure

o

a

e cor rec ive action - paragraph

5.a.

0 en Items

Summar

18 open item were closed in this report.

One was opened.

DETAILS

Persons

Contacted

J.

D.

D.

B.

+M. J.

B.

W.

"W.

G.

+W.

D.

~T.

A.

~D.

A.

  • 7

H. J.

D.

P."

+R.

C.

  • J ~

A.

M.

G.

  • S.

R.

+R.

E.

C.

Townsend,

Vice President,

Diablo Canyon Operations

and Plant

Manager

Miklush, Assistant Plant Manager,

Operations

Services

Angus, Assistant Plant Manager,

Technical

Services

Giffin, Assistant Plant Manager,

Maintenance

Services

Crockett, Assistant Plant Manager,

Support Services

Barkhuff-, equality Control Manager

Bennett,

Mechanical

Maintenance

Manager

Taggert, Director equality Support

Grebel,

Regulatory Compliance Supervisor

Phillips, Electrical Maintenance

Manager

Brooks, Acting Work Planning Manager

Washington,

Acting Instrumentation

and Controls Manager

Shoulders,

Onsite Project Engineering

Group Manager

Burgess,

System Engineering

Manager

Fridley, Operations

Manager

Gray, Radiation Protection

Manager

Connell, Assistant Project Engineer

The inspectors

interviewed several

other licensee

employees

including

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

  • Denotes those attending the exit interview on March 23,

1990.

Also attending the exit meeting

was Marvin M. Mendonca,

NRC Section

Chief.

2.,

0 erational

Status of Diablo Can

on Units 1 and

2

At the beginning of the report- period, both Units 1 and

2 were at full

power.

On February 20,

1990, operators

manually tripped Unit 1 following

the closure of the feedwater regulating valves which was apparently

precipitated

by surveillance activities in the solid state protection

system cabinets

(see Section 4.b).

.On February

22,

1990, the licensee

. gagged

one of three Unit 2 pressurizer

safety valves, after receiving

an

emergency

Technical Specification

change,

when its leakage

increased

(see

Section 4.c).

On March 4, 1990, Unit 2 shut

down for its third refueling

outage.

At the end of the report period, Unit 1 was at full power and

Unit 2 had just entered

Mode 6; core alterations.

On February 2, 1990,

a team inspection,

which reviewed the corrective

actions

and oversite

programs,

conducted

an exit meeting

(see Inspection

Report 50-275/90-01).

On February

12,

1990, after a temporary injunction

was lifted, random drug screening

began for applicable

union members.

3.

0 erational

Safet

Verification (71707)

a.

Gener al

b.

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week,

the inspectors

toured the accessible

areas of the facility to

observe

the following:

(a)

General plant and equipment conditions,

(b)

Fire hazards

and fire fighting equipment.

(c)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(d)

Interiors of electrical

and control panels.

(e)

Plant housekeeping

and cleanliness.

(f)

Engineered

safety feature

equipment alignment

and conditions.

(g)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

Radiolo ical Protection

The inspectors periodically observed radiological protection

practices

to determine whether the licensee's

program

was being

implemented in conformance with facility policies and procedures

and

in compliance with regulatory requirements.

The inspectors,

including the Diablo Canyon project inspector,

observed

the activities at the access

point for the radiological

controls areas

(RCA) on February 21; 1990, prior to the start- of the

Unit 2 refueling outage.

The inspectors

noted that personnel

leaving the area were not.exercising

good radiological practices,

in

that opportunities for potentially contaminated

personnel

to

contaminate

clean personnel

were being created.

The licensee

uses

personnel

contamination monitors

(PCMs) to monitor

personnel

exiting the

RCA.

The

PCMs are sensitive

and detect

naturally occurring radioactive

radon

and its daughter products.

The licensee

has

had the long-standing

and

common problem of radon

adhering to clothing by electrostatic

charge.

The extent to which

radon is present in the auxiliary and fuel handling buildings is in

large part dependent

on atmospheric conditions.

