ML16148A837

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Insp Repts 50-269/93-24,50-270/93-24 & 50-287/93-24 on 930829-0925.Violations Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities,Keowee Issues & Employee Concern Program
ML16148A837
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 10/18/1993
From: Harmon P, Keller L, Lesser M, Miller W, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A836 List:
References
50-269-93-24, 50-270-93-24, 50-287-93-24, NUDOCS 9311080250
Download: ML16148A837 (20)


See also: IR 05000269/1993024

Text

gA RE(;,,

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

0 8101

MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.: 50-269/93-24, 50-270/93-24 and 50-287/93-24

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.: DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name:

Oconee Nuclear Station

Inspection Conducte

August 29 -

September 25, 1993

Inspector:

'15b-

____/

PE.mon,

Senior Resident Inspector

Date Signed

6 (2-/

W. K.

tner, Resident Inspector

Date Signed

er, Resident Inspector

Date Signed

W. H. Mller, Jr., Project Engineer

Date Signed

Approved by:?V

M. S. Lesser, Setion Chief,

Date Signed

Reactor Projects Section 3A

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, surveillance testing, maintenance activities,

Keowee issues, review of licensee event reports and review of

licensee's employee concerns program (Attachment 1).

Results:

Two violations were identified. The first violation involved

inadequacies in the licensee's test program which resulted in a

Unit 3 load shed channel being inoperable for approximately six

years (paragraph 2.h).

The second violation involved a failure to

implement the fire protection plan testing requirements contained

in the Selected Licensee Commitments Manual (paragraph 6).

9311080250 931019

PDR ADOCK 05000269

a

PDR

t

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

S. Benesole, Safety Review Manager

D. Coyle, Systems Engineering Manager

  • J. Davis, Safety Assurance Manager

T. Coutu, Operations Support Manager

B. Dolan, Manager, Mechanical/Nuclear Engineering

W. Foster, Superintendent, Mechanical Maintenance

  • J. Hampton, Vice President, Oconee Site

D. Hubbard, Component Engineering Manager

C. Little, Superintendent, Instrument and Electrical (I&E)

  • M. Patrick, Regulatory Compliance Manager
  • B. Peele, Engineering Manager
  • S Perry, Regulatory Compliance
  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors

P. Harmon

  • W Poertner
  • L. Keller
  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends.

Inspectors attended some shift

0.Hro

2

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Units 1, 2 and 3 Spent fuel Pool Rooms

Station Yard Within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station

During the plant tours, ongoing activities, housekeeping,

security, equipment status, and radiation control practices were

observed.

b.

Plant Status

Units 1, 2, and 3 operated at power the entire reporting period.

c.

LPSW Valve Failure

At 1:10 p.m. on September 1, valve 2LPSW-51 failed close while in

the automatic mode of operation. Valve 2LPSW-51 is the Unit 2

main turbine oil cooler temperature control valve and throttles

low pressure service water (LPSW) flow to the main turbine oil

tank to maintain oil temperature at setpoint. When 2LPSW-51

failed close, oil temperatures increased until a main turbine oil

cooler outlet temperature alarm (117 degrees) was received in the

control room. Temperature alarms were also received on turbine

bearings 4 and 5. The operators immediately diagnosed the cause

of the temperature alarms and placed the 2LPSW-51 controller in

manual and opened the valve to reestablish LPSW flow to the oil

cooler. The licensee determined that the oil temperature detector

had failed low resulting in a close signal being applied to the

valve controller. The licensee repaired the temperature detector

and returned the valve to automatic control.

d.

Mispositioned Containment Isolation Valve

On September 2, the licensee found valve 2CF-41 approximately 7

turns open. Valve 2CF-41 is a normally closed 3/4 inch instrument

3

root valve on the Core Flood Tank 2B fill line and is a

containment isolation valve. The mispositioned valve was

identified by a non-licensed operator during makeup to Core Flood

Tank 2B when 600 psig was indicated on the local gage downstream

of valve 2CF-41. The non-licensed operator notified the control

room and the valve was determined to be approximately 7 turns

open. Valve 2CF-41 was closed and the operators verified that the

root valve on the Core Flood Tank 2A fill line was closed and that

the corresponding valves on Units 1 and 3 were also in their

required positions. Subsequent to finding valve 2CF-41 open, the

licensee reperformed the Outside Reactor Building Manual Isolation

Valve Checklist, PT/2/A/115/08, Enclosure 13.3. No other

containment isolation valves were found mispositioned.

