ML16341E326

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Insp Repts 50-275/87-20 & 50-323/87-20 on 870426-0530.Three Violations & No Deviations Noted.Major Areas Inspected:Maint & Surveillance Activities,Onsite Events,Open Items & LERs
ML16341E326
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 06/22/1987
From: Johnston K, Mendonca M, Padovan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E327 List:
References
50-275-87-20, 50-323-87-20, NUDOCS 8707140394
Download: ML16341E326 (46)


See also: IR 05000275/1987020

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

Nos:

50-275/87-20

and 50-323/87-20

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

April 26 through

May 30,

1987

L.

M. Padovan,

Acting Senior Reside t Inspector

K.

E. Johnston,

Resident Inspector

Approved by:

M.

M. Mendonca,

Chief, Reactor Projects

Section

1

p/z- ~/P w

Date Signed

Date Signed

g /z.~pi ~

Date Signed

Summary:

Ins ection from A ril 26 throu

h Ma

30

1987

Re ort Nos.

50-275/87-20

and

Areas Ins ected:

The inspection

included routine inspections

of plant

operations,

maintenance

and surveillance activities, follow-up of on-site

events,

open items,

and 1'icensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

30703,

60710,

61720,

61726,

62703,

71707,

90712,

92700,

92701,

92702,

and 93702 were applied during

this inspection.

Results of Ins ection:

Three violations and

no deviations

were identified.

8707140394

870h22

PDR

ADQCK 05000275

8

PDR

DETAILS

1.

Persons

Contacted

2.

J.

D. Shiffer, Vice President

Nuclear

Power Generation

"R.

C. Thornberry, Plant Manager

R. Lieber, Construction Superintendent

"J.

A. Sexton, Assista'nt Plant Manager,

Plant Superintendent

"J.

M. Gisclon, Assistant Plant Manager for Technical

Services

J.

D. Townsend, Assistant Plant Manager for Support Services

~C.

L. Eldridge, guality Control

Manager

K.

C. Doss, On-site Safety Review Group

R.

G. Todaro, Security Supervisor

"D. B. Miklush, Maintenance

Manager

M. J.

Angus,

Work Planning Manager

D.

A. Taggert, Director guality Support

T. J. Martin, Training Manager

W.

G. Crockett, Instrumentation

and Control Maintenance

Manager

J.

V. Boots, Chemistry and Radiation Protection

Manager

~L.

F.

Womack, Operations

Manager

"T. L. Grebel,

Regulatory Compliance Supervisor

S.

R. Fridley, Senior Operations

Supervisor

R.

S. Weinberg,

News Service Representative

D.

A. Malone, Senior I8C Supervisor

"M. W. Stephens,

I8C General

Maintenance

Foreman

The inspectors

interviewed several

other licensee

employees

including

shift foreman

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

  • Denotes those attending the exit interview.

0 erational

Safet

Verification

a 0

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas of the facility to

observe the following:

(a)

General plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

Unit 2 Restoration of Mid-Loo

0 eration

As described in Section 3.d. of NRC Inspection

Report 50-323/87-12,

on April 10, 1987, while Unit 2 was in cold shutdown with the hot

legs at mid-loop, both residual

heat

removal

(RHR) pumps were shut

off due to unanticipated

vortexing.

To preclude future interruption

of RHR flow while the plant was at mid-loop operation,

the licensee

submitted

an action plan to the

NRC (PG&E May 4, 1987, letter

DCL-87-099) for items to be completed prior to resumption of

mid-loop operation.

Via confirmatory action letter EA-87-67, dated

May 6, 1987,

NRC Region

V documented

the understanding

that Unit 2

would not be returned to mid-loop operation until the

NRC staff

concurred in the appropriateness

and adequacy of the actions

described in the licensee's

May 4, 1987, letter.

On May 18, 1987,

the licensee

forwarded

a supplemental

letter (DCL-87-113) indicating

a second charging

pump would be available for operation during the

upcoming mid-loop operations.

In order to assess

the status of completion of the licensee's

actions,

the inspectors

reviewed licensee

documents

and hardware

installations for compliance with the "Actions Completed or to be

Completed Prior to Resumption of Mid-Loop Operation" section of

DCL-87-099.

Modifications to Reactor Vessel

Refueling Level

Indication Systems

(RVRLIS) were observed

in the field, and stated

enhancements

to Operating

Procedures

(OPs)

AP-16 and A-2:II

(including availability of a second charging

pump)

and control of

work activities were verified to have

been

completed.

The

inspectors

also observed

a presentation

(given to each operating

crew) by J.

D. Shiffer, Vice President

Nuclear

Power Generation,

on

the subject of PG8E's policy regarding compliance

and adherence

to

procedures.

Regarding the "Additional Training" commitment (Item 8 of

OCL-87-099), the inspector verified operations

personnel

had

received training on the

OPs.

However, the inspector identified the

training provided

on

RHR half-loop operations utilized a training

guide which was roughly equivalent to revision

0 of the

OPs.

In

response

to commitments provided in the licensee's

May', 1987,

letter,

OPs A-2:II and AP-16 had both been

updated

through revision

number

2 to incorporate

changes

in plant operational

requirements

and emergency

response

actions.

It was not clear that training had

been provided to the operating

crews

on the revised

OPs.

In discussing

the matter with the operation

s manager,

he indicated

the differences

between

the original procedures

and later revisions

would be discussed

at the tailboard conducted

by the

SFM during

shift briefings.

Subsequent

discussions

between the

NRC and

PG8E

management

resulted in a commitment from the licensee to have

operations

management

personnel

review each step of the revised

procedures

with each operating

crew and specifically discuss

the

revised steps, prior to permitting the crew to operate

the unit at

mid-loop conditions.

The inspector witnessed

one session

of this

training,

and found the commitment was complied with.

Accordingly,

via letter dated

May 30, 1987, the

NRC rescinded its May 6, 1987,

confirmatory action letter and granted concurrence for Unit 2 to

return to mid-loop operation for the current outage.

No violations or deviations

were identified.

3.

Onsite Event Follow-u

ao

S ill of a Small

uantit

of Radioactive Water

On May 23, 1987, after replacement

of Unit 2 'post-loca

sampling

panel

PM-80, four mechanical

maintenance

personnel

conducted

a

hydrostatic test

on the Nuclear Steam Supply System

(NSSS) primary

water sample

system in the Unit 2 post-accident

sampling

room.

While walking down the system,

personnel

observed water dripping

above the

PM 80 panel

from a stainless

steel

tubing compression

fitting.

A 12 inch puddle of water had formed under the panel.

The

hydrostatic test was stopped,

the line was depressurized

and

Radiation Protection

(RP) technicians

were notified of the

situation.

Upon reaching the scene,

the

RP technician

observed

about

one cup of

water

on the floor under the panel

and sent

a maintenance

worker to

get more decontamination

supplies.

The

RP technician

surveyed

a rag

used to soak

up

some of the water and found it reading

more than

50,000 counts per minute

(CPM) (about

20 millirads beta)

on his

fisker.

A foot print was observed

next to a tygon drain line going

to the floor drain,

and accordingly, the technician

suspected

shoe

contamination.

The water apparently

had run along the underside of

the tygon hose

and had gone unnoticed.

