ML16162A506
| ML16162A506 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 11/04/1983 |
| From: | Black K NRC OFFICE FOR ANALYSIS & EVALUATION OF OPERATIONAL DATA (AEOD) |
| To: | |
| Shared Package | |
| ML16162A505 | List: |
| References | |
| TASK-AE, TASK-NT304 AEOD-NT304, NUDOCS 8312140321 | |
| Download: ML16162A506 (11) | |
Text
AEOD TECHNICAL REVIEW REPORT*
UNIT:
Oconee 1, 2, and 3 TR REPORT NO.
AEOD/NT304 DOCKET NO.:
269, 270, 287 DATE:
November 4,1983 LICENSEE:
Duke Power Co.
EVALUATOR/CONTACT: K. Black NSSS/AE:
Babcock & Wilcox/Duke-Bechtel
SUBJECT:
HUMAN FACTORS INVOLVEMENT IN EVENTS AT OCONEE 1, 2, AND 3 EVENT DATES:
821213 (manual containment valves on Oconee 3 left open on all units) 830303 (manual sample valve left open on all units by Oconee procedure) 830316 (double isolation criterion for Safe Shutdown Facility not met) 830317 (test valve on Oconee 3 emergency air lock left open) 830317-23 (inner hatch door on emergency air lock on Oconee 1 left open)
SUMMARY
Between December 1982 and March 1983, Oconee reported a series of five events related to containment integrity. Human factors were important contributors to these five events. The last two events, both of which occurred on March 17, 1983, were the subject of escalated enforcement action.
The AEOD Nonreactor Assessment Staff (NAS) undertook a review of the events because a number of events associated with the same system occurred over-a short period of time.
The review showed that corrective actions were taken for each of the events.
In addition, Oconee personnel undertook an extensive review of directives and procedures related to independent verification of performance of operational activities affecting safety-related equipment. A management audit team was also established to review operational activities to assure that they were conducted in a quality manner..
AEOD believes the response to the event represents a comprehensive effort to reduce the contribution of human error to these and other types of future events.
DISCUSSION AEOD Reactor Operations Analysis Branch recognized a series of reportable events that involved human errors by Oconee personnel and informed the.
Nonreactor Assessment Staff of the fact. The NAS undertook a review of LERs This document supports ongoing AEOD and NRC activities and does not represent the position or requirements of the responsible NRC program office.
8312140321 831104 PDR ADOCK 05000269 PDR
-2 submitted by Oconee, Inspection Reports, and Duke Power correspondence to determine whether a generic problem existed.
Table I presents a chronology of the events and management initiatives to review activities associated with containment integrity.
In December 1982, the first of the series of events was reported n which human factors contributed to degradation of containment isolation.
With Unit 3 in cold shutdown, two (instrument air) Manual Containment Isolation Valves were found open. It was determined that the valves had been open between December 6 and December 8, 1982 with the reactor coolant pressure and temperature greater than 300 psig and 200*F respectively.
Technical Specification 3.61 was violated.
The LER for the event was classified as requiring no additional review by AEOD.
Some time after the above report was made to NRC, the Oconee Operations Superintendent requested an investigat on of activities related to containment integrity within the operations group.
This investigation resulted in dis covery of two incidents:
a manual sample valve was specified to be left in the open position by Oconee procedure, even though technical sp cifications required it to be closed (it is a containment isolation valve);
and, the tie-in of the Standby Shutdown Facility (SSF) to the fuel transfer tubes failed to meet containment isolation criteria.4 The LER for the valve misposition was classified by AEOD as requiring no additional review; the disposition of the LER on the SSF was not found in WAMS. (The SSF is not operational.)
