ML16161A975

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Insp Repts 50-269/88-08,50-270/88-08 & 50-287/88-08 on 880317-0418.Violations Noted.Major Areas Inspected:Onsite in Areas of Operations,Surveillance,Maint,Physical Security, Radiation Protection & Meeting W/Public Officials
ML16161A975
Person / Time
Site: Oconee  
Issue date: 05/02/1988
From: Peebles T, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A973 List:
References
50-269-88-08, 50-269-88-8, 50-270-88-08, 50-270-88-8, 50-287-88-08, 50-287-88-8, IEB-88-001, IEB-88-1, NUDOCS 8805100036
Download: ML16161A975 (14)


See also: IR 05000269/1988008

Text

pg REGCJ4

UNITED STATES

0 oNUCLEAR

REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos: 50-269/88-08, 50-270/88-08, 50-287/88-08

Licensee:

Duke Power Company

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.:

50-269, 50-270, 50-287

License Nos.

DPR-38, DPR-47, DPR-55

Facility Name:

Oconee Nuclear Station

Inspection Conducted:

March 17 -

April 18, 1988

Inspectors:

/(A

A

/

P .

-

ne r

Senior Resident Inspector

L.D.

ert, Residen

Inspector

D e Signed

Approved by:

____

T.A.

Peebles, Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved resident inspection on-site

in the areas of operations,

surveillance, maintenance,

physical security,

radiation protection,

engineered safeguards features lineups, nonroutine

reporting, meeting with public officials, and confirmatory order review.

Results: Of the nine areas inspected, one violation was identified (Failure to

provide procedures to perform component verification on components requiring

maintenance, paragraph 6.b).

8805100036 880503

PDR

ADOCK 05000269

Q

DCD

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • M. Tuckman, Station Manager

J. Davis, Technical Services Superintendent

  • W. Foster, Maintenance Superintendent

T. Glenn, Instrument and Electrical Support Engineer

C. Harlin, Compliance Engineer

D. Hubbard, Performance Engineer

J. McIntosh, Administrative Services Superintendent

  • F. Owens, Assistant Engineer, Compliance
  • R. Sweigart, Operations Superintendent

L. Wilkie, Integrated Scheduling Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P.H. Skinner

L.D. Wert

  • Attended exit interview.

2.

Exit Interview

The inspection scope and findings were summarized on April 15, 1988, with

those persons indicated in paragraph 1 above.

The inspectors described the areas inspected and discussed in detail the

inspection findings listed below. Dissenting comments were not received

from the licensee.

Proprietary information

is not contained in this

report.

Item Number

Status

Description/Reference Paragraph

IFI 269,270,287/

Open

Improvement in Cable Room Fire

88-08-01

Detection System

UNR 287/88-08-02

Open

All Three Low Pressure Injection

Pumps Inoperable

IFI 269,270,287/

Open

RBCU Dropout Plate Inspection

88-08-03

2

Item Number

Status

Description/Reference Paragraph

(cont'd)

IFI 269/88-08-04

Open

Functional Verification Testing of the

Reactor Building Cooling System

Drop

Out Plate

VIO 269,270,287/

Open

Failure to Provide an Adequate

88-08-05

Procedure to Identify Components

Requiring Maintenance

UNR 287/88-08-06

Open

Runback During CRD System Maintenance

Bulletin 88-BU-01

Closed

Defects in Westinghouse Circuit

Breakers

LIV 269,270,287/

Open

Lack of Adequate Procedures for

88-08-07

Isolation of Equipment Containing EPSL

Components

3.

Licensee Action on Previous Enforcement Matters

This subject was not addressed in this inspection.

4.

Plant Operations (71707)

a.

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, technical

specifications (TS), and administrative controls. Control room logs,

shift turnover records, Unit 2 Refueling log and equipment removal

and restoration records were reviewed routinely.

