ML16154A637

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Insp Repts 50-269/94-20,50-270/94-20 & 50-287/94-20 on 940627-0701.No Violations Noted.Major Areas Inspected: Inservice Insp,Mods & Previous Open Items Involving safety- Related Piping Sys
ML16154A637
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 07/26/1994
From: Chou R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A636 List:
References
50-269-94-20, 50-270-94-20, 50-287-94-20, NUDOCS 9408090091
Download: ML16154A637 (10)


See also: IR 05000269/1994020

Text

ev REG&,

UNITED STATES

05

NUCLEAR REGULATORY COMMISSION

REGION II

o-

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/94-20, 50-270/94-20 and 50-287/94-20

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC

28242

Docket Nos.:

50-269, 50-270,

and 50-287

License Nos.:DPR-38, DPR-47,

and

DPR-55

Facility Name:

Oconee Nuclear Station Units 1, 2 and 3

Inspection Conducted:

June 27 - July 1, 1994

Inspector:

0

7 41

R. Chou

Date Signed

Approved by:

7

4

J.

lake, Chief

Date Signed

Ma eri als and Processes 'Section

En ineering Branch

Division of Reactor Safety

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of Inservice

Inspection, modifications, and previous open items involving safety-related

piping systems.

Results:

In the areas inspected, violations or deviations were not identified.

Two unresolved items and one inspector followup item were closed. The

licensee had weaknesses in documentation and quality control.

One support

drawing was not reverified to check its validity with the controlled document

within 14 days of installation. Two rewelds re-entered by the welder in the

weld log form on a later date were not reverified and resigned by the craft

supervisor and the welding inspector.

9408090091 940726

PDR

ADOCK 05000269

a

PDR

1.

Persons Contacted

REPORT DETAILS

Licensee Employees

      • M. E. Bailey, Regulatory Compliance Engineer
  • S. W. Baldwin, System Engineer
  • D. W. Dalton, Mechanical Engineer
  • J. M. Dave, Engineering Manager
    • B. Dolan, Safety Assurance Manager
  • J. W. Hampton, Vice President on Site
  • R. Harris, System Engineer
      • D. Kelly, Mechanical/Civil Engineer Supervisor
  • F. Linsley, Mechanical Engineer
      • B. L. Peele, Station Manager

Other licensee employees contacted during this inspection included

craftsmen, engineer, operators, mechanics, technicians, and

administrative personnel.

NRC Resident Inspectors

  • P. Harmon, Senior Resident Inspector

G. Humphrey, Resident Inspector

L. Keller, Resident Inspector

  • Attended preliminary exit Interview on June 30, 1994
    • Attended final exit Interview on July 1, 1994
      • Attended both exit Interviews

2.

Document Review on Inservice Inspection on Units 1 and 3 (73755)

At the time of this inspection, Oconee Unit 1 just restarted from a

refueling outage. During Inservice Inspection (ISI) this outage, the

licensee only had two inspection findings which required engineering

disposition.

Support No. 1-03A-1-0-439A-H23 was originally inaccessible for

inspection of items 1, 5, 6, 7, 8, 9, 10, 11 & 12 of the Bill of

Materials. Later, the licensee engineers and inspector reached the

support through an air duct. (Part of the support which could not be

inspected originally is inside of the air duct.) They still could not

inspect the support completely. Since a complete VT-3, Visual

Inspections could not be performed on this support, the piping system

was analyzed for the worse case scenario, which is, that this support

carries no load. This analysis demonstrated that the piping stresses

remained within design allowables, but loads on eight supports

increased. These eight supports were evaluated for the load increases

and all were found to remain within their design allowables. Based on

this evaluation, this support is acceptable for continued service

without additional inspection.

2

Support No. 1-53B-0-435B-DE067 was found to have a discrepancy as

documented in NRC Inspection Report 50-269, 270, 287/92-29. The

deficiency was that this support had a strut which was skewed beyond the

5-degree tolerance. The licensee issued Work Request 92054351 to repair

the strut during the previous outage and also requested a reinspection

to make sure that the problem is not reoccurring during this outage.