PT/2/A/115/08, Enclosure 13.3, had last been completed on June 18.

The licensee did not identify any evolutions since the last

completion date of the procedure that would have opened valve 2CF

41. The licensee will issue a Licensee Event Report (LER) as

required by 10 CFR 50.73. The inspectors will follow this item by

review of the licensee LER.

e.

Inoperable Reactor Building Radiation Monitors.

At 10:10 p.m. on September 3, the licensee declared the Unit 3

reactor building radiation monitors 3RIA-47,48,49 and 49A

inoperable due to water intrusion in the sample lines. The sample

lines were drained, however, subsequent monitoring determined that

water accumulation continued to occur in the sample lines. A

reactor building entry was made at 2:15 a.m. on September 5 and

the licensee determined that valve 3FDW-253 had a bonnet to body

leak and that steam was being entrained in the monitor sample

piping inlets. Valve 3FDW-253 is a 1 inch vent valve located on

the 3B steam generator feedwater line inside the reactor building.

The licensee redirected the steam leak by draping the valve with

welding cloth and securing it to the piping.

The licensee

returned the instruments to service and monitored for water

intrusion. The instruments were declared operable at 3:00 p.m. on

September 5 after the instruments exhibited expected radiation

values and trends. The licensee performed an online leak repair

of valve 3FDW-253 on September 8 to stop the body to bonnet leak

and prevent further steam cutting of the valve.

f.

C LPSW Pump Motor Replacement

At 2:32 p.m. on September 15, the licensee removed Units 1 and 2,

C LPSW pump from service to replace the pump motor due to elevated

motor winding temperatures. The licensee had previously replaced

the B LPSW pump motor for Units 1 and 2 on April 29, 1993, due to

elevated stator temperatures and had replaced the 3A LPSW pump

motor on June 30, 1993, due to a motor failure caused by

insulation breakdown on the X phase motor winding. The C LPSW

pump motor was replaced and the pump returned to service at

4

6:03 a.m. on September 16. The pump motor replacement went

smoothly and the pump was returned to service within the TS

required time frame.

g.

Independent Spent Fuel Storage Installation (ISFSI) Cask

Mispositioned in the Unit 3 Spent Fuel Pool.

At approximately 8:00 a.m. on September 20, the ISFSI storage cask

was misaligned in the Unit 3 Spent Fuel Pool.

The licensee was

placing the empty cask on the cask pit stand located in the north

east corner of the spent fuel pool when the cask was mispositioned

on the stand, resulting in the cask leaning against the north end

of the spent fuel pool.

The maintenance personnel involved in

moving the cask attempted to lift the storage cask to realign the

cask to the stand, at which time the lifting hook on the cask

trunion located opposite of the spent fuel pool wall shifted, the

trunion end cap was knocked off and the lifting hook slipped

partially off the trunion. The trunion end cap is not designed to

withstand the lifting forces involved in moving the cask but

provides guidance for the lifting hook until the hook is fully

engaged and supporting the load. With the cask cocked on the

stand the trunions were not horizontal and the one lifting hook

engaged its respective trunion, lifting the cask and allowing the

other lifting hook to shift and engage against the trunion end

cap. The licensee stopped movement of the cask with one corner of

the cask resting on the stand guide and the other corner

approximately 3 inches above the stand with both lifting hooks

partially supporting the load. The licensee secured the cask in

its present position by opening the supply breaker to the crane

and commenced to determine corrective actions to retrieve the cask

from the spent fuel pool.

The licensee initially decided to

remove the spent fuel from the fuel racks adjacent to the cask to

establish a safe radius and to ensure that fuel assemblies would

not be damaged if the cask toppled over during recovery efforts.

The licensee determined that 136 fuel assemblies had to be moved

from the adjacent fuel racks and commenced fuel movement to

relocate the assemblies in the spent fuel pool.

Fuel movement was

completed on September 22.

In conjunction with the fuel movement activities, the licensee

developed a plan and procedure to retrieve the cask from the spent

fuel pool.

The licensee's retrieval plan involved securing the

lifting hooks with a temporary collar, placing shims under the

cask to prevent excessive tilting, lowering the cask to allow the

temporary collar to be tightened to ensure full engagement of the

lifting hook on the trunions, lifting the cask and placing it

securely on the stand, removing the lifting rig for inspection,

reattachment of the lifting rig to the cask, and removal of the

cask from the spent fuel pool into the cask storage pit located

adjacent to the spent fuel pool.

5

The licensee commenced cask retrieval efforts on September 25 and

completed the transfer of the cask to the storage pit on

September 27.

