ML16148A660

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Insp Repts 50-269/92-11,50-270/92-11 & 50-287/92-11 on 920426-0523.Violation Noted.Major Areas Inspected:Operations & Surveillance Testing,Maint Activities & Followup on Previous Insp Findings
ML16148A660
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 06/11/1992
From: Binoy Desai, Harmon P, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A658 List:
References
50-269-92-11, 50-270-92-11, NUDOCS 9207270077
Download: ML16148A660 (11)


See also: IR 05000269/1992011

Text

REG&I

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

@

0

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/92-11, 50-270/92-11 and.50-287/92-11

Licensee: Duke Power Company

P.

0. Box 1007

Charlotte, NC 28201-1007

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name:

Oconee Nuclear Station

Inspection Condud ed:

il

6 - May 23, 1992

Inspector:

P..

or

esident Inspector

Date Signed

B. B. e

ide t Inspector

Date Signed

W. K. Po tner, R ident Inspector

Date Signed

Approved by: G. A lelisle,

tion Chief

Division of Reactor Projects

SUMMARY

Scope:

This routine, resident inspection was conducted in the

areas of operations, surveillance testing, maintenance

activities and followup on previous inspection

findings.

Results:

One violation involving the failure to use the proper

Reactivity Balance Procedure/Curves was identified

(paragraph 2.d).

9207270077 920612

PDR

ADOCK 05000269

G

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • H. Barron, Station Manager
  • S.

Benesole, Safety Review

  • D. Coyle, Systems Engineering

J. Davis, Safety AssuranceManager

D. Deatherage, Operations Support Manager

B. Dolan, Manager, Mechanical/Nuclear Engineering (Design)

W. Foster, Superintendent, Mechanical Maintenance

  • J. Hampton, Vice President, Oconee Site
  • 0. Kohler,. Regulatory Compliance

C. Little-, Superintendent, Instrument and Electrical .(I&E)

  • M. Patrick, Performance Engineer

B. Peele, Engineering Manager

  • S.

Perry, Regulatory Compliance

  • G. Rothenberger, Work Control Superintendent
  • P. Stovall, Superintendent, Operator Training
  • R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians,

operators, mechanics, security forcemembers, and staff

engineers.

NRC Resident Inspectors:

  • P. Harmon
  • W. Poertner

B. Desai

Attended exit interview.

2.

Plant Operationsp (71707)

a.

General

The inspectors reviewed plant operations throughout the

reporting period to verify conformance with regulatory

requirements, Technical Specifications (TS), and

administrative controls.

Control room logs, shift

turnover records, temporary modification log and

equipment removal and restoration records were reviewed

routinely.

Discussions were conducted with plant

operations, maintenance, chemistry, health physics,

instrument & electrical (I&E), and performance

personnel.

Activities within the control rooms weremonitoredon

an almost daily basis.

Inspections were conducted on

day and on night shifts, during weekdays and on

2

weekends. Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions observed were conducted as .required by the

licensee's Administrative Procedures. The complement

of licensed personnel on .each shift inspected met or

exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were

cognizant of plant conditions.

Plant tours were taken throughout the reporting period

on a routine basis. The areas toured included the

following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Iidependent Spent Fuel Storage Facility

Units 1, 2 -and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Units 1, 2 and 3 Spent Fuel Pool Rooms

Unit 2 Containment

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station

During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation

control practices were observed.

Within the areas reviewed, licensee activities were

satisfactory.

b.

Plant Status

Unit 1

Unit 1 operated at full power until May 7 when a

reactor trip occurred from 100 percent power. A loose

pin connection in the exciter circuit caused a

generator lockout which caused an anticipatory turbine

to reactor trip. The unit was taken critical later

that evening. At 3:42 a.m., on May 8,.the unit tripped

from 14 percent due to anticipatory Loss of Feedwater

Pump reactor trip. A leak in the feedwater pump

suction instrument line was found after the trip. The

unit was cooled down to the low pressure injection

(LPI) switchover mode to isolate and repair the leak.

The unit was returned to power on May 11.

On May 22

the unit was shut down due to leakage associated with

reactor coolant pump (RCP) number 1 and 2 seals.. The

unit was cooled down and remained shutdown for the

3

remainder of the report period. The seal repair

outage is expected to last 11 days.

Unit 2

Unit 2 operated at full power until May 15 when it was

shut down .due to temperature on Main Transformer Y

Phase connection exceeding 360 degrees F. Following

repairs, the unit was taken critical and returned to

power operations on May 17. On May 21, a 2A1 RCP oil

pot level low alarm was received. Power was reduced to

30 percent-and upon entry in the reactor building, the

licensee discovered that the lower oil pot vent line

was broken. Fixing the line would have required a unit

shutdown. However, a.decision was made to delay the

shutdown due to power demand. Power was increased back

up to 70 percent and the unit operated with three RCPs.