The inspectors

observed

a situation where,

on a relatively high

concentration

radon day, approaching

lunch time, with one of the

three

PCMs out of service,

approximately half of the people

attempting to exit the

RCA were alarming the

PCMs and

a substantial

line (10-15 people)

had developed.

The radiation protection

(RP)

technician responsible

for monitoring personnel

and equipment

leaving the

RCA appeared

to be overwhelmed with responding to the

alarms

and performing other tasks

such

as frisking equipment.

As a

result,

personnel

were performing self analysis of their alarms

and

loitering in line to allow radon to decay.

This presented

the

opportunity for personnel

who had alarmed the

PCMs,

and who might

have

been genuinely contaminated,

to potentially contaminate

uncontaminated

personnel.

The inspectors

presented

these findings to the

RP manager.

The

RP

manager

stated that radon

was not a health risk in the levels

existing in the auxiliary and fuel handling buildings but the number

of resultant

alarms at the

RCA exit area

tended to reduce

employee

sensitivity to alarms.

He noted that

PG8E had plans to reduce the

radon levels, possibly including the capping of a well used to

evaluate

water conditions at the containment

base.

Also, the

licensee

is considering

reducing the frisker s sensitivity to radon.

However, the

RP manager

agreed that

RP technicians

need to control

RCA exits to ensure all alarms

are adequately

assessed.

The

inspectors will observe

the licensee's

actions

regarding this matter

in future inspections.

Ph sical Securit

71707

Security'activities

were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative procedures.

On January

30, 1990, the inspector

examined the seawater

intake area

including recently completed modifications to the security

boundaries.

The inspector identified two apparent

examples of vital

auxiliary saltwater

system

(ASWS) equipment located outside

a vital

area

boundary.

The specifics

are not discussed

here

because

they

are security safeguards

information.

These findings were discussed

with the security manager

who

initiated a review of the findings and

an evaluation of the intake

security modifications.

Subsequently,

a third apparent

example of

vital

ASWS equipment located outside

a vital area

boundary

was

identified by the licensee.

~

~

The licensee's

analysis of the potential

consequences

of the three

findings assumed

the worst postulated

challenge

in accordance

with

the security plan and the effects

on

ASMS operation,

In all cases

it was found that existing control

room annunciation

and

proceduralized

response

would successfully mitigate event

consequences.

Although the potential

consequences

of the findings were not

signifscant

when

a security analysis

was performed,

they pointed to

a weakness

in the security design process.

In the two examples

identified by the inspector,

the design decisions to not include the

equipment in a vital area

were based

on faulted assumptions

of

normal

system operation.

No changes

to the security boundaries

resulted

from the licensee's

.

evaluations.

However the uncertainty which existed indicated

a

weakness

in the'ommunication

between security designers,

who have

in-depth

knowledge of the security plan but not of system operation,

and operations

and engineering

personnel,

who have in-depth

knowledge of system operation

and design but not of the security

plan.

The inspector discussed

these

concerns with the security manager

who

agreed that the interface

between security and operations

required

improvement

and committed to do

a thorough evaluation of the cause

and pursue appropriate corrective actions.

The inspector will

follow the licensee's

actions

in the course of routine .inspection.

No violations or deviations

were identified.

4.

Onsite

Event Follow-u

93702

a e

b.

Minor Earth

uake Near Diablo Can

on

On February 6, 1990,

an earthquake

of approximate

magnitude 3.6 to

3. 9 occurred '30 to 60 miles south-southwest

of the plant.

Although

most plant personnel

did not feel the earthquake,

the earthquake

triggered sensitive monitoring devices.

A plant individual did feel

physical motion and notified the control

room.

Consequently

an

Unusual

Event was declared

and plant walkdowns were initiated in

accordance

with procedures.

No damage

was identified by the

walkdowns.

Ground acceleration

was later measured

to be 0.002 g.

Unit 1 Manual Reactor Tri

Followin

Feedwater

Re ulatin

Valve

osure

At 5:30 a.m.

PST on February 20,

1990, Unit 1 reactor operators

manually tripped the reactor

from 100K power in response

to the loss

of both main feedwater

pumps.