The inspectors monitored the licensee;s activities

in the spent fuel pool .and witnessed cask retrieval evolutions in

progress. The licensee's efforts were deliberate and accomplished

in a controlled manner. Preliminary inspections of the cask did

not identify any damage. The licensee does not plan to

reintroduce the cask into the spent fuel pool until a root cause

evaluation is completed and corrective actions implemented to

prevent recurrence. The inspectors will follow the licensee's

actions in this area.

h.

Load Shed Channel 1

During the previous inspection period (NRC Inspection Report

269,270,287/93-22) the inspectors identified an Unresolved Item

concerning the past operability of Unit 3 Load Shed Channel 1.

The past operability concern resulted from the fact that the load

shed channel 1 slave relay in switchgear 3TD had been incorrectly

wired to a 120 VAC power supply in 1987, during implementation of

a modification package. The item was identified as an unresolved

item because the licensee had not completed the past operability

evaluation but had stated that the preliminary review indicated

that the channel had been operable.

The licensee completed the past operability evaluation during this

inspection period and provided the evaluation to the inspectors

for review. The licensee justification for operability was based

on the operability of the other load shed channel and non-safety

related undervoltage relays that would accomplish the load shed

function independently of the load shed channels. Technical

Specification 3.7.1.c requires that the emergency power switching

logic circuitry be operable as specified by the conditions of

Table 3.7-1.

Table 3.7-1 requires that two circuits/channels of

load shed and transfer to standby circuits (Channels A and B) be

operable during normal operation. The undervoltage relays are not

considered a portion of the emergency power switching logic

circuitry, are not considered technical specification required

components, are not safety related, and are not controlled as part

of the licensee's quality assurance program.

The inspectors discussed the issue with Region II,

NRR, and OE to

review the licensee position with respect to the past operability

of load shed channel 1 and the incorrect wiring of the switchgear

3TD channel 1 load shed slave relay. It was concluded that the

post modification testing performed after implementation of

modification TN/3/A/1426/00/0 had been inadequate and that the

load shed channel had been inoperable since 1987 when the

modification was implemented. The failure to establish an

adequate post modification test program on the Unit 3 Load Shed

Channel 1 circuity following the performance of Modification

Package TN/3/A/1426/00/0, resulting in the incorrect wiring of the

6

load shed channel 1 slave relay in switchgear 3TD going undetected

and the channel being inoperable from March 1987 to August 1993 is

identified as Violation 287/93-24-01: Inadequate Post Modification

test Program.

Within the areas reviewed, one violation was identified.

3.

Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined

for necessary test prerequisites, instructions, acceptance criteria,

technical content, authorization to begin work, data collection,

independent verification where required, handling of deficiencies noted,

and review of completed work. The inspectors witnessed the tests, in

whole or in part, to verify that approved procedures were available,

test equipment was calibrated, prerequisites were met, tests were

conducted according to procedure, test results were acceptable and

systems restoration was completed.

Surveillances reviewed and witnessed in whole or in part:

-

TI/2/A/3001/12A, Functional Test for 2RC-4 Indication Lights.

This special test procedure verified proper operation of the open

and closed indicating lights for valve 2RC-4, Pressurizer PORV

Block Valve, in the Safe Shutdown Facility (SSF) control room.

The inspectors reviewed the special test procedure, witnessed the

performance of the test from the SSF control room, and verified

that the acceptance criteria was met.

-

PT/0/A/0620/16, Keowee Hydro Emergency Start Test. The inspectors

observed the performance of this technical specification required

surveillance procedure on September 16 and September 20. On

September 16 the Keowee Unit 1 generator breaker failed to close.

On September 20, Keowee Unit 1 started but did not obtain expected

voltage of 13.8 KV. The voltage regulator was adjusted and the

test reperformed satisfactorily. This item is discussed in more

detail in paragraph 5.

Within the areas reviewed, licensee activities were satisfactory.

No violations or deviations were identified.

4.

Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work that

was not within the skill of the trade. Activities, procedures, and work

requests were examined to verify that proper authorization to begin work

was given, provisions for fire were made, cleanliness was maintained,

7

exposure was controlled, equipment was properly returned to service, and

limiting conditions for operation were met.

Maintenance activities reviewed and witnessed in whole or in part:

-

WR 93030743, Install Wiring and Test 2RC-4. This maintenance

activity installed a jumper in the control circuitry for valve

2RC-4, pressurizer PORV block valve, to provide power to the open

indicating light in the SSF control room during an SSF event.