Discussions were

conducted with plant operations,

maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis. Inspections were conducted on day and on night shifts, during

week days and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

observed were conducted as required by the Licensees Administrative

Procedures.

The complement of licensed personnel

on each shift

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1,2, and 3 Electrical Equipment Rooms

3

Units 1,2, and 3 Cable Spreading Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Units 1,2, and 3 Penetration Rooms

Unit 2 Containment

Condenser Circulating Water Intake Structure

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Unit 1 -

Unit 1.began this reporting period operating at 100%

power. The unit reduced power to about 98% on March 27 dbe

to a problem on the feedwater 1E1 heater drain pump.

The

problem was corrected and the unit returned to 100% on

March

29 where

it

operated for the

remainder of the

reporting period.

Unit 2 -

Unit 2 began this reporting period in an outage condition.

On April 7 the unit was taken critical and zero

power

physics testing was

performed.

On April 12

power

was

increased to 40% and problems developed on the Alterex

coupling and with turbine vibrations causing the generator

to be taken off the line.

The generator was brought back

on the line on April 14 and power was escalated slowly to

100% by April 15.

Unit 3 -

Unit 3 began the reporting period operating at 100%0

power.

The unit experienced a Asymmetric Rod Runback to

96% power on March 29 due to a communications problem

between the operator and a technician.

The unit returned

to 100% power on March 30.

On April 5, power was reduced

to 88% due to load considerations.

The unit continued to

operate at that level until April 17 when the tube leak in

3A steam generator increased from

.08 gpm to 1.35.

An

Unusual Event was declared at 0115 on April 18 and the unit

was

shutdown

and cooled down to cold conditions.

The

shutdown was performed in accordance with the licensees

emergency operating procedures and operating procedures.

The unit was on line for 351 days prior to this event.

b.

Fire In Unit 1 Cable Room

At approximately 8:30 a.m.

on

March 22,

1988,

a small fire was

discovered in a Unit 2 computer cabinet (not safety related), in the

Unit 1 cable room which is located just beneath the Unit 1/Unit 2

Control

Room.

Unit 2 was at cold shutdown.

Initial discovery of

the fire was due to an individual working in the Unit 2 cable room

reporting smoke. The unit supervisor and shift supervisor identified

the source of the smoke as a smoldering computer terminal board in

j.

4

Unit 2 computer cabinet G-2.

Apparently incorrect wiring during

recent maintenance caused the fire. The fire brigade was dispatched

and

the computer board

was maintained cool with carbon dioxide

extinguishers until smoldering was extinguished within five minutes

by cutting the terminal

leads to the board.

No open flames were

observed but smoke was described as light to medium and could be

smelled in the control room.

After the initial fire brigade efforts

were completed, the resident inspector entered the cable room.

Some

smoke still remained

in the cable room and deposits on adjacent

surfaces and cables indicated that the smoke emitted was more than a

minimal amount. The inspector along with operating supervisors was

concerned that a fire detector located approximately five feet away

in the overhead did not alarm.

Subsequent Instrument and Electrical

testing of the detector indicated that it

was functioning properly.

An hourly fire watch was stationed in the cable rooms as a pre

cautionary measure and the licensee requested their fire protection

engineers review the

situation.

After evaluation

by the fire

protection engineers,

it

was concluded that the system is fully

operable and meets

all current requirements.

The fire watch was

secured. The licensee feels strongly that detector sensitivity and

testing could be improved through installation of a more up to date

detection system and is considering a Nuclear Station Modification

to accomplish this. During the review by fire protection and safety

engineers a fire door was discovered open in the vertical cable shaft

in the Unit 1 cable room. This shaft connects several levels of the

auxiliary building including the equipment room and cable room and

is posted with a fire barrier sign.

The door was shut immediately

upon discovery.

The issue was promptly reported to the resident

inspector.

The licensee has

been

unable to determine how long

the door was open or why it

was opened.

