ML16148A527

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Insp Repts 50-269/91-12,50-270/91-12 & 50-287/91-12 on 910526-0629.Violations Noted.Major Areas Inspected: Operations,Surveillance Testing,Maint Activities,Spent Fuel Transfer Cask Insp & Insp of Open Items
ML16148A527
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 07/12/1991
From: Belisle G, Binoy Desai, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A525 List:
References
50-269-91-12, 50-270-91-12, 50-287-91-12, NUDOCS 9108120225
Download: ML16148A527 (9)


See also: IR 05000269/1991012

Text

1 REG&

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/91-12, 50-270/91-12 and 50-287/91-12

Licensee: Duke Power Company

P. 0. Box 1007

Charlotte, NC 28201-1007

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name:

Oconee Nuclear Station

Inspection Conducted: May 26 - June 29, 1991

Inspector:

_

_

_

. K. P ertner, Act ng Sen r es

t Inspector

Date Signed

B. B. Desai, Residen

Insp t rgned

Approved. by:

__

_

_

__

_

_

_

G. A.B 1Tsle, S

n Chief

at

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved inspection on-site in

the areas of operations, surveillance testing, maintenance

activities, spent fuel transfer cask inspection and inspection of

open items.

Results: Two violations were identified.

The first violation involved the

loss of configuration control of flow instrumentation (paragraph

2.d).

The second violation involved the operation of safety-related

systems without procedural guidance (paragraph 2.e).

0D

PDR

ADO:K 05000269

0

PDR-

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

D. Couch, Keowee Hydrostation Manager

  • T. Curtis, Compliance Manager

J. Davis, Technical. Services Superintendent

D. Deatherage, Operations Support Manager

B. Dolan, Design Engineering Manager, Oconee Site Office

  • W. Foster, Maintenance Superintendent

T. Glenn, Engineering Supervisor

  • 0. Kohler, Compliance Engineer
  • .C. Little, Instrument and Electrical Manager

H. Lowery, Chairman, Oconee Safety Review Group

  • B. Millsap, Maintenance Engineer

M. Patrick, Performance Engineer

D. Powell, Station Services Superintendent

  • G. Rothenberger, Integrated Scheduling Superintendent
  • R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians,

operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P. Harmon
  • W. Poertner
  • B. Desai
  • Attended exit interview.

2. Plant Operations. (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls.

Control room logs,

shift turnover records,

temporary modification log and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and on night shifts, during

weekdays and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

2

observed were conducted as required by the licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant.annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Units 1, 2 and 3 Spent Fuel Pool Rooms

Station Y'ard Zone within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station,

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Within the areas reviewed, licensee activities were satisfactory.

b.

Plant Status

Unit 1 operated at power for the entire reporting period.

Unit 2 operated at power for the entire reporting period.

Unit 3 operated a.t power until June 9, 1991, when it automatically

tripped on low pressure/temperature due to the Group 5 control rods

dropping into the core. The Unit was returned to service on June 10,

1991.

c. Unit 3 Reactor Trip.

At 3:06 p.m.,

on June 9, 1991,

Unit 3 experienced an automatic reactor trip from 100 percent power.

The automatic actuation of

three of the four channels of the Reactor Protection System (RPS)

on

Low Pressure/Temperature and the subsequent reactor trip was caused

by the Group 5 control rods dropping into the core during movement of

Rod 12 in Group 5. A-

blown fuse in the absolute position indication

instrumentation required Instrumentation and Electrical

(I&E)

personnel to. enter the Control

Rod Patch Panel.

Following the

replacement of the blown fuse, operations performed OP/0/A/1105/09,

4.

3

Patch Panel Verification at Power,

as required by Technical

Specification (TS) 4.7.2.1. Rod 12 of Group 5 was transferred to the

auxiliary power supply to make adjustments to its position. When the

rod was moved, .the entire Group 5 bank dropped into the core and

subsequently the reactor tripped on

Low Pressure/Temperature.

Further investigation by the licensee determined that the transfer

from the regulating to the auxiliary power supply was not complete,

leaving both power supplies connected to the control rod drives.

This resulted in four phases of the rod contactors being energized

instead of two phases.