This jumper had been inadvertently deleted during a previous

modification package and was identified as Violation 270/93-21-01

in NRC Inspection Report No. 269,270,287/93-21. The inspectors

reviewed the work package and observed the installation of the

jumper.

Within the areas reviewed, licensee activities were satisfactory.

No violations or deviations were identified.

5.

Keowee Issues

a.

Both Keowee Units out of Service for Modification

At 7:34 a.m. on September 7, both Keowee units were removed from

service to allow implementation of modification 52930, Replacement

of Keowee Transfer Circuitry for Switchgear 1X and 2X., Technical

Specification 3.7.6 allows both Keowee units to be removed from

service for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> provided the outage is scheduled and the 4160

volt standby busses are energized by a Lee Gas Turbine through a

dedicated transmission line. The purpose of the modification

package was to modify the Keowee auxiliary transfer logic scheme

to allow the Keowee unit aligned to the underground path to be

powered from the underground path and the Keowee unit aligned to

the overhead path to be powered from the overhead path. The

modification also modified the transfer to backup power supply

scheme to allow power to be restored to the preferred power supply

before transfer to the backup power supply occurred. The

modification was implemented and the Keowee units were returned to

service at 12:51 a.m. on September 8.

b.

Keowee Unit 1 Failure to Start

On September 16, the inspectors witnessed the licensee's

performance of surveillance PT/0/A/0620/16, Keowee Hydro Emergency

Start Test. This test demonstrates the following: 1) operability

of each Keowee Hydro units' emergency start circuitry from the

Oconee Control Rooms; 2) the ability of the Keowee units to reach

rated speed and voltage within 23 seconds; 3) the ability of the

Keowee units to supply 25 MW or greater to the system grid; and 4)

verification of the setpoints for time-delay relays 52-1TD and 52

2TD for the close permissive signal to the generator output

breakers ACB-1 and ACB-2. Both of the Keowee units received a

8

start signal and Unit 2 reached rated speed and voltage

satisfactorily. However, the Unit 1 generator supply breaker

(Device No. 41-52) did not close and the unit did not develop an

output voltage. The breaker closing coil energized but the

breaker did not fully actuate and the closing coil overheated.

This placed Keowee Unit 1 out of service and put the Oconee site

in a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCO per TS Section 3.7.2. The licensee promptly

realigned Keowee Unit 2 from the overhead path to the underground

path and verified that the unit was operable. Subsequent

evaluation by the licensee determined that the breaker failure was

internal to the breaker itself. The licensee initially indicated

that the breaker failure was caused by high resistance in the

closing coil contacts. The theory developed was that the high

resistance value reduced the current to the closing coil to a

value that would not close the breaker and that the closing coil

remained energized and eventually overheated. The licensee

replaced the generator breaker and performed the monthly

performance test to verify operability of Keowee Unit 1. The

monthly test starts the unit from the Oconee control room. The

inspectors questioned the decision not to perform the emergency

start test to verify operability. The licensee indicated that

personnel considerations precluded the test from continuing in

that personnel availability would be impacted since the test had

been performed just prior to the end of the scheduled workweek.

The licensee justified that performance of the monthly test would

verify operability of the generator supply breaker. The licensee

completed the Keowee emergency start test on Monday September 20.

Subsequent to replacing the generator supply breaker, the licensee

performed testing on the failed breaker. The licensee determined

that with 8 amps supplied to the closing coil, the breaker.closed

as designed. The normal current at full voltage is approximately

22 amps. The licensee also determined that current value too low

to prevent the breaker from operating did not overheat the closing

coil enough to cause damage. The licensee determined that full

voltage and current were required to overheat the closing coil to

the point of damage.. The licensee also determined that the high

resistance measured during the initial troubleshooting was most

likely caused by the overheating of the closing coil.

The coil

resistance increases significantly as the coil temperature

increases. The licensee believes that the resistance values

measured initially were influenced by the elevated coil

temperature. After further review the licensee identified that a

missing cotter pin in the latching mechanism may have caused

mechanical binding and prevented a previous trip signal from fully

resetting. The inspectors will continue to follow the licensee's

investigation.

c.