The unit was shut down on May 22 and following repairs

to the vent line the unit was brought back up on May.

23.

The unit operated at power for the remainder of

the report period.

Unit 3

Unit 3 operated at full power until April 30 when the

3A1 RCP upper oil pot level low alarm came in. Power

was reduced and approximately 15 gallons of oil was

added. On May 6 power was reduced.again to secure the

3D1 Heater Drain Pump (HDP) and isolate the 3D1 HDP

recirculation line.

The unit operated at full power

for the remainder of the report period.

c.

Unit 1 Reactor Trips

On May 7, 1992, at approximately 1:55 p.m.,

Unit 1

experienced an automatic reactor trip from 100 percent

power due to turbine trip on Main Generator Lockout.

The Main Generator Lockout was apparently caused when a

loose pin connection caused a relay to actuate

spuriously, resulting in indication that the Generator

Field Breaker was open. All systems performed normally

following the trip.

At the time of the reactor trip, there were some

housekeeping (sanding/painting) activities in progress

in the vicinity of the Generator and it was initially

speculated that the Generator Lockout was related to

the ongoing work. However, the licensee later

concluded that this did not contribute to the trip.

The licensee performed an investigation and found a

loose pin connection on pin 6 of the EHC (EHC-6)

4

terminal which is mounted inside the generator exciter

housing cabinet. The licensee concluded that vibration

caused the generator protective circuitry to be

interrupted causing the 41MXa relay to actuate when the

pin connection became loose. Relay 41MXa falsely

sensed that the Main Generator field breaker was open

and caused the Main Generator to lockout causing

turbine trip and an anticipatory reactor trip.

The licensee implemented an exempt change which

installed a hard wire bypassing the pin connection

prior to startup. Similar trips on Unit 1 had occurred

in October 1991 and December 1984. These two trips

were attributed to EHC-6 coming loose at the connector

and not the terminal, though both have the same control

logic flowpath. The exciter housing in both instances

had recently been removed for maintenance during

refueling outages. This required manipulating the

connectors. Following the trip in October 1991, the

licensee inspected and tightened all loose terminal

plug connections and connectors. However, the licensee

apparently did not suspect the pin connection within

the terminal plug to be loose. As a permanent solution

to this problem, the licensee was evaluating the

failure logic of relay 41MXa to determine if

alternative logic schemes are needed.

The unit was taken critical at 1:42 a.m. on May 8. At

approximately 3:42 a.m.,

the unit experienced another

reactor trip from 14 percent power. Just prior to the

trip, the operators had received a High Hotwell Level

alarm and the hotwell level was found to be fluctuating

between 72 inches and 79 inches. The normal level is

between 63 inches and 69 inches. There was no guidance

available to the operators with regard to responding to

the alarm and the perceived abnormality. The operators

were concerned about.losing condenser vacuum if the

Condensate Steam Jet Air Ejector suction lines were to

flood from the Condenser due to High Hotwell Level.

Based on this concern, the operators decided to use

condensate recirculation and move some water from the

hotwell to the Upper Storage Tank (UST).

Operations

personnel considered the evolution to be within "skill

of-the-craft", and did not feel that a written

procedure was required.

After verifying that condensate recirculation control

valve 1C-128 was closed, operators began opening block

valve 1C-124. Opening of valve 1C-124 initially acts

to fill a partially vacated Condensate Recirculation

pipe. The volume between IC-124 and 1C-128 is large.

5

It is believed that a significant volume of the

Condensate Recirculation pipe had been emptied by

evaporation of the water to the UST via leakage through

iC-128.

Upon opening 1C-124, a feedwater swing

developed and low suction pressure at the Condensate

Booster Pump and a low discharge pressure at 1B Main

Feedwater Pump (FWP) condition was created. The

FWP/anticipatory reactor trip RPS setpoint of 802 psig

was reached on the 1B FWP discharge. This caused the

reactor to trip. Trip response was normal with control

systems functioning as required to bring the unit to

Hot Shutdown.

The licensee concluded that the oscillations were

caused during the power increase from 0 to 15 percent.

During this period, the steam generator level is held

constant, and the steam bypass system dumps steam to

the hotwell as reactor power is raised to approximately

15 percent.

The impingement of steam from the bypass

system onto the hotwell water level causes turbulence

and false level increases at the level detectors. This

was verified during the startup on May 11.

The

inspectors determined later that some operators were

aware of this phenomenon. The operating crew on shift

at the time of the trip did not realize that false

level indications were routine during steam bypass

system operations. The inspectors discussed this event

with the licensee and the licensee agreed to review

this event to determine if additional training is

required. In addition, the licensee revised the alarm

response procedure for Emergency High Hotwell level to

reference a new enclosure to the Condensate and

Feedwater procedure, OP/1,2,3/A/1106/02. This new

enclosure provides guidance on how to reduce Hotwell

level.

