LER-1980-015, /03L-0:on 800916,valve 2LP21 Failed to Open During Performance of Engineered Safeguard Channel Test.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2701980015R03 - NRC Website |
|
text
REGULA Y INFORMATION DISTRIBUTIOSYSTEM (RIDS)
ACCESSION NBR:8010210539 DOC.DATE: 80/10/16 NOTARIZED: NO DOCKET #
FACIL:50-270 Oconee Nuclear Station, Unit 2, Duke Power Co.
05000270 AUTH.NAME AUTHOR AFFILIATION JONESJ.L.
Duke Power Co.
RECIP.NAME RECIPIENT AFFILIATION Region 2, Atlanta, Office of the Director SUBJECT: LER 80-015/03L-0:on 800916,valve 2LP21 failed to open during performance of engineered safeguard channel test.Caused by loose setscrew on motor driven pinion.Screw repaired.
DISTRIBUTION CODE: A002S COPIES RECEIVED:LTR.
ENCL iL SIZE:,
TITLE: Incident Reports NOTES:M Cunningham:all amends to FSAR & changes to Tech Specs.
05000270 AEODOrnstein:1cc.
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL ACTION:
REIDR..
04 3
3 INTERNAL:; A/D COMP&STRU06 1
1 A/D ENV TECH 07 1
1 A/D MATL & QUO8 1
1 A/D OP REACTOO9 1
1 A/D PLANT SYSIO 1
1 A/D RAD PROT 11 1
1 A/D SFTY ASSE12 1
1 A/D TECHNOLOG13 1
1 ACC EVAL BR 14 1
1 AEOD 2
2 ASLBP/J.HARD
- 1.
1 AUX SYS BR 15 1
1 CHEM ENG BR 16 1
1 CONT SYS BR 17 1
1 CORE PERF BR 18 1
1 D/DIRHUM FAC19 1
1 DIRENGINEERI20 1
1 DIRHUM FAC $21 1
1 DIRSYS INTEG22 1
1 EFF TR SYS BR23 1
1 EQUIP QUAL BR25 1
1 GEOSCIENCES 26 1
1 I&C.SYS BR 29 1
1 I&E 05 2
2 JORDANE./IE:
1 1
LIC GUID BR 30 1
1 LIC QUAL BR 31 1
1 MATL ENG BR 32 1
1 MECH ENG BR 33 1
1 MPA:
3 3
NRC PDR 02 1
1 OP EX EVAL BR34 3
3 OR ASSESS BR 35 1
1 POWER SYS-BR 36 1
1 S R39 1
1 REACT SYS BR 40 1
1 RE IE01, 1
1 RED & RISK A 41 1
1 EVA42 1
1 STRUCT ENG 8R44 1
1 SYS INTERAC B45 1
1 EXTERNAL: ACRS 46 16 16 LPDR 03 1
1 NSIC 05 1
1 TERA:DOUG MAY 1
1 2 2 1980 TOTAL NUMBER OF COPIES REQUIRED: LTTR ENCL
FRC FORM 38W U.
. NUCLEAR REGULATORY COMMISSIoN LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCK:
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMAT1ONI o
1N E
E 12 k'D 0 101-100 100 01o01-100 I(5')1411,1(l 1Q0
(
7 0
9 UCENSEa CO0 t4
" 18 UCENSa NUMBER 25 2
UCENUs TYPE so 57 CAT so CONrr EIJ L 4L+/-.X (0 15 101 010121 71 OJ0IO 1 91 116J8 0i)I 10 111 618 1010 60 GI OCCKET NUMBER sS 69 EVENT DATE 74 7
REPORT DATM 8o EVENT OESCRIPTION ANO PROBABLE CONSEQUENCES 10 o 2 On September 16, 1980, valve 2LP2Yfailed to.open during performance of the ES 0 -3 [channel test.
The valve was manually opened and declared inoperable. The o problem was corrected and the.valve declared operable within 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />, well o=
[-within the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> limit of Technical Specification 3.3.2.1d(2).
Thus, this 0 incident was of no significance with regard to safe operation, and the health [and safety of the public were not affected.
7 090 SYTTEM
CAUSE
CAUS Ecamp.
VALVs CCO COod SUBCCOS COMWPOENT CODE SG0COOa SUCCOCa 0
I
@1 [V !A I L VI 10 9J© LOi 812 12 to 19 20 SOUVATIAL OCCURRENCE REPORT ReViSIon.
LgRfllO 1"T1ARRVPOqRT NO.
coca
- - rypg pNo.
LL-8 f0'2 WF-24~IS 27 2L 29 L02 ACI UTURE EFFECT SI4UTDCVwN ArrAC,4#NT NPRO-d PRIME Comp.
COMPONENT TAKEN ACTION ON KIANIT PJETHOO NOR JSUBMITTED FOR M %us.
SIJPPUEA MAtdUPFCUen EJi IW 0 I
~
J 1ol00r LI e~J
_0 LII I L'j2 010 f 3
4a s31 44 41 42 43 hA47 CAUSE DESCRIPTION ANO CORRECflVE ACTIONS 1 The failure was caused by a loose setscrew on a motor-driven pinion. VibrationJ 1M Iwould be the most probable reason for the screw.coming out.
The loose screw was repaired and the valve returned to service. Operability of the valve was I Iveri f ied.