Keowee Unit 1 Voltage Regulator Set Less Than Rated Voltage

During the performance of PT/0/A/0620/16, Keowee Hydro Emergency

Start Test, on September 20, Keowee Unit 1 started and established

9

rated speed but did not established rated voltage of 13.8 KV. The

machine developed 13.3 KV. The procedure acceptance criteria

required that the machine develop approximately 13.8 KV. The

performance technicians initially discussed signing the step off

as complete based on the 13.3 KV value obtained. Subsequent

discussions determined that the test would be continued and a test

discrepancy initiated to resolve the low voltage concern. Design

engineering was contacted and preliminary discussions determined

that 13.3 KV was acceptable but that the voltage regulator should

be adjusted to 13.8 KV. After completing PT/0/A/0620/16, the

licensee removed Keowee Unit 1 from service to adjust the voltage

regulator. The voltage regulator was adjusted and PT/0/A/0620/16

was reperformed to verify proper operation of the voltage

regulator. The unit was returned to service at approximately 7:08

p.m. later that same day. The licensee determined that the

voltage regulator had been set at 13.3 KV during previous

maintenance activities based on information from design

engineering that the minimum acceptable voltage was 13.2 KV. The

licensee plans to revise the performance test to establish an

acceptable voltage band based on the no-load value of 13.8 KV and

is reviewing the program to ensure that the voltage regulator is

required to be set at 13.8 KV for no-load conditions.

No violations or deviations were identified.

6. Review of Licensee Event Reports (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine

if the information provided met NRC requirements. The determination

included: adequacy of description, compliance with Technical

Specification and regulatory requirements, corrective actions taken,

existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LERs were reviewed:

a.

(Closed) LER 269/92-11, Potential Single Failure During A

LOCA/LOOP Event May Result in the Loss of Emergency Power Due to

Design Deficiency.

During an engineering review, the licensee identified that a

postulated failure of the Keowee Hydro underground feeder air

circuit breaker could cause closure of the air circuit breaker to

the overhead path on the unit aligned to the underground path.

This could tie both Keowee units together through the main step up

transformer, possibly out of phase, rendering both units

inoperable.

To correct this problem, the control circuitry to the air circuit

breakers were modified by the installation of normally closed

contacts ("B" fingers) to prevent the two Keowee units from

connecting to the overhead path at the same time. Also, Timer 52

1TD was replaced with a timer that has a longer range of

10

adjustment. The new timer is set at 6 seconds instead of 4

seconds. These modifications should prevent both units from

connecting to the overhead line at the same time during emergency

starts when there is a failure of the 13.8 KV underground path to

Oconee. The inspector reviewed Work Request No. 9272588 01, ACB 1

and ACB 2 Interface Modification, and Procedure TN/2/A/0E4673/001,

Install Interlock from ACB 1 to ACB 2 and from ACB 2 to ACB 1

Replace Timer 52-1TD, and verified that this modification was

complete.

In addition, the licensee conducted a single failure analysis of

the Keowee power system. This analysis, Calculation OSC-5096,

Keowee Single Failure Analysis, identified four postulated single

failure problems. As of this inspection the potential single

failures had either been corrected by station modifications or

temporary measures had been implemented to eliminate any single

failure that could render both units inoperable and prevent the

Emergency Power System from performing its intended safety

function. The inspectors reviewed this analysis. The licensee

has completed the corrective actions for this LER.

b.

(Open) LER 269/92-14, Equipment Failure Results in the

Inoperability of Keowee Unit 2 Overhead Emergency Power Path and a

Technical Specification Violation.

While performing post-modification testing, the licensee

identified a failed relay which resulted in the inoperability of

the Keowee Unit 2 overhead emergency power path. The failed relay

was repaired by replacing a plastic stop nut, adjusting the

contact gap according to the manufacturer's instructions and

retesting the relay to ensure operability. To prevent recurrence,

the licensee initiated the following corrective action:

-

Inspect and repair other MG-6 type relays at Oconee and

Keowee.

-

Develop and implement an appropriate Preventive Maintenance

program for the MG-6 type relays.

-

Perform tests per the Keowee Design Basis Document.

The inspectors reviewed the licensee's corrective action and noted

the following status:

MG-6 RELAYS

The MG-6 relay inspection program has been completed for Keowee

(July 1993), Oconee Unit 1 (February 1993) and Oconee Unit 2 (June

1993).

The inspection of the Oconee Unit 3 MG-6 relays is

scheduled to be completed during the next scheduled refueling

outage in early 1994. Presently only four MG-6 relays have been

replaced. Four of the six MG-6 relays installed at Keowee have

11

been replaced with new ITE solid state type relays (Relay Nos.