The licensee made the appropriate notifications to the

NRC. In addition, Licensee Event Reports (LERs)

describing these events will be issued by the licensee.

The inspectors will follow.the licensee's long term

resolution of the circumstances that caused these two

reactor trips through the LERs.

d.

Reactivity Management Problems During Unit 1 .Startup

On May 12, during a review of completed procedures, the

licensee identified that during the Unit 1 startup on

May 11,

the Estimated Critical Boron Concentration

(ECB),

Estimated Critical Rod Configuration (ECP), and

the.Subcritical Multiplication (1/M) measurements were

performed by the Unit 1 Supervisor (SRO) using the Unit

2 Reactivity Balance Calculation Procedure/Curves. A

06

second, redundant calculation performed by the Shift

Manager (STA) also used the wrong procedure/curves.

Unit 1 was started up and taken critical using data

derived from Unit 2 procedures/curves. The differences

in the core characteristics between Unit 1 and 2 were

insignificant.

To account for changes in Xenon concentration, RCS

temperature, and boron concentration, the ECB as well

as the ECP are deemed valid only if performed within

one hour of criticality. Initial intent was to go

critical at 1:00 p.m. The Reactivity Balance

Calculation Procedures for Unit 1 and Unit 2, PT/1 or

2/A/1103/15, are located on the common bookshelf of

the Unit 1 and 2 Control Room. The Unit 1 Supervisor

inadvertently pulled the Unit 2 procedure/curves and

performed the ECB and ECP calculations. The STA then

used the same procedures to independently verify the

calculations. Startup was postponed several times and

consequently the ECB and ECP had to be performed three

times. Each time the Unit 2 procedure/curves were

used. Independent verification by another licensed SRO

was also performed using Unit 2 procedure/curves. ECP

based on the Unit 2 Reactivity Balance Procedure was

determined to be 65 percent on Rod Group 6.

Unit 1 was taken critical at 3:17 p.m., on Rod Group 6

at 89 percent. This was within the acceptable band of

plus/minus 1 percent delta k/k of the total inserted

rod worth. The 1/M calculations used to predict

premature criticality were also based on Unit 2

procedures. At that time there was no reason to doubt

the ECP. The next morning at approximately 6:00 a.m.,

the Unit 1 Supervisor for the night shift identified

the error during his review of completed procedures.

Appropriate personnel were notified and available

shutdown margin was verified to be within acceptable

limits. Additionally, the ECP was recalculated using

the appropriate unit procedure and was determined to be

57 percent on Rod Group 6. The critical-data was

within the acceptable band based on the revised

calculations. Consequently, the error made in

calculating the ECP did not significantly affect

startup.

The consequences of this event were insignificant due

to the similarity in the Unit 1 and Unit 2 cores.

However, this event illustrates continued problems in

the area of attention to detail and the failure of the

independent verification process to prevent such

occurrences.

Further attention is warranted in the

area of reactivity management. As an interim

7

corrective action, the licensee color coded the unit

specific Reactivity Balance Procedures. The licensee

has also initiated an upper tier Problem Investigation.

Failure to use the proper Reactivity Balance

Procedure/Curves is identified as violation 50-269/92

11-01.

The inspectors will continue to monitor the

licensee's performance in the area of reactivity

management.

e.

Operator Logs

The inspectors reviewed the operators' logs associated

with the reactor trips and noted that only three

entries consisting of a total of five lines were

entered. The inspectors have discussed the lack of

detail in operator logs in general terms with station

management on other occasions. The information being

logged is not consistent with the management guidance

provided in this area. Operations management had

agreed to address this issue, but instances of

inadequate logging persist. The inspector will

continue to monitor licensee actions pertaining to this

concern.

Within this area, one violation was identified.

3.

Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify

procedural and performance adequacy. The completed tests

reviewed were examined for necessary test prerequisites,

instructions, acceptance criteria, technical content,

authorization to begin work, data collection, independent

verification where required, handling of deficiencies noted,

and review of completed work. The tests witnessed, in whole

or in part, were inspected to determine that approved

procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to

procedure, test results were acceptable and systems

restoration was completed.

Surveillance reviewed and witnessed in whole or in part:

PT/0/A/251/13 Component Cooling Check Valve Functional

Test.

PT/0/A/600/01

Periodic Instrument Surveillance

No violations or deviations were identified.

8

4.

Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during

the reporting period to verify that work was performed by

qualified personnel and that approved procedures in use

adequately described work that was not within the skill of

the trade. Activities, procedures, and work requests were

examined to verify; proper authorization to begin work,

provisions for fire, cleanliness, and exposure control,

proper return of equipment to service, and that limiting

conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 92015377 Repair 2B LPI Pump Vent Line Leak.

