ML16154A835

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Insp Repts 50-269/95-18,50-270/95-18 & 50-287/95-18 on 950730-0909.Violations Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance Testing,Onsite Engineering & Plant Support
ML16154A835
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 10/03/1995
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A834 List:
References
50-269-95-18, 50-270-95-18, 50-287-95-18, NUDOCS 9510180353
Download: ML16154A835 (16)


See also: IR 05000269/1995018

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.: 50-269/95-18, 50-270/95-18 and 50-287/95-18

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.: DPR-38, DPR-47 and DPR-55

Facility Name: Oconee Units 1, 2 and 3

Inspection Conducted: July 30 - Sept mber 9, 1995

Inspectors:

0

V. t. Harmon, Senior esident Inspector

Date Signed

L. A. Keller, Resident Inspector

P. G. Humphrey, Resident Inspector

L. Wien, Project Manager

Approved by:

_

_

_

__

_

_

_

-

R. V. Clenjak, Chie

Date Signed

Reactor Projects Branch 3

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, maintenance and surveillance testing, onsite

engineering and plant support.

Results:

In the operations area, the inspectors were concerned with the

number and increased frequency of configuration control errors. A

violation with six examples was identified for inadequate

configuration control.

The inspectors concluded that the large

number of examples of inadequate configuration control represented

a programmatic weakness, paragraph 2.e. Prompt corrective actions

taken by the Unit 3 control room operators following a heater

drain pump trip avoided a reactor trip, paragraph 2.f.

In the maintenance area, concerns were identified regarding the

implementation of a Keowee modification. Concerns included

inadequate planning, lack of management oversight, and lack of

configuration control, paragraph 3.a.(3). The prompt and

comprehensive effort to locate and eliminate a DC ground at Keowee

was identified as a strength, paragraph 3.a.(6).

Enclosure 2

9510180353 951013

PDR ADOCK 05000269

PDR

2

In the engineering area, vendor-supplied valve data resulted in a

calculation error for the predicted Low Pressure Injection (LPI)

flow rates during accident conditions. Due to recent

modifications, the LPI systems were operable; however, they were

considered technically inoperable prior to the modifications,

paragraph 4.

In the plant support area, the inspectors reviewed the results of

the licensee's efforts at reducing personnel radiation dose for

the Unit 3 refueling outage. Outage doses were substantially

lower than previous outages, paragraph 5.a. Plant Operating

Review Committee meetings were well organized and placed

appropriate emphasis on safety, paragraph 5.b.

Enclosure 2

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • E. Burchfield, Regulatory Compliance Manager

T. Coutu, Operations Support Manager

  • D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

  • W. Foster, Safety Assurance Manager
  • J. Hampton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

  • C. Little, Electrical Systems/Equipment Manager

B. Peele, Station Manager

G. Rothenberger, Operations Superintendent

  • J. Smith, Regulatory Compliance
  • R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

Acronyms and abbreviations used throughout this report are identified in

the last paragraph.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, TS, and

administrative controls. Control room logs, shift turnover

records, temporary modification log, and equipment removal and

restoration records were reviewed routinely. Discussions were

conducted with plant operations, maintenance, chemistry, health

physics, I&E, and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis. Inspections were conducted on day and night shifts,

during weekdays and on weekends. Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

2

b.

Plant Status

Unit 1 operated at or near full power throughout the inspection

period.

Unit 2 operated at or near full power throughout the inspection

period.

Unit 3 operated at full power until August 14, 1995, when it

tripped due to a problem with the control rod drive system. The

unit returned to full power the following day. On August 31,

1995, power was reduced to 76 percent due to an entry into TS 3.7.3 (see paragraph 3.a.(3)). The unit returned to full power on

September 1, but reduced power to 59 percent on September 2, in

order to repair a leak on the 3A Feedwater Pump seal water piping.

The unit returned to full power the following day and continued at

full power throughout the remainder of the inspection period.

C.