This support was reinspected by ISI examiner and was found it to be

acceptable.

The inspector also reviewed the engineering dispositions on Item Nos.

F1.01.140 & F1.01.141 for the Unit 3 ISI inspection during the last

refueling outage around February 1994. Both items are in 3B Steam

Generator support skirt. The bolting material and gusset plate welds

were found to have a "heavy accumulation of boron, rust, and debris."

The bolting material inspected is the anchor bolts for the support

skirt, which are partially embedded in concrete. There are 48, two-inch

diameter bolts around the skirt; the material specification for the

bolts is ASTM A-490. The licensee's engineers determined that the skirt

welds were acceptable and the corrosion on the bolts did not reduce the

material below the minimum thickness requirements due to the size and

quantity of the bolts. Work Request 94003674 was written to clean and

inspect the bolt during the next refueling outage.

No violation or deviations were identified in this area.

3.

Document Review on Modification on Unit 1 (73755)

The inspector reviewed two modification packages which were completed

during this outage; the two packages were NSM# 12921 and 12971.

a.

NSM # ON-12921, Rev. 0

This modification was classified as an Urgent Modification.The

purpose of this modification was to replace the existing carbon

steel piping and valves to the Turbine Driven Emergency Feedwater

Pump (TD-EFWP) Bearing Cooler Jacket with stainless steel

materials because the piping was seriously degraded. The

modification consisted of replacing the piping downstream of

1LPSW-136 to the TD-EFWP Bearing Cooler Jacket; replacing the

piping used for backup cooling water downstream of 1HPSW-248 to

the TD-EFWP Oil Cooler; replacing the carbon steel piping from the

High Pressure Service Water (HPSW) backup to the pump jacket; and

tie into a second, new connection on the 16" HPSW header. Low

Pressure Service Water (LPSW) will no longer service the cooler.

An orifice and flow measurement instrumentation were also added

downstream of 1LPSW-137 for bearing cooling flow measurement.

This modification included replacement of about 150 feet of

corroded 2" carbon steel piping and nine valves.

The construction and QC inspection record package was reviewed by

the inspector. The review included signatures and dates by

workers, craft supervisors, QC inspectors and managers for

3

materials and tools checked out, hold points, weld inspections,

installation completions, procedure approvals, etc. There were no

problems identified by the inspector.

b.

NSM #ON-12971, Rev. 0

This modification was to correct problems which the licensee had

identified in the Low Pressure Service Water (LPSW) piping on the

discharge side of each of the three High Pressure Injection (HPI)

pump motor bearing coolers. Four Problem Investigation Process

(PIP) reports had been generated and one additional problem was

found concerning this line. The following lists a brief

description of the problems which were to be corrected by this

modification:

(1) PIP #93-0801 - Piping downstream of coolers is non-seismic.

The LPSW piping immediately downstream of the HPI pump motor

bearing coolers is Duke Class G (non-seismic) and has a

normal back pressure of 35 psig. During a seismic event,

one train could be broken and cause the other two trains to

be inoperable. The disposition of this PIP will upgrade the

piping to Duke Class F (seismic) to a common discharge

header.

(2) PIP #93-0868 - Piping design temperature is too low.

The design temperature of the LPSW piping immediately

downstream of the HPI pump motor bearing coolers is 1600F.

OSC-6015, "Operability Evaluation for PIP 0-093-0660,"

indicated that this temperature could reach approximately

200'F during accident conditions. This PIP requires this

line to be upgraded to at least 2000F.

(3) PIP #93-0694 - Low LPSW flow through the HPI motor coolers.

This PIP was written for blockage concerns in the LPSW

piping. The modification will resolve the problem.

(4) Existing Rotameters are unreliable and are easily clogged.

