ML16341E346

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Insp Repts 50-275/87-23 & 50-323/87-22 on 870531-0627. Major Areas Inspected:Operations,Plant Maint & Surveillance Activities,Followup of Onsite Events,Open Items & LERs
ML16341E346
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 07/08/1987
From: Johnston K, Mendonca M, Narbut P, Padovan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E345 List:
References
50-275-87-23, 50-323-87-22, IEB-85-003, IEB-85-3, NUDOCS 8707240051
Download: ML16341E346 (38)


See also: IR 05000275/1987023

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

Nos:

50-275/87-23

and 50-323/87-22

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

May 31 through

L.

M. Padovan,

Resident

June

27,

1987

Inspector

M~c~

Approved by:

K.

E. Johnston,

Resident Inspector

~

~

P.

P. Narbut, Senior Resident Inspector

M.

M. Mendonca,

Chief, Reactor Projects

Section

1

Date Signed

7i8/P~

Date Signed

g/z-Pd

Date Signed

Date Signed

Summary:

Ins ection from Ma

31

1987 throu

h June

27

1987

Re ort Nos.

50-275/87-23

and 50-323/87-22

Areas Ins ected:

The inspection included routine inspections of plant

operations,

maintenance

and surveillance activities, follow-up of on-site

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

25573,

30703,

61726,

62703,

71707,

73051,

73753,

90712,

92700,

92701,

92710,

93702,

and 94703

were applied duiing this inspection.

Results of Ins ection:

One violation regarding procedural

compliance

was

identified (Paragraph

3.c).

8707240051

870709

PDR

ADOCK 05000275

8

PDR

0

~

~

DETAILS

Persons

Contacted

"R.

C.

"J.

A.

"J.

M.

AJ

D

C

L

"K. C.

R.

G.

"D. B.

"D. A..

"M. G.

~J.

V.

"L

F

~T.

L.

S.

R.

R.

S.

D.

A.

B.

D.

M. J.

Thornberry, Plant Manager

Sexton, Assistant Plant Manager,

Plant Superintendent

Gisclon, Assistant Plant Manager for Technical

Services

Townsend, Assistant Plant Manager for Support Services

Eldridge, guality Control Manager

Doss, On-site Safety Review Group

Todaro, Security Supervisor

Miklush, Maintenance

Manager

Taggert, Director equality Support

Crockett, Instrumentation

and Control Maintenance

Manager

Boots, Chemistry and Radiation Protection

Manager

Momack, Operations

Manager

Grebel,

Regulatory

Compliance Supervisor

Fridley, Senior Operations

Supervisor

Meinberg,

News Service Representative

Malone, Senior I8C Supervisor

Guilbeault,

PSG Supervisor

Angus,

Mork Planning Manager

The inspectors

interviewed several

other .licensee

employees

including

shift foreman

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general construction/startup

personnel.

2.

Denotes

those attending the exit interview.

0 erational

Safet

Yerification

'a 0

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations

of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas

of the facility to

observe

the following:

(a)

General plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

(d)

Radiation protection controls.

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved

procedures.

(e)

Interiors of electrical

and control panels.

'(f)

Implementation of selected

portions of the licensee's

physical

secur ity plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

Seismic Interaction - 4 and 12 Kilovolt

KV

Switch ear

Room

While observing

12KV switchgear

on Unit 1, the inspector identified

a heavy metal three shelf cart which I8C technicians left unsecured

next to the 12KV switchgear.

In the event of an earthquake,

the

cart could have potentially impacted switchgear,

relay board panels

or other electrical cabinets.

This situation

was discussed

with the

I8C personnel

responsible for the oversight,

and was brought to the

attention of I8C management.

The cart was subsequently

properly

stored.

Unit 1 Containment

S ra

S stem Walkdown

En ineered Safet

Features

S stem Walkdown

The inspector performed

a walkdown of physically accessible

portions

of the Unit 1 containment

spray system.

Small

amounts of boron

crystal

accumulation

were observed

on the packing of three valves

and

on the outboard mechanical

seal of containment

spray

pump

(CSP)

1-1.

Additionally, a larger deposit of boron was identified on

CSP

1-1 discharge outlet valve,9001A.

This information was provided to

the licensee for resolution.

Overdue calibration stickers

were found on a level indicator and

a

pressure

indicator.

The licensee anticipates initiating a program

to remove overdue cal'ibration stickers

on this type of

instrumentation

which is not required for performance of

surveillance test procedures.

A "special calibration" sticker on

rotameter

F1929

(CSP test flow indicator used for STP P-4B)

indicated calibration was

due August 1984.

In discussion with

instrumentation

and controls personnel,

the inspector

was informed

that other instrument records indicated the calibration

was

due

August 1987.

However, since the required calibration

was designated

"special," the licensee

agreed to investigate

the adequacy of the

instrument's calibration.

No violations or deviations

were identified.

3.

Onsite Event Follow-u

'a ~

Inadvertent

Boron In ection

At 0330 a.m.

(PDT) on June 7, 1987, while Unit I was at 885 power,

the licensee

declared

a unusual

event

due to the inadvertent

injection of about

200 gallons of 20,000

ppm borated water from the

boron injection tank (BIT), which resulted

in a reduction of Tavg to

less

than

541 degrees

F.

