ML16341E547

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Insp Repts 50-275/88-01 & 50-323/88-01 on 880119-22.No Violations Noted.Major Areas Inspected:Previous Insp Findings,Solid Wastes,Licensee Repts & Licensee Identified Problems,Surveys & Monitoring & Facility Tours
ML16341E547
Person / Time
Site: Diablo Canyon  
Issue date: 02/12/1988
From: Hooker C, Yuhas G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E548 List:
References
50-275-88-01, 50-275-88-1, 50-323-88-01, 50-323-88-1, NUDOCS 8802290385
Download: ML16341E547 (16)


See also: IR 05000275/1988001

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

Nos.

50-275/88-01

and 50-323/88-01

Docket Nos.

50-275

and 50-323

License

Nos.

DPR-80 and

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California

94106

Facility Name:

Diablo Canyon Units

1 and

2

Inspection at:

San Luis Obispo County, California

Inspection

Conducted:

January

19-22,

1988

Inspector:

Approved by:

~Summar:

C.

A. Hooker, Radiation Specialist

p g)

G.

P.

Yu as, Chief

Faci li '

Radiological Protection Section

Date Signed

a

)

~

Date Signed

Ins ection

on Januar

19-22

1988

Re ort Nos.

50-275/88-01

and 50-323/88-01

findings, solid wastes,

licensee

reports

and licensee identified problems,

surveys

and monitoring,

and facility tours.

Inspection procedures

addressed

included 30703,

84722,

92700,

92701 and 83726.

Results:

Of the areas

inspected,

no violations or deviations

were identified.

88P2290385

88oooop75

PDR

+DOCK O~

@DR

'

DETAILS

1.

Persons

Contacted

a.

Pacific

Gas

and Electric

Com an

PG&E

Personnel

"J.

D. Townsend,

Plant Manager

"J.

M. Gisclon, Assistant Plant Manager

  • D. B.

Miklush, Acting Plant Superintendent,

Assistant Plant Manager

"W.

B.

McLane, Assistant Plant Manager,

Technical

Support

"K. Doss,

Senior Nuclear Generation

Engineer

  • J.

V. Boots,

Manager,

Chemistry

and Radiation Protection

(C&RP)

~C.

L. Eldridge,

Manager,

equality Control

  • R.

P.

Powers,

Seni,or

C&RP Engineer,

Supervisor

Radiation Protection

(RP)

"J.

E. Gardner,

Senior.C&RP Engineer,

Supervisor

Chemistry

  • R.

M. Taylor, Supervisor, guality Assurance

(gA)

C.

C. Miller, C&RP Engineer

"T.

L. Grebel, Supervisor,

Regulatory

Compliance

J.

A. Hays,

General

Foreman,

RP

~L. T. Moretti, Foreman,

RP

b.

NRC Personnel

"J.

L. Crews, Senior Reactor Engineer,

Region

V

"A. D. Johnson,

Enforcement Officer, Region

V

  • M. L. Padovan,

Acting Senior Resident

Inspector

  • K. E. Johnston,

Resident

Inspector

Denotes

those present at the exit interview on January

22,

1988.

In addition to the individuals identified above,

the inspector

met and

held discussions

with other members of the licensee's

and contractor's

staffs.

2.

Licensee Action on Previous

Ins ection Findin

s

92701

Closed

Followu

50-323/87-21-04

Inspection

Report

Nos.

50-323/87-21,

50-323/87-30

and 50-323/87-40 describe

previous inspection

efforts regarding the licensee

s guality Hotline (gH) investigation,

No.

gCSR-87-005,

involving radiation protection concerns of an individual

working in the radiological controlled area

(RCA) of Unit 2 during the

refueling outage.

Inspection

Report

No. 50-323/87-40

documented

the

review of the

C&RP Department's

investigation

and response

to gH

regarding this matter.

During this inspection,

the on-site

gH representative

informed the

inspector that the concerned

individual had reviewed

C&RP's reply and

had

no further concerns

or questions

regarding radiological controls that

were at issue.

The inspector

had

no further questions

regarding this

matter.

C 1 osed

Fo1 1 owu

50-323/87-40-01):

Inspection

Report No. 50-323/87-40

documented

the inspector's

review of a draft extremity exposure

evaluation of an individual who had

a radioactive fuel particle on his

sock that was not identified on an initial survey.

During this

inspection the inspector

reviewed the licensee's

final investigation

and

dose evaluation report,

Evaluation

No.

0151.