All safety systems

responded

.

normally.'he licensee

made

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency

report to the

NRC and documented

the event in a written report in accordance

with

10 CFR 50.73.

The licensee's

LER (Licensee

Event Report) 1-90-02 provides

an

accurate

description of the event and detailed explanations

of the

licensee efforts to identify the cause of the event.

Therefore

those facts will not be repeated

here.

The resident inspectors

observed

licensee

management

actions in the

event analy'sis

and attended

the plant staff review committee meeting

which approved restart of the unit.

Licensee investigative actions

were observed to be well planned

and conservative.

LER 1-90-02 is

considered

closed.

Unit 2 Leakin

Pressurizer

Safet

Valve Ga

ed

On February 21,

1990, the licensee installed

a gagging device

on one

of three safety valves

on the Unit 2 pressurizer.

The safety valve

(8010B)

had been

observed to leak on February

20.

Operators

had

observed

elevated pressurizer tail pipe temperature,

spikes in the

pressurizer relief tank (PRT) pressure,

increased

PRT level,

and

acoustic monitor alarms

on Unit 2.

These

were the

same

leakage

characteristics

that were observed

on Unit 2 safety valve 8010A

in March 1989 which ultimately resulted in a plant shutdown for

repair.

Prior to these

events,

in anticipation of such

an occur rence,

on

January

25,

1990, the licensee

submitted

a license

amendment

request

to allow continued operation with one inoperable

and gagged

pressurizer

safety valve.

On February 20,

1990 in response

to the

valves condition, the licensee

requested

an emergency

Technical

Specification

(TS) change for a one time exemption to allow

continued operation with one inoperable,

gagged pressurizer

safety

valve.

In their analysis,

the licensee

considered

the possible

consequences

on affected design basis

accidents

and concluded that

over-pressure

protection limits of the accident analysis

could be

met with two of three safety valves operable.

For conservatism,

the

licensee

included in their revised

TS a requirement to have

one

operable

and available pressurizer

power operated relief valve.

On

February 21, the

NRC approved the emergency

TS amendment

and the

safety valve gag was installed.

On February 26, operators

noted

a partial return of the symptoms

described

in the first paragraph.

Maintenance

personnel

inspecting

the valve observed that the gag

had loosened.

The licensee

consequently

obtained

a torque value for the gag from the safety

valve manufacturer

and tightened the gagging device.

Following the shutdown for the Unit 2 refueling outage,

the

inspector

noted that the gag was again loose.

This was discussed

with the maintenance

manager

who discussed

plans to have

a gag

designed with a locking mechanism for any future use.

Movement of Hi

h Radiation Material

Causes

Control

Room Ventilation

s

em

a ia son

etector

c ua ion

On February

22,

1990, the Unit 1 control

room ventilation system

shifted from normal

mode to pressurization

mode when radiation

monitor 1-RE-25 actuated.

1-RE-25, the

CRVS radiation monitor,

which actuates

at approximately 1.6 mr/hr, actuated

when radioactive

material

was transferred

from the Unit 1 spent fuel pool to a

shipping cask.

The radiation protection review prior to movement of the radioactive

material identified the fuel handling building radiation monitors

1-RE-58 and 1-RE-59 as potentially actuating,

but did not identify

the control

room radiation monitors, which are located outside

the

fuel handling building but are separated

only by sheet

metal walls.

The licensee

made

a four hour non-emergency

report after identifying

the event

as

an unanticipated

engineered

safety features

actuation.

The licensee will submit

a licensee

event report (LER).

The

inspector will review the

LER in a future inspection to evaluate

the

licensee's

actions.

Valve Line

U

Error Isolates

Boric Acid Transfer

Pum

1-1 Suction

On February 26, 1990, boric acid transfer

pump l-l was found running

in low speed with its suction valve closed.

It was subsequently

determined that the valve had been inadvertently isolated following

a boric acid batching operation approximately five to six hours

earlier.

At the time of this event,

the other boric acid transfer

pump (1-2) was out of service for seal repair but an alternate

boration flowpath was available

from the refueling water storage

tank through the charging

pumps.