Unit 1 Control Rod Drive System Patch Panel Unlocked

On July 8, 1995, at 10:15 a.m., operators discovered the Unit 1

CRD System Patch Panel was unlocked. This panel is required by TS 3.5.2.7 to be locked at all times after confirmation of proper rod

operation and sequence. The licensee entered LCO 3.0, which

requires plant shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> unless the condition is

rectified and the LCO exited. The licensee determined the panel

lock to be broken, and placed a security guard at the panel at

1:00 p.m. At that time, the LCO was exited. The lock was

repaired at 4:10 p.m.

The Station Manager decided to re-confirm proper rod operation and

sequence by completing procedure IP/1/A/0330/002D, Control Rod

Patch Verification Test. This test was completed satisfactorily

at 9:16 p.m. The decision to perform the verification test was

appropriate and conservative.

This issue will be addressed further during review of associated

LER 269/95-05, Breach of Technical Specification Due To Unlocked

Control Rod Patch Panel, submitted August 7, 1995.

d.

Unit 3 Reactor Trip

Oconee Unit 3 tripped from 100 percent reactor power on August 14,

1995, at approximately 4:45 a.m. The unit tripped on a variable

low pressure/temperature signal resulting from a reactor coolant

system low temperature condition that occurred when the group 5

control rods unexpectedly dropped into the core. The CRD

programmer was suspected of causing the rod drop since the

remaining electrical equipment, unique to the rod group, was

Enclosure 2

  • I

3

checked out and no problems were identified. The programmer was

replaced and returned to the vendor for further testing. In

addition, a temporary modification was implemented to monitor the

power supply to the CRD programmer for future evaluations.

The plant responded to the trip appropriately and all systems

performed as expected. The inspectors responded to the unit

following the trip and observed the operator activities in

progress. The operators performed effectively in responding to

the trip and stabilizing the plant.

On the evening of August 14, 1995, the inspectors attended the

PORC meeting. The committee members agreed to restart the unit

subject to the replacement of the programmer. The licensee

decision to allow plant restart was based on the evaluations from

the post trip reviews.

The inspectors reviewed the post trip report and determined that

the licensee had adequately addressed the issues identified.

e.

Inadequate Configuration Control

During the inspection period, the inspectors became concerned by

the number and increased frequency of loss of configuration

control events by the licensee. The inspectors noted these

problems through direct observation and review of the licensee's

PIP data base. The licensee's management was also concerned by

these events and initiated a formal root cause investigation to

consider the specifics of each incident and assess the adverse

trend. As of the end of the inspection period, the licensee's

investigation was still in progress. The specifics for the more

significant events are as follows:

-

On June 25, 1995, the feeder breaker for Unit 2 Low Pressure

Injection Valve, 2LP-2, was inadvertently opened. This

motor operated valve is normally closed at power and is

opened during shutdown (<450 psi) to establish decay heat

removal.

The Unit 2 Reactor Operator quickly discovered the

loss of power to 2LP-2 by noting that its control board

indication was not illuminated following a control room

board walkdown. The operator first changed the indicator

bulb and determined the bulb was not the problem. Upon

further investigation, the Unit 2 operators determined that

VOTES testing of 3LP-2 was ongoing.

The licensee's investigation revealed that a technician

associated with the 3LP-2 valve testing had inadvertently

opened the breaker for 2LP-2. Upon realizing his mistake,

the technician reclosed the breaker for 2LP-2 without

notifying operations. The technician's inadvertent breaker

Enclosure 2

4

manipulation caused 2LP-2 to be without power for 42

minutes. The licensee generated PIP-6-095-0781 to determine

the root cause and necessary corrective actions.

In addition to the original configuration control error, the

inspectors were concerned that the technician reclosed the

breaker without notifying operations. In response to this

concern, licensee management stated that it was their

expectation that any employee, upon discovering a

configuration control error, would inform operations and not

manipulate plant equipment. The loss of configuration

control for 2LP-2 is identified as Example 1 of Violation

50-269,270,287/95-18-01, Inadequate Configuration Control.