Based

on this review the

inspector

noted that the licensee's

extremity dose estimation of 1.642

rem appeared

conservative

and appropriate.

The results of the evaluation

emphasizing

the lessons

learned

were forwarded to the Training Department

for incorporation into the licensee's

radioactive particle training

program.

The inspector also observed this matter being discussed

during

a

RP radioactive particle requalification training class

on January

21,

1988.

The inspector

had

no further questions

regarding this matter.

3.

Radioactive Solid Wastes

84722 - Minimum

a.

gA Audits

gA Audit Report

No.

87248T,

dated

December

1, 1987,

was examined.

The audit was conducted

November 2-10,

1987, to verify that Diablo

Canyon

Power Plant

(DCPP)

had adequately

implemented the applicable

requirements

of the

Code of Federal

Regulations,

gA Policy,

Technical Specifications

(TS), and procedures

for the receipt,

control

and accountability,

disposal

and transportation of licensed

radioactive material.

The audit,

among other items,

included:

interviews with cognizant

management

personnel,

reviews of numerous

procedures

and documents

related to the areas

audited.

The audit identified one discrepancy that resulted in the issuance

of one Audit Finding Report (AFR), No.87-269, that required

corrective action.

The

AFR was issued to the Materials Department

for failure to notify the

C8RP Department

upon receipt of an area

monitoring, instrument that contained

a limited quantity of

radioactive material.

The

C8RP Department

had identified this item

on October

26, 1987, during a routine inventory of material stored

at the warehouse.

The package

was located in the appropriate

storage

area

and was not considered

a safety

and health problem.

Based

on a discussion with the Materials Superintendent,

the

inspector confirmed that corrective actions

appeared

appropriate.

With the exception of the one

AFR issued,

the gA auditors

concluded

that

DCPP

had been

implementing the requirements

for receipt,

control

and accountability,

disposal

and transportation of

radioactive material.

The inspector,

being familiar with the

named

gA audit team members,

determined that the audit was conducted

by qual Hied personnel.

b.

~Chan

es

The inspector

was. informed by the responsible

C8RP Engineer that

DCPP was in the process

of changing vendors for radioactive waste

solidification encapsulation

and dewatering operations.

The final

gA acceptance

and approval of the

new contract vendor was nearly

complete.

Since the last inspection of this area,

the licensee

had moved their

clean trash sorting and surveying operation

from the 115 ft. level

of the Unit 2 Fuel Handling Building to Bay No.

6 of the Waste

.

Storage Facility.

During a tour of the clean waste sorting area

on

January

20,

1988, the inspector

made the following observations.

While waste sorting was in progress, it was noted that the air

flow into the small sorting

hood appeared

nonexistent

as

indicated

by using

a very thin strip of masslin cloth.

Although the

room was equipped with an existing ventilation

exhaust

system,

the licensee

was using

a small portable exhaust

blower equipped with a shop type bag filter (non

HEPA) that

exhausted

into the

room area.

Bags of supposedly

clean waste to be sorted

and surveyed

were

overflowing (three to four feet) into the designated

zone where

marked

bags of surveyed trash were being stored.

Prior to sorting,

bags of chemical

and reagent bottles,

and

bags containing oily rags and/or rags with absorbed

paint

solvents

(noted

by odor) were not typically marked

as hazardous

waste.

Surveys of waste being sorted

appeared

to be adequate

for the

detection of any radioactive material that could be present.

The inspector

was also informed by waste sorters that only

infrequently is radioactive material

found (typically <500 net

cpm with a thin window hand held frisker) in the clean waste.

The inspector

noted that detailed records for each

b'ag sorted

were maintained at the work location.

In review of recent

sorted clean trash records

and survey data,

the inspector

observed

no problems that would indicate any lack of control of

the licensee's

inplant segregation

of radioactive

contaminated

and clean waste.

Recent daily air sample data from the waste sorting operations

indicated nothing other than natural occurring activity.

The observations

of poor air flow, exhaust

system setup,

unmarked

bags that appeared

to contain hazardous

waste,

and general

housekeeping

practices

in this area

were discussed

with the

RP

supervisory staff.

The

RP Supervisor

and other members of his staff

visited the area

and acknowledged

the inspector's

observations.

The

RP Supervisor halted the clean waste sorting operation,

and informed

the inspector that clean waste sorting would not restart until the

operation

was brought

up to normal standards.

This matter was also

discussed

at the exit meeting

on January

22, 1988.

The Plant

Manager acknowledged

the inspector's

observations

and

made assurance

that the matter

would be handled expeditiously.

~

~

~

No violations or deviations

were identified.