Tavg was recovered

by a turbine load

reduction to 60$ power.

The cause of the event

was initially stated to be leaking BIT outlet

valves.

This was subsequently

determined to be in error,

and the

cause

was determined to be equalizing of pressure

across

the double

disc of the valves creating

improper valve seating.

Operators

were performing

(STP)

M-16B "Operation of Slave Relays

K604A and

K604B (Safety Injection)."

Concurrently,

STP M-21C

"Weekly Main Turbine Valve Exercising"

was in progress.

The senior

control operator

(SCO) actuated

slave relay K604A from the

SSPS

room, causing

valve 8803A, the BIT inlet valve, to open.

The

SCO

then returned to the control

room to verify proper

component

actuations,

and complete that portion of'he test.

When he arrived

he was

summoned to the control console to assist

the control

operator

(who was experiencing

problems with turbine stop valve

number 4) in performing

STP M-21C.

While assisting with the turbine

valve testing,

operators

noted that

RCS Tavg was rapidly decreasing.

Properly assuming that the BIT outlet valves were leaking through,

the operators

closed

8803A and

ramped turbine load to about 60'l to

recover

RCS temperature

to within limits.

RCS Tavg reached

a

minimum value of 536 F, which was below the technical specifications

minimum of 541

F for 8 minutes.

Analysis indicated about

150

gallons of 12% boric acid were injected into the

RCS during this

incident.

The BIT inlet and outlet valves are the "double disc with equalizing

line" type, motor operated

gate valves.

The BIT is designed to have

low pressure

inside of the inlet and outlet isolation valve

boundary,

and high pressure

outside that boundary for proper valve

sealing.

With the conditions set

up by STP M-16B, the outlet valves

lost their sealing capability.

As corrective action to prevent recurrence,

the licensee

planned to

revise

STP M-16B to include

a step to close the equalizing valve on

valves

8801A 5

B prior to pressurizing

the BIT for this test.

Unit

2 BIT valves are of different type and require

no changes.

Also,

plant engineering

was to review the surveillance test program for

other instances

of this problem with the boron injection path

valves,

and correct the

STPs

as necessary.

Unit 2

S ill of Borated Mater from Boric Acid Stora

e Tank 2-2 to

the Auxiliar Buildin

On June

20, 1987, at 2059 hours0.0238 days <br />0.572 hours <br />0.0034 weeks <br />7.834495e-4 months <br />,

approximately thirty gallons of

borated water spilled from boric acid storage

tank (BAST) 2-2

through

a drain valve downstream of boric acid transfer

pump

(BATP) .

2-2 to the Unit.2 auxiliary building.

Chemical

and radiation

protection

(CHIRP) personnel

surveyed

the spill and roped off the

area,

but did not identify any contamination.

Prior to the event,

two clearance

requests

(CRs) were simultaneously

issued to the field.

The first,

CR 6464, required the isolation of

BAST 2-2 for the installation of a new level transmitter

(LT) 102.

The second,

CR 6262, required the draining of BAST 2-2 as well as

its isolation for inspection of the tank and maintenance

on valves

associated

with it.

One of these valves,

CVCS-2-8488B (the

BAST 2-2

drain) was clogged.

CR 6262 established

an alternate

drain path

through

BATP 2-2 and out drain valve CVCS-2-194.

The drain path

included

BATP 2-2 suction valve CVCS-2-8761B.

However, since this

valve is normally open, it was not included

on

CR 6262.

However, it

was included

on

CR 6464 as

a boundary valve to be closed.

This sequence

of events is as follows:

1535 hours0.0178 days <br />0.426 hours <br />0.00254 weeks <br />5.840675e-4 months <br />

CVCS-2-8461B

was closed isolating

BAST 2-2 from BATP

2-2 as required

by

CR 6464.

1910 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.26755e-4 months <br />

With al-1 clearance

points established

on

CR 6464 and

all boundary valves closed

as required

by

CR 6262,

CVCS-2-194 was opened draining the volume downstream

of CVCS-2"8461B.

2059 hours0.0238 days <br />0.572 hours <br />0.0034 weeks <br />7.834495e-4 months <br />

CVCS-2-8461B

was opened

when operations

reported off

CR 6464.

The volume of borated water remaining in

BAST 2-2 and upstream of CVCS-2-8461B drained through

CVCS-2-194 and to the auxiliary building floor.

2117 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.055185e-4 months <br />

The spill was reported to the control

room and

CVCS-2-8461B

was shut.

It appears

that the spill resulted

from the practice of those

writing clearances

to assume that a normally open valve does not

need to be addressed

on a clearance if it is to remain open.

While

this may be

a valid assumption

during normal operation, it would

appear that during a refueling outage,

with the overlap of

clearances,

there is the possibil'ity that

a missing clearance

point

could affect plant safety or cause

serious injury.

This is a second

example during the Unit 2 refueling outage that confusion

on

a

"

clearance

point has resulted in a spill (see Inspection

Report

50-323/87-20

paragraph 3.i.).

The licensee

has committed to review

these

events for actions

necessary

to prevent recurrence.

The

action taken by the licensee will be tracked with the issues

related

to Open Item 50-323/87-20-05.