The technician

stopped

the

work and kept personnel

from spreading

the contamination.

Access

control

was notified of possible contamination of the 85 foot

elevation level,

and access

to this area

was stopped until the

extent of the contamination

could be determined.

One of the workers

was stationed to keep personnel

out of the area,

while the

RP

technician went to get an air sampler

and radiological contamination

posting supplies".

The results of the air sample

were 0.02 Maximum

Permissible

Concentration

(MPC).

Plastic booties

were issued to

personnel

in the area.

Surveys of the four worker's

shoes

were

negative,

except for one which indicated contamination of 500 net

CPM on the left sole

and 1500 net

CPM right sole.

The shoes

were

decontaminated

and returned to the owner.

Mith access

to the contaminated

areas

under control, survey and

decontamination

of the affected areas

was started.

Originally,

contamination

was found in the Unit 2 hallway, secondary

system

sample area,

and into the west half of the penetration

area.

The

areas

were wet mopped,

resurveyed

and areas of contamination

reduced

to a final area of about

200 square feet next to PM-80.

Additional

areas

surveyed for contamination

were performed in the Unit 1

hallways

and stairways leading to the 85 foot elevation.

No

smearable

contamination

was found in these

areas.

Unit 1 Steam Generator

S/G

Snubber

Pin'Movement

and Oil Leak

As described

in Licensee

Event Report

(LER) 1-86-13, in September

1986

S/G snubber

load pins were found to have

moved out of position.

As corrective action, the licensee installed pin capture

end plates

and established

a program to measure

pin displacement

once per

quarter.

In response

to this quarterly inspection

commitment, the

pins were measured for movement in January

1987 and

on May 12, 1987.

On May 12, mechanical

maintenance

personnel

discovered pin movement

on the southeast

snubber of S/G 1-2.

An assessment

team was formed

to investigate

and quantify the pin movement.

Results of the

assessment

indicated the pin had moved about 0.6 inch away from the

measuring

hole in the capture plate,

and the pin had rotated about

10 degrees.

The set screw was found to not be tight against the

pin.

As indicated in LER 1-86-13, the licensee is committed to

continue tracking pin movement.

The resident inspector

requested

the licensee to submit a revised

LER to the

NRC providing updated

information on the pin dislocation.

While= inspecting the load pins, maintenance

personnel

also checked

level in the snubber oil reservoirs.

On S/G 1-2, the

common

reservoir for the four snubbers

was found to be low and two-to-three

gallons of oil was observed

on the floor under the snubber.

Maintenance

personnel

determined

the snubber's test plugs were the

source of the leakage.

The tubing line from the oil reservoir to

the southeast

snubber

had air entrainment,

and thus the snubber

was

technically inoperable- for an indeterminate

length of time.

The snubber

was determined to be one of two snubbers

tested

by Paul

Monroe personnel

during the Unit 1 refueling outage.

Testing

required

removal of the test plugs

and the special silver-plated

stainless

steel

washers

were not replaced with new washers

by Monroe.

In discussions

with Paul

Monroe, the licensee

concluded the

snubber'ould

be returned to operable status

by venting and fillingwith

hydraulic oil.

The vendor indicated

no damage to the snubber resulted

from air entrainment,

and the snubber would not have locked up

(potentially overstressing

RCS piping).

Venting and filling of the

snubber

was completed,

new washers

were installed in the test plugs,

and all other fifteen S/G snubbers

were checked for leakage.

All

other snubbers

had

no oil loss. This issue will be carried

as

an

unresolved

item pending resolution of snubber operability

(50-275/87-20-03).

Unit Tri

Due to Line Differential Current Rela

Actuation

On May 11, 1987, while at about 40 percent

power for demusseling

operations,

Unit 1 experienced

a unit trip and subsequent

generator/reactor trip from an inadvertent actuation of line

differential current relay 587L-I.

The appropriate

emergency

procedures

were followed and the unit was stabilized in Mode 3.

A shunt reactor

had failed at the licensee's

Midway substation

causing

a transient

on the 500

KV transmission

system.

This

transient

was propagated

to the Diablo Canyon switchyard where the

line differential current relay incorrectly actuated

causing

a unit

trip..

The tie line differential relay senses

current flow leaving

the generator

main transformer

banks

and current flow entering the

500

KV substation.

If the current leaving one end of the line

differs substantially

from the current at the other end of the line,

the relay will initiate a unit tr ip.

The licensee's

Substation

Department investigated

the cause of the

indiscriminate relay actuation.

The root cause of the differential

relay actuation

was indeterminate

and remained

under investigation

by the Substation

Department.

To prevent recurrence,

the unit trip

signal provided by the tie line differential relay was

removed from

service

pending resolution of the cause of the tie line differential

signal.

Since the tie line differential relay was not taken credit

for in the

FSAR, and

has redundant

backup protection,

the licensee

deemed this action to be satisfactory.

Inadvertent

Containment Ventilation Isolation

CVI

from Plant Vent

Monitor RM-14A

On May 18, 1987,

an Instrumentation

and Controls (ISC) technician

inadvertently

caused

a CVI while performing Surveillance Test

Procedure

(STP)-107B3 "Radiation Source Presentation

(Isotopic)

Calibration of Miscellaneous

Area Radiation Monitors...RM7..." on

Unit 2 incore seal table radiation monitor (RM)-7.

Voltage to the

RM drawer

and detector high voltage had been de-energized

by

removing the power fuses

on the front of the radiation monitor

panels.

When reconnecting

the detector signal

cable in accordance

with step 3.n.l of STP-107B3,

a small electrical

arc occurred

from

what appeared

to be residual

voltage in either the drawer or the

'etector.

The arc caused plant vent radiation monitor 2-RM-14A to

spike, causing

the CVI.

In discussions

with the

I8C technician,

the inspector

concluded this

event was not caused

by any error or carelessness

on the part of the

technician.

The possibility of grounding (to remove residual

high

voltage) the drawer high voltage supply and detector cable prior to

reconnecting

the cable

was discussed

with licensee

management.

The

licensee

concluded this practice would not be advantageous

as

a

spark would be drawn during the grounding process,

creating the

possibility of another

CYI.

However,

as

a result of the NRC's questioning the validity of the

licensee's

root cause analysis,

further investigations

were

performed by the licensee.

These investigations

discovered that low

voltage cables for the radiation monitor remote meter,

the "GMI"

circuit, and

AC power to the local alarm were not deenergized.

These circuits were the source of electrical

power to produce the

spark, rather than "residual voltage"

as the licensee previously

thought.

This example denotes

the

need for a reassessment

of the

adequacy of your root cause analysis

techniques.

STP I-207B3

specified that the channel

to be calibrated

was to be deenergized.

In this instance,

the instrument

power fuses

were removed,

but the

control power fuses

located at the rear of the panel

were not.

This

provided the remaining

AC power at the connector.

Also, the routing

of the interconnecting detector cable

made mating of the connector

extremely difficult.

To prevent .recurrence of this situation,

the cable

was rerouted to

simplify the mating process.

A second corrective action was to

instruct all

IKC personnel

that when

a procedure

specifies

deenergization

of a channel,

the intent is to deenergize

both

control power and instrument power,

unless specified otherwise.