The existing Rotameter flow switches (1LPSFS 0009,

1LPSFSO010, 1LPSFS0011) are unreliable. As a result,

Operations has to perform a quarterly "bucket" test. The

modifications will install reliable flow switches.

(5) PIP #93-0695 - Piping upstream of 1LPSW-771 is non-seismic.

The piping upstream of valve 1LPSW-771 providing backup

cooling water to the HPI pump motor bearing coolers is Duke

Class G (non-seismic). A seismically induced break in this

4

portion of the line would prevent the coolers from receiving

the required cooling water flow. The modification will

install a check valve on the class F side of 1LPSW-771 to

eliminate this problem. The modification included:

(1) Replacing/upgrading the piping and associated pipe

supports

(2) Eliminating the unused flow control valves and

thermometers

(3) Replacing three existing rotameters

(4) Adding new flow switches with a flow orifice and a

QA-1 check valve (ILPSW-931)

The inspector reviewed the installation and QC inspection package.

A problem was identified on page 1 of 1, MP/O/A/1810/014,

Enclosure 13.3- Weld Log and Piping Surface Inspection Form. This

form initially contained two welds which had been completed and

signed off by the welders on April 24 & 26, 1994, and accepted by

a QC inspector. On the bottom of the form, required craft

supervisor and welding inspector were signed and dated April 26,

1994. On May 21 and 22, 1994, two rewelds were completed and

entered by the welders and accepted by the QC inspector. The

signatures and dates of craft supervisor and welding inspector on

the bottom portion of the form were not re-entered. This is

considered a weakness in the area of documentation and quality

control.

c.

Support Calculations Review

Six pipe support calculations from the above two modification

packages were randomly selected for review. The design

calculations were partially reviewed and evaluated for

thoroughness, clarity, consistency, and accuracy. The review

included formulas, theories, assumptions, displacements,.member

sizes, stress checks, weld sizes and symbols, bolt sizes, and

standard component capacity. In general, the design calculations

were of good quality. The calculations reviewed are listed below.

Support No.

Calculation No.

Rev. No.

NSM No.

1-14B-403A-H4191

OSC-1237-00-0033

0

12921

1-14B-403A-H4195

OSC-1237-00-0037

0

12921

1-14B-403A-H4199

OSC-1237-00-0037

0

12921

1-14B-435K-H5641

OSC-0967-14-0004

0

12971

1-GH-RS-7273-04

OSC-1619-01-1005

4

12971

1-14B-5100-NS-2004

OSC-1239-10-1015

3

12971

d.

Results and Conclusions

The modification packages and calculations inspected were

acceptable except for the weakness on documentation and quality

control as stated above.

No violations or deviations were identified.

4.

Special Event Review (92700)

PIP Serial No. 1-094-0866 was reviewed. This PIP described an instance

when the LPSW, a safety-related system, was overpressurized and caused

24 gauges to be over-ranged. The licensee suspected that the gauge

damage might be caused by the overpressure or by a water hammer.

After the licensee modified the portion of LPSW and removed a check

valve, the LPSW system was hydro-tested on May 22, 1994, before it was

returned to service. The LPSW system was pressurized by High Pressure

Service Water (HPSW) to a maximum pressure of approximately 115 psig

(HPSW pressure). Some of the 100 psig pressure gauges (the gauges are

capable of sustaining 125 psig) were broken. After disassembly of a

broken gauge, the cause of failure was determined to be the result of

failure of mechanical linkages due to system vibration.

The licensee's Instrumentation and Electrical (I&E) department tested

one of the gauges and determined that the deformation of the mechanical

linkages would require approximately 500 psig, which was well above the

115 psig applied. The licensee concluded that the LPSW hydro-test did

not result in over-pressurization of the LPSW system.

On May 31, 1994, a flow test of the LPSW was performed with a flow of

about 2000 gpm through the Reactor building Cooling Units (RBCU) and

three Rosemount flow transmitters were damaged. Per the manufacturer's

catalog, the maximum range of the Rosemount flow transmitters is 750

inches of H20 (about 4000 gpm) which is well above the test flow rate of

2000 gpm. It appears that the damage to the Rosemount flow transmitters

did not result from the LPSW system flow test.