The boric acid transfer

pumps are required in Technical

Specification

(TS) 3. 1.2.2 to support

a boration flow path from the

boric acid tanks to the reactor coolant system

(RCS).

The

TS allows

the boric acid tanks flow path to be out of service for up to 72

hours.

The boric acid transfer

pumps are also required to

recirculate

12X weight boric acid through the boron injection tank

(BIT).

Surveillance

requirements

are that this flow be verified

every seven

days.

In summary, while the loss of both boric acid

transfer

pumps resulted in a loss of BIT recirculation flow and

required entry into a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement, it had limited

safety consequences.

Additionally, although it had operated for

almost six hours with its suction valve closed, boric acid transfer

pump 1-1 was tested

on February

27 and found to be undamaged.

The suction valve was closed

due to operator error.

The licensee's

analysis of the event found the following contributing factors which

ultimately resulted in the closing of the

pump suction valve:

o

The boric acid batching job was being performed without

properly using the available procedure.

The auxiliary operator

(AO) was using the procedure

located at the auxiliary control

board and did not have

a copy for use in the field.

After

reviewing the procedure at the auxiliary control board,

the

AO

made

a note to himself of the appropriate

valve to close,

he

left the note in his pocket

when

he dressed

to enter the

surface

contaminated

area to manipulate

the valve.

The

procedure

was not followed verbatim.

The

AO elected

not to

perform certain valve lineups to isolate

normal

pump suction

while draining the batch tank.

o

The

pump suction valve was probably not properly sealed.

The

valve seal

was subsequently

found broken but might have

been

broken by the A.O.

The licensee's

analysis

recognized

other minor contributors,

such

as

poor lighting and the absence

of a valve identification label, but

the root cause

was attributed to a lack of formality in performing

the job.

-In review of the event,

operations

management

determined that the

valve lineup program,

requirements

were adequate.

However, licensee

management

determined that management's

expectations

had not been

successfully

conveyed to the operators

performing the lineups.

As corrective action, in addition to the usual

event

summary

discussed

during turnover with all operation

crews,

the operations

manager

issued

a memorandum to all operations

personnel

which

restated

the elements

of the valve lineup program

and reemphasized

the necessity

to follow the program.

The memorandum

required that

all operators

read the memorandum,

sign that it had been understood,

and return

a signed

acknowledgement

to the operations

manager.

The

licensee

stated that this approach

was taken to successfully

communicate

the importance of valve lineups with all personnel

performing lineups.

The licensee's

corrective actions

seem

appropriate.

The inspectors will continue to evaluate

the adequacy of the

licensee's

equipment lineup programs.

RHR Suction Isolation Valve 0 erabilit

On March 6, 1990, through discussion with operators

in Unit 2, the

inspector

became

aware of a jumper which had been prepared

which

would allow the Residual

Heat

Removal suction valves to be opened if

for some

reason

they were inadvertently closed.

The operators

discovery of this rather obscure fact that due to the combination of

clearances

for outage

work the suction valves could be powered

closed but not powered

open again demonstrated their indepth

knowledge

and insight into plant operations.

This unlikely

circumstance

was

due to the work clearance

on the solid state

protection

system

(SSPS)

which was consequently

depowered.

Since

the

SSPS interlocks opening of the

RHR suction valves

under certain

conditions,

the operators

were precluded

from opening the valves if

they had inadvertently shut.

The operators

had prepared

jumpers

and

'arked

up electrical

schematics

to open the valves if the need

arose.

The inspector discussed

the situation with the assistant

plant

manager

(APM) for maintenance

and suggested

that

a more appropriate

solution would have

been to revise the work procedure for the

SSPS

to add the installation of the jumper as

a procedural

requirement to

de-power

SSPS.

The

APM agreed

and stated that the procedure

would

be so revised for future outages.

An action request

was issued to

track this action.

g.

Unit 2 Fuel Handlin

Buildin Ventilation Mode Shift Due to

na

e ua

e

roce ure

h.