27X/1X, 27X/2X, 27X/CX1 and 27X/CX2). The inspector reviewed

Procedure TN/5/A/2930/00, Replacement of Keowee Transfer Circuitry

for Switchgear 1X and 2X, which provided instruction and

documentation for the replacement of these four relays. No

discrepancies were noted. The annual performance of

PT/O/A/0620/16, Keowee Hydro Emergency Start Test, verifies the

operability of the new relays. An evaluation by the licensee is

in progress on the remaining two MG-6 relays installed at Keowee

(Relay Nos. 27T/1X and 27T/2X) to determine if these relays should

also be replaced. These relays perform a safety related function

during emergency start of Keowee by providing a time delay to

assure that the Oconee switchyard is isolated prior to Keowee

being aligned to the overhead path. The two remaining MG-6 relays

are verified operable by performance of PT/O/A/0610/22, Degraded

Grid Switchyard Isolation Functional Test, which is presently

proposed to be performed every 18 months. The licensee had not

identified any required modifications, repairs or replacements to

any of the MG-6 relays installed at the Oconee facility. The NRC

will continue to monitor the licensee's actions in this area.

PREVENTIVE MAINTENANCE PROGRAM FOR MG-6 RELAYS

An evaluation is in progress by the licensee to determine the

appropriate items to be included in a preventive maintenance

program for the MG-6 type relays. The results of this evaluation

will be reviewed during a subsequent NRC inspection.

TESTING REQUIREMENT OF KEOWEE DESIGN BASIS DOCUMENT

The LER states that additional tests will be performed on the

systems and components at Keowee as required by the Keowee Design

Basis Document (DBD).

The inspectors reviewed the DBD for Keowee,

OSS-0254.00-00-1031, Design Basis Specification for the Keowee

Systems and OSS-0254.00-00-2005, Keowee Emergency Power Design

Basis Document. The DBD specifies the following tests be

performed to verify that the system or component meet the DBD

requirements. The inspectors verified that an appropriate

procedure had been prepared and implemented to perform the

required test.

TEST/MEASUREMENT

TEST PROCEDURE/(FREQUENCY)

Emergency start Keowee and

PT/O/A/0620/16, Keowee Hydro

accelerate to rated speed within 23

Emergency Start Test. (Annually)

seconds.

12

TEST/MEASUREMENT

TEST PROCEDURE/(FREQUENCY)

Verify emergency start signal to

PT/O/A/0620/16, Keowee Hydro

close permissive signal for ACB-1

Emergency Start Test. (Annually)

and ACB-2 after a 4 second (+1 or -1

second).

Verify operability of overhead

PT/O/A/0610/22, Degraded Grid System

electrical path from Keowee to

Isolation Functional Test. (proposed

Oconee.

for 18 months. First and only test

performed since plant startup was

conducted May 22, 1993.)

Verify operability of underground

PT/0/A/0610/1J, Emergency Power

electrical path from Keowee to

Switching Logic Functional Test.

Oconee.

(Annually)

Verify each Keowee unit transfers

PT/O/A/0620/17, Keowee Manual

from normal power source to standby

Synchronization Test. (Annually)

power source.

Verify each Keowee unit ability to

PT/O/A/0620/16, Keowee Hydro

supply load equivalent to Oconee

Emergency Start Test. (Annually)

emergency load demand.

Verify Keowee transformer fire

MP/O/A/2000/032, Mulsifyre System

protection system will discharge

Semi-Annual Check. (Annual

1060 gpm at 54 psig.

functional test in summer and annual

dry inspection test in winter)

Specification OSS-0254.00-00-1031, Design Basis Specification for

the Keowee Systems, identifies the Keowee Hydro Station's

mechanical systems and components that support the Keowee

emergency power system. The following systems are identified as

having a safety related function:

-

Turbine Generator Cooling Water System

-

Turbine Guide Bearing Oil System

-

Turbine Sump Pump System

-

Generator High Pressure Oil Lift System

-

Governor Air System

-

Governor Oil System

Although the DBD identifies the safety related systems at Keowee,

no tests and measurement requirements Were specified to verify the

operability of these systems. There are a number of pumps,

valves, and instrumentation and control devices which are not

13

periodically tested to verify operability. This issue was

addressed by the NRC Electrical Distribution System Factional

Inspection, NRC Inspection Report 50-269,270,287/93-02, which was

conducted January 25 - March 5, 1993. The licensee, by letter

dated July 6, 1993, committed to develop testing procedures for

these components by December 31, 1993. The preparation of these

procedures was in progress during this inspection period. First

priority had been given to the preparation of test procedures for

active components such as pumps and valves and for instrumentation

and control devices which activate components such as pumps or

valves. Procedures for testing and verification of

instrumentation and control devices which provides a visual

indication, or provides an audible alarm or activates an

annunciator panel will be developed at a later date. The licensee

has not provided a commitment date to the NRC as to when the

operability of all of these components will be verified.

