ML16341E465

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Insp Repts 50-275/87-39 & 50-323/87-40 on 871109-13.No Violations or Deviations Noted.Major Areas Inspected: Previous Insp Findings,External & Internal Exposure Control, Alara,Review of Licensee Audits & Repts & Facility Tours
ML16341E465
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 12/02/1987
From: Hooker C, Yuhas G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E466 List:
References
50-275-87-39, 50-323-87-40, NUDOCS 8712210270
Download: ML16341E465 (16)


See also: IR 05000275/1987039

Text

'

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

Nos.

50-275/87-39

and 50-323/87-40

Docket Nos.

50-275 and 50-323

License

Nos.

DPR-80

and

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street

Room 1451

San Francisco,

California

94106

Facility Name:

Diablo Canyon Units

1 and

2

Inspection at:

San Luis Obispo County, California

Inspection

Conducted:

November 9-13,

1987

Inspector:

C.

A.

oo er,

Radia ion Specialist

Da

e Signed

~Summar:

~

P.

uh

Facili ie

s, Chief

Radiological Protection Section

Da

e Signed

Ins ection

on November 9-13

1987

Re ort Nos.

50-275/87-39

and 50-323/87-40

findings, external

and internal

exposure control;

ALARA; review of licensee

audits

and reports;

and facility tours.

Inspection

procedures

addressed

included 30703,

83724,

83725,

83728,

92701,

92702,

92700

and 90713.

Results:

Of the areas

inspected,

no violations or deviations

were identified.

87>~>i 0270 871203

PDR

ADOCK 05000275

8

PDR

DETAILS

1.

Persons

Contacted

a.

Pacific Gas

and Electric

Com an

PG8E

Personnel

"J.

D. Townsend,

Acting Plant Manager

  • W. B.

McLane, Acting Assistant Plant Manager,

Technical

Support

"J.

V. Boots,

Manager,

Chemistry

and Radiation Protection

(CHIRP)

"R.

P.

Powers,

Senior

CHIRP Engineer,

Supervisor,

Radiation Protection

(RP)

"T.

L. Grebel, Supervisor,

Regulatory Compliance

  • J. A. Hays,

General

Foreman,

RP

"S.

Fahey-Benson,

Nuclear Generation

Engineer

L. T. Moretti, Foreman,

RP

R. J. Harris, Supervisor, guality Assurance

(gA), On-Site Auditing

Group

R.

M. McVicker, Lead Specialist, guality Control

(gC)

T.

L. Irving,

CBRP Engineer

D.

E. Jones,

Senior Health Physicist,

Department of Engineering

Research

(DER)

D. Bell, gC Supervisor,

Nuclear Engineering

and Construction

Services/General

Construction

b.

NRC Contacts

"P.

P. Narbut, Senior Resident

Inspector

M.

L. Padovan,

Resident

Inspector

K.

E. Johnston,

Resident

Inspector

Denotes

those present at the exit interview on November 13,

1987.

In addition to the individuals identified above,

the inspector met and

held discussions

with.other members of the licensee's

and contractor's

staffs.

2.

Licensee Action on Previous

Ins ection Findin

s

Closed

Violation

50-275/87-30-01

and 50-323/87-30-01:

This violation

involved the

RP Department's

failure to follow procedures

on the use of

Temporary Instructions (TIs).

Based

on review of the

RP Departments

TI

binder and revised procedure

RCP D-600,

Personnel

Decontamination

and

Evaluation,

and discussions

with cogniiant licensee

representatives,

the

inspector

determined that effective corrective actions

had been

implemented to prevent recurrence

as stated in PG8E's timely letter dated

September

28,

1987.

The inspector

had

no further questions

regarding

this matter.

Closed

Followu

50-275/87-30-02

and 50-323/87-30-02

This item

related to the review of the resolution

between

gC and

RP on the

requirements

for issuance

of Action Requests

(ARs) and Nonconformance

Reports

(NCRs) for licensee identified problems.

Based

on the review of

'

revised procedure

RCP D-250,

Re ortin

of Radiolo ical Occurrences,

and

a

letter,

dated

September

16,

1987,

from C.

L. Eldridge to J.

V. Boots, the

inspector

determined that the licensee

had effectively resolved this

matter.

'I

Closed)

Followu

(50-275/87-30-03

and 50-323/87-30-03):

This item

involved the

C&RP Department's

use

and control of their Required

Reading

Book regarding

acknowledgements

by personnel

who had read specific

administrative

and

RP procedures.