On June 20, 1995, the licensee discovered two LPSW valves

mispositioned. These valves (3LPSW-337 and 3LPSW-342) were

found in the open position despite attached red safety tags

which indicated the required position for the valves as

closed. This is identified as Example 2 of Violation

50-269,270,287/95-18-01.

On June 21, 1995, during a refueling outage, the licensee

discovered that Unit 3 feedwater valves 3FDW-141, 142, 143,

and 144 were removed from the system with the red safety

tags attached. This constituted a breach of the tagging

boundary and is identified as Example 3 of Violation 50

269,270,287/95-18-01.

On July 16, 1995, during the startup from a refueling

outage, the 3B2 Reactor Coolant Pump lower bearing oil

cooler temperature came into alarm. The licensee's

subsequent investigation determined the LPSW inlet and

outlet valves (3LPSW-106 and 3LPSW-236) to the oil cooler

were throttled. These valves were required to be in the

full open position. The mispositioning of 3LPSW-106 & 236

is identified as Example 4 of Violation 50-269,270,287/95

18-01.

On August 1, 1995, the licensee's maintenance organization

found a Red Tag attached to the wrong component. The Red

Tag (OPS-95-2209-4) was hung on "Feeder Bkr for MCC XOD3-1"

and should have been on "XOD3 Alt Incoming FDR Bkr."

The

failure to properly tag and open the correct breaker is

identified as Example 5 of Violation 50-269,270,287/

95-18-01.

On August 30, 1995, the inspectors observed numerous

discrepancies between the position of Keowee sliding links

and their associated configuration control tags (see

paragraph 3.a.(3)). The failure to maintain configuration

Enclosure 2

5

control for Keowee sliding link R95 is identified as Example

6 of Violation 50-269,270,287/95-18-01.

The inspectors concluded that the safety significance of each

example, when taken individually, was minor. However, the large

number and increased frequency of configuration control problems

were indicative of a programmatic weakness. The inspectors noted

that licensee management was also concerned by the recent problems

with configuration control and had devoted resources to determine

root cause(s).

f.

Loss of 3D2 Heater Drain Pump

The inspectors observed operator actions in the Unit 3 control

room on August 29, 1995, when the suction valve to the 3D2 Heater

Drain Pump closed due to problems with the 302 heater level

control system. This caused a trip of the 3D2 Heater Drain Pump

and initiated a transient in the feedwater system which could have

resulted in a reactor trip. However, due to prompt corrective

actions taken by the control room operators, the plant avoided a

reactor trip. This transient occurred during a lineup change to

the feedwater system. The inspector noted that the operators

conducted a thorough briefing prior to the lineup change during

which they discussed possible plant responses. The inspector

concluded that the pre-evolution briefing was a key element in the

operators effective response, and that the operator response to

this plant challenge was prompt and effective.

Within the areas reviewed, one violation with six examples regarding

inadequate configuration control was identified. The inspectors

concluded that the large number of examples of inadequate configuration

control represented a programmatic weakness, paragraph 2.e. Operators

demonstrated alert watchstanding by quickly identifying the loss of

power to valve 2LP-2, paragraph 2.e. Prompt corrective actions taken by

the control room operators following a heater drain pump trip avoided a

reactor trip, paragraph 2.f.

3.

Maintenance and Surveillance Testing (62703 and 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures and WOs were examined to verify that proper

authorization and clearance to begin work were given, cleanliness

was maintained, exposure was controlled, equipment was properly

returned to service, and LCOs were met.

Enclosure 2

6

Maintenance activities observed or reviewed in whole or in part

are as follows:

(1) Unit 2, ATWS Mitigation AMSAC/DSS Logic Test, WO 95056264

On August 10, 1995, the inspector observed activities in

progress during the performance of IP/O/B/0276, ATWS

Mitigation AMSAC/DSS Logic Test. The activity was performed

on Unit 2 which provides a means for testing the logic of

the AMSAC/DSS. The exercise, which was required to be

performed bi-annually with the reactor operating at power,

was performed to acceptable standards.