DBD Specification OSS-0254.00-00-2005, Keowee Emergency Power

Design Basis Document, describes the operability requirements for

the Keowee Main Transformer Fire Protection System. These

requirements are verified by performance of surveillance procedure

MP/0/A/2200/032, Mulsifyre System Semi-annual Check. This

procedure requires two tests to be performed each year. One test

is a "dry test" or visual inspection to be performed during the

winter. The other test is a "wet test" or functional test to be

performed during the summer. *The wet test verifies operability of

all components of the fire protection system. The inspectors

reviewed the most recent test performed on April 30, 1992, by

procedure MP/O/A/2200/032 and noted that the Keowee fire pump had

not been tested. Sections 9.5, 11.3.25 and 11.3.26 of the

procedure specifically require the Keowee fire pump to be tested

for operability and to verify that the pump will deliver at least

1060 gpm at a pressure of 54 psi which is adjusted if lake level

is greater than 787.9 feet. Three test points are required to be

obtained and plotted on the Keowee Fire Protection Pump

Performance Curve, Enclosure 13.5 of the procedure. These

procedure steps had been deleted from the 1992 test procedure by

the "N/A" notation. The pump was not tested and verified operable

by measuring.discharge flow and pressure due to problems with a

portable flow test meter.

Upon further investigation, the inspectors determined that the

last operability test of the Keowee fire pump was performed on

October 31, 1990. Using this date as the base for establishing

the annual functional test schedule, the next test date would have

been required October 31, 1991.

However, a date of May 1, 1992,

would fall within the six month grace period permitted by TS

required surveillances. The 1991 annual test was performed on

April 30, 1992, but this test did not perform an operability test

and evaluation of the fire pump.

14

Selected Licensee Commitment Manual, Section 16.9.2, Sprinkler and

Spray Systems, Surveillance Item a.i, requires that the Keowee

Main Transformer Fire Protection System be functionally tested

annually. The failure to perform an annual functional test of the

fire pump, which is a component of the Main Transformer Fire

Protection System, is identified as Violation 269,270,287/93-24

02: Failure to Perform Functional Test of Keowee Main Transformer

Fire Protection System.

The pump was subsequently tested using a special test procedure.

This test indicated that with a Keowee Lake level above 795.5

feet, the pump would deliver the required flow of 1060 gpm at a

discharge pressure of 54 psi.

However, the difference between the

pump discharge pressure and suction pressure did not meet the past

operability requirements for the pump with a lower lake level.

Selected Licensee Commitment Manual Section 16.9.7, Keowee Lake

Level, required lake level be maintained at a level of 787.9 feet

or greater in order for the Keowee Main Transformer Fire

Protection System to be operable. Presently, the pump will not

meet the operability requirements with lake level below 795.5,

therefore the licensee has revised Selected Licensee Commitment

16.9.7 to require lake level be maintained above 795.5 for Keowee

Main Transformer Fire Protection System operability and is

evaluating corrective actions to return the system to its original

design capabilities. The licensee reviewed Keowee Lake levels to

verify that lake level had not dropped below 795.5 since the last

time the pump was verified operable.

Within the areas reviewed, one violation was identified.

7.

Employee Concerns Program (TI 2500/028)

The inspectors reviewed the licensee's employee concerns program to

determine if the the licensee had implemented a program to provide

employees, who wish to raise safety issues, an alternate path from their

normal line management to express these concerns and to encourage people

to come forward with their concerns without fear of retribution. The

results of this review are documented on the attached form.

8.

Exit Interview

The inspection scope and findings were summarized on September 28, with

those persons indicated in paragraph I above. The inspectors described

the areas inspected and discussed in detail the inspection findings.

No dissenting comments were received from the licensee. The licensee

did not identify as proprietary any of the material provided to or

reviewed by the inspectors during this inspection.

15

Item Number

Description/Reference Paragraph

VIO 50-287/93-24-01

Inadequate Post Modification Test Program

(paragraph 2.h).

VIO 50-269,270,287/93-24-02

Failure to Perform Functional Test of

Keowee Main Transformer Fire Protection

System (paragraph 6)

Attachment

EMPLOYEE CONCERNS PROGRAMS

PLANT NAME: OCONEE

LICENSEE: Duke Power

DOCKET #: 50-269, 270. 287

NOTE: Please circle yes or no if applicable and add comments in the space

provided.