During the required quarterly surveillance tests of containment, two other events were discovered. In one, a pressurization connection valve on the Unit 3 Emergency Access Air Lock Hatch had been left open and was found to be leaking air. The valve is classified as a containment isolation valve. The valve is known to have been closed on December 17, 1982, and was discovered to be open on March 17, 1983.5 In the other event on March 17, 1982, the inner Emergency Hatch door on Oconee 1.was inadvertently opened after the outer door was closed. The door remained open for four days, even though the Emergency Hatch inner/outer door open statalarm in the control room was actuated. 6 Both events were classified as requiring no additional review by AEOD. The two events were the subject of escalated enforcement action by IE.
Following the two events of March 17, Oconee personnel began a review of directives and procedures related to independe t verification of operational activities affecting safety-related equipment.
Duke provided a description of its activities in a letter to Region II dated April 29, 1983.
(The letter follows meetings with Region II on March 23, 1983 and April 19, 1983.)
Table 2 gives a brief description of the event, plant status, and cause of the above events.
FINDINGS Duke Power has reported a series of five events in which human error contributed to degradation of containment integrity. After the first event, Oconee instituted an investigation of activities related to containment integrity and discovered and reported two other events.
The final two events occurred during a required test of personnel emergency air locks. Following.these two incidents, Oconee
-3 instituted a review of directives and procedures related to independent verification of performance of operations activities affecting safety-related equipment, not limited to containment. In addition to these reviews, Oconee instituted specific corrective actions for each event designed to prevent the recurrence of the event.
Table 3 lists actions undertaken by Oconee as a result of the first, fourth, and fifth events.8 CONCLUSIONS Although none of the events contributing to degradation of containment integrity at Oconee that were reviewed by AEOD were judged to be significant, the number that occurred over a short period of time (four months) caused us to review the events. The fact that two of the events were the subject of escalated enforcement may.have resulted in greater responsiveness by the licensee than
-would otherwise have occurred. Oconee has instituted corrective actions for each event and committed itself to establishing a containment integrity procedure that includes two component check lists--isolation and verification. A similar system check procedure was instituted in the summer of 1979 on certain systems; since implementa ion, none of the systems subject to the check has been.found in a degraded mode.
A management audit team has also been established to review: the process of review and determination of compliance with regulatory requirements; the station modification process; prc-edural development; the overall audit process; and personnel qualification.+/-1
-AEOD believes the Oconee response to the events represents a comprehensive effort to reduce the contribution of human error to these and other types of future occurrences. No further action appears necessary at this time.
RefereEcTS-W
- 1. LER 287/82-15/01T
- 2. Letter to James P. O'Reilly, NRC from Hal B. Tucker, Vice President, Duke Power Company, April 29, 1983, p. 1 of documentation.
- 3. LER 269/83-07/01T
- 4. LER 269/83-05/03L
- 5. LER 287/83-04/01T
- 6. LER 269/83-10/01T
- 7. Ref. 2, p. 8 of documentation
- 8. Letter to Director, I.E. from Hal B. Tucker, Vice President, Duke Power Company, July 1, 1983 p. 4 of Attachment 2.
- 9. Ref. 2, p. 9 of documentation
- 10.
Ref. 2 p.. 10 of documentation
Table 1 0
Chronology of Events at Oconee Involving Compromise of Containment Integrity and Management Initiatives Date Event 821213 Region II was notified that 2 manual isolation valves were open LER 287/82-15 submitted 821230. Valves were open from 821206 821212 with unit above 300 psig and 200*F with fuel in core.
821231 or Management Initiative 1 - Oconee operations superintendent asked later*
for investigation related to containment integrity activities within Operations Group.
830303 As a result of Management Initiative 1, a manual sample valve was discovered being left in open position even though tech specs required valve to be closed.
Oconee procedures change required valve to be open (LER 269/83-07, submitted 830322).
830316 An engineering evaluation was conducted on March 16, 1983 as part of followup actions to Management Initiative 1. LER 269/83-05 submitted 830415; the double isolation criterion for SSF RC Makeup System was not met.
830317 Test valve on Oconne 3 RB emergency airlock was left open (LER 287/83-04).
83031.7/21 At 100% power, inner hatch door on Oconee 1 was inadvertently opened and remained open for four days. Task force formed.
