ML16148A577

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Insp Repts 50-269/91-30,50-270/91-30 & 50-287/91-30 on 910929-1102.Violation Noted.Major Areas Inspected: Operations,Surveillance Testing,Maint Activities,Event Followup,Sys Walkdowns & Open Items
ML16148A577
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 11/25/1991
From: Belisle G, Binoy Desai, Harmon P, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A576 List:
References
50-269-91-30, 50-270-91-30, 50-287-91-30, NUDOCS 9112090101
Download: ML16148A577 (9)


See also: IR 05000269/1991030

Text

kREG(Z

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/91-30, 50-270/91-30 and 50-287/91-30

Licensee:

Duke Power Company

P. 0. Box 1007

Charlotte, NC 28201-1007

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name: Oconee Nuclear Station

Inspection Conducte * Se tember 9 - November 2, 1991

Inspectors:

P. E. Harmon, Se ior es d n Inspector

Date Signed

B.Date

Signed

W..K.Poertner

esi ent In

or

Date Signed

Approved by:

6

/5

G. A. glisle, Se6*Q6n Chief

aeSgd

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine,

resident inspection was conducted in the areas of

  • operations,

surveillance testing, maintenance activities,

event

follow-up, system walkdowns, and inspection of open items.

Results:

One violation was identified, concerning the failure to take prompt

corrective action to resolve problems associated with a noncon

servative pressure/level curve that resulted in the letdown storage

tank hydrogen gas potentially being able to expand into the suction

of the high pressure injection pumps under certain small break

accident scenarios (paragraph 6.c).

c112cO9O1O1 91,126

PR- ADOCK& 05000269

PD

PDR

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

D. Couch, Keowee Hydrostation Manager

T. Curtis, Compliance Manager

  • J. Davis, Technical Services Superintendent

D . Deatherage, Operations Support Manager

B. Dolan, Design Engineering Manager, Oconee Site Office

  • W.* Foster, Maintenance Superintendent.

T. Glenn, Engineering Supervisor

  • 0. Kohler, Compliance.Engineer

C. Little, Instrument and Electrical Manager

H. Lowery, Chairman, Oconee Safety Review Group

B. Millsap, Maintenance Engineer

  • M. Patrick, Performance Engineer

D. Powell, Station Services Superintendent

s*G.

Rothenberger, Integrated Scheduling Superintendent

  • R.Sweigart, Operations Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

e

Harmon

  • M. Poertner
  • B. Desai
  • Attended exit interview.

2. Plant Operations (71707)

S

a. General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls. Control room logs,

shift turnover records

temporary modification log and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted onday and on night shifts, during

weekdays and on weekends.

Some inspections were made *during shift

change in order to evaluate shift turnover performance.

Actions

2

observed were conducted as required by the licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis. The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration.Rooms

Units 1, 2 and 3 Spent Fuel Pool Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation ,control practices were observed.

Within the areas reviewed, licensee activities were satisfactory.

b. Plant Status

Unit 1 entered the reporting period in a refueling outage.

On

September 30,

1991,

the generator was tied on the grid ending the

refueling outage.

On October 2, the unit tripped from 73% power due

to a turbine trip/reactor trip.

The problem was corrected and the

unit was returned to power operation on October 3.

Unit 2 operated at power the entire reporting period. On October 11,

1991, the unit reduced power and secured the 2B1 reactor coolant pump

due to a low oil pot level alarm.

A Reactor Building entry was made

to add oil to the oil pot, the pump was restarted and the unit was

returned to 100% power.

Unit 3 operated at power the entire reporting period.

c. Unit 1 Reactor Trip

On October 2, 1991, at 3:55 p.m., Unit 1 tripped from 73 percent

power due to a generator lockout signal.

The generator lockout

signal generated a turbine trip and subsequent anticipatory reactor

trip.

The Turbine-Generator protective relaying sensed that the

generator field breaker had opened and that the generator output

breakers were closed, although the generator field breaker had not

actually opened.

3

During the recovery an emergency feedwater start signal was initiated

when the "A" main feedwater pump (MFP)

tripped after the "B" MFP was

secured.

The "A" MFP tripped due to high discharge pressure caused

by a feedwater swing.

The "B" MFP was restarted and the emergency

feedwater system was secured.

Intermediate Range Nuclear Instrument

NI-3 failed to decrease below 10E-10 amps as expected after the unit

trip. The licensee believes that the detector is in the early stages

of failure and that the detector will become progressively worse due

to saturation at power.

The licensee declared NI-3 inoperable and

decided not to replace the detector prior to unit restart.

The

Oconee Technical Specifications do not require that both intermediate

range nuclear instruments be operable prior to criticality.

The

inspectors discussed this item with Operations Management and

expressed concern that only one intermediate range nuclear instrument

would be operable during the restart of the unit.

The detector

operated properly when power level increased above 10E-10.amps.

The generator lockout signal was determined to be caused by.loose

connectors and terminals that caused a loss of DC power to relay

41 MXA. When 41 MXA deenergized, the protective relaying sensed the

generator field breaker open with the generator output breakers

closed.