The

third corrective action to be performed

by the licensee is to review

and evaluate all radiation monitoring calibration procedures

for

possible clarification of deenergization

and energization

statements.

In order to partially solve the problem of spurious

CVIs, the

licensee

issued

design

change

(DC) 2-OJ-40119 to change

the time

constant in several

radiation monitors to slow down the response

time of the detectors

and enable

them to be less sensitive to

disturbance

and noise.

The resultant delay in response

time is less

than .1 of the total channel

response

time,

and according to the

licensee, will still meet the Technical Specifications

required

response

time for the radiation monitoring system.

This event,

and other spurious actuations,

are also being studied

by

the licensee's

Noise Reduction Task Force in an effort to determine

cause

and effective corrective action to prevent reoccurrence.

Additionally, a Radiation Monitoring System

Upgrade

Program to

replace existing radiation monitors that cause

CVIs has

been

instituted.

The replacement

radiation monitors are to be more

reliable

and less sensitive to electrical

noise.

Inadvertent

CVI from Induced Noise

On May 15, 1987,

a Unit 2 CYI occurred

as

a result of an

unidentified electrical perturbation

on an instrument

AC power bus

.

to plant vent RM-14B.

Numerous control

room alarms,

powered

by the

identical instrument

AC bus,

were received

and immediately cleared.

Accordingly, the licensee

contributed the cause of the momentary

perturbation to momentary shorting of the bus from maintenance

activities in the plant.

The corrective actions

taken

by the

licensee to prevent re-occurrence

are identical to those described

in the above

CVI for plant vent monitor RM-14A.

f.

Intermediate

Ran

e Hi

h Flux Reactor Tri

On May 11, 1987, with Unit 1 in Mode 3,

STP I-3A "Calibration

Procedure for Intermediate

Range

Channel"

was being performed

on

intermediate

range

channel

N-35, in preparation for restarting the

unit.

Mhile the channel

was being tested,

a control power fuse

on

that channel

blew, causing

an intermediate

range high flux trip on

protection channel

1.

This in turn caused

an intermediate

range

high flux reactor trip, which caused

reactor

main trip breakers

A

and

B to open.

I

The control power fuse blew just as the simulated input test signal

reached

the P-6 setpoint

and flashed the P-6 bistable.

The fuse was

replaced with a similar correctly sized fuse,

and the identical

calibration process

was repeated at least six times in an attempt to

determine if the fuse would blow again.

No failure of the fuse

occurred.

Functional test

STP I-3A was then completed with no

further interruption.

In analyzing root cause of the event,

the licensee

determined the

fuse failed due to "end-of-life," documented

the fuse failure,

and

included the fuse in a data

base for trending.

Failure of this fuse

had not occurred before.

The inspector questioned

licensee

management

as to whether

a more

indepth root cause analysis

would be more appropriate.

Further

examination of the fuse by X-rays to determine if the fuse

had

previously approached

the point of failure and possible

comparison

of electrical

loads

between

IR channels

at the P-6 setpoint were

suggested

by the inspector.

The licensee

agreed to evaluate

the

benefit of further investigation.

The blown fuse replacement policy at Diablo Canyon is that when

a

blown fuse is encountered:

1.

A determination is made

as to whether or not this has

been

a

recurring situation;

2.

A visual inspection for damage

and burned material

odor check

are made;

and

3.

If fuse failure is determined to be recurring or there is

evidence of damage,

indepth analysis

and corrective action are

required prior to returning equipment to service.

However, if fuse failure is determined to not be recur ing, and

there is not indication of damage or degradation,

the fuse

may.

be replaced with the appropriate

rated fuse.

The equipment

then functionally checked

and returned to service.

In all

cases

an Action Request is initiated to document the incident.

The licensee

investigated

the blown fuse replacement policy at

six other operating nuclear generating stations.

Five of those

consulted indicated their-policy was in agreement with Diablo

Canyon policy.

One licensee

indicated that, in some cases,

a

root cause

analysis

was performed

on the equipment, prior to

returning the equipment to service,

following the first

incident of a blown fuse.

Based

on a industry experience that

some fuses

do age,

resulting in their below rated value

open circuiting, and that

Diablo Canyon's policy is in keeping with the industry

standard,

the licensee

concluded that their policy will not be

altered.

However, the licensee

also concluded

steps

are to be

initiated to assure

the existing policy regarding documentation

of blown fuses is clearly presented

to all maintenance

and

operating personnel

on

a recurring basis.

g.

Inadvertent Start of Emer enc

Diesel Generator

2-1

On Hay 14, 1987, at 1021 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.884905e-4 months <br />,

an I8C technician inadvertently

started Unit 2 Emergency Diesel Generator

(D/G) 2-1.

The technician

had been instructed to perform the portions of I&C loop tests

associated

with diesel

generator

alarms

and annunciators.

Loop

tests

are the procedures

used

by I8C for the calibration

and testing

of instrumentation

and controls not accomplished

by a Surveillance

Test Procedure.

Although the Work Order related to the loop tests

required shift foreman 'approval, there

was

no clearance

issued for

D/G 2-1 so the loop tests

were performed

on an operable diesel

generator.

The technician

had been attempting to perform the loop

test (LT 21-19C) for jacket water pressure

'switch (PS)

229.

The

loop test

he had been issued

had

a significant error in that there

was

no direct annunciation

associated

with PS 229.

The portion of

LT 21-19C that required the annunciation testing

was related to

PS

227 and

PS 236.

This portion had been included in LT 21-19C when it

was written, due to a computer file transposition error.

The errant

loop test

was independently

reviewed

and approved

by an I8C

engineer,

and again approved

by the

I8C general

foreman for use.

To compound

an already undesirable situation,

the

I&C technician

attempted to perform the loop test,

despite its obvious errors,

without stopping the work activity and consulting his supervisor.

PS 229 is in series with a set of contacts

related to engine start

relay ESRlA.

When both sets of contacts

are

made

up they energize

jacket water pressure

relay JWPRl and

JWPR1A.

The technician

was

misled to believe,

by the loop test, that

he needed to energize

JWPR1

8

1A to accomplish the annunciation.

To do this, the

technician realized

he needed to jumper the contacts for ESR1A.

The

I8C technician

proceeded

to jumper the contacts without this action

being specifically addressed

in the loop test.

When the desired

results

were not achieved, i.e.

no annunciation,

he

assumed

his

problem was

an inadequate

jumper across

the contacts

related to

ESR1A.

Without a specific instruction in the loop test,

the

technician manually tripped

ESRlA to make

up the contacts.

Tripping

ESR1A started

D/G 2-1.

It should

have

been apparent to the I8C technician that the work

required to energize

JWPRl 4 lA was not described in LT 21-19C.

Having realized this,

he should

have stopped

work and discussed

the

loop test with his supervisor.

The first indication to the

technician that

LT 21-19C was inadequate

was that to energize

JWPR1

8

1A a jumper had to be placed across

contacts

on ESRIA.

This was

not described in the loop test.

Administrative Procedure

AP C-4Sl

"Mechanical

Bypass,

Jumper

and Lifted Circuit Log Accountability

System:

in the General

section,

paragraph

E states:

"1.

Momentary jumpers

do not require logging on a formal jumper log

but shall

be listed on the...Momentary

Jumper Status

Sheet.