(2) Purification Of Emergency FDWPT Oil, OP/2/A/1106/24

The inspector reviewed activities in progress to purify the

lubrication oil for the Unit 2 Turbine Driven Emergency

Feedwater Pump on August 3, 1995. The effort, which is

required to be performed on a quarterly basis, was in

accordance with procedure OP/2/A/1106/24, Purification Of

Emergency FDWPT Oil, and was performed to acceptable

standards.

(3) Modification of Keowee Units 1 & 2 Overspeed Protective

Circuitry, TN/5/A/2966/BL1/02

On October 12, 1992, the licensee discovered a single

failure vulnerability for the Keowee units due to the "zone

overlap" of certain differential current protective relays

(LER 269/92-16). On January 11, 1993, the on-going "Keowee

Single Failure Analysis" identified the technical

inoperability of the KHUs while generating to the grid

during certain power/lake level combinations, due to turbine

overspeed (LER 269/93-01). These vulnerabilities resulted

in the inability to simultaneously generate both KHUs to the

grid. Therefore, modification NSM-52966 was initiated to

eliminate the vulnerabilities. This modification required

NRC approval, which was granted by letter dated August 15,

1995. In a letter dated February 27, 1995, the licensee

committed to complete the modification within thirty days of

NRC approval.

Oconee's NSRB recently made an issue of Oconee's failure to

meet commitments to the NRC in a timely manner. Based on

the NSRB emphasis on meeting commitments, the licensee felt

it important to complete the modification within 30 days of

August 15, 1995. While the issue of Oconee not meeting

commitments was valid, this specific 30 day commitment was

arbitrary and extending the work beyond 30 days would not

have adversely affected safety.

Enclosure 2

7

The procedure for implementing the modification of the

Keowee units overspeed protective circuitry is

TN/5/A/2966/BL1/02. It took approximately 10 months to

develop and is very extensive (379 pages).

This procedure

was completed on August 10, 1995, and was approved on August

20, 1995. The procedure was given to Work Control

Scheduling on August 21, 1995, with the expectation that

work would begin that weekend (August 25).

The schedulers

subsequently came up with a schedule of 69 hours7.986111e-4 days <br />0.0192 hours <br />1.140873e-4 weeks <br />2.62545e-5 months <br /> to complete

the overhead path LCO portion of the work. The associated

TS LCO for the overhead path work (TS 3.7.2) allowed the

overhead path to be out of service for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The fact

that there was only three hours scheduled margin from

exceeding the LCO was apparently never communicated to

Safety Assurance or to the Oconee PORC.

The overhead path LCO was entered at 10:01 p.m., on August

28, 1995. Work was proceeding according to schedule when on

August 30, 1995, the resident inspectors identified problems

with work practices associated with the modification.

Specifically, there were six discrepancies noted between the

position of sliding links and the configuration control tags

(blue tags) associated with these links, and there were

numerous "uncontrolled" drawings at the work site intermixed

with "controlled" drawings. The resident staff informed

Oconee management of these deficiencies. After confirming

the findings, the licensee subsequently stopped work at 1:30

p.m., on August 30, 1995. The licensee implemented various

short-term corrective actions to verify all links affected

by the modification were in the correct position and tagged

as required, and removed all uncontrolled drawings from the

immediate work area. A PORC meeting was convened that

afternoon to discuss whether or not to fully complete the

work activity or to back out of the procedure in order to

restore overhead path operability prior to the LCO expiring.

It was at this PORC meeting that the majority of licensee

management first understood that the work stoppage placed

them in jeopardy of exceeding the LCO. It also became

apparent that in order to back out of the procedure, a major

change to the procedure would have to be written overnight.