(LER 269/83-10) 830321 or Management Initiative 2 - Oconee personnel undertook an extensive later review of directives and procedures related to independent verifica tion of performance of operational activities affecting safety-related equipment. (The review was not limited to systems important to containment integrity.)
Table 2 Outline of Five Events at Oconee Events Unit Plant Status Cause Two Manual Containment Oconee 3 Cold Shutdown Inadequate review-of outstanding items by shift personnel.
Isolation Valves Open Deficiency in procedure (deletion of audit from pre for 4 days between criticality check).
Dec. 8 and Dec. 12, 1982 Manual Containment Oconee.1, 2, 3 All 100% power Personnel.error; tech spec requirements were overlooked Isolation Valve Open during review of procedure for approval..
by Procedure Standby Shutdown Oconee 1, 2, 3 All 100% power Design deficiency resulting from inadequate review.
Facility Valve Lineup (SSF not operational.)
did not meet Double Isolation Criterion Emergency Personnel Air Oconee 3 All 100% power Operating procedure did not explicitly call for valye Lock Hatch Leaking Air closure.
(Valve Open)
Emergency Personnel Air Oconee 1 All 100% power Inner door inadvertently opened; statalarm ignored; Du, e Lock Hatch Inner Door never considered the requirement for independent Open for 4 days from verification for hatch procedures.
March 17 to March 21, 1983
OIE/RLG July 1, 1983 (A2)
Table 3
-Duke Power Company Oconee Nuclear Station April 29, 1983 Submittal Status of Actions
-July 1,
1983 Action Status
- 1. Air Lock Door Open Incident -
close Complete door, check other units, notify NRC, file LER
- 2. Air Lock Valve Open Incident -
close Complete valve, check other units, notify NRC, file LER
- 3. Establish Containment Integrity Complete Task Force e
Compile master list of CI components Complete
- Visual check of all accessible penetrations Complete o
Label all CI components Complete
- Control Room drawings updated Complete o
Controlled drawings revised
- 4. Establish controlling procedure for Complete
.containment integrity
- 5. Establish quarterly and prior to S/U Complete surveillance of containment integrity
- 6. Establish procedure to require effective/
Complete timely follow-through to alarm conditions
- 7. Revise SD 4.4.4 to expand modification Complete process review to all affected sections
- 8. Initial review of station procedures Complete
- 9. Revise three Operations Procedures as a Complete result of initial review
- 10.
Revise six Performance Procedures found Complete as a result of initial review
- 11.
Review incidents of past three years for Comolete incidents related to personnel error
- 12.
Review of past modifications to assure Complete procedures have been appropriately updated
OIE/RLG July 1,. 1983 (A2 Table 3 (continued)
Action Status
- 13. Revise/implement SD 4.2.5 to reflect Complete results of past/recent incidents
- 14.
Revise/implement SD 4.2.1 on procedures Complete
- 15.
Revise/imple-eat other SDs as required as As needed a result of these changes
- 16.
Review procedures, again; based on new SDs Complete
- 17.
Establish interim programs Complete
- 18.
Conduct an independent management audit Complete
- 19.
Incorporate Lessons Learned into operational Schedule to be established activities at McGuire and Catawba
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PrOFM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB II 2-6i11 3 1 S-0011I LICENSEE EVENT REPORT EXPIRES 4-30-62 CONTROL BLOCK:
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9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T
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60 61 DOCKET NUMBER 68 49 EVENT DATE 74 75 REPORT DATE 10 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES o
On July 5, 1983, at ul448, while trying to determine the source of water influx to certain waterboxes, valve ICCW-1 was fully opened, thus causing CCW-8 to open, thus losing the prime on the Emergency CCW System discharge line and.rendering this system inoperable.
During inoperability, the CCW pumps had power and provided cooling flow through the condensers.
If all station power was lost, the main steam relief valves were available.
Thus, the health and safety of the public were not
____ -affected by this incident.
7 8
a8 SYSTEM CAUSE CAUSE
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27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD.6 PRIME COMP.