2

Momentary jumpers shall

be controlled by an approved procedure,

work order,

shop work follower, or clearance

request."

Therefore, to place

a jumper on the electrical

equipment of an

operable diesel

generator,

logging and control of the jumper

was

required.

This is an apparent violation (Open Item

50"323/87-20-01).

The second indication to the technician of the inadequacy of LT

21-19C is that it did not require the operation of ESRlA. If the

technician believed this was required to complete the loop test,

he

should

have consulted his supervisor.

A technician

should not,

operate

relays

on operable

safety related

equipment

unless

explicitly directed to by procedure.

As corrective action the

concerned

individual was counselled.

In addition, the licensee

has

undertaken

a program to instruct all plant personnel

on the

importance of procedural

compliance.

As stated previously,

LT 21-19C included

a significant error, in

that portions of. another

loop test

had been included with it.

This

error misled those issuing the test to the field to believing there

was

an annunciator

associated

with PS 229.

Had there not been

an

annunciator test portion of LT 21-19C, the test would not have

been

issued to the field.

A second

weakness

in the loop test is it did not include

a

prerequisite to have the diesel

declared

inoperable for the test.

PS 229 performs

a safety related function, redundant with PS 230, to

energize jacket water pressure

relays

JWPR1 and lA, when the jacket

water pressure

reaches

operating pressure.

Among other functions,

JWPRl and lA supply signals to shut the starting air solenoid valves

and to flash the generator field.

With the jumper installed, if PS

229 failed high (with it contacts

closed)

JWPR1 and

1A would

10

energize

immediately placing the diesel

generator

in a possibly

inoperable condition.

Loop test

21-19C was generated

as

a result of the loop test writer'

guide Administrative Procedure

AP C-454 "Instrumentation

and

Controls

Loop Test Program."

AP C-454 was issued in July 1986, in

an effort to upgrade

the loop test program, in response

to gC

findings of the inadequacy of the loop test program.

The guidance

provided in AP C-454 appears

to be adequate

to generate

loop tests

appropriate to the circumstances.

However, the adequecy of the

implementation of AP C-454 is questionable

in light of LT 21-19C.

As corrective action with regards

to the inadequacy of LT 21-19C,

the licensee

has initiated the following corrective Wtjons:

1.

A review of associated

loop tests for the

same data sheet error

contained in LT 21-19C.

2.

A discussion with all loop test originators

and reviewers

on

how the transposition error occured.

3.

A review of the conformance of the loop test program to ANSI

N18.7 1976Property "ANSI code" (as page type) with input value "ANSI</br></br>N18.7 1976" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. and the development of an action plan to review all

safety related

loop tests

based

on the review of the program.

The inspector

has found, in general, that the quality of loop tests

has. suffered in the effort to produce the numbers required for the.

current refueling outage.

The licensee's

corrective actions related

to the adequacy of the loop test program will be tracked

as

an

unresolved

item (Open Item 50-323/87-20-02).

D/G 2-1 was inadvertently started at 1021 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.884905e-4 months <br />.

It's actuation

was

immediately apparent

in the control

room and was recorded in the

control operator's

logs.

10 CFR 50.72(b)(ii) requires that the

licensee notify the

NRC within four hours of any event or condition

that results in manual or automatic actuation of an Engineered

Safety Feature

(ESF).

The shift foreman

on duty did not recognize

the inadvertent diesel

generator start to be reportable

and,

accordingly, did not make

a report to the

NRC until 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br />

(after it was identified by his supervisor

as reportable).

Another

recent

example of weakness

in the operations

department's

implementation of reporting requirements

for events

was the late

reporting to the County of San Luis Obispo of the main turbine fire.

The late reporting of the diesel start event is an apparent

violation of 10 CFR 50.72.

(Open Item 50-323/87-20-03).

Vortexin

of RHR

Pum

2-2 Durin

Cavit

Draindown

On Hay 12,

1987, in preparation to replace

a source

range detector

on Unit 2, operators

were pumping down the water level in the

reactor vessel cavity, transfer ring the water to the Refueling Mater

Storage

Tank (RMST) at about 3,000 gallons per minute (gpm)

utilizing Residual

Heat

Removal

(RHR) pump 2-2.

An operator

was

stationed

inside containment to visually observe water level in the

11

cavity.

The wide range

and narrow range reactor vessel

refueling

level indication system

(RVRLIS) was available to operators

in the

.

control

room.

Operating

Procedure

(OP) B-2:VI was in use to control

the pumpdown,

and specified that the

RHR pump was to be stopped

when

water level in the reactor vessel

reached

the 113'levation

as

indicated

by RVRLIS.

A disparity between

RVRLIS and actual

observed

cavity water level

was identified when wide range

RVRLIS indicated

115 1/2'hile actual

observed

level inside containment

was reported

to be 117'.

Discussions

were held on the Shift Foreman

(SFM),

Senior

Control Operator

(SCO),

and Control Operator

(CO) level in an

attempt to identify the cause of the disparity.

However,

pumpdown

was allowed to continue

as the disparity increased.

When

RVRLIS

reached 113'levation,

10 minutes after identification of the

disparity,

RHR flow was throttled back, but the

RHR pump was not

stopped

as required

by OP B-2:VI.

Operators

assumed

indicated

RVRLIS water levels were incorrect,

since

an operator inside

containment

was directly visually identifying cavity water level.

Over the next

2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> period, the

RHR pump was allowed to vortex

twice,

even though discussions

and assessments

were conducted

by the

operators

on at least three occasions for periods varying from 6

minutes to 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

However, having not stopped

RHR pump operation

once water level indication disparities

were observed,

and failure

to obtain upper management

review and concurrence of a systematic

approach for problem resolution of a first-of-a-kind problem prior

to continuation of plant evolutions are considered

to be improper

operation of the facility outside established

procedural

guidelines.

Due to the complexity of this event,

a detailed description is

provided below.

In preparation to replace Unit 2 source

range detector

N-31, water

in the refueling cavity was to be pumped to the

RWST by

RHR pump 2-2

discharging through the

RHR heat exchanger

and valve 8741

(RHR

return to RWST).

Normal

RHR system discharge

to loop 3 and 4 cold

legs

was to be isolated,

and cavity pumpdown rate

was to be

controlled using HCV-637 (RHR Hx 2-1 outlet flow control valve) with

RHR pump 2-2 recirculation valve in automatic.

An

On-The-Spot-Change

to

OP B-2:VI "RHR - Draining the Refueling

Cavity" was issued

and approved to control the evolution.

Precautions

were included in the procedure to caution against

dropping the water level in the reactor vessel

to the point where

suction to the

RHR pumps could be potentially lost.

The reactor

was

to be completely defueled prior to initiating cavity draindown.

Narrow range

RVRLIS was to be enabled

and hooked

up to a multipoint

recorder,

and providing low level alarms.

OP B-2:VI specified

once

water level in the refueling cavity was lowered to about

one foot

above the reactor vessel

flange, the refueling cavity pumpdown rate

was to be throttled back using HCV-637.

OP B-2:VI further directed

that when water level

was lowered to about

1 foot below the reactor

vessel

flange (approximately

113 foot elevation

on RVRLIS or tygon

tube indication),

RHR pump 2-2 was to be stopped

and final vessel

pumpdown

was to be accomplished

using the refueling water

purification system.