Load Reduction

Due to Partial

Loss of Solid State Protection

S stem

SSPS

Train A

On June

15,

1987, Unit 1 was operating at lOOX power with I8C

technicians

performing

STP I-9A "Trip Actuating Device Operational

Test 12kv Undervoltage,

Underfrequency"

on 12kv Bus

D reactor

coolant

pump

(RCP) undervoltage

(uv) and underfrequency

(uf) relays.

At 2213 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.420465e-4 months <br /> the control

room received

a

SSPS general

warning

"Train A" alarm and

a "protection channel

activated"

alarm.

Protection set II bistables for RCP

uv and uf,

RCP breaker

open,

low

auto stop oil pressure,'nd

turbine stop valve 04 simultaneously

began flashing on and off.

Control

room personnel

paged the

IEC

technician located at the 12kv switchgear relay board,

and

ascertained

that the technician

had accidentally partially closed

the metal

panel

door on instrumentation test leads,

causing

an

electrical short in Train A of the

SSPS.

This short blew the Train

A input excitation fuse,

and accordingly the shift foreman

(SFM)

conservatively

determined Train A of the

SSPS to be inoperable.

The

ILC technician in the control

room placed the Train A multiplexer in

normal

and the previously identified bistable lights stayed lighted,

indicating the bistables

were tripped.

The

SFM declared

a

Notification of Unusual

Event,

and required notifications were made.

A turbine

rampdown

was also initiated at 2227 hours0.0258 days <br />0.619 hours <br />0.00368 weeks <br />8.473735e-4 months <br />,

as required

by

plant Technical Specifications.

The

SSPS input excitation fuse was

replaced,

and

STPs I-16 A1, A2, and

A3 were performed to verify SSPS

Train A operability.

At 0015 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />, Train A was returned to

service,

the unusual

event

was exited,

and the load rampdown

was

terminated.

Unit 1 was stabilized at 76K reactor

power before

turbine load was

vamped

back to lOOX power.

During performance of the

STP, the I8C technician positioned the

RCP

undervoltage test switch to the off positi'on and proceeded

to the

back of the switchgear relay panel to remove the test leads.

The

technician

moved the door, pinching the leads,

and caused

the

electrical short.

However steps 3.g.4)

and 3.g.5) of STP I-9A

specify the general

purpose multimeter test leads

are to be removed

and then the

RCP undervoltage test switch is to be returned to the

off position.

Had the technician followed the procedure

(and

accidentally pinched the test leads with the test switch in the test

position) the bistables

would not have tripped.

Failure to follow

the steps of the

STP is an apparent

procedure violation (Open Item

50-275/87"23-01).

The inspector attended

the licensee's

Technical

Review Group

(TRG)

session to observe

the licensee's

determination of root cause of the

incident.

TRG participants

concluded

"personnel

error

due to

failure to follow procedures"

was the root cause.

A lack of

procedural

emphasis

on the steps of returning the system to service

was identified as

a contributory cause.

As corrective action to

prevent recurrence,

the technician

was counselled

on the need to

adhere to procedures,

and licensee

management

is considering other

~

(

~

actions.

Additionally, STP I-9A is to be revised to clarify removal

from service

and return to service steps.

Recently,

I8C technicians

have

been responsible for creating several

events involving failure to comply with procedures.

On April 19,

1987,

a

RCP uf relay was determined to be inoperable,

but the

channel

was not tripped due to I8C technician failure to follow a

procedure.

On May 14,

1987,

an emergency diesel

generator

was

inadvertently started

when

an I8C technician did not log a "jumper

wire" as required,

and went beyond his loop test instructions.

PG8E's

June

15, 1987, letter (number DCL-87-136) to the

NRC

delineated corrective actions

taken to assure

procedural

compliance.

Considering this June 15th incident, apparently additional

management

attention to this subject area

may be warranted.

One violation and

no deviations

were identified.

4.

Maintenance

The inspectors

observed portions of, and reviewed records

on

selected

maintenance activities to assure

compliance with approved procedures,

Technical Specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts were appropriately

certified.

a ~

Circuit Breaker Corrective Maintenance

On April 12, 1987,

RHR pump 2-2 would not start.

.The problem was

identified on action request

(AR) 0068952,

non-conformance

report

(NCR) DC2-87-EM-N043,

and work was performed

on work order C0012513,

The problem was identified as

a bent bracket

on the closing coil of

the

pump circuit breaker.

The bent bracket allowed spacer

washers

to slip and bind the solenoid plunger which pushes

a lever to close

contacts to energize

the closing spring charging motor.

Repairs

were

made

and the breaker tested satisfactorily

on test power.

Subsequent

operations

of the breaker

were satisfactory.

The

licensee

also

examined

29 additional circuit breakers

to determine

if the problem was isolated:

All 29 breakers

were found to be

satisfactory.

On June 2, 1987, in preparation for reactor vessel

pump down,

RHR

pump 2-2 was shutdown

and

pump 2-1 was started to maintain

RHR

cooling in accordance

with operating procedure

(OP) A-2-II.

RHR

pump 2-2 was to be used to transfer water to the refueling water

storage

tank

(RWST).

When an attempt to start

pump 2-2 was

made,

the

pump would not start

due to malfunction of the pump's electrical

breaker.

The inspector

examined the

pump breaker with licensee

maintenance

management.