On March 7, 1990, while performing a design

change

on the Unit 2

spent fuel pool radiation monitor,

2 RM-58, the fuel handling

building ventilation system

(FHBVS) transferred

from normal to

iodine removal

mode.

The transfer occurred

when the "high alarm"

relay associated

with RM-58 actuated.,

It actuated

when technicians,

following steps

in the design

change

package, lifted a lead which

supplied

power to the relay.

The relay, which actuated

on loss of

power, initiated the

FHBVS mode transfer to iodine removal.

The licensee

made

a four hour non-emergency

report since the

FHBVS

transfer

was classified

as

an unanticipated

engineered

safety

feature actuation.

A nonconformance

report

(NCR DC2-90-TI-N010)

was initiated.

The

NCR stated that

a licensee

event report (LER)

was required.

The inspector will review the licensee's

actions

during review of the

LER.

Isolation of Unit 1 Feedwater

Pressure

Transmitters

On March 9, 1990, Unit 1 was at 100K power,

and Unit 2 was shut

down

and in a refueling outage.

A senior control operator

(SCO)

performing valve lineups for a work clearance

on Unit 2, erroneously

isolated three Unit 1 steam generator

pressure

transmitters.

One of

the isolated pressure

transmitter outputs drifted from approximately

800 psig to 540 psig.

This resulted in alarms in the Unit 1 control

room.

The Unit 1 control

room operator

asked the Unit 2 operator if

they had

an evolution in process

which would produce

such

an

indication and the possibility of the isolation of steam generator

pressure

transmitters

on the wrong unit was quickly suspected.

An auxiliary operator

(AO) was dispatched

to intercept the

SCO.

The

Unit 1 transmitters

were then valved back in, seven minutes after

they had been isolated.

Two of the three transmitters

had not begun

to drift low. If one other transmitter

had drifted low, a reactor

trip and safety injection could have

been experienced.

The isolation of all three

steam generator

pressure

transmitters

on

one

steam generator is not allowed by the Technical Specifications.

The licensee

made the appropriate

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

non-emergency

report

regarding the inadvertent entry into technical specification 3.0.3.

Although this was another

example of valve lineup problems,

the

inspector

was encouraged

with the self critical tone in the review

performed

by operations

management

and the individual involved.

The

inspectors will review the event following receipt of the licensee

.

event report.

j.

Unit 2 Boron In'ection Tank (BIT) Removal

Post

oned

One of the planned licensee modifications for the Unit 2 refueling

outage

was the removal of the boron injection tank BIT.

Shortly

following the

commencement

of the Unit 2 outage,

the licensee

decided not to proceed with the BIT removal.

Just prior to the

outage,

the license

amendment authorizing removal of the BIT had

been

issued

by the

NRC.

At the close of the report period the

licensee

was pursuing

a countermanding

license revision to postpone

the BIT removal.

The decision to postpone

the BIT removal

was primarily due to

questions

raised

by the engineering organization

and

a

guality

Assurance

(gA) audit regarding the adequacy of the design

change.

The identified problem area

concerned

the identification of

additional

components

whose environmental qualifications might not

be adequate

for the slightly harsher

post accident

environments that

would be experienced with the boron injection provided by the BIT.

The inspectors will follow the gA review and subsequent

licensee

actions during routine activities.

5.

Haintenance

62703)

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

certified.

a 0

Auxiliar Saltwater

S stem Pi in

Gou ed Durin

Excavation

During a review of modifications to the seawater

intake area the

inspector discovered that on September

21, 1989, during excavation

for power and telecommunication lines,

a buried portion of safety

related auxiliary saltwater piping was struck and gouged

by a

backhoe

bucket.

This event

was documented

in an "action evaluation"

or AE which was

a portion of a general

action request for

installation of the non-safety telephone

and power lines.

The

response

to the problem included

non destructive

examination of the

pipe for wall thickness

and recommendations

by the onsite project

engineering

group

(OPEG) for the recoating

and reburial of the pipe.

However,'ecause

of the "non-safety related" status of the=-original

action request,

root cause

mechanisms

were not put in place to

determine

why the pipe was inadvertently uncovered in the first

place.