12

From an initial cavity water level of about 138'elevation)

cavity

pumpdown was initiated,

and continued at a rate of approximately

3,000

gpm.

Wide range

RVRLIS LI-956 indicated agreement with the

"Reactor Vessel

Refueling Level" alarm received at 137'".

The

trend recorder

read

1 1/2" less.

The cavity water level

was being

observed

by an operator stationed

inside containment to confirm

control

room indications.

The temporary narrow range

RVRLIS

recorder

was not functioning (in violation of the procedure)

and I8C

technicians

were investigating the problem.

At 115'" wide range

RVRLIS, the watch inside containment reported water level to be

'117'.

Possible

causes

for the 1 1/2'isparity were discussed

by

operations

personnel

as

pumpdown continued.

It was decided that a

correlation check between

RVRLIS and visual level could be

accurately~erformed

only at the vessel

flange level.

Wide range

RVRLIS incficated

a level of 114', but visually the level appeared

to

116 1/2'a

2 1/2'isparity).

Pumpdown flow rate

was not throttled

at 115'ince visually the level

was at 116 1/2'nd the operators

questioned

the accuracy of the

RVRLIS.

Shortly thereafter,

wide

range

and narrow range

RVRLIS both indicated

113 1/2'hile the

watch reported

a 116 1/2'evel (disparity increasing to 3').

HCV-637 was closed

and

FCV-641B then opened in automatic,

placing

RHR pump

2-. 2 on recirculation.

This was contrary to the

May ll,

1987,

OTSC to

OP B-2:VI, which specified in step

14 that

RHR pump

2-2 be stopped at "approx. 113'VRLIS on tygon tube indication."

At this point,

RVRLIS alarm setpoints

were changed

from wide range

values to narrow range values of 107'" (low) and 113'" (high).

Discussions

regarding discrepancies

between indicated level

and

observed

level continued for about

an hour and centered

around

possible

causes

such

as

improper venting, valve lineups,

and

instrumentation errors.

An auxiliary building auxiliary operator

(AO) was sent into containment to verify RVRLIS lineup.

Inside

containment,

the watch indicated level dropped about

3 inches but

was still at about 116'o

116 1/2'.

RWST level trended

up very

slowly and

RVRLIS still dropped but at a much slower rate.

The

SFM,

SCO and

CO agreed that the continued

change in levels

was

due to

leakby past the seat

on butterfly valve HCV-637, causing about 200

gpm flow to still be going to the

RWST.

A decision

was

made to

allow RHR pump 2-2 to continue to run on recirculation to allow

visual cavity level to slowly drop to reactor vessel

flange level

(114'levation) at the rate of about 200

gpm.

The auxiliary

building AO reported that the

RVRLIS lineup inside containment

was

good.

A senior reactor operator

(SRO) was sent into containment to

independently verify the

RVRLIS lineup was correct.

I8C was still

unable to get the temporary

RVRLIS recorder to work.

At about

1 1/2 hour s after the first discrepancy

between

RVRLIS and

direct visual indication inside containment

was noted,

an

approximately

4 amp fluctuation of the

RHR pump 2-2 motor was

observed

by the

SFM, and the

pump was shutdown.

RVRLIS indicated

107'hile the watch inside containment

reported the cavity water

level at 116 1/2'.

The

SRO inside containment

doubted cavitation of

the

RHR pump since water remained in the cavity.

During the next

forty minute period, the

SRO inside containment

checked

the

RVRLIS

13

lineup and found it to=be satisfactory,

while the auxiliary AO

vented

RHR pump 2-2 and found little air in the pump.

Simultaneous.

discussions

were held in the control

room to address

the discrepancy

between

RVRLIS and actual

observed

level in the cavity.

Since

no

fuel was in the reactor,

the

SFM concluded that additional plant

evolutions should

be performed at that time to indentify and correct

whatever procedural

or indication problems

were causing the

discrepancy.

The limiting factor to the evolutions

was to protect

the

RHR pump from damage.

Inside containment,

the

SRO placed the

tygon tube level

guage in service.

The refueling water purification pump was started to pump water

from

the refueling canal to the

RWST, and cavity water was lowered to

114'.

Concurrently, for about six minutes,

discussions

continued

on

the

RVRLIS indication problem.

One possible explanation

given for

the fluctuating amps

on the

RHR pump was that the

pump recirculation

valve (FCV-641B) might have

been cycling due to flow being near the

valve's flow control setpoint.

Accordingly, to assess

this possible

explanation,

the

AO was directed to close

manual

valve V-8741

stopping discharge

to the

RWST.

The

RHR pump was then started

on

recirculation with an

AO stationed at the

pump to listen for

cavitation.

Valve 8809B was then opened

by the

CO and HCV-637 was

throttled to direct flow to the loop 3 and 4 cold legs.

Pump

amps

again fluctuated,

the

pump was shutdown,

and both valves were

closed.

No sounds of pump cavitation were detected

by the

AO at the

RHR pump.

For the next 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 20 minutes,

the indication problem was again

discussed.

Inside containment,

the watch reported cavity level to

be at 115'nd decreasing.

The

RHR pump was vented

once again, with

little air found.

Further discussion

regarding possible

causes

of

the encountered

problems continued.

The

SRO inside containment

reported tygon tube level indication reading

107 1/2

, agreeing with

both wide and narrow range indication (LI-956 and LI-957).

A

decision

was then

made not to restart the

RHR pump due to numerous

indications that water level inside the reactor vessel

was low, even

with

1 foot of water above the flange in the cavity.

After a brief discussion,

a decision

was

made to reflood the vessel

from the

RWST.

Valve SI-2-8980

was cracked

open to reflood the

vessel

and check

RVRLIS indication.

Both wide and narrow RVRLIS

showed

an increase after about thirty seconds.

The inside

containment

watch reported

no change in cavity level,

even though

RYRLIS indicated

a 5'evel

increase.

Eventually, the watch inside

containment reported

numerous "fountains" of water coming out of the

upper internal

package

rod cluster control guide tubes,

and

RVRLIS

indicated level at 114'.

At that time, SI-2-8980

was shut and

RVRLIS stabilized at 115'levation.

Operators

then concluded that

even though about

2 1/2'f water remained in the cavity above the

vessel

flange, the water level inside the reactor vessel

had been

lowered to 7'elow the flange.

Prints of the Unit 1 and Unit 2 top hat assemblies

were obtained,

and the explanation of the discrepancy

between indications

became

14

apparent.

The upper internals

package

was forming

a seal

on the

reactor vessel

flange since

no fuel assemblies

were in the core.

With fuel installed in the core, the leaf springs

on the fuel

assembly

top plate provided enough lifting force to unseat

the upper

internals

package

from the upper internals

support

ledge

when the

reactor

head

was not installed.

With the upper internals

package

seated

on the support ledge,

the only drain path from the refueling

cavity to the reactor vessel

was through the rod cluster control

assembly

guide tubes

and the head cooling flow holes in the upper

support plate.

Since the guide tubes

extend about

2 feet above the

vessel

flange,

once water level in the refueling cavity drops to the

two foot (116'levation) level, flow from the cavity to the reactor

vessel

is limited to the capacity of the head cooling flow holes

which is significantly less

than

RHR pump capability.