During this inspection the inspector

observed that the

C&RP department

had effectively implemented

new

administrative controls to ensure that acknowledgements

were

appropriately

documented for procedures

read

by C&RP personnel.

The

inspector

had

no further questions

regarding this matter.

Closed

Followu

(50-275/87-30-05

This item involved the licensee's

clarification of requirements

for determination of the

need for a

Notification of Unusual

Event

(NUE) based

on process

monitor alarms.

Based

on review of revised procedure

EPG-l,

Accident Classification

and

Emer enc

Classification,

the inspector

determined that the licensee

had adequately clarified the classification

of NUEs based

on process

monitor alarms.

The inspector

had

no further

questions

regarding this matter.

0 en) Followu

(50-323/87-21-04

Inspection

Report Nos.

50-323/87-21

and 50-323/87-30

documented

previous inspection efforts regarding the

licensee's

Quality Hotline (QH) investigation,

No.

QCSR-87-005,

involving

radiation protection concerns of an individual working in the

radiological controlled area

(RCA) of Unit 2 during the refueling outage.

Based

on discussions

with cognizant licensee

representatives

and review

of the

C&RP Department's

response,

dated October 26, 1987, to

QCSR

87-005, it appeared

that the licensee

had adequately

addressed

the

individual's radiation protection concerns.

The

C&RP Department

calculated that the individual could have received

an additional 4.9 mrem

to the head that would not have

been indicated

by the monitoring devices

that were worn on the chest.

This item will*remain open until the

licensee's

QH has closed the matter.

Closed

Followu

50-323/87-21-02

The inspector

observed air flowing

from the licensee's

radioactive

laundry cleaning facility to the outside

yard area.

During this inspection,

the inspector

observed that

administrative controls

had been

implemented to keep specific doors

closed to ensure that the laundry facility would be maintained at a

negative pressure relative to the outside environment.

The licensee

was

also in the process

of evaluating

changes

in the ventilation system to

improve system performance.

The inspector

had

no further questions

regarding this matter.

Radiolo ical Controls

This part of the inspection

covered the areas

of:

external

exposure

control; internal

exposure control;

and

ALARA.

The inspector

reviewed

QA

audits

and

QC surveillance reports,

procedures,

records of radiation

and

contamination

surveys,

select Special

Work Permits

(SWPs)

and associated

surveys,

personnel

exposure files, and

a post Unit-2 refueling outage

ALARA report.

The inspector also observed

workers in the

RCAs, held

discussions

with licensee

representatives,

and conducted facility tours

to determine

the licensee's

compliance with 10 CFR Part 20, Technical

Specifications

(TSs),

licensee

procedures

and recommendations

as outlined

in various industry standards.

Inspection

Report

Nos.

50-275/87-21

and 50-323/87-21 also

documented

previous inspection efforts in these

areas.

a.

Audits and

Sur vei llances

QA Audit Report

No.

87161T was reviewed.

The audit was conducted

June 15-July -ll, 1987, to verify that Diablo Canyon

Power Plant

(DCPP), Nuclear Operations

Support

(NOS),

and Department of

Engineering

Research

(DER) had effectively implemented

the

requirements

of the

Code of Federal

Regulations,

DCPP TSs,

QA

Policy,

and departmental

procedures

established

for radiation

protection personnel

monitoring and dosimetry processing

programs.

The audit report documented

an extensive list of records

reviewed

and the

number of samples

examined.

The inspector

determined that

the auditors

were appropriately qualified for the audit.

No

deficiencies

were identified that resulted in Audit Finding Reports

(AFRs) being issued to

DCPP or NOS; however, four AFRs were issued

to

DER documenting minor program deviations.

The inspector

noted

that the identified deviations

were administrative in nature

and did

not represent

a significant safety problem.

Based

on an interview

with the on-site

DER representatives,

the inspector

confirmed that

corrective actions

appeared

to be appropriate.

The following QC Surveillance

Reports

were reviewed:

QCS

87-0270,

Termination of Com leted

SMP Packa

es,

performed

June 4,

1987.

QCS 87-0234,

Personnel

Airborne Ex osure Trackin

, performed

June 6-11,

1987.

QCS 87-0335,

Radiolo ical Controls for Entr

Into Areas

Havin

a Hi

h Potential for Radiation

QCS 87-0366,

Radiolo ical Controls for Unit 2 Turbine

Buildin

Buttress,

performed August 28,

1987.

QCS 87-0385,

Radiolo ical Controls Associated with Leak

Re airs of RCS-l-PCV-455B, performed

September

29,

1987.