The magnetic fields produced by the rod

contactors were 180 degrees out of phase, effectively cancelling each

other.

As a result, the contactors opened and the rods in Group 5

dropped into the core. The failure to fully transfer to. the Auxiliary

power supply was due to the transfer switch for Rod 12 of Group 5

failing in the mid-position.

The switch was replaced prior to

startup.

-Maintenance engineering personnel are investigating

possible ways to change the transfer logic to alert the operator that

the transfer has not fully occurred.

The possibility of replacing

the transfer switch with an

improved version is also being

investigated.

The post trip response was normal; however, the following exceptions

were noted:

RPS channel "A" did not trip.

The trip setpoints for all four

channels were checked and found to be within tolerance. The "A"

channel was found to be calibrated towards the lower tolerance

limit, while the other three channels were calibrated toward the

upper limit.

Therefore, the plant had already tripped before

the setpoint .was reached for the "A" channel.

Following the trip, MS-19 (Turbine Bypass Control Valve A) was

continuously cycling even though steam pressure remained

constant. The valve was found to be cycling about 4.5 inches,

and sticking about 1 inch from the closed position. Adjustments

were made and the cycling of the valve was terminated.

As a

result of MS-19 opening and closing, MS-5 (Main Steam Relief

Valve) seated, then re-lifted following the trip. In addition,

the line from MS-19 to the condenser experienced large swings

due to a water hammer. One axial support and one spring support

bed plate were damaged and two elbows were slightly distorted.

The licensee attributed the water hammer to a temporary

modification

which

installed

a

condensate/feedwater

recirculation line to the turbine bypass line.

This source of

water, in addition to leakage by the turbine bypass valves, was

postulated to

be more than the drain line capacity.

Consequently, water accumulated at the bypass line low point.

The licensee has rerouted the recirculating line to the turbine

building drains. In addition, the.licensee has plans to replace

the turbine bypass lines during the next refueling outage.

4

The licensee conducted an investigation of the trip and'events that

occurred as part of this trip.

The inspectors witnessed actions

taken by the operators as well as participated in the post trip

meeting. No problems were identified. The licensee notified the NRC

as required by 10 CFR 50.72 (b)(2)(ii).

Unit 3 was returned to power operation on June 10, 1991.

d. Low Pressure Injection (LPI) Flow Instrument 2FT-4A Inoperable.

On May 30,

1991,

during performance of PT/2/A/0203/6A,

LPI Pump

Performance Test, the 2B LPI header flow instrument 2FT-4A on the

Unit 2 control panel did not indicate flow when the 2B LPI pump was

started.

Subsequent investigation by the licensee determined that

the instrument was valved out of service.

The instrument was

returned to service and an investigation was initiated to determine

how configuration control of the flow instrument was lost. The LPI

flow instruments had been calibrated less than a week prior to the

.pump performance test due to problems identified with the span values

used to calibrate the instruments.

Flow instrument 2FT-4A had been

independently verified at that time as being returned to service in

the controlling procedure.. The licensee was unable to conclusively

determine that the flow instrument had been left valved out of

Il

service after the instrument was calibrated; however,

the most

probable cause was determined to be oversight on the technicians part

when the work control copy of the procedure was combined with the

official copy of the procedure in the control room.

The failure to

maintain configuration control

on flow instrument 2FT-4A is

identified as Violation 50-270/91-12-01: Inoperable Flow Instrument.

The operators did not declare train "B" of the low pressure injection

system inoperable when the flow instrument failed to indicate flow.

-When questioned by the inspector the control room SRO stated that the

system was still operable because flow indication was available on

the plant computer. The LPI flow instruments on the Unit 2 control

board are non-seismic, non-class 1E, air operated instrumentation and

are scheduled to be replaced during the next refueling outage with

instrumentation that meets the requirements of Regulatory Guide 1.97.

The computer point flow indication is also a non-class 1E indication.

The licensee's position is that use of the computer point for

operability of the LPI system is acceptable until the flow

instrumentation is upgraded to meet the requirements of Regulatory

Guide 1.97.

The inspectors have expressed concerns in previous

inspections about the adequacy of the ECCS flow instrumentation. and

the amount of time. that has elapsed without upgrading the instru

mentation.