On June 11, 1994, the 181 Reactor Building auxiliary cooler supply

header was found to be leaking and a 3" header end cap was separated

from the supply header after a loud noise was heard. All of the

pressure gauges on the 1BI auxiliary cooler were also found to be broken

at this time. Meantime, operations was performing PT/O/A/0160/03,

"Component Test of ES Channels 5 & 6."

It was suspected that the

performance of PT/O/A/0160/03 resulted in a water hammer in the

auxiliary coolers because the pressure in IB1

auxiliary cooler, due to

the higher elevation of the cooler, might be below the system vapor

pressure resulting in a water hammer due to vapor cavities.

6

On June 13, 1994, two of the Rosemount flow transmitters could not be

recalibrated and were replaced. A third Rosemount flow transmitter was

recalibrated; all of the Bailey flow transmitters could be recalibrated.

At the same time, the pressure gauges on the 1A, 1C, and 1D Reactor

Building auxiliary coolers were also found to be damaged and were

replaced. The licensee concluded, at that time, that a pressure

transient had not occurred in the LPSW system.

On June 15, 1994, insufficient LPSW flow on the "lA" decay heat removal

train was discovered. The key connecting the manual operator to the

valve stem was found to be sheared on 1LPSW-254. The failed key was

determined to be due to excessive stress. Therefore, the insufficient

LPSW flow shown above could have been the result of a water hammer.

On June 18 and 21, 1994, Reactor Cooling Pump (RCP) 1A2 and IBI cooling

coils were found to be leaking. The licensee concluded that the RCP

cooling coil leaks did not result from a water hammer in the LPSW system

because the valves were not in service during that period.

Based on the above events, the licensee suspected that PT/O/A/0160/03

might result in a water hammer. To determine if PT/O/A/0160/03 resulted

in a water hammer in the LPSW system, TT/1/A/0251/48, "ES channels 5&6

LPSW Functional Test" was performed to simulate the valve manipulations

of PT/O/A/0160/03. Upon performing TT/1/A/0251/48, there were no

indications of a water hammer.

Therefore, the licensee concluded that the damage to pressure gauges was

due to vibration and would bring vibration experts to investigate the

problem. The root cause of the damaged Rosemount transmitters and the

leaking 1B1 auxiliary supply header is still unknown. A possible

explanation is that the damaged components may have been subjected to an

air pocket. The licensee will continue to observe the system during

operation.

The inspector agreed with the licensee's decision to continue to observe

the system operation. No violations or deviations were identified in

this area.

5.

Previous Open Items (92701)

a.

(Closed) Unresolved Item (UNR) 50-269,270,287/91-05-01, Improper

Gap Between Washer and Snubber Rod Bearing

Excessive gaps were found between washers and rod bearings for

snubbers and sway struts during a previous inspection. A %" gap

on Support No. 3-07A-6-0-2400A-H72 was found. The licensee did

not inspect the gaps and did not have a procedure to inspect them.

Conceivably, with an excessive gap, the snubber or sway strut

movements, or impact due to the pipe movement, could cause damage

to the rods or pins. Per the manufacturers catalog the

construction tolerance for the gap should be 1/16-inch.

7

The inspector discussed the gap problem with the licensee

engineers and reviewed the information provided. The licensee

sent a letter on March 8, 1993, to Grinnnell Corporation, 1341

Elmwood Ave. Cranston, RI 02910 and requested guidelines or an

acceptable gap tolerance for inspection. The Grinnell Corporation

provided the following reply to the licensee in a letter

FB/V/3163D, dated April 16, 1993:

The gap between pipe clamp halves is a concern when

evaluating potential damage to the rods or pins in the area

of the spherical bearing and washer.