Secondly,

neither

management

nor operations

personnel

were

notified to address

operability concerns of the gouged pipe.

10

Administrative Procedure

C-12, "Identification and Resolution of

Prob1ems

and Nonconformances,"

establishes

guidelines for the

initiation of Action Request

(ARs).

Action evaluations

(AEs) are

associated

with individual

ARs and are

used to request

assistance

in

the resolution of the

AR.

However,

AP C-12 does not allow AEs to be

used to document

new problems.

The procedure

requires

a new

AR to

be created

for

a new problem

so that the problem receives

appropriate

review from gC and plant supervision.

Since the

existing non-safety related

AR, for the installation of utilities to

the intake,

was

used to document the safety related

ASW pipe damage,

appropriate

reviews were not performed.

The inspector brought this finding to the attention of the system

engineer,

who was

unaware of the event

and initiated an appropriate

AR.

The inspector also discussed

the event with plant and

gC

management.

A non-conformance

report was subsequently written. It

was determined,

at that time, that based

on the non-destructive

examination

and burial instructions

contained in the AE, the

ASW

piping was operable.

Four issues

were focused

on in nonconformance

report; the

administrative

aspects

as to why a new AR was not generated,

the

technical

aspects

of the

ASW pipe operability, the lack of security

measures

while the piping was exposed,

and the work control aspects

which allowed inadvertent excavation of the

ASW pipe.

The

nonconformance

report review determined that the General

Construction

(GC) excavation permit did not identify the location of

ASW pipe.

Although drawings indicated that the

ASW pipe was five

feet underground,

GC uncovered

the pipe at 18 inches.

With respect to the administrative aspects,

the

NRC maintenance

team

of July 1988 (Inspection

Report 50-275/88-15)

issued

a Notice of

Violation for failure to implement

AP C-12 and initiate an

AR for a

new problem.

Although actions

were taken to clarify AP C-12 and

training was conducted for all required to implement the procedure,

the corrective actions

were apparently

not successful

in this case.

The failure to establish

an appropriate

AR in a timely manner is an

apparent violation (50-275/90-05-01).

The roots of this event appear similar to the Notice of Violation

issued in Inspection

Report 50-275/89-34,

where

GC personnel

erected

scaffolding over the Unit 2 vital batteries without obtaining the

required engineering

review.

These

events

seem to indicate

a lack

of sensitivity toward operating units

on the part of GC personnel.

Additionally plant management

was slow to react to this problem.

The problem was brought to the attention of plant management

on

March 1,

1990 and security issues specifically discussed.

It was

not until March 22 that the security department

was notified to

perform an evaluation for compensatory

measures.

The licensee

should address

in their response

to the Notice of

Violation; the issues

of ASW security

and operability while the line

was excavated,

the adequacy of work control, the adequacy of repairs

11

performed,

actions to increase

the sensitivity of construction

personnel

and any improvements

planned in timely response

to

identified problems.

Check Valve Ins ection

The inspectors

examined

and were satisfied with the licensee

actions

pursuant to the discovery of minor check valve internal

interferences

(rubbing).

During planned inspection of check valves

in Unit 2 during the refueling outage

the licensee

examined valve

SI-2-88188 which was

a check valve

>n the emergency

core cooling

system.

The valve and other similar Velan check valves

had their

internals

replaced in the last refueling outage

due to a disk

rotation and cocking problem.

During the current outage the

licensee

sampled

one valve for freedom'of motion and noted slight

rubbing of the end of the hinge

arm against the valve body.

The

rubbing resulted in a burnished

area estimated

to be several

mi ls

deep.

Check valve movement

was not significantly hampered

according

to engineering

personnel.

Three other similar valves were then

disassembled

and

no additional

rubbing was found.

The licensee

planned to increase

the existing chamfer

on the hinge

arm ends to eliminate the interference

in accordance

with vendor

instructions.

This problem is not considered

to be

a generic issue

because

of the minor amount of rubbing.

Significant rubbing would

have

been observed at original assembly.