The loose connectors and terminals had been disconnected

during the refueling outage to allow removal of the Alterex housing.

The connectors and terminals were repaired/tightened and the unit was

restarted on October 3, 1991.

d. Keowee Unit 2 Failure to Start

On October 4, 1991,

Keowee Hydro Unit.2 failed to start when the

Keowee hydro operator attempted to load the unit on the grid at the

request of the load dispatcher. The Keowee hydro operator contacted

the control room and the hydro unit was declared. inoperable and

Keowee unit 1 was verified operable per the requirements of Technical.

Specification 3.7.2(a)(1) within one hour.

Subsequent investigation

by the licensee determined that a set of contacts in the normal start

protective circuitry were dirty and prevented the local start signal

from initiating a start of the hydro unit. The licensee determined

that the hydro unit would still have started from an emergency start

signal.

The dirty contacts were cleaned and the hydro unit was

tested and returned to service.

No violations or deviations were identified.

3. Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined for

necessary test prerequisites, instructions, acceptance criteria, technical

content, authorization to begin work,

data collection,

independent

4

verification where required, handling of deficiencies noted, and review of

completed work.

The tests witnessed, in whole or in part, were inspected

to determine that.approved procedures were available, test equipment was

calibrated, prerequisites were met,

tests were conducted according to

procedure,

test results were acceptable and system restoration was

completed.

Surveillances reviewed and witnessed in whole or in part:

PT/1/A/230/1B

HPSW to HPI Motor Cooler Flow Test

PT/2/A/600/12

TDEFW Pump Performance Test

Within the areas reviewed, licensee activities were satisfactory.

No

violations or deviations were identified.

4. Maintenance Activities (62703)

a. Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade.

Activities,

procedures,

and work requests were examined to verify; proper

authorization to begin work, provisions for fire, cleanliness, and

exposure control, proper return of equipment to service, and that

limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 94608C

Repair 3PR-34

Within the areas reviewed, licensee activities were satisfactory.

No violations or deviations were identified.

b. Inadequate Post Modification Test

During the Unit 1 refueling outage, valve 1MS-89 was replaced by the

station modification process.

Valve 1MS-89 is the downstream

isolation valve for the main steam pressure control valve to the

turbine driven emergency feedwater pump turbine.

The weld on the

upstream side of the valve is required to be hydrostatically tested

(hydroed) to the main steam pressure requirements,

1313 psig and the

weld on the downstream side of the valve is required to be hydroed to

the auxiliary steam pressure requirements,

720 psig, per the system

drawing.

While preparing to hydro the downstream side of 1MS-89,

operations decided to open 1MS-89 and use the upstream isolation

valve for the pressure control valve (1MS-86) as the hydro boundary.

Subsequent to the hydro,

the post modification testing package

associated with 1MS-89 was signed off as being complete based on the

valve being hydroed to 720 psig.

Subsequent review of the

modification package-by the licensee after the unit was returned to

power identified that the upstream weld on 1MS-89 should have been

5

hydroed to 1313 psig.

Therefore, the post modification test was

inadequate.

Valve 1MS-89 is a normally locked open valve and had

remained locked open throughout the unit startup.

Subsequent to

determining that 1MS-89 had not been tested to the proper hydro test

pressure, a white tag was placed on the valve to ensure that the

valve would remain open until the upstream weld could be properly

tested.

The inspectors expressed concern that the modification

package had been completed and signed off without an adequate post

modification hydro test being performed; however,

the valve was

adequately tested assuming that the valve remained locked open

throughout the operating cycle.

The licensee identified this item

and based on the fact that an adequate post modification test was

performed if the valve remained.in the open position, no enforcement

action will be pursued.

The licensee plans to perform the required

hydro test the next time the unit is brought to a cold shutdown

condition.

No violations or deviations were identified.

5. Low Pressure Service Water (LPSW) System Walkdown (71710)

The inspectors performed a system walkdown on the accessible portions of.

the Unit 3 LPSW system.

The LPSW system provides normal and emergency

cooling. for components in the Turbine Building, Reactor Building and

Auxiliary Building.

The Unit 3 LPSW system consists of two LPSW pumps

that take a suction off the condenser circulating water system and two

supply headers that are crossconnected at the LPSW pump discharge. The

LPSW system is designed such that one LPSW pump should be able to provide

all the required cooling during accident conditions.

The LPSW pumps

receive an automatic start signal on an Engineered Safeguards (ES) signal.

However,

the non-safety portions of the LPSW system outside the Reactor

Building do not isolate on an ES signal.

The inspectors determined that

the Unit 3 LPSW system was aligned correctly, but discrepancies were noted

on the system drawing., the operating procedure valve lineup checklist and

the operating procedure electrical checklist. The discrepancies were not

significant in nature and were discussed with the licensee. The.licensee

is scheduled to perform a Design Basis Document (DBD) review on the LPSW

system as part of the DBD program. This effort had not started as of this

inspection period. The licensee has performed a Self Initiated Technical

Audit (SITA) on the LPSW system previously. The inspectors did not review

the LPSW SITA during the inspection period but plan to review the SITA

results during the next inspection period.