Based

on review of the above

QC Surveillance

Reports,

the inspector

noted that

no deficiencies

were identified in report nos.

QCS

87-0270,

QCS 87-0335,

QCS 87-0366,

and

QCS 87-0385.

Report

No.

QCS

87-0234 identified deficiencies

in administrative controls that

resulted in the issuance

of four ARs that required corrective

action.

The inspector 'verified that corrective actions

appeared

to

be appropriate.

No violations or deviations

were identified.

b.

External

Ex osure Control

The inspector

reviewed the licensee's

current quarter to date

radiation exposure

reports

and selected

personnel

exposure files of

workers involved with the Unit 2 refueling outage.

The inspector

noted that

Form NRC-4s,

NRC-5s

and termination letters

were

completed

and retained

as appropriate.

Updated

Form NRC-4s were

researched

prior to'xceeding

the 10'CFR 20. 101(a) limits and

no one

had exceeded

10 CFR 20.101(b) limits.

The inspector

reviewed the tollowing procedures,

documents

and

records:

Procedures

NPAP C-200

General

Re uirements for Radiation Protection

~Pro

rama

RCS-1

RCP G-100

RCP D-220

External

Ex osure Control

Radiation

Work Permits

Entr

Into Plant Areas Which Have

a Hi h

Potential for Radiation Overex osure

RCP D-600

Personnel

Decontamination

Evaluation

Documents

Records

and

Re orts

Letter from R.

P.

Powers to J

~

V. Boots

and J.

A. Sexton,

Control of 'Hot Particles't

DCPP

Interim Re ort, dated

October 26,

1987.

Radiological

Occurance

Reports

(RORs) from June

2 through

November 10,

1987

'ersonnel

Contmaination

Reports

from July 2, 1987, through

November 10,

1987.

SWP 87-00677,

Weld

Re air Crack Below Valve CVCS-1-8495,

dated

November

10,

1987.

SWP 87-00675,

Char in

Pum

2-1

Mechanical

Seal

Re lacement

and

November 9, 1987.

Maintenance

Includin

All Su

ort Work, dated

Licensee

Event Report

(LER) No. 1-87-015-00,

Failure to Meet

the

Re uirements of Technical

S ecification 6. 12

Hi h Radiation

Area

When an Area Was Left Unlocked,

dated October 26, 1987,

discussed

in paragraph

4.b. of this report.

. Based

on the reviews,

observations

and interviews with workers in

the

RCAs, the inspector

determined that the licensee

was effectively

implementing their external

exposure control program.

During the inspection,

on November ll, 1987, at about 3:45 p.m.,

a

C&RP Technician, while surveying contaminated

personal

clothing that

had been

saved for decontamination

and/or disposal,

identified a

radioactiv'e particle

on the toe portion of a sock that indicated

a

count rate of 37,000

cpm with a hand held frisker.

The initial

survey of the sock

on October 30,

1987, identified only a 150

cpm

hot spot with a hand-held frisker.

The sock

had been worn by a

C&RP

technician working in the licensee's

waste sorting enclosure.

Since

the 37,000

cpm particle

had not been observed

during the initial

survey,

the licensee

immediately initiated an investigation to

identify the isotopic mixture of particle, evaluate

the potential

dose to the

C&RP Technician,

and determine

why the higher reading

had not been identified on October 30,

1987.

The licensee

informed

the inspector. of this incident on November 12,

1987, at about 9:00

a.m.

The licensee identified the particle

as being

an irradiated

fuel fragment of about 0.079 pCi.

The licensee's

draft exposure

evaluation estimated

an extremity dose of about 1.6

rem based

on

their initial investigative data.

The licensee's

final

investigation report of this matter will be examined during

a

subsequent

inspection

(50-323/87-40-01,

Open).

No violations or deviations

were identified.

Internal

Ex osure Control

The inspector

reviewed the licensee's

current exposure

report that

provided seven

day and quarter

to date

MPC-hours for radiation

workers,

selected

whole body counting records,

and

MPC work and log

sheets

from selected

SWP packages.

Based

on these

reviews

and

discussions

with licensee

representatives,

there

was

no indication

that any individual exceeded

the 40-hour control measure

requiring

an evaluation pursuant to 10 CFR 20. 103(b)(2).

During the review of air sample results

and

MPC work sheets

from

select

SWP Packages,

the inspector

noted that there were several

instances

where errors were

made when the licensee

performed

hand

calculations to determine air sample results

and

MPC fractions.

The

errors did not represent

a significant safety problem due to the low

concentrations

involved; however,

they did indicate

a lack of

attention to detail.