The resident inscectors

routinely check fire barriers on a daily basis and this door is often

checked and has not previously been found open. The inspectors have

not frequently found fire barrier doors left open and feel that

generally a high level of attention is given to fire protection

equipment at the station.

Because of the serious potential con

sequences of a fire in the cable room, resolution of future action

on the detection system is identified as an Inspection Followup Item

50-269,270,287/88-08-01; Improvement of Cable Room Fire Detection

Systems. The inspectors will continue to monitor the status of fire

barriers particularly in the cable and equipment room areas.

c.

All Three

Low Pressure Injection Pumps Administratively Inoperable

(Unit 3)

At 8:00 a.m.

on April 6,

1988,

it

was discovered that during the

previous night shift maintenance personnel had lubricated the fast

couplings of all three low pressure injection (LPI)

pumps and post

maintenance performance testing had not been completed.

Unit 3 was

5

at 88% power during this period.

Technical Specification 3.3.2

requires under the existing plant conditions that two independent

LPI trains shall be operable.

Additionally it

permits tests or

maintenance to be performed on any component of the LPI system if the

redundant LPI train is operable.

All three LPI pumps were declared

inoperable at 8:00 a.m.

because if

incorrect lubrication had been

performed the ability of the pumps to function as required would

have been impaired.

The resident inspector was in the Unit 1/2

Control Room at the time and was immediately informed.

The licensee

called the NRC Operations Center as required by 50.72.b.2. iii(B).

Performance testing to verify proper lubrication and pump operability

was completed on one LPI pump

by 10:30 a.m.

and by approximately

11:30 testing of all three pumps had been satisfactorily completed.

Due to the short time. interval required to verify operability and

no reason to suspect that the pumps would not actually perform as

required if

necessary, Unit 3 remained at 88% power.

(Technical

Specification 3.0 would have required the unit to be in hot shut

down within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.)

Initial investigation indicates that the

maintenance workers did not correctly follow station- procedures

and that poor training and/or communications contributed to this

incident.

Pending licensee and inspector followup investigation,

this item is identified as Unresolved Item 287/88-08-02:

All Three

Low Pressure Injection Pumps Inoperable.*

5. Surveillance Testing (61726)

a. Surveillance tests were reviewed

by

the inspectors to verify

procedural and performance adequacy.

The completed tests reviewed

were

examined for necessary test prerequisites, instructions,

acceptance criteria, technical content, authorization to begin work,

data collection,

independent verification where required, handling

of deficiencies noted,

and review of completed work.

The tests

witnessed,

in whole or in part, were inspected to determine that

approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure,

test results were acceptable and systems restoration was completed.

Surveillances reviewed or witnessed in whole or in part:

PT/2/A/261/07

Emergency Condenser Cooling Water Gravity Flow

Test (Unit 2)

PT/3/A/202/11

High Pressure Injection Pump Performance Test

(Unit 3)

PT/0/A/160/03

Reactor Building Cooling System Engineered

Safeguards Test (Unit 2)

PT/2/A/600/22 Motor Driven Emergency Feedwater Pump Suction

Check Valve Test (Unit 2)

  • Unresolved

items are matters about which more information is required to

determine whether they are acceptable or may involve violations or deviations.

6

PT/0/A/600/15 Control Rod Drive Movement (Unit 1)

TT/2/A/0711/10 Low Power Physics Testing-Measurement of

Temperature Coefficients.

b.

Reactor Building Cooling System Dropout Plates

In response to observations made during the review of a licensee's

Problem Investigation Report (PIR)

concerning maintenance

on the

Reactor Building Cooling Unit (RBCU)

dampers,

the inspectors looked

into the operation and testing of the RBCUs.