No violations or deviations were observed.

6

6. Inspection of Open Items (92700)(92701)(92702)

The following open items were reviewed using licensee reports, inspection,

record review, and discussions with licensee personnel, as appropriate:

a. (Closed) LER 269/91-02:

Licensed Operator Improperly Exempted From

Requalification Exam Due to a Management Deficiency, Results in TS

Violation.

This LER was submitted to the NRC on May 3, 1991.

Immediate corrective actions taken involved taking the licensed

operator off the active duty roster and notifying the NRC that this

license was not considered current.'

Subsequent corrective actions

included the successful completion of a makeup exam by the operator

and notification to the other Duke Power nuclear stations to assure

proper testing of facility representatives.

In addition,

ETQS

Standard 2306.0 was revised on September 1, 1991.

Based on these

actions, thi.s item is closed.

b. (Closed) LER 269/90-09:

Inappropriate Operator Actions to Control

and Maintain Minimum Level in Emergency Feedwater Inventory Tank

Resulted in a TS Violation.

As part of the planned corrective

actions, training, described in training package 90-12, was given to

all licensed operators concerning control of condensate inventory

when operating in the feedwater. cleanup mode of operation.

The

licensee reviewed the upper surge tank low level computer alarm

setpoint and raised from seven feet decreasing to eight feet

decreasing.

Also, after review of operating procedures, it was

decided not to change the procedure controlling feedwater cleanup

activities.

Instead, the licensee placed a tag near the controller

for the auxiliary steam supply to the 'E' heaters cautioning the

operators to monitor UST level while in the feedwater cleanup mode of

operation. Based on these actions, this item is closed.

C. (Closed) Unresolved item 269,270,287/91-26-02:

LDST .Pressure/Level

Curve.

This item identified that the existing operating curve

defining maximumletdown storage tank (LDST) pressure and level was

nonconservative and that the potential. existed for hydrogen intrusion

into the suction of the high pressure injection pumps under certain

small break .loss of coolant accidents as level in the borated water

storage tank (BWST)

decreased.

This item was identified as an

unresolved item pending further review by the NRC and licensee. The

inspectors determined that the licensee was aware that the LDST

pressure/level curve was nonconservative as early as the December

1990 timeframe when the High Pressure Injection (HPI) System Design

Basis Document was issued.

The licensee at that time carried this

item as an open item on a design engineering punchlist.

The

inspectors had also questioned the adequacy of the curve as a result

of the routine inspection program around this same timeframe and had

been told that Design was reviewing the basis of the curve and would

document its adequacy but based on preliminary reviews the curve

appeared acceptable.

The inspectors continued to question the

adequacy of the curve and in April of 1991 when the licensee again

7

stated that the official calculation had not yet been performed but

that the curve was probably acceptable, the inspectors were shown an

unofficial calculation performed by Design in January of 1991 that

showed there was a 1 psi margin before hydrogen intrusion could occur

at the HPI pump suctions.

The inspectors questioned the margin

available in the calculation and also questioned the assumptions on

which the unofficial calculation was based.

The licensee stated in

the April timeframe that the unofficial calculation was a very rough

calculation with overly conservative assumptions and methodology.

The inspectors were again assured that Design would perform an

official calculation to document the adequacy of the

LDST

pressure/level curve.

However, a timeframe for completion was not

given.

Subsequent to these events,

the licensee performed the official

calculation in September 1991 and determined that the existing LOST

pressure/level curve was inadequate and that the HPI system had been

operated since initial power operation in a condition that was

outside the design basis of the HPI system.

This calculation was

performed as. a result of corrective action for an April 1991 event

where the operators exceeded the the original pressure/level curve

during hydrogen addition to the LDST. The inspectors are not

convinced .that.the review of the pressure/level curve would have

occurred in September for any other reason except for the corrective

action as a result of exceeding the. original curve.

As a result of

this review, the licensee determined that hydrogen intrusion into the

suction of the HPI pumps would have occurred during a small break

LOCA, assuming no operator action if .a

HPI BWST suction valve failed

to open on an ES signal and all three HPI pumps started.

The

licensee also determined that the HPI system had operated on a

routine basis in a condition where hydrogen intrusion into the

suction of the HPI pumps could have occurred even if both HPI BWST

suction valves opened during a small break LOCA assuming no operator

action. The inspectors consider that the licensee actions to resolve

this issue were untimely and that the unofficial calculation was

inadequate in identifying the operability concern and should have

identified to the licensee the importance of completing the review of

the pressure/level curve in an expeditious manner.

The failure to

take prompt corrective action to resolve the LOST pressure/level

curve issue is identified as Violation 269,270,287/91-30-01:

Inadequate Corrective Action to Resolve Operability Concern.

8

7.

Exit Interview (30703)

The inspection scope and findings were summarized on November 1, 1991,

with those persons indicated in paragraph 1 above.

The inspectors

described the areas inspected and discussed in detail the inspection

findings.

The licensee did not identify as proprietary any of the

material provided to or reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

VIO 269,270,287/91-30-01

Inadequate Corrective Action to

Resolve Operability Concern (paragraph

6.c).