Although a rough contingency plan had been considered prior

to beginning the work (i.e., they knew the step in the

procedure from which they could back out), a specific back

out procedure was not developed ahead of time. The PORC

decided that despite the uncertainties associated with

backing out of the procedure, it was prudent to pursue the

back out option. It was also at this PORC meeting that the

Compliance Department was directed to begin preparing a NOED

package in case there were problems with backing out of the

modification or with operability testing.

Enclosure 2

8

Work was resumed at 11:30 p.m., on August 30, 1995 (10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />

delay).

Problems were experienced executing the back out

from the modification such that the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCO expired

(10:01 p.m.) and TS 3.7.3 was entered. TS 3.7.3 required

the shutdown of all three Oconee units within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> if

the overhead path is not returned to service. The licensee

requested a NOED from TS 3.7.3 in order to extend the time

to shut down the units from 12 to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> so that the units

could be shut down sequentially rather than in parallel.

The NRC gave approval to extend the time to shut down the

units from 12 to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The back out procedure and

operability testing were successfully completed in the early

morning hours of September 1, 1995. TS 3.7.3 was exited at

2:36 a.m., on September 1, 1995. Prior to exiting TS 3.7.3,

Unit 3 had reduced power to 76 percent (Units 1 & 2 remained

at 100 percent).

The inspectors were concerned with various aspects of the

modification implementation including scheduling, work

control, configuration control and management oversight.

The inspectors concluded that the licensee's commitment to

complete the modification within 30 days was made without

fully considering the scope of the work involved. The

inspectors concluded that the 30 day commitment resulted in

inadequate time for Work Control to plan and schedule a very

complex and comprehensive work activity. The inspectors

further concluded that appropriate contingency plans for

backing out of the work were not developed in sufficient

detail prior to beginning the work. This contributed to

exceeding the LCO in that the back out procedure did not

anticipate several equipment responses that required

significant LCO time to resolve.

Additionally, the inspectors concluded that management

oversight was minimal until the inspectors identified work

process errors. There was only one supervisor assigned to

oversee the modification implementation even though the work

was being accomplished on a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> basis by two teams (day

shift and night shift). Given the importance of the work

activity and the pressures of schedule, greater management

oversight would have been appropriate. Additionally, the

inspectors considered having "uncontrolled" drawings

intermixed with controlled drawings at the work site a poor

work practice.

After the inspector pointed out the examples of

discrepancies between the blue tags and sliding link

positions, licensee personnel determined that all but one

were the result of the technicians neglecting to

remove/update the tag after closing a link per the

Enclosure 2

9

controlling procedure. However, for one of the examples

(sliding link R95), the licensee personnel erroneously

concluded that the closed link (which conflicted with the

blue tag) should have been opened per the controlling

procedure and therefore opened the link. In reality, the

procedure (step 8.45) required the link to be closed.

Therefore, in an effort to correct a perceived misposition

problem, the licensee personnel created an actual

mispositioned link. As previously addressed in paragraph

2.e. of this report, the failure to maintain configuration

control for Keowee sliding link R95 is identified as Example

6 of Violation 50-269,270,287/95-18-01.

The inspectors noted that there was not a consistent

understanding among station personnel on the purpose and

programmatic aspects of blue tags. The inspectors noted

that the only written description of blue tags and their

usage was contained in Maintenance Directive 4.4.13, ONS I&E

Configuration Control Work Practices. The inspectors

concluded that this directive did not contain sufficient

information to ensure configuration control would be

maintained. For example, the directive did not address when

to hang or remove the tag, or how to handle multiple

components on the same tag.

In response to the concerns raised over exceeding the 72

hour LCO and the request for a NOED, the licensee agreed to

postpone any further work on the modification until a root

cause assessment was completed. The licensee chartered an

incident investigation team composed of non-Oconee Duke

Power personnel to investigate the event. As of the end of

the inspection period the licensee's investigation was not

complete.

(4) Bi-Annual Inspection of Keowee Unit 2 Turbine, WO 95026904

On August 7, 1995, the inspector accompanied licensee

personnel on an inspection of the Keowee Unit 2 spiral case

and turbine. The inspector noted that the area was free of

debris and that there was no apparent damage to any of the

turbine blades and wicket gates. All activities observed

were satisfactory.