Poor Cleanliness

Controls for Tem orar

S stems

On March 8,

1990 the licensee

experienced difficulty and delay in

attempting to drain

down the reactor vessel

for head

removal.

The

temporary system,

the reactor vessel

refueling level indicating

system,

RYRLIS was discovered to have

a blocked line which precluded

venting the reactor vessel

head freely.

Subsequent

disassembly

showed that

a tape cleanliness

barrier was

left installed

on a subassembly.

The cleanliness

barrier (tape)

was

not removed

when the subassembly

was installed in the system

and

became

a blockage.

The licensee

documented

the problem

on a quality evaluation to

ensure

a root cause

is determined.

There were

no safety

implications directly applicable

from this event.

The licensee

is

very interested

in successfully preventing recurrences

due to the

cost of schedule

delays.

Modification Work Observed

The inspector

observed portions of the Unit 2 modification work in

progress

on the following modifications:

installation of digital feedwater control system

installation of a revised seismic trip

12

modification to,the

AMSAC (accident mitigation system actuation

'ircuitry)

system annunciation

replacement

of the plant process

computer

P-250

Gammametrics

cable replacement

due to a 10 CFR Part 21 report

Rosemount pressure

transmitter replacement

due to'an

NRC

bulletin

The inspector also observed solid state protection system work on

suspect electrical

connections

which had to be checked for tightness

in accordance

with a vendor technical bulletin (Westinghouse

technical bulletin 89-06).

One violation and

no deviations

were identified.

6.

Sur vei 1 lance

(61726)

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance'with

TS requirements

and plant

procedures.

The inspectors verified that test equipment

was ca'librated,

and acceptance

criteria were met or appropriately dispositioned.

a.

Dail

Heat Balance

The inspector

reviewed the performance of a daily heat balance

on

Unit 2 prior to the refueling outage.

The heat balance

was

performed in accordance

with surveillance test procedure

STP

R-2B

without the use of the plant process

computer which had been taken

'ut of service for replacement.

The inspector.

reviewed the data

and the procedure

and found the

licensee's

actions acceptable.

No violations or deviations

were identified.

7.

Licensee

Event

Re ort Follow-u

92700

a.

Status of LERs

The

LERs identified below were closed out after review and follow-up

inspections

were performed

by the inspectors

to verify licensee

, corrective actions:

Unit 1:-'8-29 (Revision 1), 88-30 (Revision 1), 88-18, 88-34,

89-07, 89-08, 89-09, 89-10, 89-11,

89-17

Unit 2:

88-16 (Revision 1), 89-06, 89-08, 89-09,

89-11

No violations or deviations

were identified.

13

8.

0 en Item Follow-u

(92703

92702)

a.

(Closed) Unit 1 Enforcement

Items 50/275/89-23-01'2

and

03

The inspector

reviewed the licensee's

January

2, 1990,

response

to

three violations contained in Inspection

Report 50-275/89-23

(dated

December

1, 1990).

The cause

and corrective actions described

for

the violations concerninq the application of the equality Assurance

(gA) program to boric acsd heat tracing (50-275/89-23-03)

and the

control of the hydrogen

purge containment isolation valves

(50-275/89-23-02)

were found to be acceptable.

The items are

considered

closed.

With respect

to the overtime violation, the inspector

reviewed the

January

2, 1990, letter,

LER 50-275/89-17,

and

a February 21,

1990,

supplemental

response

provided in response

to an

NRC information

-request.

The February 21, 1990,

response clarified the root cause

to include a."...programmatic

breakdown

and

a lack of procedural

guidance

including plant management

oversite."

The letter also

discussed

in greater detail the scope of overtime violations and to

whom the licensee will apply the overtime restrictions

in the

future.

Additionally, the licensee

committed to have equality

Control monitor the effectiveness

of corrective action

implementation during the Unit 2 refueling outage.

The inspector

found these

actions

acceptable

(Enforcement

Item 50-275/89-23-01,

.

and Licensee

Event Report 50-275/89-17,

closed).

10.

Exit

30703

On March 23,

1990,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.