The instrumentation on Unit 3 was replaced during the

last refueling outage and Units 1 and 2 are scheduled to have the

instrumentation replaced during the next scheduled refueling outage.

Within this area, one violation was identified.

5

e. Core Flood Tank (CFT) Level Problems.

On May 25, 1991., during calibration of the Unit 3 "B" CFT channel 2

level instrument, the indicated level changed from 12.76 feet to

12.54 feet after the channel was calibrated. Channel 1 indicated

13.04 feet.

The channel 2 level instrument had been calibrated due

to the mismatch in indicated level between the two level instruments.

The Technical Specification (TS) lower limit for CFT level is 12.56

feet. Based on the channel 2 level instrument being less than the TS

limit the operators decided to add water to the "B" CFT.

The

operators attempted to makeup to the CFT per OP/3/A/1104/01,

Core

Flooding System; however,

the boric acid mix tank pump would not

pump.

The operators decided to crossconnect the "A" and ."B" CFTs

through the 1 inch sample lines to sluice water from the "A" CFT to

the "B" CFT.

The valves were opened and water level increased to

12.59 inches in the "B" CFT.

OP/3/A/1104/01 did not contain

procedural guidance for sluicing CFTs and a procedure change to

incorporate this method of increasing CFT level into the procedure

was not initiated. The procedure for sampling the CFTs specifically

requires that the non sampled CFTs sample valve be verified shut.

The failure to meet the procedural requirements of OP/3/A/1104/01 for

makeup to the "B" CFT is identified as Violation 50-287/91-12-02:

Failure to Follow Procedure.

The inspector also questioned the, acceptability of crossconnecting

CFTs during normal power operation.

TSs require that both CFTs be

operable when the unit is at power.

If the break location during a

loss of coolant accident was on a core flood tank injection line the

unaffected CFT would be crossconnected to the faulted CFT through the

1. inch sample line.. Based on the inspectors concern, the licensee

performed an engineering evaluation and determined that 25 percent of

the water volume in the non-faulted CFT would not be injected into

the core, however the core would remain covered under this condition.

The inspectors still question the acceptability of crossconnecting

the CFTs.at power since 25 percent of the non-faulted CFT would not

inject into the core and the sample valves do not receive power from

a safety related power supply and by design could not be shut during

a design basis accident.

The licensee is evaluating whether. a

procedure change to allow sluicing the CFTs should be included in the

controlling procedure.

Within this area, one violation was identified

f. Failure of Keowee Unit 1 to Start during Performance Test.

During the performance of PT/0/A/620/09, Keowee Unit 1 failed to

start due to failure of the generator breaker to close. The unit was

declared inoperable, a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement was entered, and an

investigation into the. cause was initiated by the licensee.

The

failure of the generator breaker to close was attributed to the

X-relay contacts not closing at set turbine speed.

A pivoting

6

mechanical finger within the X-relay was found not reset causing the

X-relay contacts to remain open upon energization of the coil.

The

mechanical finger was physically reset and the performance test was

successfully run.

The licensee in conjunction with the manufacturer

is investigating the cause of the failure.

Pending further

evaluation, the licensee is visually verifying that the X-relay is

reset, following each shutdown of the Keowee units and logging that

the relay is reset in the Keowee operators log. The inspectors will

continue to monitor the licensee's actions regarding this issue.

g. Motor Control Center (MCC) Breaker Coordination Problems.

On May 29, 1991, the licensee determined that a breaker coordination

problem existed on MCCs 1, 2, and 3XS2. If an'overcurrent condition

occurred on non-safety panelboards 1, 2, or 3KM during an accident

the feeder breaker to the respective XS2 MCC could trip open prior to

the supply breaker to the non-safety panelboard tripping.

The

licensee found this problem as a result of an ongoing design review

of breaker and relay trip settings to address previously identified

problems in this area.

The panelboard supply was removed from the

safety-related MCC and transferred to a non-safety-related MCC. The

inspectors followed the licensee's immediate corrective actions to

resolve the breaker coordination problem and will followup on this

item via the licensee'.s LER.

3. Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined for

necessary test prerequisites, instructions, acceptance criteria, technical

content, authorization to begin work,

data collection, independent

verification where required, handling of deficiencies noted, and review of

completed.work. The tests witnessed, in whole or in part, were inspected

to determine that approved procedures were available, test equipment was

calibrated, prerequisites were met, tests were conducted according to

procedure,

test results were acceptable and systems restoration was

completed.

Surveillances reviewed and witnessed in whole or in part:

IP/O/A/0400/11

Keowee 125V DC Control Battery Test

PT/3/A/0251/01

LPSW Pump Performance Test

PT/O/A/600/19

Surveillance of 4160 and 600 Volt. Breakers

PT/3/A/0150/22L

Functional Test for HPSW Supply to TDEFW Pump

PT/3/A/6O0/01

Periodic Instrument Surveillance

PT/2/A/600/01

Periodic Instrument Surveillance

PT/1/A/600/01

Periodic Instrument Surveillance

PT/2A/0/600/13A

MDEFW Pump Performance Test

PT/1/A/251/01

LPSW Pump performance Test

Within the areas reviewed, licensee activities were satisfactory.

No violations or deviations were identified.

7

4. Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within

the skill of the trade.

Activities, procedures, and work requests were

examined to verify; proper authorization to begin work, provisions for

fire, cleanliness, and exposure control, proper return of equipment to

service, and that limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 52049J

Replace CRD Breaker CB-2

WR 99938

Exempt Change to Route KM from 1XS2 to 1XO

WR 33203

Replace Transfer Switch between Auxiliary and

Normal Power Supply

WR 33485

Troubleshoot Sullair Primary Instrument Air Compressor

Within the areas reviewed, licensee activities were satisfactory.

No Violations or deviations were identified.

5. - Spent Fuel Transfer Cask Inspection (55050)

On May 29, 1991, the inspector met with licensee representatives to review

the status of a spent fuel canister which was rejected by the licensee.

It was rejected during receipt inspection due to code rejectable lack of

fusion (LOF)

indications depicted in vendor supplied radiographs.

The

canister in question (DSC-1) had been fabricated by Equipos Nucleares SA

(ENSA), of Spain in accordance with ASME Code Section III, NC (83W85), see

NRC Inspection Report Nos. 50-269,270,287/90-21, paragraph 5, for further

details.

Since the close of the inspection discussed in the referenced

Inspection Report, the licensee met and discussed the problem with the

vendor,

re-radiographed the weld in question repeatedly in order to

duplicate shooting techniques and film sensitivity and attempt to locate

the rejectable indication. When none of these attempted was successful in

locating.the indication, the licensee performed a detailed review of the

fabrication records and discovered that the weld in question, (LW-205-1),

had been ground/dressed following radiography, to prepare it for surface

examination. Therefore, on the basis of the on-site radiographs, and the

recently discovered grinding records, the licensee concluded that the

indications observed in the vendor radiographs were no longer there as

they had been removed during the grinding of this weld.

By memorandum,

the licensee's Level III Examiner indicated the on site radiographs meet

code requirements and do not show rejectable indications.

The inspector

reviewed the vendor' and licensee produced radiographs, reviewed the vendor

documents presented and concurred with the licensee's decision that the

subject canister meets applicable code standards and is therefore

acceptable for the application.

No violations or deviations were identified.

8

6.

Inspection of Open Items (92700)(92701)(92702)

The following open items were reviewed using licensee reports, inspection,

record review, and discussions with licensee personnel, as appropriate:

(Closed) Violation 50-269,270,287/89-05-02:

Failure to follow

Procedures Due to Inadequacies in CMD Training and Qualifications.

The inspector reviewed the licensee response dated April 13, 1989,

and supplemental response dated October 2, 1990.

The licensee is

scheduled to complete the training and qualification of Construction

Maintenance Division personnel performing Nuclear Modification Work

in December 1992.

Based on the scheduled completion date, this item

is closed.

7. Exit Interview (30703)

The inspection scope and findings were summarized on July 3, 1991, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings. The

licensee did not identify as proprietary any of the material provided to

or reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

50-270/91-12-01

Violation -

Inoperable Flow

Instrument, paragraph 2.d.

50-287/91-12-02

Violation -

Failure to Follow

Procedure,.paragraph 2.e.