It was noted that the solenoid plunger did not operate

smoothly and did, not close the spring charging motor contact.

The mechanics

who performed the corrective action were assembled

at

the breaker

and the corrective action taken in April discussed.

They verified that the plunger (as left) had moved freely after the

bracket repair in April and was not acting freely (differently)

during this examination.

The licensee

prepared

an investigative plan prior to disassembly

of

the plunger solenoid.

The results of that investigation

showed that

the washer pack had slipped laterally, partially binding the

solenoid.

The washer'pack

sl.ipped because

a copper retaining sleeve

was not fully engaged

in a depression

machined in the surface of the

coil mounting bracket for this purpose.

The inspector

examined the vendor technical

manual for the breaker.

It was noted that there

was

a lack of assembly detail provided by

the vendor.

The licensee

stated that they had, during the previous

year,

purchased further detail drawings

from the vendor but that

these did not provide details of the solenoid assembly,

either.

The licensee

has resolved the breaker

solenoid problem by adjusting

the bracket to ensure

the copper sleeve is fully retained in its

machined

grooves.

Additionally, a licensee

maintenance

engineer

stated that the breaker overhaul

procedure will be revised to

include

a dimensional

requirement for the bracket

and spacer to

preclude

recurrence.

The licensee's

investigative

and corrective

actions

appeared

acceptable.

Leakin

RHR Sockolet Weld

On June 2, 1987,

leakage

was noted from a residual

heat

removal

(RHR) system line while

RHR was in service.

The licensee

made 'a 4

hour reportable

event notification to the

NRC.

The weepage

was from

a weld on a 3/4" vent line on the hot leg recirculation

RHR piping

in containment

(high point vent 2-932).

The weepage

was located at

a sockolet fitting weld to the 3/4" piping.

The licensee

elected to do a thorough root cause

analysis

and

removed (by sawing) the entire weld and

a portion of the sockolet

fitting below it and a portion of the 3/4" pipe above it.

The

removed section

has

been sent off site for analysis for root cause.

The piping was refit to the remaining sockolet

and rewelded.

The inspector

examined the repair weld and found it met visual weld

acceptance

standards.

The license's

investigative

and corrective

actions

appeared

acceptable.

Re air of Incore Instrumentation

Seal

Table

Leaks

The inspector

observed repairs

made to two leaking incore

instrumentation

seals.

The maintenance

was performed in MODE 5,

cold shutdown, with the level in the pressurizer

at approximately

50K.

Since in this condition

a static

head exists at the seal

tabl'e,

the disassembly

and replacement

of the seals

required the

use

of a freeze

seal

on the incore instrumentation

guide. tubes.

The freeze

seal

was accomplished

in accordance

with Maintenance

Procedure

M-89, "Freeze Sealing of Piping."

The coolant

used in

this application

was carbon dioxide.

The inspector

noted that

precautions

were observed.

The precautions

require the freeze

zone

to be in an area free of stress

risers

(welds,

bends, fittings,

etc.).

The. inspector also observed

the replacement

of two seals.

This was

accomplished

according to a contractor procedure

which had been

reviewed

and approved

by the Plant Safety Review Committee.

The

seal

replacement

was

done

by site Mechanical

Maintenance with the

guidance of the contractor.

Mechanical

Maintenance

and the job'

quality control inspector received training from the contractor

which include the use of a guide tube seal

mock up.

The inspector

noted that a quality control inspector

observed

the maintenance

and

gC hold points were met.

In addition,

a special

work permit was

issued for the work and

a radiation technician assisted

in the

operation.

No violations or deviations

were identified.

5.

Surveillance

By direct observati'on

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

a.

Calibration of the

K3 Constant for the Pressurizer

Pressure

In ut to

the Over

Tem erature Delta Tem erature

OTDT

Set oint

The inspector

observed portions of a partial performance of

Surveillance Test Procedure

(STP) I-6B2, "Calibration of Pressurizer

Pressure

Protection

and Safeguards

Functions,"

performed

on Unit 2

pressurizer

pressure

channel

PC-457.

The calibration was to

summator

PM-457C which is the channel's

input to the

OTDT setpoint

calculator.

The summator

module was recalibrated to reflect

Amendment

13 changes

to the Unit 2 Technical Specifications

(TS)

regarding the

OTDT setpoint

K3 constant.

The

TS change reflects

an

increase

in the Unit 2 enthalpy hot channel factor for its second

cycle.

A change in the safety limit allows the licensee to reduce

the reactor coolant system pressure

input to the

OTDT setpoint.

The inspector

noted that as found data

was taken

on the summator

module prior to its calibration.

It was also noted that an approved

procedure

was

used

and was followed by the technician.

In addition,

calibrated instrumentation

was

used

and the work was performed with

the knowledge of the shift foreman.

The inspector

independently

verified that the values the summator

module was recalibrated

to

were consistent with the

TS revision.

A

9

b.

Licensee Surveillance

Ins ections

Re uired b

ASME Section XI

The inspector

examined licensee

surveillances

performed in

accordance

with the ISI program

as detailed in section

6. of this

report.

c.

En ineered

Safe

uards

Valve Interlocks

The inspectors

observed

power production. personnel

perform a portion

of STP V-7B "Test of Engineered

Safequards,

Valve Interlocks

and

RHR

Pump Trip from RWST Level Channels."