4.

Licensee

Event

Re orts

LERs

and Licensee Identified Problems

92700

~and 83726

The following LERS and problems

were reviewed on-site:

a.

LERS

LER No. 1-87-027-00,

Radiation 'Monitor Alarm and Hot Particle

Caused

Fuel Handlin

Buildin Ventilation

S stem

Chan

e

Actuation

of En ineered Safet

Feature

due to Failure to Perform Surve

,

dated January

19, 1988.

This event occurred

on December

20, 1987,

in the Unit 1 Fuel Handling Building during reracking

when

a hot

particle (Co-60) was apparently

removed from the Spent

Fuel Pool,

while a diver tender

was taking slack out of an air grinder's

hose

that

had tangled with the divers air hose.

The hot particle

exhibited dose rates sufficient to cause

the

FHB radiation. monitor

(RE-58) to alarm and cause

automatic initiation of the ventilation

system into the iodine removal

mode.

Based

on the potential

radiological safety significance,

the licensee

immediately initiated

an investigation of this event in accordance

with Nuclear Plant

/

The licensee's

Event Investigation Report

No. 87-02,

Hot Particle

Event of December

20, 1987,

was also examined during this

inspection.

Based

on review of the licensee

s investigation,

discussions

with

the contract divers

and cognizant licensee

representatives,

and

observations

during several

tours of the Unit 1

FHB during diving

operations,

the inspector

observed that:

The licensee

had appropriately identified the hot particle to

be 45.5

mi llicuries of Co-60.

The licensee

had also

conservatively calculated that

had the diver tender

come in

contact (0.5 seconds)

with the hot particle with his hands,

he

could have received

an extremity dose of 895 mrem and

5 mrem to

other portions of the body.

The licensee's

approach

and

methodology for dose calculations

and estimates

appeared

reasonable.

10 CFR 20. 101 limits the extremity dose to 18.75 rem/quarter.

Root causes

of this event,

as determined

by the licensee,

was

a

lack of:

1) adequate

procedure policy; 2) communication

between

the

CHIRP technician staff and management

concerning the

accelerated

weekend work activities and reduced staff; and 3)

recognition of work activities in the pool which could provide

a mechanism for production and transport of hot particles to

the surface of the pool.

Corrective actions

appeared

appropriate

and

had been effectively implemented to preclude

recurrence.

~

'

LER No. 1-87-026-00,

Mode 1

Power

0 eration

Entr

While in Action

Statement

TS 3.6.2.2. a In Violation of TS 3.0.4

due to Lack of

Procedural

Guidance,

dated January

19,

1988.

This event occurred

on

December

17, 1987, at 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br />

and involved the failure to

maintain the

NaOH concentration

in the Spray Additive Tank at the

TS

required concentration

of 30-32K prior to entering

Mode 1.

The

concentration

had been adjusted to 29.5X and the responsible shift

chemistry

foreman

had incorrectly rounded the analysis

data to 30K,

which was reported to the shift foreman.

The licensee's

analysis

for determining the

NaOH concentration

has

an accuracy of +0.2X.

On

December

17, 1987, at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />,

the Senior

C8RP Engineer

(Chemistry Supervisor)

observed

the error when reviewing the

previous shift work activities.

The Shift Foreman

was immediately

notified.

Draft LER No. 01-88-01,

Failure to Per form Technical

S ecification

3. 3. 3. 10. b

Re uired Plant Vent Air Sam ler Flow Estimate

Due to

Personnel

Error.

This event occurred

on January

1, 1988, with Unit

1 in Mode 1,

and involved the failure of a shift chemistry

technician to review the shift turnover log sheet per Administrative

Procedure

A-10151, Relievin

the Watch.

The applicable

T.S. Action

Statement

(51) requiring

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

sample flow rate estimate for the

plant vent monitor (RE-24)

had been

noted in the shift turnover

log

on the previous shift.

According to cognizant licensee

representatives,

the

LER would be issued within the

30 day time

limit requirement.

The above

LERS were reviewed for event description,

root cause,

corrective actions,

generic applicability and report timeliness.

No violations or deviations

were identified.

Action Re uest

No.

A0097157

During the inspection,

on January

20, 1988, at about

1816 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.90988e-4 months <br />,

while initiating a radioactive liquid discharge,

from the

No.

2

Laundry Holdup Storage

Tank, the liquid radwaste

monitor RE-18

alarmed

and automatically terminated the discharge.

This was the

first liquid radwaste

discharge

following a spent resin transfer

earlier in the day.