In reviewing this event,

the

NRC identified several

improper actions

by the licensee.

For

a first-of-a-kind operation

such

as this,

a

more thorough

and indepth

assessment

of the evolution should

have

been provided prior to beginning draindown.

The entire process

lacked the fundamental of a cautious

analyzed

approach.

At the

first indication of a disparity between

RVRLIS and actual

observed

level,

pumpdown of the cavity should

have

been

stopped,

an

assessment

made,

a planned out organized

approach

developed,

and

upper management

involvement and concurrence

obtained prior to

proceeding with any plant evolutions.

OTSC, Revision 0, to

OP B-2:VI, specified in step

14 "when the water

level in the refueling cavity'has

been

lowered to approximately I

foot'elow the reactor

vessel

flange, stop

RHR pump 2-2

(approximately 113'n

RVRLIS or tygon tube indication)."

Within 10

minutes of recognizing the inconsistency

between

RVRLIS and observed

cavity water level, both

WR and

NR RVRLIS indicated 113'.

However,

the

RHR pump remained

running for a period of about

1 I/2 hours

after the inconsistency

was observed until level dropped to

107'levation.

The

pump was also later restarted.

The plant evolutions

conducted

below the 107'levation water level constitute operations

outside the scope of OP B-2:VI.

Accordingly, these actions

are

considered

an apparent violation of the procedure

(Item

50-323/87-20-04).

As corrective action,

OPs B-I:VI and A-2:II were revised to define

proper

RHR flow rates

and emphasize

importance of operator reliance

on RVRLIS.

Additionally three

memos were issued to the operating

staff.

The first was

an Operations Shift Order issued

by the senior

operations

supervisor stressing

the need to perform operations

in

accordance

with good procedures.

A second

memo to all operations

personnel

was issued

by the operations

manager

regarding

use of

procedures.

Both memos stressed

that if a procedure is not

adequate,

or if unforeseen

circumstances

develop,

the operation in

process

must stop

and further guidance

be obtained prior to

resumption of work.

This philosophy is to apply regardless

of

impact on outage

schedules,

plant startup,

or required load changes.

15

The third memo from the operations

manager to shift supervisors,

shift foreman,

and shift technical

advisors

addressed

guidelines for

handling investigations of significant occurrences

and providing

information to upper management.

Additionally, PG8E

s Vice

President of Nuclear Power Generation

conducted

discussions

with

each operating

crew regarding several

items including following

procedures,

stopping work when things are not going according to

plans or when questions

develop,, and involvement of proper people

(including management)

in decision making process.

Unit 2 Refuelin

Water

S ill to the Auxiliar Buildin

On May 8, 1987,

between

1757 and 1811 hours0.021 days <br />0.503 hours <br />0.00299 weeks <br />6.890855e-4 months <br />,

several

hundred gallons

of contaminated

water spilled into the Auxiliary Building from the

Unit 2 Refueling Water Storage

Tank (RWST) through

an open flange

downstream of charging

pump 2-3 (the positive displacement

charging

pump).

The flange was

opened

when the charging pump's relief valve,

CVCS-2-8116,

had been

removed for maintenance.

Airborne and

contamination related to the spill were relatively minor and the

spill was cleaned

up within a matter of hours.

Prior to the spill, the licensee

had been preparing to establish

a

boration flow path,

as required

by TS 3.1.2.1,

in anticipation of

reloading the core.

Coincidentally,

maintenance

was being performed

on CVCS-2-8116.

On the

same clearance,

work had been completed

on

Volume Control Tank (VCT) discharge isolation valves

CVCS-2-LCV 112

B8C.

To establish

a boration flow path, the status of a number of

the clearance

boundary valves for the above work was affected.

With

work on CVCS-2-LCV 112C complete, it could

now be used

as

a boundary

valve in lieu of RWST to charging

pumps isolation valves SI-2-8805

A8J3.

In accordance

with Administrative Procedure

(AP) C-6S1,

"Clearance

Request/Job

Assignment," the shift foreman requested

the work

planning operations

coordinator to review and reissue

the clearance

to establish

a new work boundary.

In reviewing the clearance,

which

had

a total of 52 clearance

points,

the operations

coordinator noted

that charging

pump 2-3 suction isolation valve CVCS-2-8473

was

on

the clearance

but did not notice that it was listed as

open with a

"caution" tag and not closed

as

he assumed.

CVCS-2-8473

had been

left open

as

a drain path from the charging

pump suction header

through the charging

pump 2-3 separator stabilizer

and CVCS-2-558 to

the miscellaneous

equipment drain tank.

Although CVCS-2-8473

needed

to be closed

as

a boundary valve to establish

a boration flow path

since the operations

coordinator thought it was closed, it was

inadvertantly left open.

The operations

coordinator

added

two

clearance

points to the clearance,

including one for CVCS-2-LCV

112C,

and forwarded it to the operations

department

clearance

coordinator.

The clearance

coordinator reviewed the clearance

and,

just as the operations

coordinator

had done,

noted that CVCS-2-8473

was

on the clearance

but did not note its position.

The clearance

was then forwarded to the Shift Foreman

(SFM) for review and

dispositioning.

Neither the

SFM nor anyone

on his crew noted that

CVCS-2-8473

was listed incorrectly on the clearance

as

opened.

16

At 1721 hours0.0199 days <br />0.478 hours <br />0.00285 weeks <br />6.548405e-4 months <br /> the two new clearance

point valves were positioned,

tagged,

and verified.

At 1757 hours0.0203 days <br />0.488 hours <br />0.00291 weeks <br />6.685385e-4 months <br /> operations

reported off valve

.

SI-2-8805A by re-establishing

power to its breaker.

Operations

had

expected

SI-2-'8805A to remain closed,

however,

since the

YCT was

empty,

(another

requirement of the clearance),

a low level automatic

charging

pump suction transfer

signal

opened the

RWST isolation

valve.

With CVCS-2-8473 open,

a path

was established

from the

RWST

through SI-2-8805A to CVCS-2-8473, to the stabilizer separator,

through charging

pump 2-3,

and finally out the open flange for

relief valve CVCS-2-8116.

At 1810 hours0.0209 days <br />0.503 hours <br />0.00299 weeks <br />6.88705e-4 months <br />,

a security guard notified

the control

room that water was leaking out of the charging

pump 2-3

room.

At 1811 hours0.021 days <br />0.503 hours <br />0.00299 weeks <br />6.890855e-4 months <br /> the operator discovered that SI-2-8805A had

opened automatically and

he closed it.

It was estimated that 1300 gallons of water had drained from the

RWST.

Although the actual

volume of water spilled to the auxiliary

building could not be accurately

determined, it was estimated to be

several

hundred gallons.

Accurate measurment of the water spilled

was not possible

since the

RWST capacity is 400,000 gallons,

and

only a fraction of a percent of change in level of 400,000 gallon

RWST was observed.

In addition, the majority of that volume drained

through

CVCS-2-558 to the Miscellaneous

Equipment Drain Tank (NEDT)

and the actual

level

change of the

MEDT is not trended.

Therefore,

it was not possible to establish

the actual

volume of water spilled

to the Auxiliary Building.