Interlocks

on various

ECCS

valves were verified to perform correctly,

by attempting to open

valves

once they had been aligned to pretest positions specified in

the procedure.

Interlock operability was then determined,

based

on

whether or not the valves

moved.

Prerequisites,

specified in the

procedure,

were verified by the inspectors

to have

been

met prior to

performing the test.

Pretest

alignments

were also reviewed.

During testing,

the inspectors

observed

procedural

steps

wer'e being

complied with.

However, the inspectors identified test personnel

had failed to .list initial positions of 13 valves

on Table

DS-4A as

required

by the procedure.

In discussion with the test personnel,

the inspector ascertained

that the valve positions

had

been

verified, but erroneously

not documented

on the table.

The table

was updated to include the information.

A post test review of the

procedure

would most likely have identified this omission.

From

discussions

with the test personnel,

the inspector determined the

individuals were trained

and familiar with the procedure.

No violations or deviations

were identified.

6.

Inservice Ins ection

ISI

The inspector

examined three areas'f

ISI in Unit 2 to verify the

inspections

were performed in accordance

with applicable

codes

and

standards.

This examination

was performed

subsequent

to an intensive examination of

the ISI area

conducted in a special

inspection

by Region I personnel

and

independent

measurements

by a

NRC non-destructive

examiner to confirm the

licensee results.

The special

inspection

included

a review of

non-destructive

examination

(NDE) procedures,

the ISI program

(and

changes

and exceptions),

personnel

qualifications,

and completed

data.

The special

inspection also included the performance of non-destructive

examination

by

NRC personnel

using

NRC equipment.

The special

NRC

inspection will be reported separately

(reference

NRC report

50-323/87"16).

For this inspection

however, the resident inspector

observed

the

performance of three ISI examinations

as follows:

1)

An ultrasonic volumetric examination of weld joint WIB-291 on

accumulator injection loop 4 (one inch thick stainless

steel

piping).

The inspector

observed

the calibration process

and the

10

,

inspection

process

and examined the records

generated

as

a result.

All work observed

was performed properly by qualified

NDE examiners;

The examiners

properly recorded

the areas

which were inaccessible

for examination

(due to pipe restraint crush blocks)

and recorded

an

indication believed to be geometric in nature.

2)

A magnetic particle surface examination of longitudinal weld joint

l<ICG 3-1LS on Hain Steam outlet piping on Steam Generator

2-1 was

observed

in part.

Due to a lack of adequate

cleaning,

the licensee

examiners

did not perform the formal examination of record,

but did

perform their calibration

and demonstrated

their inspection

technique for the inspector.

No indications

were observed.

3)

A visual examination of pipe support 412-166SL for

pressurizer

power operated relief valve PCV-455C was observed.

The ISI visual

includes examinations for damage,

debris, corrosion,

wear, bolt

tightness,

snubber settings,

presence

of necessary

snubber

washers,

and snubber

alignment.

All inspection results

were satisfactory.

Additionally, the inspector

examined available

code repair/replacement

activities.

For this outage,

the activities included the removal

and

replacement of two accumulator fill fittings which had

a history of

weepage

during operation.

They were cut out for analysis

and replaced

with new material.

Additionally, the RHR'sockolet weld repair was

observed

as described

in the maintenance

section of this report.

No violations or deviations

were identified.

Inde endent

Ins ection

a.

Unit 2 Enhanced

0 erational

Safet

Verification

During its first year of operation,

the Unit 2 operational

aspects

were subjected

to enhanced

operational verification by the resident

and regional staff and supplemented

by team inspection

and the

Augmented Inspection

Team (AIT) involved in the April 10, 1987,

"Loss of RHR" event.

However, since the operation of Unit 2 is

controlled by essentially

the

same procedures,

personnel

and quality

systems

as Unit I, no attempt to separate

the Units has

been

made.

The findings of the enhanced

view of Unit 2 have

been discussed

in

previously issued reports

and will be reviewed in summary fashion

shortly in the upcoming Systematic

Assessment of Licensee

Performance

(SALP).

Since Unit 2 is in its first refueling cycle, the required

enhanced

safety verification period is considered

complete.

The key lessons

derived from the enhanced verification were:

o

Greater

adherence

to the precepts of procedure

compliance is

required.

NRC findings have noted the

need for improved

quality of procedures;

that is, procedures

should

be specific

where specifics

are desired

and general

in areas

where only

general

guidance is required.

Secondly,

procedure

compliance

needs to be emphasized.

On shift operational

personnel

have

the authority to change

the. procedure

but not the authority to

deviate

from it.

Greater formality o'f commun'ications

between the departments

is

required.

NRC findings have

shown problems arising from verbal

transmission of work completion status

between

departments.

Examples

included completion status

work on the containment

door by maintenance

and work planning,

completion status of

work on the rod control system

by I8C, and failure to notify

operations

of an inoperable

underfrequency trip found during an

I8C surveillance test.

Improved operator

awareness

of reportability requirements

is

required.

Throughout the first year of operation of. Unit 2, the

licensee

has

made several

late reports to the

NRC, apparently

due to the need for increased

operator

knowledge in the area of

reporting.

o

Improved formal action plans

subsequent

to events to gather

facts, chart actions

necessary

to fully resolve

problems

identified, and to develop meaningful root causes

are required.

b.