The Reactor Building

Cooling

(RBC)

System is provided to remove heat from the reactor

building (RB) following an accident and to cool the RB during normal

operation. The Reactor Building Spray system also removes

RB heat

following an accident. The RBCU system consists primarily of 3 axial

flow fans, motor-operated discharge damper.s,

fusible linked dropout

plates and associated distribution ductwork. The discharge dampers

are not treated as safety related components because between the

outlet of each cooler and its motor-operator discharge damper is a

dropout plate. These plates are a'ttached to the RBCU ductwork with a

hinged bracket and fusible metal link arrangement. The fusible links

are designed to melt at approximately 150 degrees F, releasing the

hinged brackets and allowing the plates to drop clean of the ductwork

to provide an

RBCU exhaust path (regardless of damper or lower

ductwork condition).

The inspector after discussion with the

licensee noted that functional testing of the dropout plates had not

been

performed,

and

no preventive maintenance

or surveillances

had been performed

on these plates since their installation.

It

should be noted that the licensee had recently formulated a plan to

functionally test the RBC system. This test will probably include a

test of the fusible dropout plate, operation of the fans and coolers

and airflow measurements

through the fusible patch

pathways at

elevated containment pressures (simulating

"accident" pressures)

following conduct of the Integrated Leakrate Test (ILRT).

This test

is tentatively scheduled for the End of Cycle 11 Unit 1 outage (the

next scheduled ILRT outage).

The inspector during a tour of the RB examined the dropout plates,

particularly the hinged bracket and fusible link arrangements. As a

result of concerns expressed by the inspector, the licensee also

conducted an inspection of the dropout plates (Work Request 53447G)

just prior to RB closeout. This inspection verified that the path

way was clear for the plates to drop,

connecting hardware

on the

fusible links was correctly installed, and retaining cables were of

sufficient length to allow the plate to drop free of the opening if

actuated. A sampling of the fusible links was examined to ensure

that the links were the proper type. The bracket hinges were cleaned

and lubricated.

While the favorable results of this inspection

answered the inspector's questions about the operability of the

7

dropout plates,

such operability checks should be performed each

refueling cycle. Although each plate is 30 square feet in area, with

full fan outlet pressure against it

if

the dampers or ductwork are

blocked and the plates operation is mostly passive in nature, their

correct functioning is relied upon for removal of

RB heat under

accident conditions. A simple verification that the ability of the

plates to dropout has not been defeated should be required.

This

item is identified as Inspection Followup Item 269,270,287/88-08-03:

RBCU Dropout Plate Inspection.

The inspectors agree that the licensees planned functional testing of

the RBCU's will more thoroughly verify the post-accident capabilities

of the RBC system and should be conducted as planned at the next ILRT

outage. This item is identified as Inspection Followup Item 269/88

08-04:

Functional Verification Testing of the Reactor Building

Cooling System Dropout Plates.

No violations or deviations were identified.

6.

Maintenance Activities (62703)

a. Maintenance activities were

observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade.

Activities,

procedures

and

work requests

were

examined

to verify proper

authorization to begin work, provisions for fire, cleanliness, and

exposure control,

proper return of equipment to service,

and that

limiting conditions for operation were met.

b. Failure to Properly Identify Component Prior to Performing Mainte

nance

On February 11, 1988, a spill of 400-600 gallons of radioactive water

occurred as a result of operator error during maintenance on a High

Pressure Injection (HPI)

System instrument root valve.

Details of

the incident are set forth in Inspection Report 269,270,287/88-01.

.The inspectors have reviewed the results of the licensees investiga

tion into the incident and the completed and planned corrective

actions.

Although errors

made

by personnel

in the

operation,

maintenance,

and planning and scheduling departments contributed to

this incident, the inspectors concur with the root cause identified

as failure on management's part to ensure an adequate component

verification program was implemented. Through a series of errors,

an orange tag (used to help locate and identify equipment needing

repairs) was attached to the incorrect instrument root valve (Unit 1

instead of Unit 2).

The procedure which addresses orange tags gives

no guidance as to how this tag is to be used.

Additionally, a

8

photograph of the wrong valve was attached to the work request and

some incorrect location guidance was written on the work request.