7 I9D PACIUTY (1)
METI00 O)
STATUS PotR OTHE STATUS DISCOVERY DISCOVY OCRIPTON II LE 1@
L Of 0 n2 I NAB I ~LU L..LLQ@
NA LJ Engineered Safeguard Channel Testingi 7
9 O12 13 4494 ACTIVITY CONTENT 80 IIEASE0 OF RELEAS AMOUNT OP ACTIVITY C
O D LzJ @ Ill NA NA 7
80 to it PERSONNEL EXPOSUREs NUMBER TYPE
DESCRIPTION
II 0I lololo 1z J&@
NA 7
8 9 11 12 13 PERSONNEL INJURIES NUMBER
DESCRIPTION
[TL]J Iof o
Lf NA 7
a 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE
DESCRIPTION
N~
NA 7
8 9 10 rULICITY Co 20 0O~ptpo NA III C!USEIIriI I
10 t
69 O
S 8 0 010 53'
.~~~ ~
~
DISCOVERY~r J
L J ne PO f7OV 4A 3ESC 3I 81ON 7
B1 EnierdSfgar hne0etn
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000270/LER-1980-003-01, /01T-0:on 800507,deborating Demineralizer Was Placed in Svc While Plant in Cold Shutdown & RCS Drained Down.Rcs Boron Concentration Reduced from 1,895 Ppm to 1,539 Ppm.Apparently Caused by Incorrect Chemistry Records | /01T-0:on 800507,deborating Demineralizer Was Placed in Svc While Plant in Cold Shutdown & RCS Drained Down.Rcs Boron Concentration Reduced from 1,895 Ppm to 1,539 Ppm.Apparently Caused by Incorrect Chemistry Records | | | 05000270/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000270/LER-1980-006-03, /03L-0:on 800625,at 40% Full Power,Valve 2LP21 Failed to Open Electrically on Command.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | /03L-0:on 800625,at 40% Full Power,Valve 2LP21 Failed to Open Electrically on Command.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | | | 05000270/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000259/LER-1980-009, Has Been Cancelled | Has Been Cancelled | | | 05000270/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000270/LER-1980-014-03, /03L-0:on 800822,concentrated Boric Acid Storage Tank Pump Removed from Svc Due to Oil & Flange Leaks.Caused by Torn Oil Seal,Worn Worm Gear,Bad Flange Gasket & Stuck Pressure Relief Valve.Items Replaced | /03L-0:on 800822,concentrated Boric Acid Storage Tank Pump Removed from Svc Due to Oil & Flange Leaks.Caused by Torn Oil Seal,Worn Worm Gear,Bad Flange Gasket & Stuck Pressure Relief Valve.Items Replaced | | | 05000270/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000270/LER-1980-015-03, /03L-0:on 800916,valve 2LP21 Failed to Open During Performance of Engineered Safeguard Channel Test.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | /03L-0:on 800916,valve 2LP21 Failed to Open During Performance of Engineered Safeguard Channel Test.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | | | 05000287/LER-1980-016-03, /03L-1:on 801123,fire Detectors String B-2 Went Into Alarm Condition.Caused by Dust Buildup in Detector. Detector Cleaned & Verified Operable | /03L-1:on 801123,fire Detectors String B-2 Went Into Alarm Condition.Caused by Dust Buildup in Detector. Detector Cleaned & Verified Operable | | | 05000287/LER-1980-016, Forwards LER 80-016/03L-1.Detailed Event Analysis Encl | Forwards LER 80-016/03L-1.Detailed Event Analysis Encl | | | 05000270/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000270/LER-1980-020-03, /03L-0:on 801013,during Performance of Es on-line Test,Valve 2FDW-103 Failed to Close During Cycling.Caused by Failure of Torque Switch.Valve Manually Closed.Bad Torque Switch Replaced | /03L-0:on 801013,during Performance of Es on-line Test,Valve 2FDW-103 Failed to Close During Cycling.Caused by Failure of Torque Switch.Valve Manually Closed.Bad Torque Switch Replaced | | | 05000270/LER-1980-022-01, /01T-0:on 801011,four Holes Were Knocked in Fire Barrier Between Cable Spread Room & Turbine Bldg W/O Establishment of Hourly Fire Watch.Caused by Failure to Provide Proper Notificaion.Hourly Fire Watch Established | /01T-0:on 801011,four Holes Were Knocked in Fire Barrier Between Cable Spread Room & Turbine Bldg W/O Establishment of Hourly Fire Watch.Caused by Failure to Provide Proper Notificaion.Hourly Fire Watch Established | | | 05000270/LER-1980-022, Forwards LER 80-022/01T-0 | Forwards LER 80-022/01T-0 | | | 05000270/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000270/LER-1980-024-03, /03L-0:on 801105,HPI Pump 2B Declared Inoperable Due to High Upper Bearing Temp.Caused by Isolation of Normal Cooling Water Supply to Unit 2 HPI Pumps,Personnel Error, Equipment Malfunction & Design Deficiency | /03L-0:on 801105,HPI Pump 2B Declared Inoperable Due to High Upper Bearing Temp.Caused by Isolation of Normal Cooling Water Supply to Unit 2 HPI Pumps,Personnel Error, Equipment Malfunction & Design Deficiency | | | 05000270/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000270/LER-1980-025-03, /03L-0:on 801217,HPI Pump 2B Declared Inoperable Because Motor Indicated High Upper Bearing Temp.Caused by Personnel Error in Replacing Oil.High Bearing Temp Probably Due to Restricted Cooling Water Flow | /03L-0:on 801217,HPI Pump 2B Declared Inoperable Because Motor Indicated High Upper Bearing Temp.Caused by Personnel Error in Replacing Oil.High Bearing Temp Probably Due to Restricted Cooling Water Flow | | | 05000269/LER-1980-040-01, /01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented | /01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented | | | 05000269/LER-1980-040, Forwards LER 80-040/01T-0.Detailed Event Analysis Encl | Forwards LER 80-040/01T-0.Detailed Event Analysis Encl | |
|