Secondar

Pi

e Wall Thinnin

Pro

ram

As a result of the feedwater pipe rupture incident at the Surry Unit

2 site

on December

9, 1986, the resident inspector inquired into the

Diablo Canyon a'ctions to monitor secondary

pipe wall thinning.

Several

meetings

were held and the following information obtained:

Prior to the Surry event,

Diablo had a secondary wall thinning

program in place.

This program dealt primarily with monitoring wall

thickness

in areas of two phase

flow such

as extraction

steam lines.

This program accounted for such problems

as described

in IE Notice

82-22 and

INPO

SOER 82-11.

The program sampled

29 locations for

examination in the first and third refueling outages.

The

examination

done during the first Unit 1 refueling showed

no erosion

evident.

Subsequent

to the Surry event the licensee

established

an Action

Plan

and Task Force to examine potential single phase

flow erosion.

The licensee

prepared

an inspection plan for the Unit 2 first

refueling outage

based

on information obtained

from IE

Notice 86-106, industry guidance

and their

own experience

in fossil

plants.

The licensee

examine

67 locations in the Unit 2 outage including

single phase

and two phase flow locations.

The purpose

was to

obtain baseline

information for future examinations.

Two areas of concern were identified on branch connections

on the

H.P. Turbine Exhaust Line.

Approximately one-third of the pipe wall

'a

~

was eroded in a relatively local area.

Projected

wear rates

indicate

minimum wall thickness

could be achieved prior to the next

refueling outage.

Therefore,

the licensee

performed

a weld repair.

Because of the Unit 2 finding, Unit 1 was examined

and

had

a similar

finding.

The licensee

intends to monitor the Unit 1 location and

develop

a permanent correction for both Units.

An additional erosion location in Unit 2 was identified in an

extraction

steam line to feedwater

heater

81.

The licensee

determined the cause to be a malfunctioning moisture separator.

There

was

a through wall leak at one branch, significant thinning at

another,

but no evidence of erosion at the remaining 4 branch

connections.

Unit 1:locations did not show erosion.

The Unit 2

through wall leak was repaired.

The licensee

task force will continue to monitor developments

in the

erosion area per the licensee

correspondence

examined.

The licensee

management

was queried regarding the secondary

complications of the Surry event, specifically inadvertent fire

protection discharges

and malfunctioning security devices

(due to

the steam environment).

The licensee

stated that these

complications

had been considered

but are not of credible concern at

Diablo.

No violations or deviations

were identified.

8.

Radiolo ical Controls

~

~

~

The inspector

observed radiological controls exercised

in the containment

work described

in this report.

Aspects

observed

included access

control,

radiation protection personnel

monitoring of work areas,

and examination

of the applicable radiation work permits.

The inspector discussed

job

coverage with involved workers

and Health Physics

(HP) technicians.

Individual radiation workers were observed

donning protective clothing,

undressing

and frisking.

Response

to one skin contamination

was

observed,

and health physics actions

were immediate

and proper.

0

The licensee initiated a hot particle program which required special

training on the part of radiation workers

and health physics technicians.

Although fission product particles

have not been

a problem at Diablo,

events at other facilities prompted licensee

management

to initiate the

training program to prepare

personnel

to recognize

and deal with the

problem should it occur.

The residents

attended

both the worker and

health physics training and found it well presented

and informative.

No violations or deviations

were identified.

9.

Licensee

Event

Re ort Follow-u

a.

Status of LERs

Based

on an in-office review, the foll'owing LERs were closed out by

the resident inspectors:

13

Unit .1:

87-06, 87-07,

87-08

Unit 2:

87-07, 87-08,. 87-09

The

LERs were reviewed for event description,

root cause,

corrective

actions taken,

generic applicability and timeliness of reporting.

b.

Red Tele

hone

vs

LER Trackin

The licensee

has evaluated

the following 10 CFR 50.72 events for

reportability under 50.73 and

has determined that 50.73 report is

not required.

The resident inspectors

have

examined the licensee's

rationale

and determined that regulatory requirements

have

been

met.

50.72 Report

Date/Unit

Event

Reference

NCR

etc.

6/15/87 - Unit 1

NRC DC1"87"TI"N075. 10 CFR 50.73

Initiation of plant report

required for completion

shutdown

due to

SSPS of plant

.

shutdown,

only.

Unit Train A

inoperability was stabilized at

76K power.

No violations or deviations

were identified.

10.

0 en Item Follow-u

Follow-u

Item on Missin

Snubber

Washers

0 en Item

50-323/86-30-01

Closed

During the Unit 1 refueling outage

(September

through

December,

1986) the licensee identified a wide spread

problem with missing

washers

on piping snubbers.

Washers

are required

between the

snubber

paddle

and its brackets to allow + 5 degrees

of

misalignment.

The licensee identified the cause to include

inadequate

snubber reinstallation instructions

and procedures,

the

difficulty of installing washers

in radiation areas

which required

anti-contamination clothing and the failure to recognize that the

deletion or change of washers

is

a design

change.