These errors occurred primarily due to poor communications, personnel

error and the fact that both valves (Unit 1 HPI instrument root valve

and Unit 2 HPI instrument root valve) are located at opposite ends of

the same room and are identical unlabeled valves.

When maintenance

workers entered the HPI room to work on the Unit 2 HPI instrument

root valve, they compared the number on the work request with the work

request number on the posted orange tag.

They also compared the

photograph of the valve to the actual valve. Satisfied that they had

located the correct component,

they began mistakenly working on the

Unit 1 HPI instrument root valve. Since Unit 1 was operating at full

power the ensuing spill occurred as the valve packing was loosened.

Despite the numerous personnel errors which contributed to this

incident, the emphasis must always be placed on the vital role of

absolute correct component verification by workers about to begin

maintenance on any safety related equipment.

The

importance of

this verification process has long been recognized as an essential

contribution to plant safety especially at this three unit site. The

resident inspectors closely monitor the

implementation of this

process and other licensee measures to prevent wrong unit or wrong

train events.

On February 25,

1988, valve 2MS-83,

a 6" main steam check valve in

the supply line to the turbine driven emergency feedwater pump on

Unit 2, was

removed in error.

The valve that was supposed to be

removed was 2MS-85 (another 6" check valve). This problem occurred,

in part, because the orange tag was on a column in the general area

of the valve and a photograph was taken of MS-83 not MS-85.

Adding

to this problem was that the tags and labels had been removed when

the lagging was removed.

On

February 20,

1988,

workers entered an incorrect room to begin

maintenance on an important primary valve, discovered their mistake

during component verification and immediately corrected themselves.

This error was recognized by the workers although no procedure has

been developed for assuring that correct component verification has

been performed prior to commencing work on a component.

The licensee has implemented a component verification documentation

system to provide some assurance that the component is the correct

component, but there are

no instructions provided to workers

detailing methods to perform this verification.

This is

a very

important process,

especially at a three unit station where many

instrumentation valves are not labeled.

The lack of a formal

documented program for performing correct component verification is

identified as Violation 269,270,287/88-08-05; Failure to Provide

Procedures to Perform Component Verification on Components Requiring

Maintenance.

9

c.

Runback During Control Rod Drive system Maintenance (Unit 3)

A Unit 3 control rod (Group 4, Rod 2) position indication reed switch

malfunctioned on March 27, 1988. This caused an erroneous indication

of that rods Absolute Position Indication (indicated less than fully

withdrawn).

Since the rod was indicating greater than 7 inches

difference between its position and the average position of Group 4

rods,

an "asymmetric

fault" signal was generated within the rod

control circuitry.

Since the unit was operating at greater than

60 percent of full power a Control Rod Drive (CRD)

"Out Inhibit"

condition was activated. The Integrated Control System (ICS) cannot

automatically move Group 7 rods outward.

Under normal operation the

ICS automatically positions Group 7 rods to control reactivity as

required by the ICS generated "neutron error'" signal.

Operation of

Unit 3 has continued with the rod control station being placed in

manual if outward rod motion is required. Inward rod motion and rod

trip functions have not been affected. On March 29 at approximately

1:00 p.m.

an Instrument and Electrical (I&E)

Technician performing

trouble shooting of this problem inadvertently caused

a reactor

runback.

The apparent cause of the runback was that the outlimit

fuse for Rod 2 of Group 4 was pulled out of the circuit.

Since the

ICS was in automatic and an "asymmetric fault signal" was present, a

runback was initiated. The control room operators immediately took

action to verify that an actual dropped rod had not occurred and

began taking the ICS to manual.

The technician replaced the fuse

and the runback was terminated at about 96 percent full power.

The

licensee has initiated a Problem Investigation Report addressing the

event. The reason for the fuse being pulled while the ICS was still

in automatic is being investigated.

Pending further examination

by the licensee and the inspectors,

this item is identified as

Unresolved Item 287/88-08-06: Runback During CRD System Maintenance.