(5) Keowee Unit 2 Turbine Guide Bearing Temperature Instrument

Calibration, WO 95039370

On August 23, 1995, the inspector observed portions of this

calibration activity in progress. The inspector verified

that the work was being accomplished in accordance with an

approved procedure, that all test equipment was properly

Enclosure 2

10

calibrated, and that the Keowee operator was aware of the

work in progress. All activities observed were

satisfactory.

(6) Keowee Unit 2 Ground Hunt, WO 95067298

On August 28, 1995, the annunciator for Keowee Unit 2 DC

positive ground came into alarm. The inspector observed the

subsequent ground hunting efforts and concluded that the

ground hunt received adequate support from Oconee

Engineering and I&E personnel.

The inspector noted that

even though Keowee Unit 2 was technically operable, an

operability run was performed to verify the ground had no

effect on unit operation. The inspector considered this a

conservative decision. The operability run was successful

and upon securing the unit, the annunciator cleared. The

alarm later recurred and the licensee was able to determine

the cause to be a pinched wire in the field breaker.

Replacement of this wire successfully eliminated the ground.

The inspector concluded that the licensee's prompt and

extensive ground hunting effort constituted a strength in

corrective maintenance.

(7) Route Chiller Discharge To CCW, WO 59011388

The inspector observed activities in progress during the

implementation of Nuclear Station Modification NSM 52990 on

August 3, 1995. The effort involved a piping and valving

modification to reroute the cooling water discharge (Low

Pressure Service Water) from the Auxiliary Building Air

Handlers to the Units 1 and 2 Condenser Circulating Water

(CCW) discharge piping. The air handler discharge was

previously routed to the Chemical Treatment Pond. The work

document referenced MP/0/B/1810/015, Welding-Piping And

Valve Removal and Replacement Of Class "G", "H", and QA

Condition 3, which was being utilized for the activity. The

inspector determined the work was in accordance with

approved procedures.

b.

The inspectors observed surveillance activities to ensure they

were conducted with approved procedures and in accordance with

site directives. The inspectors reviewed surveillance

performance, as well as system alignments and restorations. The

inspectors assessed the licensee's disposition of any

discrepancies which were identified during the surveillance.

Enclosure 2

11

Surveillance activities observed or reviewed in whole or in part

are as follows:

(1) Reactor Building Spray Pump Test, PT/2/A/0204/07

The inspectors observed performance testing of the Unit 2

Reactor Building Spray Pumps. The quarterly test was

conducted on August 22, 1995, to demonstrate operability of

the pumps. The inspectors verified that the appropriate LCO

status was entered as required during the time that the

testing was in progress. The results of the test were

within acceptable tolerances and the test was performed to

acceptable standards.

(2) Keowee Unit 2 Load Rejection Test, TT/O/A/620/08

The inspectors observed testing of Keowee Unit 2 performed

on September 3, 1995. The test was performed following

modification work to verify that Unit 2 would disconnect

when supplying power to the grid and realign to a "speed no

load" condition in the event of an emergency start signal

from ONS. The testing was required to verify operability of

the unit as an emergency power supply to ONS when generating

power to the grid. The testing was successful and the unit

performed as expected.

(3) Keowee Unit 2 Operability Verification, OP/O/A/1106/19

On September 1, 1995, the inspector observed the operability

test of Keowee Unit 2 to the overhead path. The inspector

observed that the test was conducted in accordance with

procedures and achieved acceptable results.

Within the areas reviewed, concerns were identified regarding the

implementation of a Keowee modification. Concerns included inadequate

planning, lack of management oversight, and lack of configuration

control, paragraph 3.a.(3). The prompt and comprehensive efforts to

locate and eliminate a DC ground at Keowee were identified as a

strength, paragraph 3.a.(6).

4.