The licensee's

investigation of this event determined

the cause to

be the inadequate

review of the clearance.

The licensee initiated a

human performance

evaluation to determine if there is a need to

revise the clearance

procedure.

The effectiveness

of the evaluation

will be tracked

as

an unresolved

item.

(Open Item 50-323/87-20-05).

Containment Ventilation Due to Source

Check on Wron

Radiation

Monitor

On May 25,

1987, in preparation for the planned discharge

of waste

evaporator

condensate

tank 0-2, auxiliary operators

were in the

process of performing the pre-discharge

checks

on Unit 1 RM-18, the

liquid radwaste effluent monitor,

as required

by OP

G-1: II "Liquid

Radwaste

System - Processing

and Discharge of Liquid Radwaste."

The

operator

proceeded

to the radiation monitor racks in the control

room, located the controls for RM-18, and proceeded

to the nearest

telephone to establish

communications with another operator at the

auxiliary building control board.

After establishing

communications,

he returned to the

RM-18 controls

and proceeded with

the source

check.

Instead of operating controls for source

checking

RM-18,

he inadvertently initiated a source

check

on RM-14B, the

plant vent radiogas

monitor, which had its controls located directly

below the controls for RM-18.

RN-14B exceeded its high trip

setpoint while being source

checked, initiating a CVI signal.

As no

containment venting was in progress,

only the isolation valves for

RMs-11812, the containment

radiogas

and air particulate monitors,

closed

as

a result of the signal (in accordance

with plant design).

17

The signal

was reset,

and RMs-11812 were unisolated

and returned to

service.

The root cause of this event

was personnel

error.

A contributing

cause

was poor human factor engineering

in the labeling of the

radiation monitoring racks in the control

room.

As corrective action, the operator involved was counseled

as to his

improper actions.

Additionally, the licensee

indicated the labeling

on the radiation monitoring racks in the control

room will be

assessed,

and revised

as necessary

to improve

human factor

considerations.

k.

Performance of Testin

on Wron

Unit

On May 25,

1987

IBC technicians

performed portions of loop test for

RCS loop 1 delta

T deviation

on the wrong unit.

The loop test

was

scheduled to be performed

on Unit 2, which was in a refueling

outage,

but was inadvertantly attempted

on Unit 1.

This resulted in

the tripping of the overtemperature

delta

T reactor trip bistable

for that loop and the bistable for overtemperature

delta

T

anticipatory rod stop

and turbine runback.

In all cases

two out of

four logic is required to initiate action

and all other channels

remained in service

so

no automatic

responses

were actuated.

The

details =of this event

and the results of the licensee's

investigation

and actions taken to prevent recurrence will be

included in the next inspection report,

50-275/87-23

(Open Item

50"275/87-20-01).

Three violations and

no deviations

were identified.

4.

Maintenance

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement, parts

were appropriately

certified.

a ~

Diesel Generator

Instrument

Panels

The inspector observed portions of preventive maintenance activities

for diesel

generator

instrument panels.

The observed activities

were performed in accordance

with maintenance

instructions with

appropriate prerequisites

and precautions

observed.

The inspector

noted that relays

(Westinghouse

ARD relays) within the

instrument panel

were similar to relays at Palo Verde which had

a

problem with debris in the relay.

The inspector discussed this

problem with the electrical

foreman.

The electrical

foreman planned

to evaluate

the need for further inspection of the relay.

18

b.

Motor 0 crated Valve

MOV

Tor ue Switch Settin

The inspector

observed electrical

maintenance

personnel

perform

torque switch setting

on eight inch

MOV SI-2-8804B

(RHR heat

exchanger

2 to the SIS pumps).

The valve motor operator

was

a

Limitorque model

SMB-1.

Work was accomplished

in accordance

with

work order C0013380

and approved

On-The-Spot

changes

to Maintenance

Procedure

E-53.10B "Limitorque Operator Torque Switch Adjustment."

Manual

hand wheel closing thrust readings of 9440,

9580,

and 9280

pounds

were recorded

and were witnessed

by a gC inspector.

These

readings

exceeded

the minimum acceptable

value of 8550 pounds

thrust.

The gC inspector also witnessed

the motor closing thrust

(torque switch setting),

which was found to be 21470,

21420,

and

21160 pounds

(due to motor inertia).

These values did not exceed

the stem stud

maximum yield of 25540 pounds thrust and were thus

also acceptable.

Test equipment,

including the load cell set,

was calibrated.

From a

review of documentation

associated

with recent valve operator

maintenance,

the inspector

determined

the proper grease

(Exxon

Nebula

EPO)

had been

used in the main gear case.

C.

Containment

Sum

to

RHR

Pum

2-2 Suction Isolation Valve

The inspector observed portions of a corrective electrical

maintenance activity performed

on the containment

sump to

RHR pump

2-2 suction isolation valve (SI-2-8989B).

During

December of 1986,

the licensee

performed

an environmental qualification inspection of

the valve operator motor,

and discovered

a hairline crack on one of

the limit switch rotors.

Since the defect was determined

not to,

affect the operability of the valve, the licensee

scheduled its

replacement for the refueling outage.

The- inspector witnessed portions of the limit switch rotor changeout

and determined that a-certified replacement part was used.

In

addition, appropriate

technical specifications

were

met.

Tagouts

and administrative approvals

were obtained

and qualified personnel

performed the job.

d.

Main Steam Safet

Valve Settin

with H draulic Assist

On the evening of May 12, the inspector witnessed

the performance of

Maintenance

Procedure

(MP) M-4.11 "Main Steam Safety Valve Setting

with Hydraulic Assist" for Unit 1 main steam relief valve 1-RV-7.

1-RV-7 had apparently lifted the previous

evening at a point lower

than the 1035 psi setpoint for the 10K steam

dumps.

The nominal

setpoint for the lowest set main steam relief valves is 1065 psi +

or - 11 psi.

Lifting prior to the actuation of the

10K steam

dump

indicated that the setpoint for 1-RV-7 had drifted low.

Unit 1 was,

at that point, in MODE 3.

Prior to proceeding to

MODE 2, the

licensee

performed

MP M-4.11 to set the relief valve within

tolerance.

19

The inspector

noted that all prerequisites

were met and that the

test was performed

by qualified personnel.

In addition,

communications

were established

between

the maintenance

personnel

and the control

room.

The inspector also observed that

a qualified

QC specialist

observed

the testing in accordance

with an appropriate

QC inspection plan.

The as found lift point of the relief valve was

found to be approximately

1048 psi.

The valve was reset to

approximately

1075 psi.

The difference

between

the as found lift

point and the lift point reported

by operations

was attributed to

the response

time of the

10% steam

dumps

and the accuracy of the

control

room steam pressure

chart recording.

Hot Bendin

of Unit 2

RHR Pi in

On May 4, 1987, swing shift mechanical

maintenance

personnel

heated

a portion of Unit 2

RHR Train A piping to 1200 degrees

Fahrenheit,

in

an attempt to hot bend the pipe, without the use of a qualified

procedure.

The details of this occurrence

and the results of the

licensee's

investigation

and actions

taken to prevent recurrence

will be included in a subsequent

inspection/investigation.

This

occurrence will be tracked

as an. unresolved

item (Open Item

50-323/87-20-06).