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__CAUSE DESCRIPTION AND CORRECTIVE ACTIONS@
IUnit 1 -refuelinez shutdown. Units 2 and 3 - 100%.
Tnhe cause o: this incident wasi 1:1 6isonnei error in that the connection between the two valves was not considered.
12 IThe valves were closed and the CCW emergency discharge piping was reprimed.
The 13Iresponsible person was counseled, and appropriate personnel will review the 14Istation rep~ort.
a1 9
P A CILITY-MEHDO STATUS POWER OTNER STATUS D
YC DISCOVERY DESCRIPTION X
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s0 PERSONNEL. EXPOSURE S NUMBER TYPE DESCRIPTION ACIN 17I01 01 0 1Z1(NA I
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DUKE POWER COMPANY P.O. Box 33189 CHARLoTTE, N.C. 28242 RAL B. TUTGKER rELPHONE VICE PRasmENT
.(704) 373-4531 July 19, 1983 Mr..James P. O'Reilly, Regional Administrator U..S. Nuclear Regulatory Commission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30303
Subject:
Oconee Nuclear Station Docket No. 50-269
Dear Mr. O'Reilly:
Please find attached Reportable Occurrence Report RO-269/83-14. This report is submitted pursuant to Oconee Nuclear.Station Technical Specification 6.6.2.1.a(2) which concerns an operation subject to a limiting condition for operation which was less conservative than the least conservative aspect of the limiting condition for operation established in the Technical Specifica tions, and describes an incident which is considered to be of no significance with respect to its effect on the health and safety of the public.
Very truly yours, Hal B. Tucker JCP/php Attachment cc:
Document Control Desk U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Mr. J. C. Bryant NRC Resident Inspector Oconee Nuclear Station INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Mr. John F. Suermann Office of Nuclear Reactor Regulation
- A U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Duke Power Company Oconee Nuclear Station Report Number:
RO-269/83-14 Report Date:
July 19, 1983 Occurrence Date:
July 5, 1983 Facility:
Oconee Units 1, 2, and 3, Seneca, South Carolina Identification of Occurrence:
Loss of prime on the condenser circulating water (CCW) emergency discharge line due to CCW-8 being opened.
Conditions Prior to Occurrence:
Oconee 1 - Refueling shutdown Oconee 2 -
100%
Oconee 3 -
100%
Description of Occurrence:
On July 5, 1983, at about 1448, in an effort to try to determine the source of influx of water to the lAl, 1B2, and 102 water boxes, the Condenser Al Emergency Outlet Valve, 1CCW-1 was opened. When this valve was fully opened, this caused the Emergency Discharge Valve to the tailrace, CCW-8, to open.
This resulted in a loss of prime on the Emergency Condenser Circulating Water (CCW) System discharge line and rendered this system inoperable per Technical Specification 3.4.5.
Apparent Cause of Occurrence:
The cause of this occurrence was personnel error.
The responsible person failed to consider the interlock between ICCW-1 and CCW-8 in his decision to open 1CCW-1. A contributing cause to this occurrence was the component failure of valve ICCW-1 in not isolating the discharge system from the condenser.
Analysis of Occurrence:
During the period the Emergency CCW System was inoperable, the CCW pumps had power and were providing cooling flow through the condensers and thus removing heat. Additionally, the probability of a loss of all station power. during the short time (88 minutes) the Emergency CCW System was inoperable is extremely low.
In the event of a loss of power during this 88 minutes the main steam relief valves were available to steam the OTSGs to the atmosphere.
The health and safety of the public were not affected by this incident.
Corrective Action:
Valves 1CCW-1 and CCW-8 were shut and the CCW emergency discharge piping was reprimed. At 1620, the CCW Emergency Discharge System was declared overable.
The responsible person has been counseled on.his error ano the importance of quality job planning.
Operations personnel will review this report with emphasis on the interlock between CCW-8 and the condenser outlet valves.