The inspector discussed

this matter with the

C&RP management staff who acknowledged

the inspectors

observations.

During facility tours the inspector

observed respiratory

equipment

being properly used, air sampling being performed

as required

and

areas

posted pursuant to 10 CFR 20.203(d)(2).

No violations or deviations

were identified.

'

'

d.

ALARA

The inspector

reviewed the licensee's

Unit 2 first refueling outage

ALARA report.

This 22 page report was very detailed

and compared

the difference in the person-rem

accumulated,

with supporting data

for each major refueling outage activity of Unit 1 and Unit 2.

The

report also discussed

the benefits of reactor coolant system forced

oxygenation.

The report outlined problems encountered,

lessons

learned,

and reasons

that exposures

were reduced or additional

exposure

incurred.

The report

summary

showed

a comparison of

exposures

of various Unit 2 outage activities with national

outage

exposures

for the major repetitive high dose jobs at Pressurized

Water Reactors.

The licensee

determined that Unit 2 exposures

were

only about

43X of the national

average.

The licensee

had not confirmed their ALARA goals for 1988;

however,

a tentative

goal of 620 person-rem

was being considered.

In 1988

the licensee will experience

a refueling outage for Unit 1 and Unit

2, completion of .the Unit 1 spent fuel pool rerack operation,

commencing

about

November 16, 1987,

and the complete

spent fuel pool

rerack operation for Unit 2.

The licensee's

ALARA goal

achievements

were discussed

in Report Nos.

50-275/87-21

and 50-323/87-21.

No violations or devi ati ons were identi fied.

4.

Licensee

Re orts

Semiannual

Radioactive

Release

Re ort

The licensee's

Semiannual

Radioactive

Release

Report for the period

of January

1, 1987,

through June

30, 1987,

was reviewed in-office.

This timely report was issued

as required

by 10 CFR 50.36a(a)(2)

and

TS 6.9. 1.6,

and included

a summary of the quantities of radioactive

liquid and gaseous

effluents

and solid waste released

as outlined in

NRC Regulatory Guide 1.21.

The report also included the off-site

dose

due to releases

of radioactive liquids and gaseous

effluents.

Administrative procedure

changes

to the Process

Control

Program,

Environmental Monitoring Procedure

(A-7), and the Offsite Dose

Calculation Procedure

(CAP A-8) were also discussed

in the report.

No errors or anomalies

were identified (50-275/87-SA-02

and

50-323/87-SA-02,

closed).

b.

LER

LER 87-015-00,

Failure to Meet the

Re uirements of Technical

S ecification 6. 12

Hi

h Radiation Area

When an Area was Left

Unlocked was reviewed in-office and on-site during the inspection.

The inspector verified that the reporting requirements

were met,

causes

were identified, corrective actions

appeared

appropriate

and

had been

implemented to prevent recurrence.

The inspector also

determined that no individual had received

any additional or unsual

radiation exposure.

Based

on the guidance provided in 10 CFR 2,

Appendix C, Part V.A., a Notice of Violation will not be issued.

The inspector

had

no further questions

concerning this matter.

c.

NCR

NCR No.

DC1-87-TC-N114 was reviewed during the on-site inspection.,

This

NCR involved an unplanned,

monitored release

of gaseous

radwaste

from Gas

Decay Tank No. 1-3 on October

22,

1987.

The

licensee

determined that the cause of the release

was

due to a

valving misalignment following minor maintenance

on the Boric Acid

Evaporator.

The licensee

determined that

a total of 0.715 curie of

gaseous activity was released

via the plant vent.

The release

was

not significant and'epresented

about

0. 104K of the

TS release

rate

limit.

Based

on review of the licensee's

evaluation

and discussion

with cognizant plant staff, the inspector

had

no further questions

regarding radiologi.cal

concerns.

The inspector toured various

areas

of the auxiliary and fuel handling

buildings of Unit 1 and Unit 2, the waste storage building and the

laundry facility.

The inspector

made independent

measurements

using

an

NRC RO-2 portable ion chamber,

S/N 2691,

due for calibration

on January

8, 1988.

In addition to the observations

discussed

in other sections

of this

report, the inspector

observed that all radiation areas

and high

radiation areas

were posted

as required

by 10 CFR Part 20,

and access

controls were consistent with TS 6. l2 requirements

and licensee

procedures.

No violations or deviations

were identified.

6.

Exit Interview

The inspector

met with the licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on November 13,

1987.

The scope

and findings of the inspection

were summarized.

The inspector

informed the licensee

representatives

that

no apparent

violations or deviations

were identified.