The review and approval

by a

QC planner of the work order allowing

the hot bending of safety related piping indicates

a lack of

familiarity of the

QC planner of the heat sensitizing effects of

heat

on austenitic stainless

steel.

It should

be apparent to all

QC

planners that any time heat is applied to safety related piping a

special

process

procedure is required.

In addition, the licensee's

procedure

which provides the work control document review guidelines

for QC planners

showed weakness.

The inspector

reviewed Quality

Control Procedure

QCP-10.4

"Work Control

Document Review."

The

purpose of the procedure is to define the method for the Quality

Control Department's

review of work control documents

and as

such is

the governing procedure for the

QC planner's

review of work orders.

The instructions in the procedure state that the

QC planner

"...shall review the work control document for technical

and quality

requirements

using the appropriate checklist included in the

appendices

to this procedure."

However, the appendices

of QCP 10.4

does not include

a checklist for the review of work orders although

the work order format for work control

documents

has

been in use

since July l986.

Had the checklist in the appendices

of,QCP 10.4

been

updated in a timely manner following the initiation of the work

order system, it is possible

the

QC planner reviewing the package

would have required the use of a special

process

procedure.

Independent of the inspector's

review and the corrective actions of

the licensee

related to this event,

the Quality Control Department

also identified the deficiencies

contained in QCP 10.4.

A review of

Quality Control Procedures

was performed

by QC during the months of

April and May, 1987 to verify compliance with quality assurance

requirements

and other committments.

This review concluded that

QCP

10.4 needed

to be revised to reflect the work document

system

presently being used.

The inspectors

questioned

why a revision to

20

No

gCP 10.4 was not initiated with the institution of the work order

system.

This issue

and the timely revision of gCP 10.4 will be

tracked

as

an unresolved

item.

(Open Item 50-323/87-20-07).

violations or deviations

were identified.

5.

Surveillance

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

a ~

Stroke Time Testin

of Steam Generator

1-2 Blowdown Sam le

Containment Isolation Valve 1-FCV"248

The inspector witnessed the performance of Surveillance Test

Procedure

(STP) V-2J "Exercising 5 Position Verification of Power

Operated

Valves for Outside Containment Isolation Valves" and

STP

V-3S2 "Exercising Phase

A Containment Isolation Valves

(Steam

Generator

Blowdown)" on steam generator

1-2 blowdown sample

containment isolation valve 1-FCV-248.

For these tests,

1-FCY-248

was cycled for the observation of the actual

valve position and an

isolation time of less than

10 seconds.

The tests

were performed in

accordance

with the procedure

by the operations

crew under the

supervision of the Unit 1 senior control operator.

The valve testing

was required

when it had failed to reposition

properly during the performance of STP I-lllA"Functional Test of

Steam Generator

Blowdown Sample Effluent Liquid Monitor RM-19,"

which required the stroking of 1FCV-248.

The valve was closed,

as

required

by the TSs

and declared

inoperable.

STPs V-2J and V-3S2

were performed after corrective maintenance.

With the completion

and review by the Unit 1 shift foreman of STPs V-2J and V-3S2,

1FCV-248 was returned to service.

b.

Unit 2 Containment Isolation Valve Local

Leak Rate Testin

The inspector witnessed

the performance of STP V-600 "General

Containment Isolation Valve Leak Tests"

on a number of containment

isolation valves.

The inspection

was performed to satisfy

NRC

inspection procedure

61720 "Containment

Local

Leak Rate Testing."

However, this inspection

was not complete at the end of the

inspection period and therefore will appear in the next inspection

report,

50-323/87-22.

No violations or deviations

were identified.

6.

Unit 2 Refuelin

Outa

e

a 0

Fuel

Assembl

Reconstitution

The inspector

observed portions of the licensee's

efforts to replace

damaged

fuel rods in three fuel assemblies

with inert steel

rods.

21

Sampling of primary reactor coolant for Unit 2 during power

operations

indicated that there

had been

some

damage to fuel rods..

As a result, the licensee

performed ultrasonic testing

on all fuel

assemblies

after they had been placed in the spent pool

and

identified three assemblies

with one

damaged fuel rod a piece.

The

licensee

contracted

Westinghouse

to replace the

damaged

fuel rods

with inert steel

rods,

a process

known as fuel reconstitution.

The procedure for fuel reconstitution

includes the following steps:

1)

The-fuel assembly is taken from its spent fuel rack position

and placed in a canister in a special

elevator.

2)

The lid on the canister is shut, the assembly rotated

on its

axis,

and the bottom lid is opened

exposing the bottom nozzle.

3)

The bottom nozzle is removed.

Since the nozzle is welded to

screws which attach to the

RCCA guide thimbles (24 locations)

some weld grinding is required.

4)

The faulty fuel rod is lifted from the assembly

and placed in a

special

rack that can hold a number of rods.

The rack is

placed in a corner location in the spent fuel racks.

A steel

rod is inserted in the position of the old fuel rod.

5)

A new nozzle is placed

on the assembly,

with new screws

attaching it to the 24 guide thimbles.

The screws

are then

crimped 'to the nozzle with a special

crimping tool.

6)

The canister lid is closed

and the fuel assembly is rotated to

its upright position,

removed from the elevator

and placed in

the spent fuel racks.

The fuel reconstitution

was performed using

a licensee

approved

Westinghouse

procedure.

The inspector observed that steps

in this

procedure

were executed carefully and methodically.

The four member

Westinghouse

team appeared qualified and knowledgeable of their

procedure.

The torquing of the nozzle screws

and the crimping of

the screws

was accomplished with calibrated instruments

to values

established

in the procedures.

The inspector

noted that precautions

and limitations were observed.

Proper controls were established

for the fuel handling area.

Of

note,

a "hot particle zone"

was established for the area

around the

spent fuel pool in an effort to control the spread of hot particles.

To date,

the licensee

has

had little problems with hot particles.

However, they are proceeding with caution in the fuel handling area

since the most likely source of hot particles

are the tools that are

used at at other plants

and brought to Diablo Canyon.

All personnel

gaining access

to the "hot particle zones"

are required to attend

a

lecture

on the control of the particles.

No violations or deviations

were identified.

22

7.

ualit

Hotline Effectiveness

~

~

~

The inspectors

reviewed the licensee's

evaluation of guality Hotline

concerns87-001 through 87-006.

The concern evaluations

were in

accordance

with the licensee

s guality Hotline policies

and procedures.

The guality Hotline Summary Reports acceptably

addressed

the concerns

and

documented

the-actions

taken.

In discussions

with various site personnel,

the inspectors

were informed

that there

was

a feeling that use of the guality Hotline by an individual

could result in repercussions.

This feeling was conveyed to Hotline

management,

Mr. Lieber.

Mr. Lieber indicated

he would address

this issue

in the- next

GONPRAC meeting.

This will be followed as followup item

(Open Item 50-275/87-20-02).

No violations or deviations

were identified.

8.

Licensee

Event

Re ort Follow-u

a.

Status of LERs

Based 'on an in-office review, the following LERs were closed out by

the resident inspectors:

Unit 1:

86-14, 86-17, 87-05

No violations or deviations

were identified.

9.

Exit

On June 10,

1987 an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.

I>>