A.

PROGRAM:

1. Does the licensee have an employee concerns program?

(Yes or No/Comments)

Yes

2. Has NRC inspected the program? Report #

No

B.

SCOPE: (Circle all that apply)

1. Is it for:

a. Technical? (Yes, No/Comments)

Yes

b. Administrative? (Yes, No/Comments)

Yes

c. Personnel issues? (Yes, No/Comments)

Yes

2. Does it cover safety as well as non-safety issues?

(Yes or No/Comments)

Yes

3. Is it designed for:

a. Nuclear safety? (Yes, No/Comments)

Yes

b. Personal safety? (Yes, No/Coments)

Yes

c. Personnel issues - including union grievances?

(Yes or No/Comments)

Yes

Issue Date:

XX/XX/XX

- 1 -

2500/XXX

4. Does the program apply to all licensee employees?

(Yes or No/Comments)

Yes

5. Contractors?

(Yes or No/Comments)

Contractor employees may raise safety concerns by contracting the

station's Safety Assurance Manager.

6. Does the licensee require its contractors and their subs to have a

similar program?

(Yes or No/Comments)

No

7. Does

the licensee conduct an exit interview upon terminating

employees asking if they have any safety concerns?

(Yes or No/Comments)

Yes

C.

INDEPENDENCE:

1. What is the title of the person in charge?

None

2. Who do they report to?

Corporate Management

3. Are they independent of line management?

Sometimes

4. Does the ECP use third party consultants?

No

5. How is a concern about a manager or vice president followed up?

By Human Resources and Executive Management

D.

RESOURCES:

1. What is the size of staff devoted to this program?

Oconee Human Resources Staff - 8, but not devoted full time.

2. What are ECP staff qualifications (technical training,

interviewing training, investigator training, other)?

Tyoically four years work experience in the Human Resource area.

2500/XXX

- 2 -

Issue Date:

XX/XX/XX

E.

REFERRALS:

1. Who has followup on concerns (ECP staff, line management,

other)?

Human Resources Staff

Safety Assurance Management

F.

CONFIDENTIALITY:

1. Are the reports confidential?

(Yes or No/Comments)

Yes

2. Who is the identity of the alleger made known to (senior management,

ECP staff, line management, other)?

(Circle, if other explain)

Human Resources staff professional working on the investigation.

3. Can employees be:

a. Anonymous? (Yes, No/Coments)

Yes

b. Report by phone? (Yes, No/Comments)

  • I

Yes

G.

FEEDBACK:

1. Is feedback given to the alleger upon completion of the followup?

(Yes or No - If so, how?)

Yes

2. Does program reward good ideas?

No

3. Who, or at what level, makes the final decision of resolution?

No level defined.

4. Are the resolutions of anonymous concerns disseminated?

Changes are communicated.

5. Are resolutions of valid concerns publicized (newsletter,

bulletin board, all hands meeting, other)?

Changes are communicated.

Issue Date:

XX/XX/XX

- 3 -

2500/XXX

H.

EFFECTIVENESS:

1. How does the licensee measure the effectiveness of the program?

Employee feedback, employee opinion survey.

2. Are concerns:

a. Trended? (Yes or No/Comments)

Yes

b. Used? (Yes or No/Comments)

Yes

3. In the last three years how many concerns were raised?

Closed? ______

What percentage were substantiated?

No technical concerns were raised.

4. How are followup techniques used to measure effectiveness

(random survey, interviews, other)?

Employee opinion survey

5. How frequently are internal audits of the ECP conducted and by

whom?

No audits performed.

I.

ADMINISTRATION/TRAINING:

1. Is ECP prescribed by a procedure? (Yes or No/Comments)

Yes

2. How are employees,

as well as contractors,

made aware of this

program (training, newsletter, bulletin board, other)?

Employee Benefits material,

Company Procedure Manual, notices GET

Training and Orientation training for new employees.

ADDITIONAL COMMENTS:

(Including characteristics which make

the program

especially effective or ineffective.)

The licensee's ECP program is primarily an administrative and personnel conerns

program.

The person completing this form please provide the following information to the

Regional Office Allegations Coordinator and fax it to Richard Rosano at 301-504

3431.

NAME:

TITLE:

PHONE #:

W. K. Poertner/ Resident Inspector/(803) 882-6927 DATE COMPLETED: 9/10/93

2500/XXX

- 4 -

Issue Date:

XX/XX/XX