The Auxiliary Control Operator notified a a

Chemistry Technician that RE-18 had tripped, flushed the system

lines

and re-initiated the discharge.

This was in violation of

procedures

OP G-1: 11, Li uid Radwaste

S stem - Processin

and

Dischar

e of Li uid Radwaste,

and

CAP A-5, Li uid Radwaste

Dischar

e

Mana ement,

which require termination of the discharge

permit so

that an evaluation

can

be made

and resampling of the source of

discharge.

After about

one hour into the discharge,

a

CHIRP Foreman

observed

a note related to the RE-18 trip, immediately investigated

the matter,

had the discharge

terminated,

and calculated

the

potential

release

rate which was about 0. 11K of TS limit.

The

licensee

informed the inspector of this event

on January

21, 1988,

at about

0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br />.-

The radioactive resin transfer

system

and the liquid radwaste

system

share

some

common lines.

The licensee

has

had previous problems

as

'

result of this system sharing

and

RE-18 alarms.

Inspection

Report

No. 50-275/87-30 describes

these

problems

and the need for

procedural

changes

to reduce

RE-18 alarms,

which was also noted

as

a

followup item (50-275/87-30-04).

The inspector discussed

the licensee's

recurring problems associated

with the shared

systems

and

RE-18 alarms at the exit meeting

on

January

22, 1988.

The inspector. also encouraged

the licensee to put

extra effort on resolving the problems

due to the shared

systems.

The inspector's

observations

were acknowledged

by the Plant Manager.

The licensee's

final investigation of this event will be examined in

a subsequent

inspection

(50-275/88-01-01,

Open).

5.

Surve

s and Monitorin

. 83726

The inspector

reviewed two licensee

personnel

exposure

evaluation reports

due to particle contaminations

to determine

the licensee's

compliance

with 10 CFR Part 20 and licensee

procedures.

Radiolo ical Occurrence

Re or t No. 87-15848,

dated

December

20,

1987.

This report and associated

exposure

evaluation involved an individual who

had

a Co-60 particle of about 0.073

uCi on his chin.

This individual had

been performing decontamination activities

on a spent fuel rack removed

from the Unit 1 SFP.

The licensee

evaluated

the event

and assigned

a

dose of 635

mrem to the skin of the whole body using the total time this

individual had been in the radiologically controlled area.

10 CFR 20. 101

limits the whole body skin dose to 7.5 rem/quarter.

Extremit

Ex osure Calculation,

dated January

7, 1988.

This event

involved a. suspected

radioactive particle when

a diver performed

an

underwater

survey of himself during Unit 1 rerack operations.

While the

diver was vacuuming the floor area,

previously occupied

by a fuel rack,

the under water dose rate meter

showed fluctuations

from a 5 mrem/hr

background to 20 mrem/hr.

An underwater

survey,

by the diver, indicated

a reading of 54 mrem/hr on his left forearm.

The dive was terminated

and

the diver surfaced.

The surface

survey did not detect

any readings

above

the normal

background (0.2-0.5 mrem/hr) readings.

Based

on the plants

good fuel history and analysis of contaminates

that had been

encountered

during rerack operations,

the licensee

assumed that a Co-60 particle was

the cause for the reading

on the divers forearm.

The licensee

evaluated

and assigned

an extremity dose of 404 mrem to the individual.

In review of the above events

and through discussions

with licensee

representatives,

the inspector

observed that the licensee's

evaluations

appeared

to be conservative,

methodology for calculations

and doses

assigned

appeared

reasonable.

No violations or deviations identified.

~

'

'

6.

Fat il it

Tours

83726

The inspector

toured various areas of the auxiliary, fuel handling,

waste

storage

and turbine buildings of Units 1 and

2 on several

occasions.

The

inspector

made independent

radiation measurements

using an

NRC RO-2

portable

ion chamber,

S/N 2694,

due for calibration February 5, 1988.

In addition to observations

noted in the above paragraphs,

the inspector

noted that radiation areas

and high radiation areas

were posted

as

required

by 10 CFR Part 20.

Licensee

access

and posting controls for

high radiation areas

were observed to be consistent with TS, Section

6. 12,

and licensee's

procedures.

No violations or deviations

were identified.

7.

Exit Interview

The inspector

met with the licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on January

22,

1988.

The scope

and findings of the'inspection

were summarized.

The inspector

informed the licensee

representatives

that

no violations or

deviations

were identified.

The inspector's

observations

concerning

areas

of improvement discussed

in

this report were acknowledged

by the licensee.