The functions of the gap between pipe clamp halves is to

accommodate the spherical bearing and to permit the rod eye

to rotate in a 100 cone of action. If the gap is too large

the bending stress in the stud becomes unacceptable.

Additionally, there is a concern that in the unlikely event

of bearing dislodgement, a large gap would permit

unacceptable movement of the bearing.

It is the opinion of Grinnell Corporation that once our

clamps are properly installed with all nuts locked

(particularly the load stud nuts), normal operating

conditions will not affect the gap ("S" dimension) of the

clamp. Any overloading condition would warrant a

reinspection of the clamp.

The concern that an excessive gap between the spacer washer

and spherical bearing could cause damage to the rods or pins

is not shared by Grinnell.

From the above reply to the licensee, the Grinnell Corporation

implied that excessive gaps could result in damage to the support

due to failure of the stud or through bearing dislodgement; but

they failed to specify what gap size could be tolerated.

Per discussion with the licensee engineers, .the inspector learned

that the licensee will not establish inspection tolerances for the

gap, since the manufacturer will not provide a definitive

inspection tolerance. The inspector will close this item and

refer the question to NRR.

b.

UNR 50-269, 270, 287/91-23-01, Maintenance Corrective Action

Program

An investigation process for the failure of the internal threads

on one of the anchor heads during the concrete tendon surveillance

was not initiated and the failure was not considered to be an item

reportable to the NRC. The licensee did not initiate a root cause

investigation based on the non-conformance program to investigate

the failure of the internal threads. Later, the licensee

engineers indicated that this problem would be written in Station

8

Directive (SD) 4.5.5, Problem Investigation Process, which is a

lower tier program. The more significant non-conformances were

handled by a Problem Investigation Report (PIR). The inspector

also found that this event would not be a reportable item to NRC

since the tendon was evaluated to be acceptable and operable.

The inspector discussed the problems with the licensee engineers

and reviewed the information provided. The licensee rewrote the

Problem Investigation Report (PIR) to combine all other procedures

into it and to include all non-conformances. The new PIR is

divided into four categories from the least significant non

conformance to the most significant non-conformance and were

classified and evaluated by the same people in each displine.

Based on the actions taken by the licensee, this item is

considered closed.

c.

Inspector Followup Item (IFI) 50-270/93-16-01, Pipe Support

Related Defects Found During Inservice Inspection

This matter identified three problems to be followed and the

corrective actions reviewed. The problems were a bent rod,

standing water in the Quench Tank, and a base plate gap between

the base plate and concrete.

The inspector discussed the problems with licensee engineers and

reviewed the information provided. The bent rod was replaced.

The standing water disappeared toward the end of outage during the

licensee reinspection. A shim was installed between the base

plate and concrete per Work Request 93027412 and Work Order 94024506-01.

The inspector reviewed the construction and QC inspection package

for the above work request and work order. A minor deficiency was

found in that the support drawing attached to the package for

construction was not validated within 14 days of the construction.

The drawing was initiated, obtained, and verified from the

document controlled area on March-9, 1994;-the-work was completed

between April 12 and 14, 1994. The support drawing was not

reverified and revalidated within 14 days of April 12, 1994. The

inspector considered this problem to be a minor weakness in

document control, therefore, this IFI is considered closed.

6.

Exit Interview

The inspection scope and results were summarized on June 30 and July 1,

1994, with those persons indicated in paragraph 1. The inspector

described the areas inspected and discussed in detail the inspection

results listed below. Proprietary information is not contained in this

report. Dissenting comments were not received from the licensee.

(Closed) Unresolved Item 50-269, 270, 287/91-05-01, Improper Gap Between

Washer and Snubber Rod Bearing (paragraph 5a).

9

(Closed) Unresolved Item 50-269, 270, 287/91-23-01, Maintenance

Corrective Action Program (paragraph 5b).

(Closed) Inspector Followup Item 50-270/93-16-01, Pipe Support Related

Defects Found During Inservice Inspection (paragraph Sc).