The inspectors observed portions of the work activities

associated with WR 92015377 to repair minor leaks on the 2B

low pressure injection pump casing vent line connection and

the pump suction line connection. The work activity

involved disconnecting the lines and cleaning the

connections then reassembling the lines. The inspectors

observed that work activities did not commence on the pump

until at least five hours after the pump had been isolated

by operations for maintenance even though the removal of the

2B LPI pump placed the unit in a twenty four hour limiting

condition for operation.

The post maintenance test for this activity consisted of

filling and venting the pump and performing a visual

inspection of the pipe connections. The pressure -head of

the borated water storage tank, approximately 20 psig,

supplied the pressure source. However, the pump casing vent

would experience a pressure approaching the pump discharge

pressure, approximately 170 psig. The inspectors questioned

the adequacy of the post maintenance test and were told by

the operations staff that the test performed was adequate

and that running the pump was not required.

The work activities associated with the LPI pump (WR 92015377) are considered to be an example of poor

scheduling. The operations group's acceptance of the post

maintenance testing of the LPI pump is considered to be an

example of poor post maintenance testing.

No violations or deviations were identified.

9

5.

Inspection of Open Items (92700)(92701)(92702)

The following open item was reviewed using licensee reports,

inspection, record review, and discussions with licensee

personnel, as appropriate:

(Open) Vio 50-287/91-35-01, Example b

This violation involved the inadvertent dilution of the

Concentrated Boric Acid Storage Tank (CBAST) on Unit 3. The

violation specified that procedures were not followed in

that a valve had been mispositioned which caused an

unmonitored dilution of the CBAST. The event occurred

December 17, 1991. The licensee's investigation and

assessment of the event were completed during this

inspection period. The investigation and report was

performed by the site Safety Review Organization. The

report was comprehensive and accurate regarding the root

cause and contributing causes of this event. Several poor

work practices were identified along with recommendations

for correction.

The report as written contains elements of an effective

investigation and corrective action program. The resident

staff will review licensee management's.response to the'

report for inclusion in the closure of the violation.

6.

Low Pressure Service Water Pump Deadheading Issues

NRC Inspection Report Nos. 50-269, 270, 287/92-09 described

a February 9, 1992, event involving an instance of a

deadheaded Low Pressure Service Water (LPSW) pump. The pump

is shared between Unit 1 and Unit 2. With Unit 1 shut down

at the time, decreased cooling demands and maintenance

activities required the isolation of LPSW to several

components. As a result, total system flow decreased to the

point where the two running pumps interacted with each other

and the weaker pump experienced deadheading or intermittent

zero flow. Operators realized a pump was deadheading based

on the intermittent surging sounds of the LPSW piping

directly above the control room. This was confirmed by the

B.LPSW pump discharge pressure and pump current instruments

in the control room. After checking the pumps locally and

verifying that the B LPSW pump's discharge check valve was

closed, the operators stopped the B pump and the surging

noise stopped.

Following this incident, the inspectors questioned if the

LPSW pump had been damaged. The licensee performed ASME

Section XI testing on the pump and concluded that it was

operable. The inspectors expressed concern to the licensee

that the ASME Section XI testing did not appear adequate to

10

identify damage that could be caused by deadheading. The

licensee, based on information from the pump vendor,

reiterated that the testing performed was acceptable and

that additional testing was not required.

Because of the LPSW incident described, the inspectors

questioned the licensee's response to NRC Bulletin 88-04,

Safety-Related Pump Loss. The licensee stated that the

response, dated January 15, 1990, was adequate. That

response stated that the LPSW system design does not

preclude pump interaction that could lead to deadheading,

but the system configuration would be maintained with

adequate flow paths and total system flows above the minimum

required for deadheading. The Bulletin also requires that

if the system design does not preclude the possibility of

pump-to-pump interaction that could result in deadheading,

the system must be evaluated for flow division including

actual line and component resistances for the as-built

configuration. The evaluation should include development of

head versus flow characteristic curves of the installed

pumps, and actual test data for the "strong" versus -"weak"

pump flows.

This evaluation was not performed, and a basis

for minimum flow requirements has not been established. The

licensee has not determined the minimum flow above which

they stipulated the system would be operated.

The licensee's response to Bulletin 88-04 will be discussed

with the NRC Office of Nuclear Reactor Regulation.

7.

Exit Interview (30703)

The inspection scope and findings were summarized on May 28,

1992, with those persons indicated in paragraph 1 above.

The inspectors described the areas inspected and discussed

in detail the inspection findings. The licensee did not

identify as proprietary any of the material provided to or

reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

Vio 50-269-92-11-01

Unit 2 ECP Procedures Used to Start

Up Unit 1 (paragraph 2.d).