7.

Resident Inspector Safeguards Inspection (71881)

In the course of the monthly activities, the Resident Inspectors included

review of portions of the licensee's physical security activities.

The

performance of various shifts of the security force was observed in the

conduct of daily activities which included; protected and vital areas

access controls, searching of personnel,

packages and vehicles, badge

issuance and retrieval, escorting of visitors, patrols and compensatory

posts. In addition, the inspectors observed protected area lighting and

protected and vital areas barrier integrity,

and verified interfaces

between the security organization and operations or maintenance.

No violations or deviations were identified.

10

8.

Inspection of Open Items (92701)

The following open items are being closed based on review of licensee

reports,

inspection,

record review, and discussions with licensee

personnel, as appropriate:

(Closed) 88-BU-01:

Defects in Westinghouse Circuit Breakers.

Based

on the licensee's response dated March 7, 1988, which states that

Oconee Nuclear Station does not utilize Westinghouse

DS circuit

breakers in any class 1E applications, this item is closed.

9.

Radiation Protection Procedures for the Resident Inspector (71709)

The inspector continued to look closely at selected radiological protec

tion program activities to ensure compliance with requirements

and

licensee procedures.

Because of the Unit 2 refueling outage and its

associated work

in radiological

areas, the inspector had frequent

opportunities to

observe implementation of radiological

protection

procedures. The inspectors noted an apparent inconsistency in the wearing

of personnel monitoring equipment. It was observed that many personnel

wear both their film badge and direct reading dosimeter on a neck chain

inside their Anti-C coveralls. This is contrary to posted examples and

training conducted on the proper way to don coveralls and wear dosimetry

equipment. The concerns are that the beta detection window on the film

badge may not be facing outward and also that it

is difficult for

personnel to check the reading on their pocket dosimeter once inside

areas if

it

is worn inside the coveralls on a neck chain. The inspector

discussed these observations with licensee management.

After some

analysis, the licensee acknowledged that enforcement of proper wearing of

personnel monitoring equipment has been inconsistent. The station manager

issued a Staff Note to all station personnel prohibiting the use of neck

chains for dosimetry devices whenever cloth coveralls (with a pocket) are

being worn.

The inspectors will continue to observe radiological protection activities

with emphasis on correct wearing of dosimetry equipment.

10.

Meeting With Public Officials (94600)

On March 21 at 4:00 p.m.,

the inspectors met with local officials from

Pickens County.

At the county council meeting

held in the Pickens

Courthouse,

the residents made a presentation that introduced the

inspectors and discussed the NRC responsibilities both in Washington and

Region II. The inspectors also provided the officials with names of NRC

supervisory personnel and phone numbers locally and in Atlanta.

The following local representatives were present at the meeting:

Mr. Robert R. Nash, Pickens County Council Chairmen

Mr. Weyman B. Dublin, Jr., Vice Chairman

Mr. Charlie D. Grant, Councilman

Mr. 'Claude V. Marchbanks, Councilman

Mr. Marion C. Owens, Councilman

Mr. Weldon Day, Administrator

Mr. Bill Hendricks, S.C. State Representative

Copies of the outline.attached to Inspection Report 269,270,287/88-01 were

provided to interested personnel present at the meeting.

The resident inspector met individually with Mr. Larry Abernathy, Mayor of

Clemson at Clemson City Hall on March 31. Mr. Abernathy was given a copy

of the above outline and the inspector held a discussion with him covering

the material presented at the two previous county council meetings.

11.

Confirmatory Order Concerning Reactor Building and Decay Heat Removal

Coolers

Problems caused by fouling of reactor building cooling units (RBCU)

and

low pressure injection (LPI)

decay heat removal coolers and lake water

temperatures have been a subject in several reports in 1987,

including

Report Nos.

50-269,270,287/87-13,17,25,29,30 and 44.