The licensee

took the following actions to prevent recurrence:

1)

Revision of the testing procedures

(Maintenance

Procedures

M-55. 1,.2,8.4) for Anchor Darling, Pacific Scientific,

and

Grinnel Hydraulic snubbers.

The revision included specific

requirements

for the installation of snubbers.

2)

Revision of Surveillance Test Procedure

(STP) M-78A, "Snubber

Visual Inspection," to provide specific criteria for spacer

washer inspection.

'J

14

b.

c ~

d.

3)

Training of maintenance

personnel,

involved in Unit 2 refueling

outage

snubber work, based

on the revised procedures.

The inspector reviewed the revised

procedures

and found the washer

guidance

included in each to be adequate.

The inspector also

reviewed the snubber training lesson

plan and noted it included

specific training on washer inspection

versus

the washer

installation criteria.

In addition,

the. inspector attended

Technical

Review Group

(TRG) meetings

which discussed

root cause

and

corrective .actions

needed to address

the snubber washer issues.

The

inspector

found these

meetings

thorough in identifying root cause

and establishing

corrective'actions, to prevent recurrence.

Based

on

the above, this item is closed

(Closed 50-323/87-30-01).

Notice of Violation Re ardin

Potentiall

Distractin

Activities in

t e Contro

Room

en Item 50-323/87-12-02

C osed

NRC Inspection

Report 50-323/87-12 identified

a violation of AP

A-103 "Control

Room Access,"

where inappropriate

wording (a form of

distraction)

was put on an annoying,

unused,

flashing annunciator

window located

on

a Unit 2 control

room panel.

PGSE letter number

DCL-87-134 contained

a response

to this violation, and identified

corrective steps

taken to avoid

a repetition of this type of

situation.

These corrective actions,

also identified in IR

50-323/87-12,

have

been

completed

and were found to be appropriate

for the situation.

Accordingly, this item is closed.

Notice of Violation on Timeliness of Problem Resolution

0 en Item

86-18-01,

C osed

NRC Inspection

R'eport 50-275/86-18 cited

a concern

regarding failure

of the licensee to correct

a condition adverse

to quality in a

timely fashion.

In response

to the Notice of Violation, the

li.censee

issued letter DCL-86-241 specifying corrective actions

taken,

and an additional action required to prevent recurrence.

This action

was to ensure that an independent

walkdown or dry run of

a revised

procedure is performed,

as applicable,

as part of the

procedure's

independent verification process.

The inspector verified AP-C3S1 "Surveillance Testing

and Inspection"

was revised to add the statement:

"procedure

changes

that affect the

testing

sequence,

the testing requirements,

or add

new components

should

be walked down in the field to verify workability."

Accordingly, this item is closed.

Notice of Violation Re ardin

Ino erable

Reactor Coolant

Bus

Underfre uenc

Tri

Channe

Returned to Service

0 en Item

50-275/87-13-02

C osed

On April 19, 1987,

one underfrequency

channel

on Unit

1 was not

tripped within six hours of the discovery of its inoperability as

required

by the Technical Specifications.

The event

was caused

by

personnel

error, in that guidance

provided in the "Precautions"

section of the Surveillance Test Procedure

(STP) being performed

was

15

overlooked

and not followed.

Inadequate

communications

between the

plant technician performing the

STP and the control

room operators;

was

a contributing factor to this event.

The inspector

has reviewed the licensee's

June 11, 1987,

response

to

the Notice of Violation contained in inspection report 50-275/87-13

in addition to attending site Technical

Review Group

(TRG) meetings

regarding this subject.

The licensee's

corrective actions

are

as

follows:

o

The individuals involved have

been counseled

on the importance

of procedural

compliance,

including observance

of all

procedural

sections.

o

Surveillance Test Procedure

STP I-9A, "Trip Actuating Devise

Operational

Test,

12 kv Undervoltage,

Underfrequency" will be

revised

by July 15,

1987, to provide additional detail

on the

steps to be taken if a relay is found inoperable.

o

An Incident Summary Report, which is required reading

by

control

room operators,

was prepared

stressing

the importance

of good communications.

o

Administrative Procedure

C-6S4, "Control of Equipment

Required

by the Plant Technical Specifications" will be revised

.by July 15, 1987, to require that the operability of equipment

being returned to service;be verified by the organization

performing the post maintenance

operability check by signing

the technical specification action tracking sheet prior to a

return to operable

status.

The inspector

finds that the corrective actions identified to

address

the issue of miscommunications

between plant personnel

and

the control

room when returning equipment to service to be

acceptable.

However, the issues

of procedural

compliance

and timely

revision to

STP I-9A will be addressed

in conjunction with the

Notice of Violation contained in this report regarding

a June

15,

1987, incident where

an I8C technicians failed to follow STP I-9A.

Based

on the above,

enforcement

item 50-275/87-13-02 is closed.

Follow-u

on the Pro er Im lementation of Vendor Installation

Information Received with Re lacement

Parts

0 en Items

50-275/87-08-01

50"323/87-07-01)

This item was

open

because

the inspector

had insufficient time to

establish

the flow path that ensured

occasional

vendor installation

information reviewed with spare parts

was properly translated

into

installation instructions.