Onsite Engineering (37551 and 92903)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

On June 21, 1995, technicians observed that the LPI header A and B

throttle valves had different stroke lengths. Further investigation

revealed that a vendor-supplied drawing had provided an erroneous flow

Enclosure 2

12

coefficient for the two valves. This error resulted in a non

conservative value for the LPI pump runout calculation for the Loss of

Coolant Accident/Loss of Offsite Power event. On July 24, 1995, the

licensee declared that all three units' LPI systems had been inoperable

in the past during a period when the valves had been powered by non

safety power and no credit could be taken for valve operator

performance. During that time, operating personnel may not have been

able to throttle LPI flow during an event and prevent pump runout. The

power to the Unit 2 valves was upgraded to safety-related in 1993, and

Units 1 and 3 in 1994. After upgraded power was provided, assurance for

valve operator performance and thus valve throttling was provided to

control flows and prevent pump runout. Therefore, the operability

concern was no longer valid.

This issue will be addressed further during review of associated LER 269/95-06, Low Pressure Injection System Technically Inoperable Due To

Design Error, issued August 23, 1995.

Within the areas reviewed, licensee activities were satisfactory.

5.

Plant Support (71750 and 40500)

The inspectors assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the following areas were reviewed:

a.

Radiological Controls and Health Physics

The inspectors reviewed the licensee's efforts at dose reduction

during the Unit 3 refueling outage, which was completed July 23,

1995. The licensee expected high total dose accumulation for the

outage due to the unusually high Reactor Coolant System (RCS)

activity levels. RCS activity in Unit 3 had been high for

virtually the entire cycle due to failed fuel pins.

The licensee implemented several measures designed to reduce the

outage dose in accordance with ALARA. These included increased

RCS crud burst and cleanup times during shutdown, as well as

special prophylactic measures at critical access points.

As a result of these efforts, the total accumulated personnel dose

was 164 REM, a record low for a refueling outage at Oconee. The

licensee's efforts to reduce the RCS activity levels was cited as

a strength in inspection report 50-26,270,287/95-11. The results

achieved over the course of the refueling outage confirm the

effectiveness of those efforts.

Enclosure 2

13

b.

Self-Assessment

During the inspection period, the inspectors attended routine and

special PORC meetings. The PORC members were well prepared for

the meetings which addressed a wide range of technical and

programmatic issues. The meetings were well organized, candid

dialogue was encouraged, and emphasis was placed on safety.

Within the areas reviewed, licensee activities were satisfactory.

6.

Exit Interview

The inspection scope and findings were summarized on September 13, 1995,

with those persons indicated in paragraph 1 above. The inspectors

described the areas inspected and discussed in detail the inspection

findings addressed in the Summary and listed below. No dissenting

comments were received from the licensee. The licensee did not identify

as proprietary any of the material provided to or reviewed by the

inspectors during this inspection.

Item Number

Status

Description/Reference Paragraph

Violation 269,270,287/

Open

Inadequate Configuration Control,

95-18-01

Six Examples (paragraph 2.e)

7.

Acronyms

ALARA

As Low As Reasonably Achievable

AMSAC

Accident Mitigation System Actuation Circuitry

ATWS

Anticipated Transients Without Scram

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

CRD

Control Rod Drive

DC

Direct Current

DSS

Diverse Scram System

FDWPT

Feedwater Pump Turbine

I&E

Instrument & Electrical

KHU

Keowee Hydro Unit

LER

Licensee Event Report

LCO

Limited Condition for Operability

LOCA

Loss of Coolant Accident

LOOP

Loss Of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

NOED

Notice Of Enforcement Discretion

NSRB

Nuclear Safety Review Board

NSM

Nuclear Station Modification

ONS

Oconee Nuclear Station

PORC

Plant Operating Review Committee

PIP

Problem Investigation Process

Enclosure 2

14

RCS

Reactor Coolant System

RPS

Reactor Protection System

REM

Roentgen Equivalent Man

TS

Technical Specifications

WO

Work Order

Enclosure 2