NRC Confirmatory

Orders of April 10,

1987 and August 19,

1987,

placed restrictions of

Operation

on Oconee Unit 2.

The orders required that Unit 2 not be

operated at any power levels after the end of cycle 9 until the LPI and

RBCU coolers had been cleaned and tested and had been approved for full

power operation by Region II.

The licensee cleaned and tested the coolers during the EOC 9 refueling

shutdown.

The licensee determined that Unit 2 could be safely operated

at power levels up to 100% with Lake Keowee water temperatures up to 85

degrees F.

Region II

personnel

witnessed cleaning and testing

and

reviewed the findings.

On April 7,

Region II

lifted the restrictions

imposed by the Confirmatory Orders.

12.

Information Meeting With DPC Staff Concerning Emergency Power Switching

Logic At Oconee

On April 12,

1988,

Duke Power Company met with Region II staff in the

Atlanta office to provide information concerning a situation identified

by DPC in which Oconee had operated outside of their design basis for a

limited period of time. This concerned the very complex Emergency

Power

Switching Logic (EPSL)

which is designed to insure a reliable source of

power is available to safety-related components required to maintain the

plant in a safe condition.

At this meeting, DPC personnel provided a

12

basic explanation of how the EPSL system functioned and the events that

identified how the operation outside of the design basis occurred.

The

information provided showed that the conditions needed to place the plant

in this situation were very rare and had occurred only five times since

the plant commenced operation and each of these times were for less than

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

In addition, a probabilistic risk analysis was performed for

this condition and the results indicated an E-7 core melt frequency.

The

licensee is developing detailed procedures to assure the plant is not

placed into this condition during future maintenance involving components

associated with the EPSL system.

Additional information concerning this

occurrence is contained in LER 269/88-04 dated April 6, 1988.

The licensee has performed additional review of this subject and has

concluded that the root cause of this problem is not a design deficiency

as described in LER 269/88-04,

but is due to an inadequate procedure.

They will be submitting a revision to this LER in the near future. Based

on the Licensee's discussion in Region II, the information provided in LER 269/88-04, and the resident inspectors in depth review of this occurrence,

this item is identified as a Licensee Identified Violation (LIV) 269,270,

287/88-08-07:

Lack of Adequate Procedures for Isolation of Equipment

Containing EPSL Components.

This is based on the guidance provided in

10 CFR 2 Appendix C section V.A which allows the

NRC to not issue a

violation that meets the following tests:

(1) It

was identified by the licensee -

this was identified by the

licensee while performing a design engineering review of a Technical

Specification Interpretation requested by the operating staff at the

plant.

(2) It fits a severity level IV or V -

due to the extreme improbability

of this series of events occurring (i.e. a LOCA and a loss of offsite

power within 20 to 25 seconds -

anything less than 20 seconds or

greater than 25 seconds would not create this problem, while work was

being conducted causing these control power fuses to be removed),

which was calculated to be E-7, the severity level would appearto be

level IV.

(3) It

was reported -

the report was made as required by 10 CFR 50.72

section (2)(iii)(D).

(4) It

is being corrected -

procedures are being developed to prohibit

activities

that will

allow this condition to occur.

Interim

corrective actions have also been established.

(5) It

was not a violation that- could reasonably be expected to have

been

prevented by the licensee's corrective action for a previolus

violation.

13

13.

Unit 2 End of Cycle 9 Refueling Outage (71711) (Unit 2)

The Unit 2 refueling outage was completed on April 6 approximately 4

days ahead of schedule.

Major work reformed during the outage included

chemical cleaning both OTSG's,

refueling, installing dams in the primary

side of cold legs, eddy current testing and plugging and sleeving of steam

generator tubes, work on all four reactor coolant pumps and motors,

and

various non-safety related work.

Portions of the startup and power

escalation following the outage were observed by the inspectors.

The

evolutions observed were conducted in accordance with approved procedures

that had been appropriately revised to reflect changes made during the

outage period.

No violations or deviations were identified.