The inspector

met with the Procurement Specialist

Group and

warehouse

personnel

and determined that the intended control process

flowed as follows:

C

16

Parts

received with special

instructions

are noted by warehouse

personnel

and the special

documents

forwarded to

PSG personnel

in

accordance

with "PSG Notebook Entry 850" which is an in house

instruction.

The inspector verified warehouse

receivers

were aware

and

had been trained

on the subject.

The

PSG group receiving such information forwards

such vendor

documentation

to the plant engineering

manager

who in turn is

required to log the document

and send

an information copy to the

appropriate plant department

and to the Nuclear Operations

Support

(NOS) department

in the general office which is responsible

to track

necessary

actions including vendor manuals

changes

through to

completion.

The system is described

in Procedure

NPAP E-14

"Supplier Documentation

and would appear

to eventually provide the

necessary

undated

procedures

to insure satisfactory installation

instructions.

There may be

a problem however during the time this process is

occurring.

Specifically (in the case of the replacement

connecting

rod for the control

room refrigeration compressor originally

questioned

by the inspector)

the part was "dedicated" for use in

August of 1986

by RPE H-0008.

The vendor technical

manual

was in

process of being updated providing the

new installation torque

values in June of 1987.

IIf the part had to be used in the intervening

10 months the part

would be available for use without updated instructions

being

available.

This matter

was discussed

with the manager of NOS and

he

committed to investigate

and determine if corrective action such

as

a "hold" on such

par ts is warranted until such time as the

instructions

are issued.

Secondly the engineer in NECS responsible for the system

was

questioned

whether

he had followed the instructions of procedure

E-14 for notifying NOS of the vendor information received

and

specifica'fly whether

he had initiated the notification form of

procedure

E-14.

In both cases

he stated

he had not and was not

aware of the procedure

E-14 but worked to Engineering

Department

procedures

instead.

This was discussed

with the manager of NOS who

committed to examine the situation

and determine if a problem

existed.

No

This item remains

open pending resolution of the above

conmitments

of the

NOS manager

and the determination

by

WPC whether the part was

installed to the proper torque.

violations or deviations

were identified.

ll.

Im lementation of Securit

Force Strike Plans

On June

16, 1987,

a vote by the bargaining unit members of the United

Plant Guard Workers of America

(UPGWA) failed to ratify a labor agreement

between

UPGWA and American Protective Services

(APS).

Accordingly,

UPGWA

sanctioned

a strike of APS bargaining unit employees

which began at 0400

hours

on June

17, 1987.

Security personnel

employed

by APS predominately

perform non-security plan functions outside the protected

area,

but also

17

fill selected

security plan required positions.

The inspector

reviewed

the licensee's

activities in preparation for the impending strike.

Staffing of all security plan required positions

(by non-striking General

Construction

(GC) security officers,

PGKE armed responders,

and security

supervisory

personnel')

was reviewed,

and found to be adequate.

Upon

strike implementation,

various audits

and security system status

assessments

were

made

by the licensee.

Approximately 200 badge

packets

were identified as having been

placed in incorrect

badge rack locations.

This was the only apparent

attempt

by striking security personnel

to

disrupt security activities during the strike.

Picketing of the job site

entrances

began at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />

on June

17, 1987,

and continued for the

duration of the strike, without disrupting entering or exiting vehicles.

For informational purposes,

this event

was reported to the NRC's

Operations

Center at 0940 hours0.0109 days <br />0.261 hours <br />0.00155 weeks <br />3.5767e-4 months <br />.

The licensee

informed the inspector all

GC security officers had been

"Appendix B" certified.

Selected

security functions were observed

during

the strike duration,

and were found to be satisfactory.

At approximately

1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br />

on June

19, 1987, the contract

was ratified and normal

security staffing was obtained at 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br />.

The return to work was

without incident.

.

Detailed descriptions

on this event are withheld due to its designation

as security safeguards

information.

No violations or deviations

were identified.

Licensee

Res

onse to IE Bulletin 85-03, "Motor-0 crated

Valve Common Mode

Far ures...

In response

to portions of NRC Temporary Instruction 2515/73,

the

inspector

observed

technicians setting valve operator limit switches

and

torque switches

on motor operated

valves

(MOVs) SI-2-8804B and

RHR-2-9003B.

Adjustments to MOV SI-2-8804B were previously described

in

section 4.b of NRC Inspection

Report 50-323/87-20.

Work on .RHR-2-9003B

was performed in accordance

with Action Request

A75289 and Work Order

C14370.

Torque switch adjustments

were performed utilizing Maintenance

Procedure

(HP)

E 53.10B "Limitorque Operator Torque Switch Adjustment"

and

MP

E 53.10D "Limitorque Operator Limit Switch Adjustment."

Operator

housings

were found to be free of rust and moisture,

and contacts

wert

clean

and free of corrosion.

Where possible,

the inspector also verified

correct lubricants were being used.

In total,

17

MOVs had their limit

and torque switches adjusted.

The licensee

indicated

as found limit and

torque switch settings

(with the valves not necessarily

under full delta

p) were within tolerance.

HP M-51.13 was also reviewed to verify the procedure

required staking of

the lock nut for the operator

stem nut.

Documentation

regarding

use of

Durez, Melamine,

and Fibrite material in the switches

was also reviewed

by the inspector.

No violations or deviations

were identified.

r

18

13.

Exit

On June

26,

1987,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph I.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.